LER-1979-040, Supplemental LER 79-040/03L-1:on 791213,during Instrument Check,Variations in Suppression Pool Level Noted Between Reading on Control Room Panel 901-3 & Local Sight Glass, Exceeding Tech Specs.Caused by Crud on Sensing Lines |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2541979040R00 - NRC Website |
|
text
NRC FCRM 366 U.S. NUCLEAR REGULATORY CoMMisSloN (7 771 UPDATE REPORT--
PREVIOUS REPORT DATE l-11-80 LICENSEE EVENT REPORT CONTROL BLOCK: l l
l l
l l
lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6
@ l l l L l Q l A l D l 1 lgl 0 l 0 l 0 l - l 0 l 0 l0 l-l 0 l 0 l 0 l@l 4 l 1 l 1 l 1 l 1 l@l l
lg 7
8 9 LICENSEE CODE 14 15 LICENSE NUMSER 25 26 LICENSE TYPE 40 S7 CATSd CON'T 10111 Eu""C lL}@l0l5l0l0l0121514l@ll 121Il317191@l01310171810l@
?
8 60 61 DOCK ET NUMB E R 68 69 EVENT DATE 74 75 REPORT QATE 80 EVENT DESCRIPTION AND PRCSABLE CONSEQUENCES h lo l2l l During routine instrument check, slight variations in the suporession pool level have i Fo tal I been noted between the reading in the control room, on panel 901-3, and tne local I
l o l41 l sight glass.
Due to these variations the Technical Specification 3.7.A.l b limit for l lo tel I suppression pool level was exceeded on December 13, 23, 28, 1979, and on January 8 l
l 0 l6 l l and 9, 1980.
Since the suppression pool temperature was moderate and because the l
lo l7l l limits for suppression pool level are conservative, safe plant operation was not i
10181 l jeopardized.
I 7
8 9 60 SYSTEM
CAUSE
CAUSE COMP.
VA LVE CODE CODE SUSCODE COMPONENT CODE SUSCODE SUSCODE l0l9l l S l A l@ lE lg l ElQ l l l N l 5 l T l R lU [Q {@ l Zl@
7 8
9 to 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVIS3CN LER/RO EVENT YE A R R EPORT NO.
CODE TYPE N O.
O aE g 17 [9 l
[--J l 0 l 4 l 01 y
[0_l 3 l l Ll l--j l1 l 0
yu
_ 21 22 23 24 26 27 N
a 30 31 32 TKN AC ON ONP NT M
HOURS SS i FOR 8.
S PPLIE MANUFA RER l A lgl34Fl@
l Zl@
Q@
l 0l 0l 0l 0l l Y l@
l Y l@
l Nl@
lB l0 l8 l0 ]@
33 3b 36 37 40 -
41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h lijoll A partial blockage of the instrument sensing lines, due to postulated crud buildup, I
lTTi l l reduced instrument response. Further investigation found a crack in the upoer I
i,121 I section of the local sight glass. The instrument lines were backflushed and the l
gl instrument was recalibrated.
The local sight glass was replaced.
In each case the l
33141; suppression pool level was immediately restored to normal.
l 7
8 9 80 ST S
% POWER OTHER STATUS IS O RY DISCOVERY 0ESCRIPTION lt l s l l El@ l 0l 9l 7lgl NA l
lAlgl Operational Event l
ACTIVITY CO TENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE Q J @ l Z l@l NA l
l NA l
PERSONNEL EXPOS ES NUMSER TYPE
DESCRIPTION
l i l 7 l l 0l 0 l 0 l@l Z l@l NA l
PERSONNE L INJURIES NUMBER
DESCRIPTION
g l0l0l0l@l NA l
r 7
8 9 11 12 80 LOSS OP OR D AMAGE TO FACILITY TYPE
DESCRIPTION
8 I Zlg[
NA l
7 8 9 10 80 ISS
DESCRIPTION
2 o l
NA l
lllllll;;;;;l~
7 8 9 to 68 69 80 3 J. Kopacz 309-654-2241 ext. 178 o NAME OF PREPARER PHONE:
8003200385
1.
