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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J3301994-10-0707 October 1994 LER 94-011-00:on 940908,manual Reactor Trip Initiated Due to MSIV Failure During part-stroke Test.Solenoid Valve & Number of Pins Replaced & MSIVs Tested satisfactorily.W/941007 Ltr ML20024J3291994-10-0303 October 1994 LER 94-027-00:on 940903,determined That Channel B Linear Range Nuclear Instrument Inoperable as Result of Connector J6 Being Disconnected from Jack.Connector J6 Reinstalled.W/ 941003 Ltr ML20029E5291994-05-13013 May 1994 LER 94-007-00:on 940414,determined That Valve Stroke Time Acceptance Criterion Exceeded System Response Time.Caused by Programmatic Error During Initial Startup.Corrective Action: Stroke Time Acceptance Has Been reduced.W/940513 Ltr ML20029E1361994-05-11011 May 1994 LER 94-007-00:on 940412,CRAC & Ebfs Were Inoperable Due to Previous Charcoal Testing Performed to Industry Std Different than Ts.Corrective Actions:Ts Changed to Reflect Newest Charcoal Testing procedure.W/940511 Ltr ML20029D8491994-05-0202 May 1994 LER 94-006-00:on 940407,plant Did Not Meet Requirements of LCO 3.7.6.1 Re Two Independent Control Room Emergency Ventilation Sys.Caused by Inadequate Work Organization. Corrective Action:Revised OP 2315A.W/940502 Ltr ML20029D6221994-04-29029 April 1994 LER 94-005-00:on 940401,determined That Both Facilities of Ebfs Had Never Been Tested in Accordance W/Ts.Caused by Program Failure/Personnel Error.Corrective Action: Surveillance Was Completed satisfactorily.W/940429 Ltr ML20029D2531994-04-28028 April 1994 LER 94-008-00:on 940329,discovered That Data in OPS Form 2604P-2,was Recorded Incorrectly.Caused by Program Failure, Procedure Deficiencies & Technical Error.Corrective Action: Recalculated ESF Equipment Circuit response.W/940428 Ltr ML20046C7771993-08-0606 August 1993 LER 93-010-00:on 930707,reactor Trip Input to Turbine Trip Portion of ESFAS Declared Inoperable Due to Inadequate Surveillance Testing.Test to Verify Operability Written & performed.W/930806 Ltr ML20046C2161993-08-0303 August 1993 LER 93-017-00:on 930701,possible Inoperability of Power Operated Relief Valve Blocking Valves Caused by Original Design Basis.Changed Designs & Performed tests.W/930803 Ltr ML20046B0311993-07-23023 July 1993 LER 93-012-01:on 930524,turbine & Reactor Tripped During Mussel Cook (Thermal Backwash) Due to Lack of Heat Removal Capabilities from Main Generator Stator Water Cooling Sys. Installed Thermoconductivity filler.W/930723 Ltr ML20045H8991993-07-15015 July 1993 LER 93-009-00:on 930617,determined That Suppl Leak Collection & Release Sys May Have Been Inoperable During Certain Weather Periods in Past.Caused by Failure to Account for Chimney Effect.Suppl Will Be sent.W/930715 Ltr ML20045H4021993-07-0909 July 1993 LER 93-007-00:on 930611,plant Mgt Discovered Reduction in EDG Fuel Oil Storage Capacity Per SER & Fsar,Constituting Event Outside Design Basis of Plant.Caused by Inadequate Design Interface.Temporary Tanker utilized.W/930709 Ltr ML20045H8921993-07-0909 July 1993 LER 93-005-01:on 930311,discovered That Automatic RPS Actuation Occurred on 930222 & Not Immediately Reported to Nrc.Caused by Personnel Error.Memo Sent to All Licensed Operators/Personnel Re Reporting requirements.W/930709 Ltr ML20045H8571993-07-0909 July 1993 LER 93-008-00:on 930614,one Channel of Electrical Environmentally Qualified Temp Monitor for Main Steam Valve Bldg Found Indicating Improperly.Caused by Personnel Error. Manual Logging of Temp initiated.W/930709 Ltr ML20045F5891993-07-0202 July 1993 LER 93-013-00:on 930603,noted That Main Turbine Generator EHC Sys Caused an Increase in Pressurizer Pressure,Resulting in Reactor Trip,Due to Closing of Intercept & Cv.Operators Performed EOP & Sys Performed as expected.W/930702 Ltr ML20045F6881993-07-0202 July 1993 LER 93-004-02:on 930222,reactor Trips on SG Low Water Level Occurred.Caused by Automatic Trip of MFW Pump B on Low Suction Pressure Due to High FW Flow Rates.Classroom Training on Main & Afwc Received by Licensed Operators ML20045D9041993-06-23023 June 1993 LER 93-012-00:on 930524,reactor Trip Occurred Due to Turbine Trip & Malfunction Caused Feedwater Regulating Valve a to Stay Approx 56% Open.Caused by Lack of Heat Removal Capabilities.Hand Wheels secured.W/930623 Ltr ML20045D8601993-06-21021 June 1993 LER 93-006-00:on 930525,two HPSI Discharge Check Valves Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Personnel Error.Test Written & Performed to Demonstrate Valve operability.W/930621 Ltr ML20045D9031993-06-21021 June 1993 LER 92-003-01:on 920207,discovered