ML19309E119

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LER 80-012/03L-0:on 800314,during Routine Power Operation, Hydraulic Snubber on Hanger 490001 Found W/No Visible Fluid Level.Caused by Seal Deterioration Due to High Vibration. Snubber Replaced
ML19309E119
Person / Time
Site: Millstone Dominion icon.png
Issue date: 04/11/1980
From: Crockett J
NORTHEAST UTILITIES
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19309E116 List:
References
LER-80-012-03L, LER-80-12-3L, NUDOCS 8004180411
Download: ML19309E119 (1)


Text

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7 60 Gl DOCKET NUMBER CH C'J EVENT DATg 74 75 HEPORT DATE B0 EVENT DESCRIPTION AND PHODADLE CONSEQUENCES h t o 121 } During routine power operation, a hydraulic snubber on hanger 490001 was found with no I o 3 l visible fluid level. The snubber was replaced and subsequently tested and found to I o 4 I operate erratically, indicating air had been introduced. The unit was operated per I o s l Technical Specification 3.7.8.1. The snubber is an ITT Grinnell, Fig. 200, 3-1/4 inch 'I o o l bore by 5 inch stroke unit. No safety significance as snubber is non-safety related. I 10171 1 I 101811 I 7 8 D 80 DE CODE 5 BC E COMPONENT CODE SU8C dE 5 E lol9l lH lB l@ LEj@ l B l@ l Sl Ul Pl 01 RJ Tl@ W@ QJ @

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