LER NUMBER:
LER/R0 79-40/03L-l II.
LICENSEE NAME: Commonwealth Edison Company quad-Cities Nuclear Power Station Ill.
FACILITY NAME: Unit One IV.
DOCKET NUMBER: 050-254 V.
EVENT DESCRIPTION
On December 13, 1979, while on shift rounds, an equipment attendant checked the suppression chamber level at the local sight glass. The sight glass indicated a level of +.4 inchas.
The lower sensing line was then opened and the sight glass was drained. When this was done, the level then corrected to a level of -2.2 inches. During this time the control room Indication dorpped from -1/4 inches to -2.0 inches.
On December 23, 1979, the Unit One operator found the suppression chamber level above normal.
By pumping water to the main condenser, suppression pool level was lowered to -1/2 inches by control room indication. An equipment attendant was then dispatched to verify the level at the local sight glass.
The local sight glass indicated a suppression pool level of -2 inches.
On December 28, 1979, an instrument mechanic backflushed the sight glass sensing lines and calibrated transmitter 1-1626.
Following this work the suppression chamber level by local indication was found to be +2.25 inches.
On January 8, 1980 the Suppression Chamber level instrumentation appeared to be sensing level inaccurately.
Level in this instance was found at the lower procedural limit and was immediately increased. The instrumentation was checked and as a result the final level was +2.5 inches. The water level was immediately restored to normal by removing water inventory.
On January 9, 1980 the suppression chamber level was found to be low.
In this instance both the control room instrument and the local sight glass indicated -2.0 inches. Water was immediately added to correct the level.
VI.
PROBABLE CONSEQUENCES OF THE OCCURRENCE Minimal safety implications result from these occurrences.
The suppression pool level is maintained to assure total condensing of steam from a reactor blowdown at full power.
Due to a large factor of safety designed into the pressure suppression system, total steam condensing would result even with slightly higher or lower water levels. Therefore the system would have operated as designed.
Vll.
CAUSE
This instrumentation and associated sensing lines are subject to crud buildup from the suppression chamber water. This buildup caused partial blockage in the sensing lines and reduced the response of the instruments. Therefore, after the first two events, a recalibration of the transmitter gave the correct water level but did not clear the sensing lines.
Therefore, when the level changed, the instrument did not respond correctly.
A subsequent investigation found a crack in the upper section of the local sight glass. This is believed to have caused some deviation in the accuracy of the local level readings.
Vill.
CORRECTIVE ACTION
in each case the immediate action was to correct the suppression chamber level to within limits. A calibration check (QlS 1) of transmitter LT-1-1626 was then performed.
Upon reoccurrence, further investigation disclosed a partial blockage of the sensing lines. This was corrected by backflushing the sensing lines, on December 28, 1979 On January 15, 1980 when a crack in the local sight glass was found, the sight glass was replaced. The level was then monitored daily for seven days to verify conformance between the local sight glass and the control room instrument indication.
To improve the reliability of the transmitter, transmitter internals are to be replaced in the future.
Parts are on order and will be installed on a simely basis.
The level transmitter is manufactured by Barton Instrument Company model 352. The new internals are to be Barton model 368-352.
The suppression pool level readings are currently being taken once a week at the local sight glass to assure conformance with the control room instrument.