Potential Barrier Breach Via Direct Openings Around Main Feedwater Bypass Line Penetrations.On 920130,plant Entered Mode 4 W/O Encl Bldg Integrity.Erosion/Corrosion Exam Procedure Modified ML20045D3091993-06-18018 June 1993 LER 93-005-00:on 930520,cold Over Pressure Protection Sys Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Mgt Deficiency.Overlap Task Force Will Continue to Review Procedures Associated W/Reactor trip.W/930618 Ltr ML20045A4491993-06-0404 June 1993 LER 93-009-00:on 930506,inlet & Outlet skid-mounted Isolation Valves to Radiation Monitor Found Shut.Caused by Procedure Noncompliance by I&C Personnel.Personnel Will Review & Edit Radiation procedures.W/930604 Ltr ML20045A2321993-06-0101 June 1993 LER 93-008-00:on 930505,determined That Electrical Starter for Both Charging Pumps Inoperable.Caused by Program Failure.Administrative Controls Have Been Established to Ensure Minimum TS requirements.W/930601 Ltr ML20044C9191993-05-0707 May 1993 LER 93-002-01:on 930206 & 07,Train a & Train B CR Pressurization Sys Failed 18-month Surveillance Test, Respectively.Caused by Moisture in Air Banks & Pressure Oscillations.Air Banks purged.W/930507 Ltr ML20044C9331993-04-30030 April 1993 LER 91-002-01:on 910118,engineering Evaluation Determined That Operation of Four Vital 120-volt Ac Buses,On Alternate Sources,Unsatisfactory.Caused by Failure to Update TS to Reflect Configuration.Inverter Sys replaced.W/930430 Ltr ML19346B2411992-08-20020 August 1992 LER 92-018-00:on 920722,both RHR Trains Rendered Inoperable Due to Procedure Deficiency.Both Trains of RHR Restored to Operable Condition & Surveillance Procedures for Both Trains revised.W/920820 Ltr ML20024H3241991-05-24024 May 1991 LER 91-001-01:on 910110,electro-hydraulic Control Sys Failure Occurred,Causing Reactor Trip.Caused by Turbine Trip.Both EHC Pump Discharge Filters Changed Out & Pump B Replaced W/Spare pump.W/910524 Ltr ML20029C1281991-03-18018 March 1991 LER 91-004-00:on 910216,unexpected Trip of 'B' Steam Generator Feed Pump & Subsequent Manual Reactor Trip Occurred.Cause Unknown.Monitoring Capability Added to Sgfp Circuitry & Design Change made.W/910318 Ltr ML20029B6001991-03-0707 March 1991 LER 91-004-00:on 910205,leakage Found During Local Leak Rate Testing for Four Containment Isolation Valves.Caused by Improper Valve Seating.Valve Removed from Svc & Sent to Mfg for overhaul.W/910307 Ltr ML20029B6031991-03-0404 March 1991 LER 91-002-00:on 910202,setpoint Drift Identified During Testing of Main Steam Safety Valves.Caused by Inadequate Design.Nine out-of-tolerance Valves Reset within Specified +1% Tolerance ML20029B5981991-03-0404 March 1991 LER 91-003-00:on 910203 & 16,spurious Control Bldg Isolation Signals Received from Train a Control Bldg Ventilation Inlet Radiation Monitor.Caused by Equipment Malfunction.Detector replaced.W/910304 Ltr ML20029A6501991-02-19019 February 1991 LER 91-001-00:on 910117,discovered That Source Check Surveillance Procedure to Verify Operability of Beta Scintillation Radiation Detectors Did Not Meet TS Requirements.Surveillance Procedure revised.W/910219 Ltr ML20028H4261990-12-27027 December 1990 LER 89-005-01:on 890330,intermittent Connection While Sliding Module Into Position Caused Automatic Test Insertion Circuit to Send Signals Greater than Normal Pulse Thus Allowing Three SIAS Modules to actuate.W/901227 Ltr ML20028H4391990-12-27027 December 1990 LER 90-015-01:on 900919,inadvertent Isolation of Containment Isolation Valves Occurred.On 900920,inadvertent Actuation of Sias,Containment Isolation Actuation Sys & Encl Bldg Filtration Sys occurred.W/901227 Ltr ML20028H4271990-12-27027 December 1990 LER 90-021-00:on 901127,LCO Paragraph 3.0.3 Entered.Caused by Poor Communications.Mgt Reviewed Event & Events Leading Up to Incident & Concluded That Increased Awareness W/ Respect to Sys Status Must Be pursued.W/901227 Ltr ML20028H4401990-12-24024 December 1990 LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Gripper Coil Power Cable.Connector Replaced & Power Loop checked.W/901224 Ltr ML20028G9421990-09-26026 September 1990 LER 90-012-00:on 900827,automatic Reactor Trip Occurred During Bypass Switch Operations.Caused by Operator Error. Procedure Sp 2601D Revised to Incorporate Separate Section on Performing calibrs.W/900926 Ltr ML20028G9111990-09-18018 September 1990 LER 89-008-01:on 891002,determined That Plant Failed to Perform Functional Check of Control Board Annunciators During Channel Functional Tests.Caused by Personnel Error. Procedures Revised Re Annuciator testing.W/900918 Ltr ML20044B0441990-07-10010 July 1990 LER 90-007-00:on 