05000298/LER-1980-007-03, /03L-0:on 800310,during Surveillance Testing of Standby Liquid Control Pumps,Standby Liquid Control Pump 1B Would Pump Only 36.5 Gpm at 1,215 Psig.Caused by Wear & Pitting to Seating Surface

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/03L-0:on 800310,during Surveillance Testing of Standby Liquid Control Pumps,Standby Liquid Control Pump 1B Would Pump Only 36.5 Gpm at 1,215 Psig.Caused by Wear & Pitting to Seating Surface
ML19309F181
Person / Time
Site: Cooper Entergy icon.png
Issue date: 03/25/1980
From: Ballinger P
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19309F176 List:
References
LER-80-007-03L, LER-80-7-3L, NUDOCS 8004280579
Download: ML19309F181 (1)


LER-1980-007, /03L-0:on 800310,during Surveillance Testing of Standby Liquid Control Pumps,Standby Liquid Control Pump 1B Would Pump Only 36.5 Gpm at 1,215 Psig.Caused by Wear & Pitting to Seating Surface
Event date:
Report date:
2981980007R03 - NRC Website

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NRc FQRM 366 U. S. NUCLEAR REGULATO3Y COMMISSION (7 77)

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stc pu-n "1 R" I yould pump 36.5 gpm at 1215 psig. Tech. Spec. Section 4.4.A.2.b requires the SLC l

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ig i, pystem to provide 38.2 gpm at 1215 psig from each pump. The redundant pump, SLC Pump l l n,,, j

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