LER-1980-004, /03L-0:on 800409,w/plant at Normal Steady State, Emergency Diesel Generator Failed to Start During Routine Surveillance Test.Second Attempt Unsuccessful.Caused by Broken Vane in Starting Air Motor.Air Motor Replaced |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2661980004R03 - NRC Website |
|
text
a gu 3s4
^
~~
~~
~
~
' U.' S. NUCLEA2 C E 2 ULATORY' COMastSSION (7 771 8 00 0 ti " 2 -
UCENSEE EVENT REPORT 5
6@
. CONTaOt 8tOCx: l l
l l
l l
l i, TEA.E,R,NT c. Ty,E Ato cEcuenEn iN,ocuATiON:
I Io R lWIIl P l B l Hl 1 l@l 0 l 0 l-l 0 l 0 l 0 l 0 l 0 l-l 0 l 0 @l 4 l1 l1 l1 l 1 @l l
l@
7 8 9 UCENSEE CODE 14 15 LICENSE NUMSER 2i i
- - 26 LICENSE TYPE JU S7 CAT te CON'T Qj@l 0 l 5 l 0 l 0 l 0 l 2 l 616 l@l 01410 l9 l 8 l 0 l@l 0 l 4 l 2 l 5l 8 l 0 l@
O i suC 7
C 60 el DOCKET NUMBER 88 69 EVENT DATE 74 7S REPORT DATE 80 l
EVENT DESCRIPTION AND,RO8A8tE CONSEQUENCES h O 2 lAt 0422 on 4"9-80, with the plant at normal steady state, the emergency I l Diesel generator failed to start during a routine surveillance test.
A_)
O 3 lsecond start attempt at 0435 was also unsuccessful.
At this time the 4Dl O 4 F6 Tin IEDG was declared inoperable and removed from service for maintenance.
l lThe operability of the redundant EDG was verified at 0436.
This placed i O s 1
lthe plant in a degraded mode allowed by T.S.
- 15. 3. 7.B. l.e, but reportablq 0,
i g gunder T.G.
15.6.9.2.B.2.
I 7
8 9 80 I
'SI[E
- TE sSCiOE sues"Oo'E sSCOOE CO COMPONENT Coot l El El@ g@ g@ lMl Ol Tl Ol Rl Xl@ {@ g @
O 9 7
8 9
10
$1 12 13 18 19 20 I
_EVENTYEAR REPORT NO.
CODE TYPE NO.
SEQUENTIAL OCCURRENCE REPORT REVISION LE R /RO
@Rg
_l218 l 0l b l010l4l l_/_j l0 l3 l y
b
[_0J 22 23 24 26 27 28 29 30 31 32 j
TAKEN A TO PL NT ME HOURS S
ITT FOR 8.
L MAN F CTURER l Al@[_Z_j@
[Z_J@
W@
l010l0l0l W@
[Y_j@
W@
lI l 0 l 7 l 5 l@
33 J4 JS 36 31 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i O Rhe first start failure was caused by a broken vane in the startina air I i i lmo to r.
The second start failure could have been caused by the air motorI pr by a shutdown timer initiated by the operator following the first l
, 2 l
l failure.
The air motor was replaced and operability of the Diesel was l
, 3 g Iverified.
A redundant start system would have functioned on loss of AC.I 7
8 9 OO
$A $
% PO"fER OTHERSTATUS DISCO R DISCOVERY oESCRIPPON I
[ E_j@ l 0 l 7l 9 l@l N/A l
W @ Operator observation l
i s ACTIVITY CO TENT AMOUNTOP ACTIVITY @ l LOCATION OP RELEASE @
RELEasEo OP RELEASE [Z_j @ g' exposures lN/A l N/A l
i s l
PE RsONNEt oEsCRiPTiON @
NuueER TvPE l0 l 0 l 0 l@[Z_j@l N/A l
i 7 I
PERsONNE L iN;u' dies oEsCRiPTiON@
NuMeER l0 l 0 l 0 l@l N/A l
i a 7
s 9 is i2
=0 TY E DE R PT
@lN/A l
i 9 7
8 9 10 30 DESCRIPTlON ibSUE @l N/A i
lIll111111lll$
2 O 7
8 9 10 60 69 80 C*
Y PHONE:
NAME OF PREPARER I-.
l
[
ATTACHMENT TO LICENSEE EVENT REPORT NO. 80-004/03L-0 Wisconsin Electric Power Company Point Beach Nuclear Plant Unit 1 Docket No. 50-266 l
On April 9, 1980, at 0422 hours0.00488 days <br />0.117 hours <br />6.977513e-4 weeks <br />1.60571e-4 months <br /> while performing a routine surveillance test the 4D emergency diesel generator failed to start, and an " emergency diesel G02 starting circuit disabled" alarm annunciated.