900611,discovered That Surveillance Procedure 2609E Re Encl Bldg Filtration Sys Testing - Refueling Not Performed Prior to Entering Mode 4.Caused by Personnel Error.Missed Surveillance performed.W/900710 Ltr ML20044A1581990-06-18018 June 1990 LER 90-017-00:on 900518,loss of Both Trains of HPSI Occurred.Caused by Cognitive Failure by Licensed Operator. Personnel Counseled on Causes of Event & Importance of Recognizing When Event reportable.W/900618 Ltr ML20043H2021990-06-15015 June 1990 LER 90-005-00:on 900503,identified Potential for High Energy Line Break in Auxiliary Steam Sys That Could Degrade Plant Areas Determined as Mild Environs.Probably Caused by Incorrect Conclusions from Analysis in 1973.W/900615 Ltr ML20043G1031990-06-12012 June 1990 LER 90-016-00:on 900513,steam Generator B lo-lo Signal Generated Reactor Trip Signal,Causing Automatic Start of motor-driven Auxiliary Feedwater Pumps a & B.Caused by Inadequate Guidance.Procedure revised.W/900612 Ltr ML20043G3921990-06-11011 June 1990 LER 90-014-00:on 900519,manual Reactor Trip Initiated as Result of Anticipated Turbine Trip Due to Condenser Vacuum. Caused by Design Deficiency in That Traveling Screen Capacity Inadequate.Traveling Screen modified.W/900611 Ltr ML20043F7021990-06-11011 June 1990 LER 90-015-00:on 900512,feedwater Isolation Occurred While Opening Msivs.Caused by MSIV 2 Opening Faster than Other Msivs,Resulting in Swell in Steam Generator 2.Steam Generator Level Restored to normal.W/900611 Ltr ML20043F8261990-06-0707 June 1990 LER 90-006-00:on 900508,reactor Manually Tripped When Decreasing Levels Noted in Steam Generator 1 & Feedwater Regulating Valve Indicated Full Open.Caused by Valve Stem Separating from Plug.Feedwater Flow restored.W/900607 Ltr ML20043D4711990-05-30030 May 1990 LER 85-002-01:on 850302 & 25,unplanned Actuation of Containment Purge Valve Isolation Occurred.Caused by Personnel Error.Caution Signs Placed on Radiation Monitors & Reset Button on Monitor Made inaccessible.W/900530 Ltr ML20043A7841990-05-16016 May 1990 LER 90-013-00:on 900416,manual Reactor Trip Initiated Due to Imminent Loss of Condenser Vaccum.Caused by Inadequate Administrative Guidance When Debris Collected on Trash Rack. Severe Weather Procedure revised.W/900516 Ltr ML20042G7201990-05-0707 May 1990 LER 90-012-00:on 900406,review of Steam Generator Blowdown Monitor High Radiation Alarm Setpoint Revealed That Setpoint Was Nonconservative.Caused by Administrative Deficiency. Correct Setpoint installed.W/900507 Ltr ML20042E6751990-04-20020 April 1990 LER 90-002-00:on 900322,Tech Spec Action Statement 3.3.3.10 Not Entered for Out of Svc Stack Gas & Particulate Radiation Monitor.No Particulate Radiation Increases Detected.Caused by Personnel error.W/900420 Ltr ML20042E1621990-04-0909 April 1990 LER 90-009-00:on 900309,automatic Turbine Trip W/Subsequent Reactor Trip Occurred Due to High Stator Cooling Water Temp. Caused by Failure of Mechanical Linkage on Fisher & Portor Controller.Controller Replaced w/spare.W/900409 Ltr ML17223A7901990-04-0202 April 1990 LER 89-009-01:on 891025,radiation Monitor RM 8262 Inlet Valve (2-AC-82) Found Closed.Caused by Personnel Error. Isolation Valve Opened,Sample Flow Restored & Radiation Monitor Restored to Operable status.W/900402 Ltr 1994-05-02
[Table view] Category:RO)
MONTHYEARML20024J3301994-10-0707 October 1994 LER 94-011-00:on 940908,manual Reactor Trip Initiated Due to MSIV Failure During part-stroke Test.Solenoid Valve & Number of Pins Replaced & MSIVs Tested satisfactorily.W/941007 Ltr ML20024J3291994-10-0303 October 1994 LER 94-027-00:on 940903,determined That Channel B Linear Range Nuclear Instrument Inoperable as Result of Connector J6 Being Disconnected from Jack.Connector J6 Reinstalled.W/ 941003 Ltr ML20029E5291994-05-13013 May 1994 LER 94-007-00:on 940414,determined That Valve Stroke Time Acceptance Criterion Exceeded System Response Time.Caused by Programmatic Error During Initial Startup.Corrective Action: Stroke Time Acceptance Has Been reduced.W/940513 Ltr ML20029E1361994-05-11011 May 1994 LER 94-007-00:on 940412,CRAC & Ebfs Were Inoperable Due to Previous Charcoal Testing Performed to Industry Std Different than Ts.Corrective Actions:Ts Changed to Reflect Newest Charcoal Testing procedure.W/940511 Ltr ML20029D8491994-05-0202 May 1994 LER 94-006-00:on 940407,plant Did Not Meet Requirements of LCO 3.7.6.1 Re Two Independent Control Room Emergency Ventilation Sys.Caused by Inadequate Work Organization. Corrective Action:Revised OP 2315A.W/940502 Ltr ML20029D6221994-04-29029 April 1994 LER 94-005-00:on 940401,determined That Both Facilities of Ebfs Had