05000298/LER-1980-030-03, /03L-0:on 800813,during Normal Surveillance Testing of RHR Motor Operated Valves,Rhr Loop B Suppression Pool Cooling Inboard Throttle Valve Would Not Operate.Caused by Failure of Key Between Motor Pinion Gear & Motor Shaft

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/03L-0:on 800813,during Normal Surveillance Testing of RHR Motor Operated Valves,Rhr Loop B Suppression Pool Cooling Inboard Throttle Valve Would Not Operate.Caused by Failure of Key Between Motor Pinion Gear & Motor Shaft
ML19338C792
Person / Time
Site: Cooper Entergy icon.png
Issue date: 08/21/1980
From: Doan P
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19338C788 List:
References
LER-80-030-03L, LER-80-30-3L, NUDOCS 8009050289
Download: ML19338C792 (1)


LER-1980-030, /03L-0:on 800813,during Normal Surveillance Testing of RHR Motor Operated Valves,Rhr Loop B Suppression Pool Cooling Inboard Throttle Valve Would Not Operate.Caused by Failure of Key Between Motor Pinion Gear & Motor Shaft
Event date:
Report date:
2981980030R03 - NRC Website

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60 61 DOCK ET NUM8ER 68 69 EVENT DATE 14 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h f'oTil During normal surveillance testing of RHR motor onerated valves. RMR-MO-34B. tha RMRl l o 131 l'B" Loop suppression cool cooline inboard threrele un1va unn1A nne nnavnea-Thf= 4e i nno,2klo nel 10141 h repetitive occurrence (ref. T FR 76-14 nna 77-11). The "A" Run Tnnn une "u"

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RHR-M0-34B1 10l71 failed in the normally closed position. There were no adverse affects to the public l l o is I health and safety.

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