05000317/LER-1980-028-03, /03L-0:on 800515,during Performance of Routine Test,Diesel Generator 12 Failed to Reach Rated Speed in Less than 10-s Until Third Attempt.Caused by Intermittent Female Pin & Crack in Bakelite Spacer of Anphenol Connector

From kanterella
(Redirected from ML19318A091)
Jump to navigation Jump to search
/03L-0:on 800515,during Performance of Routine Test,Diesel Generator 12 Failed to Reach Rated Speed in Less than 10-s Until Third Attempt.Caused by Intermittent Female Pin & Crack in Bakelite Spacer of Anphenol Connector
ML19318A091
Person / Time
Site: Calvert Cliffs 
Issue date: 06/13/1980
From: Bauer E, Heibel R
BALTIMORE GAS & ELECTRIC CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19318A081 List:
References
LER-80-028-03L-01, LER-80-28-3L-1, NUDOCS 8006180443
Download: ML19318A091 (2)


LER-1980-028, /03L-0:on 800515,during Performance of Routine Test,Diesel Generator 12 Failed to Reach Rated Speed in Less than 10-s Until Third Attempt.Caused by Intermittent Female Pin & Crack in Bakelite Spacer of Anphenol Connector
Event date:
Report date:
3171980028R03 - NRC Website

text

uWLeigntwnrwtuwv p,

CONTnol 8 LOCK: l l

l l

l l lh (PLEASE PRINT 0;) TYPE ALL REQUIRED INFO".MATISNI g

1 8

fo ITl l r410 I c l c l NI I l@l 0101-10101010101-l o l o l@l 411 11 11111@l I

l@

7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE Jo

$7 CAT 58 CON'T I'oI"Sl T,"C U:.j@l0l5l0l010l3l1l7l@l015l115l810l@l0161113I810l@

~

7 8

60 81 DOCKET NUM8ER 68 69 EVENT oATE 74 7%

RETORT oATE 80 EVENT nESCRIPTION AND PROSABLE CONSEQUENCES h ITT M i Durino the cerforrance of a routine test #12 diesel cenerator (DG) failed to 1

ITT3"I I reach rated speed in less than 10 seconds until the third attemot. The first I o 141 l attenot was at 0300. At 0320 the diesel was left runnino as recuired by F6 Tin i

.S. 3.8.1.1.

At 1005 #12 diesel was taken out of service for repairs. The T

io is i l DG was returned to service at 1600 on 5/15/80. Both offsite AC power sources I o I 7 l 1 and the redundant DG remained operable during the event. This is not a l o is i i repetitive occurrence.

sVSSC7[o'Es"NESE Co'o'E

  • ^ i! ' s*8CioE CouPoNENT CooE

^

Co l o_L9_)

l E l E l@ [E_j@ l A l@ l El Ll El Cl Ol UlO l X l@ LI.J @

7 8

9 10 11 12 13 18 19 20 SE OUENTi AL OCCUR R E NCE RE PC RT REVtsloN LEA EVENT YEAR REPORT NO.

CooE TYPE No.

@,ago/Ro la lo I l-l I of 21 81 1/l I ol al LLJ L-l LoJ g

21 22 23 24 26 27 28 29 30 31 32 K N ACTO oN PL NT ME Hour $

$8 i PoR > 8.

S PPLIE MANUFA URER I c l@l z l@

l 21@

l 21 @

l 01 Ol0 10 I lY l@

l Nl@

l Al@

l Al 31 81 C 33 34 36 36 3J 40 41 42 43 44 4

CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 11101 l investication revealed an intermittentfemale contact oin and a crack in the bakelite t i 13 i i spacer of the amphenol. connector for the 250 RPti speed switch.

It is assumed that u..it of the soeed li l 2 l Ithis ennnectnr had hann mieh naloa 2+

enint Ti:e e p, c c

en-o iil3; l switch caused the starting circuit to time out and initiate a start failure and ii i4i Iexciter shutdown sonnanca ST

% power OTHERSTATUS oISCo RY otScoVERY oESCRIPTioN na i

l a l@l ny->+nr nwe- +4c-l.LLsJ LEJ@ l il ol nl@l

'5

' !riviry C# TENT A

RELEA$t@o of RELE ASEL,2]@l NA I

l NA.

LoCATidN oF RELEASE AMOUNT oF ACTivlTY IZl 1 6 PERsoNN[L ExPosOEs

~

oEsCRiPrioN@

NUv8eR TvPE FTT11010101@l z l@l NA

' PERsoNNEt iN;U4Es oEsCRiPTioN@

NUuSER li l e l l 01010 l@l NA ~

7 8 9 11 12 Ei

" s'C%'A'o' '" @

'5 PE l1l9I[Z_j@l NA 7

8 9 10 ITTol L @of CRIPTroN tS$UE l

NA I

LllIllIIII11 7

8 9 10 68 69 i

l'401 DFC 47?P/e7 m R. P. Heibel/E. R. %or psoNg:

NA'.*E OF PREPARER 9'gg-.- -- ----

s.)

LER NO.

80-28/3L DOCKET fl0.

50-317 EVEtiT DATE 05/15/80 REPORT DATE 06/13/80 ATTACH"ENT CAUSE DESCRIPTION ArtD CORRECTIVE ACTI0 tis:

(C0!1 tit!UED)

The amphenol female plug was replacad, The diesel is tested on a weekly basis and no further action is contemplated.

6 9