Never Been Tested in Accordance W/Ts.Caused by Program Failure/Personnel Error.Corrective Action: Surveillance Was Completed satisfactorily.W/940429 Ltr ML20029D2531994-04-28028 April 1994 LER 94-008-00:on 940329,discovered That Data in OPS Form 2604P-2,was Recorded Incorrectly.Caused by Program Failure, Procedure Deficiencies & Technical Error.Corrective Action: Recalculated ESF Equipment Circuit response.W/940428 Ltr ML20046C7771993-08-0606 August 1993 LER 93-010-00:on 930707,reactor Trip Input to Turbine Trip Portion of ESFAS Declared Inoperable Due to Inadequate Surveillance Testing.Test to Verify Operability Written & performed.W/930806 Ltr ML20046C2161993-08-0303 August 1993 LER 93-017-00:on 930701,possible Inoperability of Power Operated Relief Valve Blocking Valves Caused by Original Design Basis.Changed Designs & Performed tests.W/930803 Ltr ML20046B0311993-07-23023 July 1993 LER 93-012-01:on 930524,turbine & Reactor Tripped During Mussel Cook (Thermal Backwash) Due to Lack of Heat Removal Capabilities from Main Generator Stator Water Cooling Sys. Installed Thermoconductivity filler.W/930723 Ltr ML20045H8991993-07-15015 July 1993 LER 93-009-00:on 930617,determined That Suppl Leak Collection & Release Sys May Have Been Inoperable During Certain Weather Periods in Past.Caused by Failure to Account for Chimney Effect.Suppl Will Be sent.W/930715 Ltr ML20045H4021993-07-0909 July 1993 LER 93-007-00:on 930611,plant Mgt Discovered Reduction in EDG Fuel Oil Storage Capacity Per SER & Fsar,Constituting Event Outside Design Basis of Plant.Caused by Inadequate Design Interface.Temporary Tanker utilized.W/930709 Ltr ML20045H8921993-07-0909 July 1993 LER 93-005-01:on 930311,discovered That Automatic RPS Actuation Occurred on 930222 & Not Immediately Reported to Nrc.Caused by Personnel Error.Memo Sent to All Licensed Operators/Personnel Re Reporting requirements.W/930709 Ltr ML20045H8571993-07-0909 July 1993 LER 93-008-00:on 930614,one Channel of Electrical Environmentally Qualified Temp Monitor for Main Steam Valve Bldg Found Indicating Improperly.Caused by Personnel Error. Manual Logging of Temp initiated.W/930709 Ltr ML20045F5891993-07-0202 July 1993 LER 93-013-00:on 930603,noted That Main Turbine Generator EHC Sys Caused an Increase in Pressurizer Pressure,Resulting in Reactor Trip,Due to Closing of Intercept & Cv.Operators Performed EOP & Sys Performed as expected.W/930702 Ltr ML20045F6881993-07-0202 July 1993 LER 93-004-02:on 930222,reactor Trips on SG Low Water Level Occurred.Caused by Automatic Trip of MFW Pump B on Low Suction Pressure Due to High FW Flow Rates.Classroom Training on Main & Afwc Received by Licensed Operators ML20045D9041993-06-23023 June 1993 LER 93-012-00:on 930524,reactor Trip Occurred Due to Turbine Trip & Malfunction Caused Feedwater Regulating Valve a to Stay Approx 56% Open.Caused by Lack of Heat Removal Capabilities.Hand Wheels secured.W/930623 Ltr ML20045D8601993-06-21021 June 1993 LER 93-006-00:on 930525,two HPSI Discharge Check Valves Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Personnel Error.Test Written & Performed to Demonstrate Valve operability.W/930621 Ltr ML20045D9031993-06-21021 June 1993 LER 92-003-01:on 920207,discovered Potential Barrier Breach Via Direct Openings Around Main Feedwater Bypass Line Penetrations.On 920130,plant Entered Mode 4 W/O Encl Bldg Integrity.Erosion/Corrosion Exam Procedure Modified ML20045D3091993-06-18018 June 1993 LER 93-005-00:on 930520,cold Over Pressure Protection Sys Declared Inoperable Due to Inadequate Surveillance Testing. Caused by Mgt Deficiency.Overlap Task Force Will Continue to Review Procedures Associated W/Reactor trip.W/930618 Ltr ML20045A4491993-06-0404 June 1993 LER 93-009-00:on 930506,inlet & Outlet skid-mounted Isolation Valves to Radiation Monitor Found Shut.Caused by Procedure Noncompliance by I&C Personnel.Personnel Will Review & Edit Radiation procedures.W/930604 Ltr ML20045A2321993-06-0101 June 1993 LER 93-008-00:on 930505,determined That Electrical Starter for Both Charging Pumps Inoperable.Caused by Program Failure.Administrative Controls Have Been Established to Ensure Minimum TS requirements.W/930601 Ltr ML20044C9191993-05-0707 May 1993 LER 93-002-01:on 930206 & 07,Train a & Train B CR Pressurization Sys Failed 18-month Surveillance Test, Respectively.Caused by Moisture in Air Banks & Pressure Oscillations.Air Banks purged.W/930507 Ltr ML20044C9331993-04-30030 April 1993 LER 91-002-01:on 910118,engineering Evaluation Determined That Operation of Four Vital 120-volt Ac Buses,On Alternate Sources,Unsatisfactory.Caused by Failure to Update TS to