The operator immediately went to stop on the diesel generator control switch after receiving the alarm, which initiated the diesel shut-down timer.
The alarm cleared when reset and correct system lineup was verified by the Shift Supervisor.
A second attempt to start the diesel was made at 0435 hours0.00503 days <br />0.121 hours <br />7.19246e-4 weeks <br />1.655175e-4 months <br /> and the diesel again failed to start.
Failure of the diesel to start this time, however, could possibly be attributed to the shut-down sequence initiated by the operator after the first start failure.
When the operator turned the diesel control switch to stop he initiated the shut-down sequence which consists of reducing diesel speed to idle for 11 1/2 minutes followed by a three and one-half minute complete shut-down period.
The diesel cannot be manually started except for a fast start during the complete shut-down phase, although if the diesel were in automatic a start signal would override the shut-down sequence.
Upon receiving the second start failure, the 4D diesel was declared inoperable for maintenance, and operability of the redundant 3D emergency diesel generator was verified at 0436 hours0.00505 days <br />0.121 hours <br />7.208995e-4 weeks <br />1.65898e-4 months <br /> on April 9.
This placed the plant in a degraded mode of operation allowed by Technical Specification 15.3.7.B.l.e.
When inspected to determine the problem, a faulty relt.y in the "not in automatic" alarm circuit was discovered.
Failure of this relay should not have prevented a diesel start however.
Although after replacement of the relay, the diesel functioned properly during a subsequent operability verification test.
The 4D emergency diesel generator was returned to service at 1035 hours0.012 days <br />0.288 hours <br />0.00171 weeks <br />3.938175e-4 months <br /> on April 9.
On April 16 additional testing of the diesel was conducted to try and determine the exact cause of the April 9 start failure.
The relay was removed and a diesel start was attempted.
The diesel failed to start on a manual remote start signal but did start on a fast start signal.
The relay was installed again and a diesel start was again attempted.
The diesel failed to start again on a manual start.
This indicated that there was another problem with the diesel.
The diesel had been in Start System 2 during all these attempts and it was postulated that the problem may be with Start System 2.
The start system selector switch was switched to-System 1 and the diesel started on a manual remote signal.
. An investigation of the No. 2 air start system identified a broken vane in one of the air starting motors.
The air motor was replaced and operability of the diesel was verified on April 16.
The diesel is equipped with two independent air starting systems, each of which is capable of starting the diesel.
During a manual remote start, one of the start systems is selected and the other system does not function.
During an automatic start, however, the system selected will function first and the second system will kick in automatically if the diesel does not start within a specific time.
This fact was verified when the diesel started upon a fast start signal with the defectiva motor still installed and Start System 2 selected.
Thus, the diesel would have started during an actual loss of off-site power.
Routine surveillance testing of each emergency diesel generator is performed biweekly.
The priority air start system selected is alternated monthly.
Removal of one emergency diesel generator from service because of its failure to start placed the plant in a degraded mode of operation allowed by Technical Specification 15.3.7.B.l.e and reportable in accordance with Technical Specification 15.6.9.2.B.2.