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000265/LER-1979-001-03, /03L-0 on 790104:during Monthly Operability Test, Inlet Air Heater on a Standby Gas Treatment Sys Was Found Inoperable.Caused by Setpoint Drift of Flow Switch 1/2-7541-8A | /03L-0 on 790104:during Monthly Operability Test, Inlet Air Heater on a Standby Gas Treatment Sys Was Found Inoperable.Caused by Setpoint Drift of Flow Switch 1/2-7541-8A | | | 05000254/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000265/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000254/LER-1979-001-03, /03L-0 on 790107:high Steam Line Flow Alarm & Automatic Isolation of Reactor Core Isolation Cooling Steam Supply Line Occurred.Caused by Failure of Micro Switch Inside Steam Line High Flow Differential Pressure Switch | /03L-0 on 790107:high Steam Line Flow Alarm & Automatic Isolation of Reactor Core Isolation Cooling Steam Supply Line Occurred.Caused by Failure of Micro Switch Inside Steam Line High Flow Differential Pressure Switch | | | 05000265/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000265/LER-1979-002-03, /03L-0 on 790110:during Routine Insp of Reactor Water Cleanup Pump Rooms,Small Leak Was Found on 2-1205B Cleanup Pump Suction Line.Cause Unknown.Leak Was Isolated & Linear Indication on Flange Ground Out | /03L-0 on 790110:during Routine Insp of Reactor Water Cleanup Pump Rooms,Small Leak Was Found on 2-1205B Cleanup Pump Suction Line.Cause Unknown.Leak Was Isolated & Linear Indication on Flange Ground Out | | | 05000254/LER-1979-002-03, /03L-0 on 790110:during Freon Test,Noted That Freon Penetration Through Charcoal Absorbers Exceeded Tech Spec Max.Caused by One of Charcoal Clamping Levers Not Being Fully Latched | /03L-0 on 790110:during Freon Test,Noted That Freon Penetration Through Charcoal Absorbers Exceeded Tech Spec Max.Caused by One of Charcoal Clamping Levers Not Being Fully Latched | | | 05000254/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000265/LER-1979-003-03, /03L-0 on 790214:during High Temp Isolation Calibr Procedure,Temp Switch TS 2-2373A Was Found to Trip in Excess of Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibrated & Retested | /03L-0 on 790214:during High Temp Isolation Calibr Procedure,Temp Switch TS 2-2373A Was Found to Trip in Excess of Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibrated & Retested | | | 05000254/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000265/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000254/LER-1979-003-03, /03L-1 on 790119:MSIV Local Leak Rate Showed Seven Valves Leaking Excessively.Causes Unspecified.Valve Stroke Adjusted,Certain Valves Dismantled,Discs & Seats Were Lapped & Machined | /03L-1 on 790119:MSIV Local Leak Rate Showed Seven Valves Leaking Excessively.Causes Unspecified.Valve Stroke Adjusted,Certain Valves Dismantled,Discs & Seats Were Lapped & Machined | | | 05000254/LER-1979-004, Forwards LER 79-004/01T-0 | Forwards LER 79-004/01T-0 | | | 05000254/LER-1979-004-01, /01T-0 on 790122:piece of Control Rod Drive Return Nozzle Thermal Sleeve Retaining Ring Was Missing.Cause Unknown | /01T-0 on 790122:piece of Control Rod Drive Return Nozzle Thermal Sleeve Retaining Ring Was Missing.Cause Unknown | | | 05000265/LER-1979-004-03, /03L-0 on 790211:suction Isolation Valve Mo 2-1001-50 Failed to Close from Control Room.Caused by Failed Circuit Breaker in Valve Motor Control Center. Valve Taken Out of Svc for Repair During Outages | /03L-0 on 790211:suction Isolation Valve Mo 2-1001-50 Failed to Close from Control Room.Caused by Failed Circuit Breaker in Valve Motor Control Center. Valve Taken Out of Svc for Repair During Outages | | | 05000265/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000254/LER-1979-005-03, /03L-0 on 790123:during Unit 1/2 Diesel Generator Monthly Load Test Qos 6600-1,pilot Solenoid Valve to Air Starting Motors Failed & Unit 1/2 Diesel Was