Reflect Configuration.Inverter Sys replaced.W/930430 Ltr ML19346B2411992-08-20020 August 1992 LER 92-018-00:on 920722,both RHR Trains Rendered Inoperable Due to Procedure Deficiency.Both Trains of RHR Restored to Operable Condition & Surveillance Procedures for Both Trains revised.W/920820 Ltr ML20024H3241991-05-24024 May 1991 LER 91-001-01:on 910110,electro-hydraulic Control Sys Failure Occurred,Causing Reactor Trip.Caused by Turbine Trip.Both EHC Pump Discharge Filters Changed Out & Pump B Replaced W/Spare pump.W/910524 Ltr ML20029C1281991-03-18018 March 1991 LER 91-004-00:on 910216,unexpected Trip of 'B' Steam Generator Feed Pump & Subsequent Manual Reactor Trip Occurred.Cause Unknown.Monitoring Capability Added to Sgfp Circuitry & Design Change made.W/910318 Ltr ML20029B6001991-03-0707 March 1991 LER 91-004-00:on 910205,leakage Found During Local Leak Rate Testing for Four Containment Isolation Valves.Caused by Improper Valve Seating.Valve Removed from Svc & Sent to Mfg for overhaul.W/910307 Ltr ML20029B6031991-03-0404 March 1991 LER 91-002-00:on 910202,setpoint Drift Identified During Testing of Main Steam Safety Valves.Caused by Inadequate Design.Nine out-of-tolerance Valves Reset within Specified +1% Tolerance ML20029B5981991-03-0404 March 1991 LER 91-003-00:on 910203 & 16,spurious Control Bldg Isolation Signals Received from Train a Control Bldg Ventilation Inlet Radiation Monitor.Caused by Equipment Malfunction.Detector replaced.W/910304 Ltr ML20029A6501991-02-19019 February 1991 LER 91-001-00:on 910117,discovered That Source Check Surveillance Procedure to Verify Operability of Beta Scintillation Radiation Detectors Did Not Meet TS Requirements.Surveillance Procedure revised.W/910219 Ltr ML20028H4261990-12-27027 December 1990 LER 89-005-01:on 890330,intermittent Connection While Sliding Module Into Position Caused Automatic Test Insertion Circuit to Send Signals Greater than Normal Pulse Thus Allowing Three SIAS Modules to actuate.W/901227 Ltr ML20028H4391990-12-27027 December 1990 LER 90-015-01:on 900919,inadvertent Isolation of Containment Isolation Valves Occurred.On 900920,inadvertent Actuation of Sias,Containment Isolation Actuation Sys & Encl Bldg Filtration Sys occurred.W/901227 Ltr ML20028H4271990-12-27027 December 1990 LER 90-021-00:on 901127,LCO Paragraph 3.0.3 Entered.Caused by Poor Communications.Mgt Reviewed Event & Events Leading Up to Incident & Concluded That Increased Awareness W/ Respect to Sys Status Must Be pursued.W/901227 Ltr ML20028H4401990-12-24024 December 1990 LER 90-019-00:on 900606,automatic Reactor Trip from Negative Flux Rate Signal Occurred Due to Dropped Control Rod.Caused by Broken Connection in Gripper Coil Power Cable.Connector Replaced & Power Loop checked.W/901224 Ltr ML20028G9421990-09-26026 September 1990 LER 90-012-00:on 900827,automatic Reactor Trip Occurred During Bypass Switch Operations.Caused by Operator Error. Procedure Sp 2601D Revised to Incorporate Separate Section on Performing calibrs.W/900926 Ltr ML20028G9111990-09-18018 September 1990 LER 89-008-01:on 891002,determined That Plant Failed to Perform Functional Check of Control Board Annunciators During Channel Functional Tests.Caused by Personnel Error. Procedures Revised Re Annuciator testing.W/900918 Ltr ML20044B0441990-07-10010 July 1990 LER 90-007-00:on 900611,discovered That Surveillance Procedure 2609E Re Encl Bldg Filtration Sys Testing - Refueling Not Performed Prior to Entering Mode 4.Caused by Personnel Error.Missed Surveillance performed.W/900710 Ltr ML20044A1581990-06-18018 June 1990 LER 90-017-00:on 900518,loss of Both Trains of HPSI Occurred.Caused by Cognitive Failure by Licensed Operator. Personnel Counseled on Causes of Event & Importance of Recognizing When Event reportable.W/900618 Ltr ML20043H2021990-06-15015 June 1990 LER 90-005-00:on 900503,identified Potential for High Energy Line Break in Auxiliary Steam Sys That Could Degrade Plant Areas Determined as Mild Environs.Probably Caused by Incorrect Conclusions from Analysis in 1973.W/900615 Ltr ML20043G1031990-06-12012 June 1990 LER 90-016-00:on 900513,steam Generator B lo-lo Signal Generated Reactor Trip Signal,Causing Automatic Start of motor-driven Auxiliary Feedwater Pumps a & B.Caused by Inadequate Guidance.Procedure revised.W/900612 Ltr ML20043G3921990-06-11011 June 1990 LER 90-014-00:on 900519,manual Reactor Trip Initiated as Result of Anticipated Turbine Trip Due to Condenser Vacuum. Caused by Design Deficiency in That Traveling Screen Capacity Inadequate.Traveling Screen modified.W/900611 Ltr ML20043F7021990-06-11011 June 1990 LER 90-015-00:on 900512,feedwater