1 l
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000266/LER-1980-001-01, /01T-0:on 800202,during Routine Calibr of Pressure Transmitters for Motor Driven Auxiliary Feed Pumps, Transmitter Isolation Block Valves Discovered Closed.Caused by Inadvertent Closing of Isolation Valves.Snubbers Added | /01T-0:on 800202,during Routine Calibr of Pressure Transmitters for Motor Driven Auxiliary Feed Pumps, Transmitter Isolation Block Valves Discovered Closed.Caused by Inadvertent Closing of Isolation Valves.Snubbers Added | | | 05000266/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000301/LER-1980-001-01, /01T-0:on 800221,during Full Power Operation, Momentary Loss of Red Instrument Bus Occurred,Resulting in Power Range Channel N41 Failing Low.Caused by Faulty Capacitor in 2DY01 Power Supply.Capacitor Replaced | /01T-0:on 800221,during Full Power Operation, Momentary Loss of Red Instrument Bus Occurred,Resulting in Power Range Channel N41 Failing Low.Caused by Faulty Capacitor in 2DY01 Power Supply.Capacitor Replaced | | | 05000301/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000301/LER-1980-002-01, /01T-0:on 800227,primary-to-secondary Leak Was Identified in Steam Generator a Resulting in Shutdown of Unit.Caused by Leaking Tube at Position R18C37.Six Defective Tubes Found in Steam Generator a | /01T-0:on 800227,primary-to-secondary Leak Was Identified in Steam Generator a Resulting in Shutdown of Unit.Caused by Leaking Tube at Position R18C37.Six Defective Tubes Found in Steam Generator a | | | 05000266/LER-1980-002, Updated LER 80-002/01T-01:on 800311,during 800 Psi Secondary to Primary Hydrostatic Leak Test,Tubes R23C44 & R8C37 & Plug End R23C50 Found Leaking.Eddy Current Insp Performed.Tube Holes & Leaking Explosive Plugs Were Plug Welde | Updated LER 80-002/01T-01:on 800311,during 800 Psi Secondary to Primary Hydrostatic Leak Test,Tubes R23C44 & R8C37 & Plug End R23C50 Found Leaking.Eddy Current Insp Performed.Tube Holes & Leaking Explosive Plugs Were Plug Welded | | | 05000266/LER-1980-002-01, /01T-0:on 800311,during shutdown,800 Psi secondary-to-primary Hydrostatic Leak Test of B Steam Generator Revealed Tube R23C44 Leaking,Tube R8C37 Wet & Plug End R23C50 Wet.Tube Holes Will Be Weld Plugged | /01T-0:on 800311,during shutdown,800 Psi secondary-to-primary Hydrostatic Leak Test of B Steam Generator Revealed Tube R23C44 Leaking,Tube R8C37 Wet & Plug End R23C50 Wet.Tube Holes Will Be Weld Plugged | | | 05000301/LER-1980-002, Updated LER 80-002/01T-1:on 800227,during Normal Operation, Indication of Increasing primary-to-secondary Leak in a Steam Generator Noted.Caused by Leaking Tube in a Steam Generator Position R18C37 | Updated LER 80-002/01T-1:on 800227,during Normal Operation, Indication of Increasing primary-to-secondary Leak in a Steam Generator Noted.Caused by Leaking Tube in a Steam Generator Position R18C37 | | | 05000266/LER-1980-003, Forwards LER 80-003/03T-0 | Forwards LER 80-003/03T-0 | | | 05000301/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000266/LER-1980-003-03, /03T-0:on 800318,during post-mod Testing of Containment Spray Sys,Relay 1CSB Would Not Latch.Caused by Latching Mechanism Misalignment.Latch Adjusted & Proper Operation Verified on 800318.Similar Relay Bench Tested | /03T-0:on 800318,during post-mod Testing of Containment Spray Sys,Relay 1CSB Would Not Latch.Caused by Latching Mechanism Misalignment.Latch Adjusted & Proper Operation Verified on 800318.Similar Relay Bench Tested | | | 05000301/LER-1980-003-01, /01T-0:on 800408,while Testing Pressurizer Logic Channels,Pressurizer Level Channel 427 Was Momentarily Failed Low by Instrumentation & Control Technicians.Caused by Personnel Error.Event Discussed W/Personnel | /01T-0:on 800408,while Testing Pressurizer Logic Channels,Pressurizer Level Channel 427 Was Momentarily Failed Low by Instrumentation & Control Technicians.Caused by Personnel Error.Event Discussed W/Personnel | | | 05000266/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000301/LER-1980-004-03, /03L-0:on 800417,during Seismic Analysis of as-built safety-related Sys Per IE Bulletin 79-14, Discovered Overstressed Condition in Component Cooling Sys Piping.Caused by Lack of Support Upstream of Juncture | /03L-0:on 800417,during Seismic Analysis of as-built safety-related Sys Per IE Bulletin 79-14, Discovered Overstressed Condition in Component Cooling Sys Piping.Caused by Lack of Support Upstream of Juncture | | | 05000301/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000266/LER-1980-004-03, /03L-0:on 