Shutdown. Caused by Mechanical Failure of Valve.Valve Was Replaced | /03L-0 on 790123:during Unit 1/2 Diesel Generator Monthly Load Test Qos 6600-1,pilot Solenoid Valve to Air Starting Motors Failed & Unit 1/2 Diesel Was Shutdown. Caused by Mechanical Failure of Valve.Valve Was Replaced | | | 05000254/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000265/LER-1979-005-03, /03L-0 on 790223:2A Recirculation Motor Generator Field Breaker Opened,Causing Flow Mismatch.Caused by Loosening of Coupling Between Main Shaft & Recirculation Motor Generator Set Tachometer.Tachometer Coupling Reset | /03L-0 on 790223:2A Recirculation Motor Generator Field Breaker Opened,Causing Flow Mismatch.Caused by Loosening of Coupling Between Main Shaft & Recirculation Motor Generator Set Tachometer.Tachometer Coupling Reset | | | 05000265/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000254/LER-1979-006-03, /03L-0 on 790125:during Primary Containment Isolation Valve Closure Timing,Valve AO 1-1601-21 Failed to Close in 10 Seconds.Caused by Improper Adjustment of Valve Speed Control from Operational Wear.Control Was Readjusted | /03L-0 on 790125:during Primary Containment Isolation Valve Closure Timing,Valve AO 1-1601-21 Failed to Close in 10 Seconds.Caused by Improper Adjustment of Valve Speed Control from Operational Wear.Control Was Readjusted | | | 05000254/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000254/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000254/LER-1979-007-03, /03L-0 on 790201:main Steam Line Leak Detection Temp Switches TS 1-261-16A,MTS 1-261-18A & TS 1-261-15C Tripped in Excess of Setpoint.Caused by Instrument Setpoint Drift.Temp Switches Recalibrated | /03L-0 on 790201:main Steam Line Leak Detection Temp Switches TS 1-261-16A,MTS 1-261-18A & TS 1-261-15C Tripped in Excess of Setpoint.Caused by Instrument Setpoint Drift.Temp Switches Recalibrated | | | 05000254/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000254/LER-1979-008-03, /03L-0 on 790202:temp Switch TS-1-1360-15D Had Trip Setpoint in Excess of Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibrated & Satisfactorily Tested | /03L-0 on 790202:temp Switch TS-1-1360-15D Had Trip Setpoint in Excess of Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibrated & Satisfactorily Tested | | | 05000254/LER-1979-009-03, /03L-0 on 790203:bed Plate Drain Valves AO 1-4999-57,58 & 60 Did Not Fully Close.Caused by Corrosion & Failure of Internal Return Springs.Springs Replaced & Valves Satisfactorily Retested | /03L-0 on 790203:bed Plate Drain Valves AO 1-4999-57,58 & 60 Did Not Fully Close.Caused by Corrosion & Failure of Internal Return Springs.Springs Replaced & Valves Satisfactorily Retested | | | 05000254/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000265/LER-1979-009, Forwards LER 79-009/03L-0.Corrects Docket Number of Original Forwarding Ltr | Forwards LER 79-009/03L-0.Corrects Docket Number of Original Forwarding Ltr | | | 05000265/LER-1979-009-03, /03L-0:on 790429,switch Trip Positions Found at Greater than 10% of MSIV Closure.Caused by Failure to Set Field Calibr for Switch Trip Point Limit.Switches Were Adjusted to 10% Closure or Less | /03L-0:on 790429,switch Trip Positions Found at Greater than 10% of MSIV Closure.Caused by Failure to Set Field Calibr for Switch Trip Point Limit.Switches Were Adjusted to 10% Closure or Less | | | 05000254/LER-1979-010-03, /03L-1 on 790205:diesel Fire Pump 1/2A Out of Svc Beyond Tech Spec Limit.Caused by Personnel Error.Pump Returned to Svc | /03L-1 on 790205:diesel Fire Pump 1/2A Out of Svc Beyond Tech Spec Limit.Caused by Personnel Error.Pump Returned to Svc | | | 05000254/LER-1979-010, Forwards LER 79-010/03L-1 | Forwards LER 79-010/03L-1 | | | 05000265/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000265/LER-1979-010-03, /03L-0 on 790514:2A Fuel Pool Radiation Monitor Failed Upscale & Failed Again on 790601 & 02.Caused by Failure of GM-tube in Sensor Conventor Unit.Tube Finally Replaced W/Amperex 18529 | /03L-0 on 790514:2A Fuel Pool Radiation Monitor Failed Upscale & Failed Again on 790601 & 02.Caused by Failure of GM-tube in Sensor Conventor Unit.Tube Finally Replaced W/Amperex 18529 | | | 05000254/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000254/LER-1979-011-03, /03L-0 on 790202:drywell Vent Valve AO 1-1601-23 Closed in Excess of Tech Spec Max Time Limit.Caused by Worn & Leaking Seals on Air Operating pistons.U-cup Piston Seals Replaced | /03L-0 on 790202:drywell Vent Valve AO 1-1601-23 Closed in Excess of Tech Spec Max Time Limit.Caused by Worn & Leaking Seals on Air Operating pistons.U-cup Piston Seals Replaced | | | 05000265/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000265/LER-1979-011-03, /03L-0 on 790521:three Cables Not Installed in Accordance W/Drawings.Caused by Error in Cable Routing During Initial Const.Reroute of Cables Will Take Place During Nov 1979 Refueling Outage | /03L-0 on 790521:three Cables Not Installed in Accordance W/Drawings.Caused by Error in Cable Routing During Initial Const.Reroute of Cables Will Take Place During Nov 1979 Refueling Outage | | | 05000265/LER-1979-012-03, /03L-0 on 790622:nut Inadvertantly Droppoed Into Diesel Generator Winding During Preventive Maint.Outage Time of Generator Extended 20 Minutes Beyond 1.5-h Time Limit. Caused by Personnel Error | /03L-0 on 790622:nut Inadvertantly Droppoed Into Diesel Generator Winding During Preventive Maint.Outage Time of Generator Extended 20 Minutes Beyond 1.5-h Time Limit. Caused by Personnel Error | | | 05000265/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000254/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000254/LER-1979-012-03, /03L-0 on 790214:air Found Blowing Through Weld on 3/4 Inch Vent Line.Caused by Component Failure.Vent Line Inserted Into Sockolet & re-welded | /03L-0 on 790214:air Found Blowing Through Weld on 3/4 Inch Vent Line.Caused by Component Failure.Vent Line Inserted Into Sockolet & re-welded | | | 05000254/LER-1979-013-03, /03L-0 on 790217:check Valves 1-263-2-31B & 1-263-42A Failed to Check Flow Through Instrument Lines. Caused by Dirt in Valve Internals.Internals Removed,Cleaned & Reassembled | /03L-0 on 790217:check Valves 1-263-2-31B & 1-263-42A Failed to Check Flow Through Instrument Lines. Caused by Dirt in Valve Internals.Internals Removed,Cleaned & Reassembled | | | 05000254/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000265/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000265/LER-1979-013-03, /031-0 on 790712:while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for Pump Suction Valve 1C RHR Tripped & Could Not Be Reopened.Caused by Loose Electrical Connections at Breaker | /031-0 on 790712:while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for Pump Suction Valve 1C RHR Tripped & Could Not Be Reopened.Caused by Loose Electrical Connections at Breaker | | | 05000254/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000265/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000265/LER-1979-014-03, /031-0 on 790723:steam Inlet Valve Mo 2-1301-16 Failed to Close During Reactor Core Isolation Cooling Monthly Valve Operability Test.Caused by Component Failure of Torque Switch on Valve Mo 2-1301-16.Switch Replaced | /031-0 on 790723:steam Inlet Valve Mo 2-1301-16 Failed to Close During Reactor Core Isolation Cooling Monthly Valve Operability Test.Caused by Component Failure of Torque Switch on Valve Mo 2-1301-16.Switch Replaced | | | 05000254/LER-1979-014-03, /03L-0 on 790214:automatic Blowdown Timers Exceeded Tech Spec Limits During Tests.Caused by Instrument Setpoint Drift.One Timer Readjusted,Another Replaced | /03L-0 on 790214:automatic Blowdown Timers Exceeded Tech Spec Limits During Tests.Caused by Instrument Setpoint Drift.One Timer Readjusted,Another Replaced | |
|