Isolation Occurred While Opening Msivs.Caused by MSIV 2 Opening Faster than Other Msivs,Resulting in Swell in Steam Generator 2.Steam Generator Level Restored to normal.W/900611 Ltr ML20043F8261990-06-0707 June 1990 LER 90-006-00:on 900508,reactor Manually Tripped When Decreasing Levels Noted in Steam Generator 1 & Feedwater Regulating Valve Indicated Full Open.Caused by Valve Stem Separating from Plug.Feedwater Flow restored.W/900607 Ltr ML20043D4711990-05-30030 May 1990 LER 85-002-01:on 850302 & 25,unplanned Actuation of Containment Purge Valve Isolation Occurred.Caused by Personnel Error.Caution Signs Placed on Radiation Monitors & Reset Button on Monitor Made inaccessible.W/900530 Ltr ML20043A7841990-05-16016 May 1990 LER 90-013-00:on 900416,manual Reactor Trip Initiated Due to Imminent Loss of Condenser Vaccum.Caused by Inadequate Administrative Guidance When Debris Collected on Trash Rack. Severe Weather Procedure revised.W/900516 Ltr ML20042G7201990-05-0707 May 1990 LER 90-012-00:on 900406,review of Steam Generator Blowdown Monitor High Radiation Alarm Setpoint Revealed That Setpoint Was Nonconservative.Caused by Administrative Deficiency. Correct Setpoint installed.W/900507 Ltr ML20042E6751990-04-20020 April 1990 LER 90-002-00:on 900322,Tech Spec Action Statement 3.3.3.10 Not Entered for Out of Svc Stack Gas & Particulate Radiation Monitor.No Particulate Radiation Increases Detected.Caused by Personnel error.W/900420 Ltr ML20042E1621990-04-0909 April 1990 LER 90-009-00:on 900309,automatic Turbine Trip W/Subsequent Reactor Trip Occurred Due to High Stator Cooling Water Temp. Caused by Failure of Mechanical Linkage on Fisher & Portor Controller.Controller Replaced w/spare.W/900409 Ltr ML17223A7901990-04-0202 April 1990 LER 89-009-01:on 891025,radiation Monitor RM 8262 Inlet Valve (2-AC-82) Found Closed.Caused by Personnel Error. Isolation Valve Opened,Sample Flow Restored & Radiation Monitor Restored to Operable status.W/900402 Ltr 1994-05-02
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
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Genord Offe:s Seicen Street. Berhn Connsettut 7 N s D a'EIe N n N ec coTmn7 '
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!' Nonneast Nuew energy conwany (203)666-6000 :
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i Det.ober 10. 1989 j MP-1360!i ,
Re: 10CFR50.73(a)(2)(v) !
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l U.S. Nuclear Regulatory Commission Document Control Desk '
Washington, D.C. 20555
Reference:
Facility Operatinc License No. NPF-49 !
Docket No. 50-4'23 i Licensee Event Report 88-026-03 ,
Gentlemen: f This letter forwards Licensee Event Report 88-026-03 submitted as an update to report i a sicnificant change made to the modification proposed in LER 88-0 6-02. LER's 88-626-00, 88-026-01 and 88-026-02 were submitted pursuant to 10CFR50.73(a)(2) t (v), any event or condition that alone could have prevented the fulfillment of the safety -
. function of systems that are needed to mitigate the consequences of an accident. ;
Very truly yours, >
NORTHEAST NUCLEAR ENERGY COMPANY i A
cact -
Steph E. Scace Station Superintendent ,
Millstone Nuclear Power Station ;
SES/Rh%mo
Attachment:
LER 88-026-03 cc: W. T. Russell, Region 1 Administrator W. J. Raymond, Senior Resident inspector, Millstone Unit Nos.1, 2 and 3 D. H. Jaffe, NRC Project Manager, Millstone Unit No. .s
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F ACluTY NAME o) UQ4r L1 NsMbEh (4) L+M l hillistone Nuclear Power Stetion Unit 3 of si of of op l213 1lOFl015 I lilLE 14)
Potential Damage to Safety Related Eouipment Due to Design inadeouaev EVENT C# ATE (bl (EA NUMpEA t$) rstpOAT DATFI? OTMF A F A0ttreit $ NvotvED se t MONTP- DAY YEAR YEAR A MONTH DAY YEAR fA WIYNAMES j ofsiofofof I I i i
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Po sottairinav) 60 73(al(2HH3) 60 73 aM2 ital LICENSEE CON' ACT FOR TH!S LER f12' NAME TE LE PHONE NUMBE A Akk A CODI Robert N. Keller Engmeer, Ext. 5507 2 0l3 4l4l7l-llj7l9l1 I
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On November 15,1986 at 1630 hours, with the plant in hiode 1 at 100Fe power, engineering postulated a scenario which could, in the extreme case, result in a loss of redundant trains of safety related (vital) equipment. It was discovered that certam circumstances could lead to hiillstone Unit 3 becoming isolated from the hiillstone Station Switchyard while on-line. This cotid lead to an out-of-phase fast transfer to the Reserve Station Service Transformer (RSST) resulung in a potentially damaging transient on both trains of vital 4160V busses.