800409,w/plant at Normal Steady State, Emergency Diesel Generator Failed to Start During Routine Surveillance Test.Second Attempt Unsuccessful.Caused by Broken Vane in Starting Air Motor.Air Motor Replaced | /03L-0:on 800409,w/plant at Normal Steady State, Emergency Diesel Generator Failed to Start During Routine Surveillance Test.Second Attempt Unsuccessful.Caused by Broken Vane in Starting Air Motor.Air Motor Replaced | | | 05000266/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000266/LER-1980-005-03, /03L-0:on 800417,during Normal Operation,Review of Security Logs Revealed That Designated Fire Brigade Was Below Min Supervision Requirements on Three Occasions.Caused by Operations Personnel Designation Error | /03L-0:on 800417,during Normal Operation,Review of Security Logs Revealed That Designated Fire Brigade Was Below Min Supervision Requirements on Three Occasions.Caused by Operations Personnel Designation Error | | | 05000301/LER-1980-005-03, /03L-0:on 800609,during Training Walkdown of Safeguards Electrical Supply Cabinets,Noted That Tie Breaker Between AO5 & AO6 Safeguards Buses Was Shut.Probably Caused by Improper Electrical Lineup After Loss of Ac Test | /03L-0:on 800609,during Training Walkdown of Safeguards Electrical Supply Cabinets,Noted That Tie Breaker Between AO5 & AO6 Safeguards Buses Was Shut.Probably Caused by Improper Electrical Lineup After Loss of Ac Test | | | 05000301/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000266/LER-1980-006-03, /03L-0:on 800417,during Analysis of as-built safety-related Piping Sys Per IE Bulletin 79-14,overstressed Condition Discovered in Cooling Sys Piping.Caused by Lack of Support Between Valves Upstream of Juncture | /03L-0:on 800417,during Analysis of as-built safety-related Piping Sys Per IE Bulletin 79-14,overstressed Condition Discovered in Cooling Sys Piping.Caused by Lack of Support Between Valves Upstream of Juncture | | | 05000301/LER-1980-006-01, /01T-0:on 800617,during Safeguards Logic Test W/ One Emergency Diesel Generator Out of Svc,Auto Containment Spray Pump Actuation Threatened During Loss of Ac & high- High Containment Pressure.Caused by Personnel Error | /01T-0:on 800617,during Safeguards Logic Test W/ One Emergency Diesel Generator Out of Svc,Auto Containment Spray Pump Actuation Threatened During Loss of Ac & high- High Containment Pressure.Caused by Personnel Error | | | 05000301/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000266/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000301/LER-1980-007-01, /01T-0:on 800619,at Full Power,Test IT-04 Was Performed W/Emergency Diesel Generator 3D Out of Svc. Emergency Safeguards Train Equipment Would Have Been Inoperable on Loss of Ac Power.Caused by Personnel Error | /01T-0:on 800619,at Full Power,Test IT-04 Was Performed W/Emergency Diesel Generator 3D Out of Svc. Emergency Safeguards Train Equipment Would Have Been Inoperable on Loss of Ac Power.Caused by Personnel Error | | | 05000266/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000266/LER-1980-007-01, /01T-0:on 800611,blue Instrument Bus 1Y02 Was de-energized,resulting in de-energization of 3 Containment Pressure Channels.Caused by Personnel Error.Power Restored & Instrumentation Returned to Normal | /01T-0:on 800611,blue Instrument Bus 1Y02 Was de-energized,resulting in de-energization of 3 Containment Pressure Channels.Caused by Personnel Error.Power Restored & Instrumentation Returned to Normal | | | 05000301/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000266/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000266/LER-1980-008-03, /03L-0:on 800606,during Normal Operation,Testing Revealed That Relay 1-247/AO2X in Train B Would Not Drop Out to Initiate Undervoltage Trip Function.Cause Not Determined. Relay Replaced & Tested Satisfactorily | /03L-0:on 800606,during Normal Operation,Testing Revealed That Relay 1-247/AO2X in Train B Would Not Drop Out to Initiate Undervoltage Trip Function.Cause Not Determined. Relay Replaced & Tested Satisfactorily | | | 05000301/LER-1980-008, Forwards LER 80-008/01T-0 | Forwards LER 80-008/01T-0 | | | 05000301/LER-1980-008-01, /01T-0:on 800912,following Trip from Full Power, Main Steam Stop Valve B Failed to Close Upon Receiving Close Signal.Caused by Deposit Buildup on Valve Shaft &/Or Hardening of Gland Packing | /01T-0:on 800912,following Trip from Full Power, Main Steam Stop Valve B Failed to Close Upon Receiving Close Signal.Caused by Deposit Buildup on Valve Shaft &/Or Hardening of Gland Packing | | | 05000301/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000301/LER-1980-009-03, /03L-0:on 801101,during Normal Operation, Performance of ICP 2.14 Found P8 Permissive Bistable from Channel N44 to Be Set at 50.5%.Caused by Instrument Drift. Bistable Adjusted & Tested Satisfactorily | /03L-0:on 801101,during Normal Operation, Performance of ICP 2.14 Found P8 Permissive Bistable from Channel N44 to Be Set at 50.5%.Caused by Instrument Drift. Bistable Adjusted & Tested Satisfactorily | | | 05000266/LER-1980-009, Forwards LER 80-009/01T-0 | Forwards LER 80-009/01T-0 | | | 05000266/LER-1980-009-01, /01T-0:on 800728 While in Cold Shutdown & During Hydrostatic Leak Test of Steam Generators,Two Dripping Explosive Plugs & Two Wet End Plugs Noted.Cause Not Stated. Dripping Plugs Weld Repaired | /01T-0:on 800728 While in Cold Shutdown & During Hydrostatic Leak Test of Steam Generators,Two Dripping Explosive Plugs & Two Wet End Plugs Noted.Cause Not Stated. Dripping Plugs Weld Repaired | | | 05000266/LER-1980-010-03, /03L-0:on 800827,during Normal Operation,After Redundant Containment Spray Pump Recirculation Phase Suction Valve Maint,Operability Test Was Not Performed.Caused by Personnel Failure to Fully Comprehend Maint Procedures | /03L-0:on 800827,during Normal Operation,After Redundant Containment Spray Pump Recirculation Phase Suction Valve Maint,Operability Test Was Not Performed.Caused by Personnel Failure to Fully Comprehend Maint Procedures | | | 05000266/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000301/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000301/LER-1980-010-03, /03L-0:on 801117,safety Injection Pump 2P15A Motor & Pump Shaft to Coupling Keys Found to Be Sheared.Cause Undetermined.Pump & Motor Checked for Damage,Keys Replaced & Pump Operability Verified | /03L-0:on 801117,safety Injection Pump 2P15A Motor & Pump Shaft to Coupling Keys Found to Be Sheared.Cause Undetermined.Pump & Motor Checked for Damage,Keys Replaced & Pump Operability Verified | | | 05000301/LER-1980-011-03, /03L-0:on 801118,axial Flux Difference Deviated from Target Band.Caused by Improper Interpretation of Tech Specs Resulting in Failure to Lower High Neutron Flux Setpoint.Instruction Clarified | /03L-0:on 801118,axial Flux Difference Deviated from Target Band.Caused by Improper Interpretation of Tech Specs Resulting in Failure to Lower High Neutron Flux Setpoint.Instruction Clarified | | | 05000301/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000266/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000266/LER-1980-011-03, /03L-0:on 800926,found That,Aug 1977-Sept 1980, Containment Spray Sys Spray Additive Valves Were Tested Per ASME Program Requirements Instead of Per Tech Specs.Caused by Administrative Error Re NRC | /03L-0:on 800926,found That,Aug 1977-Sept 1980, Containment Spray Sys Spray Additive Valves Were Tested Per ASME Program Requirements Instead of Per Tech Specs.Caused by Administrative Error Re NRC | | | 05000266/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000266/LER-1980-012-03, /03L-0:on 801005,logs Showed Decrease in Holdup Tank Pressure During 801002-05.Evaluation Showed Leak on Compression Fitting on Inlet to Valve IPCV-1022C.Caused by Improper Reinstallation of Valve After Cleaning | /03L-0:on 801005,logs Showed Decrease in Holdup Tank Pressure During 801002-05.Evaluation Showed Leak on Compression Fitting on Inlet to Valve IPCV-1022C.Caused by Improper Reinstallation of Valve After Cleaning | | | 05000301/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000301/LER-1980-012-03, /03L-0:on 801202,slippage Found in Shaft Driven Seal Water Pump Impeller Resulting in Overheating of Throttle Bushing.Caused by Reduced Seal Water Flow Due to Loosening of Pumping Ring.Shaft Sleeve & Bushing Replaced | /03L-0:on 801202,slippage Found in Shaft Driven Seal Water Pump Impeller Resulting in Overheating of Throttle Bushing.Caused by Reduced Seal Water Flow Due to Loosening of Pumping Ring.Shaft Sleeve & Bushing Replaced | | | 05000266/LER-1980-013, Forwards LER 80-013/01T-0 | Forwards LER 80-013/01T-0 | | | 05000266/LER-1980-013-01, /01T-0:on 801113,suction to 1P4B Boric Acid Transfer Pump Isolated,Rendering Pump Inoperable.Probably Caused by Personnel Error in Returning Valve Lineup to Normal Following Recirculation & Sampling | /01T-0:on 801113,suction to 1P4B Boric Acid Transfer Pump Isolated,Rendering Pump Inoperable.Probably Caused by Personnel Error in Returning Valve Lineup to Normal Following Recirculation & Sampling | |
|