On December 29, 1968, with the plant in hiode 1 at 75Fe power, three relays were identified that, assuming a single failure, also could result in the postulated scenario.
Root cause of both events is inadequacy in plant design. The out-of-phase transfer scenario postulated had not been previously identified.
As a resuh of the first event, administrative controls were implemented to realign the 4160V busses to the RSST when either of the switchyard breakers were open. As a result of the later esent, the power supply to the 4160V busses was manually abgned to the RSST. W)th the 4160V busses supphed by the RSST, the sceriatio is no longer feasible since the busses are in the post fast transfer state. A modification was l completed on June 22,1989 to ehmmate the last transfer on undervoltage. I
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FACILITY NAME (1) DoCCT NVMBER '2l tFo N W PrA <ti FACsE 138 YEAR E Millstone Nuclear Power Station U"" 3 ~ ~
0l6l0l0l0l4l2l3 $l8 0l 2l6 0l3 0l 2 OF 0l5 TEXT tit more space is roos'**c. use tiocition.' NRc Form 3%A e) (17)
.. 1. Decenntion of Event j-On November 18,1966 at 1630 hours, with the plant in Mocie 1 at 100% power, plant engineering
, reported that a scenario had been postulated that could, in the extreme case, result in a loss of redundant trains of safety related (vital) equipment. This scenario was discovered during an engineering review of the effects of a main generator coastdown. Immediate action included the implementation of administrative controls to reduce the probability of occurrence of the postulated scenario. In addition, engineenng initiated a Significant Safety Hazard Evaluauon in compliance with 10CFR21. " Reporting of Defects and Noncomphance" The following is a description of the events sequence that could lead to a loss of redundant safety related equipment (refer to Figure 1 for the one-hne configuration of offsite and onsite power for Millstone Unit 3).
With Millstone Unit 3 main generator on-hne, this scenario can be initiated in one of two ways. f
- 1. Switchyard breaker 150-14T-2 is open or out of service for repairs and breaker 150-13T-2 opens automatically to isolate a fauh on the switchyard north bus.
- 2. Switchyard breaker 15G-13T-2 is open or out of service for repairs and breaker 150-14T-2 opens automatically to isolate a fault on the Millstone-Southington 348 transmission kne.
Both situation 1 and 2 result in the isolation of the main generator from the Millstone Station Switchyard. Under these circumstances, the main generator breaker would remain closed. The turbine subsequently tnps due to a power mismatch or turbine overspeed. A turbine-generator coastdown would follow. Since the main generator breaker receives no signal to open and excitation is still present, the main generator continues to provide power via the Normal Station Service Transformers (NSST's) to the Unit 3 6900V and 4160V electrical distribution systems.
Based on a computer model of the generator coastdown, voltage on the 4160V busses would decay to 3220V at approximately 76 seconds after the turbine tnp. At this time the model predicts that the main generator frequency would be approximately 40HZ.. At 3220 volts, the undervoltage relays on non-vital busses 34 A and 34B actuate. After a 2 second time delay, all motor loads off of 34A and 34B tnp and also the supply breakers from NSST-A to bus 34A and 34B trip. The tripping of the norma) supply breaker irutiates a " fast transfer" to the Reserve Stauon Service Transformer " A" (RSST-A). Dunns this fast transfer, the RSST-A supply breakers to the vital busses 34C and 34D close approximately 6 cycles after the NSST-A supply breakers open. Due to the fact that motor loads remain connected to vital busses 34C and 34D during this 6 cycle interval, voltage /frequeracy on the busses is not expected to change significantly. Therefore, the RSST supply at 4160V/60Hz will not match the vital bus conditions of 3:20V/.10Hr. Vital bus connected loads will remain connected unless the fast transfer is not successful. Thus, the transient could damage the connected vital loads before the protective relays open RSST to 34C and 34D bus breakers.
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TEXT (It more space is recurrec. Use 60011:0441 NRc Form 3t4A 8) (17)
- l. Deciminn nr Event Cont'd. !
On December 29,1988 at 1600 hours, with the plant operating in Mode 1 at 75% power, 585 degrees F. 2250 psia, it was determined that a single failure of any one of three relays located at ,
the Millstone Station Switchyard could also cause this turbine-generator trip /coastdown and subsequent out-of-phase 4160V bus supply transfer. This determination was made dunng a Switchyard Electrical Protection Drawing review resulting from the irutial discovery of the postulated scenario. These relays of concern are the Pilot Wire Differential Relay 87PWY/U3, Pilot Wire Monitor and Transfer Tnp Relay 36PWY/U3, and the Pilot Wire Tnpping Relay 94PWY/U3. j At 1617 on December 29. 1968, the power supply to the 4160V busses was manually transferred to the RSST. In this configuration the bus transfer scheme is defeated, thereby chminating the possibihty of an out-of-phase transfer.
!!. Cause of Event The root cause of these events is design inadequacy. The turbine generator coastdown/out-of-phase transfer scenario is an event which was not considered in the original design basis of the plant. Therefore, design of systems and circuitry to prevent such an event is not in compliance with apphcable Regulatory Guides or 10CFR des 1Fn criteria.
Ill. AnMysis of Event These events are being reported in accordance with 10CFR50.73(a)(2)(v'), as a discovery of a design inadequacy which alone could have prevented the fulfillment of the safety function of r structures or systems that are needed to shutdown the reactor and sustain it in a safe shutdown condition, remove residual heat, control the release of radioacuve material, or miugate the consequences of an accident.
The postulated scenario could, in the extreme case, result in an overvoltage/overcurrent transient that could cause damage to the connected loads of the vital (safety related) bus. It can be l considered a common mode failure in that both trains of operating saftty related equipment would be simultaneously subjected to the transient.
Although the fast transfer schemes are similar, the non-vital 6900V busses would not oe exposed to this type of transient because the undervoltage triays do not initiate the opening of their supply breakers from NSST-B. The undervoltage relays would shed all loads ! rom the busses, so the motors would not be subject to the undervoltage/underfrequency condition experienced while the busses remain connected to the generator dunng coastdown. Control room operators would have the option to manually transfer the 6900V feed over to the RSST-B dunng the coastdown without the threat of equipment damage.
Pertaining to the November 16,1988 event, a seview of the Millstone Station Switchyard Log revealed that there were 12 instances where breaker 150-13T-2 m 150-14T-2 was open with ,
Millstone Unit 3 on-line. The durations vary in length from 7 minutes to 790 minutes, with 10 less ,
tnan 40 minutes. These were all due to manual switching evolutions (i.e., the breakers never opened automatically).
I For the December 19,1988 even., the only failure mode of the specihed relays which could initiate l the postulated scenario is spontaneous operatica. The relays, which are normally deenergized, l would have to expenence a change of state due to shock or a susmic event. Since the relays are l not Class IE and have not been 6eismically tested, the profile of parameters required to cause this change of state is u*iknown.
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[. IV. CorrecWe Action j immediate corrective action included placement of caution tags on the Main Control Board status indicator lights for the 15G-13T-2 and 150-14T-2 swnchyard breakers. The tags require control room operators to manually transfer the Unit's offsite power supply to the Reserve Station Service Transformer, in the event that either of the two switchyard breakers open for any reason. When 3 the vital husses are supplied via the RSST's, the Fast Transfer Scheme is disabled, thus effectively preventmp the possibihty of this scenario from occurring. Engineennp reviewed possible scenarios with station power supplied from the RSST's and determined that it would not have a negauve impact on plant operations. This is based on the fact that a Loss of Power (LOP) event will still result in a transfer to the Emergency Diesel Generators, and, if required, the operators can manually switch back to the NSST's.
On January 12, 1969, a temporary circuit modification was made which prevents the out-of-phase transfer from occurring. The modtheation removed the undervoltage trip of the NSST supply
, breakers to the non-vital busses, effecuvely preventing a " fast transfer" on undervoltage. All other i
aspects of the fast transfer were unaffected by the modification. The postulated scenario (or any i loss of vohage at the NSST) will now result in a
- slow transfer", where the vital busses isolate from the non-vital busses and become connected to the RSST (if RSS'I voltape is greater than 90G) or Emergency Diesel Generators. This interma rnodificauon permitted the plant to return to the normal electrical configuration with the NSST supplying all 4160V loads.
On June 22, 1989, a permanent modification was completed to shminate the fast transfer on an undervoltage condition. This change employed a contact from the relay that receives the signal from the non-vital undervoltage relays to block the high speed closure of the supply breaker from the RSST. All other aspects of the fast transfer scheme remain unchanged. The fast transfer will still function as designed whenever the NSST supply breaker opens automatically for reasons other than undervoltage (i.e., overcurrent, current differential, etc.). An undervoltage condition on the non-vital busses will result in a slow tr msfer, where the vital to non-ntal bus ue breaker opens and the supply breaker from the RSST closes. In addition to the above, a modification was made to ensure that whenever switchyard breakers 250-13T-2 and 150-14T-2 art both open, the main generator output breaker and NSST supply breakers (both 4160V and 6960V) will trip. This will result in a 4160V and 6900V bus supply fast transfer to the RSST.
V. Additional informntir n l
LER 50-423/86-026 reports a plant tnp related to Emergency Diesel Generator Surveillance testing with the 4160V busses supplied by the RSST.
The B Emergency Diesel Generator was started for surveillance testing. When the B Emergency Diesel Generator was paralleled to the emergency 4160V bus 34D, the normal to emergency bus tie breaker opened on reverse overcurrent trip, deenergizing the normal bus 34B. The cause of this event was procedural dehciency. The apphcable operatmg procedures have been corrected.
EIIS CODES Synems Comnonents Switchyard System - FK Inter-Tie Transformers (NSST & RSST) - XFMR Switchyard Breakers - BKR j Relay - RLY
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