LER-1978-036, /04T-0 on 781212:discharge of Floor Drain Sample Tank Was Made W/O Effluent Monitoring Required by Tech Specs,Because Flushing Valve of Radwaste Effluent Monitor Was Inadvertently Left Open |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2981978036R04 - NRC Website |
|
text
NRC F oRM 366 U. S. NUCLEAR REGULATORY COMMISSION 11J7)
LICENSEE EVENT REPORT CONTROL BLOCK: l l
l l
l l
l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6
lo lil h IE lC lp lR l1 lhh b l-l0l0l0l0l-l0 0l0l@l4l1l1l1l1 @l l
l@
7 8 9 ulCENSEE C00s *
'14
/
26 LICENSE TYPE JO 5 7 C A T $8 CON'T lolil
%"RM lt l@l0ls101010l2I9l8 hl1 l? l1 l?l7 lR hl1 l? l1 1 5l7 lo h I
8 60 61 DOCK ET NUV8 E R tA 63 EVENT DATE 14 73 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l o l 2 l l Discharge of the floor drain sample tank without adequate effluent nOnitorine as re-g g 9 quired by Section 2.4.1.b.3.a and b of the CNS Environmental Technical Specifications.l g,
,A flushing valve of the radwaste effluent monitor was inadvertently left open. A l
g g
- sample of the tank had been taken and analyzed prior to discharge. A similar event
[ o 16 l l was reported on November 10, 1976 under report number 50-298-76-46 and October 20.
I l1975.
l o
i 0
8 l
SYSTEM
CAUSE
C AUS E COMP.
VALVE CODE CODE SUSCODE COVPONENT CODE SUBCODE SUBCODE m
IMIC l@ W@
n @ l z l zl z l z [ z l z l@ Lz_J@ L1J @
7 8
9 to 11 12 13 18 la 20 SEQUENTlxL OCCURRENCE REPORT REVISION LE R RO EVENT YE AR REPORT NO.
CODE TYPE N O.
@ gE g l21 7l 8l l_[
[ 0l 3l 6 y
l0l4l W
[--J [0_]
22 23 24 26 2'
N N
3J 31 32 TAK N A TO O PLANT ETH HOURS 22 SB IT D FOR dL B.
SUPPLIE MANLF AC URER lH lgl34 zl@
l zl@
[ zl@
l 0l 0l 0l 0l W@
lN Q lzl@
z l 9 l 9 l 9 l@
33 35 36 3/
40 di 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i
o l Operator failed to secure the flush of the liquid radwaste effluent ronitor prior en I
discharge of the floor drain sample tar.
Occurrence discussed with the operator I
,,,,y involved and Environmental Event Report will be routed to all Operations personnel.
l l i l 31 l 11 141 1 80 7
8 9 ST S
% POWER oTHE R ST A TUS ISCO RY OISCOVERY OESCPiPTION 0 lgl N/A W hl Onorarnr 0%nrvnrinn l
E lg l 1 0
i 5
AC TIVI T Y CO TENT RE LE ASE D OF RELE ASE AVOUNT OF ACTIVITY LOC ATION OF RELEASE 3
I 1
8 9 to _
1.48 X 10 mc1 l
l nicch,ren c,n,1 y @ [_pj @ l i
6 11 44 45 80 PE RSONNE L E XPO5URE S NUV8ER TYPE D E SC RIPTION U7 1010 101@Lz_J@l N/A I
PE R SON N d',N;u'a', E S NUY9ER
DESCRIPTION
li la l l0 010 l@l N/A l
7 8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY TYPE DE SCRIP TION v
[ h!
N/A l
i 9 7
b 9 10 80 8
ISSU E D DE SCRIPTION x 44 L _ Nja m I
llllllI11IIl,;
2 o E U 13ff 80g es 69 7
NAYE OF PREPARER M. G. Williams PHONE:
6 09-A M-1R11 g
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000298/LER-1978-029-03, /03L-0:on 780814,core Spray Time Delay Relay Did Not Operate within Required Time Frame.Caused by Type of Relay Used & Inactivity After Repairs.Design Change Will Be Prepared to Replace Relay | /03L-0:on 780814,core Spray Time Delay Relay Did Not Operate within Required Time Frame.Caused by Type of Relay Used & Inactivity After Repairs.Design Change Will Be Prepared to Replace Relay | | | 05000298/LER-1978-029, Forwards LER 78-029/03L-0 | Forwards LER 78-029/03L-0 | | | 05000298/LER-1978-030-03, /03L-0:on 780815,13 Primary Containment Penetrations Not Leak Tested.Caused by Penetrations Not Identified During Preoperational Testing.Penetrations Will Be Added to Tech Spec Table 3.7.2 & Will Be Tested | /03L-0:on 780815,13 Primary Containment Penetrations Not Leak Tested.Caused by Penetrations Not Identified During Preoperational Testing.Penetrations Will Be Added to Tech Spec Table 3.7.2 & Will Be Tested | | | 05000298/LER-1978-030, Forwards LER 78-030/03L-0 | Forwards LER 78-030/03L-0 | | | 05000298/LER-1978-031-03, /03L-0 on 780912:Cooper-Bessemer Diesel Engine Type KSV-16-T Main Bearing Overheated.Main Bearing 10 Was Damaged Due to Minimal Oil Flow During Engine Coastdown. Caused by Foreign Particles in Oil | /03L-0 on 780912:Cooper-Bessemer Diesel Engine Type KSV-16-T Main Bearing Overheated.Main Bearing 10 Was Damaged Due to Minimal Oil Flow During Engine Coastdown. Caused by Foreign Particles in Oil | | | 05000298/LER-1978-031, Forwards LER 78-031/03L-0 | Forwards LER 78-031/03L-0 | | | 05000298/LER-1978-032, Forwards LER 78-032/03L-0 | Forwards LER 78-032/03L-0 | | | 05000298/LER-1978-032-03, /03L-0 on 780918:during Normal Oper,After Cooling Down the Torus,Rhr Heat Exchanger 1B Bypass RHR-MO-66B Failed to Oper,Due to Loose Set Screw on Yoke of Limiterque SMB-3 Operator | /03L-0 on 780918:during Normal Oper,After Cooling Down the Torus,Rhr Heat Exchanger 1B Bypass RHR-MO-66B Failed to Oper,Due to Loose Set Screw on Yoke of Limiterque SMB-3 Operator | | | 05000298/LER-1978-033, Forwards LER 78-033/03L-0 | Forwards LER 78-033/03L-0 | | | 05000298/LER-1978-033-03, /03L-0 on 781016:cable HP58,Div 1,was Found Routed Thru Div 11 Riser Under Panel 9-3.Caused by Personnel Error During Constr.Redundant Sys Were Operable | /03L-0 on 781016:cable HP58,Div 1,was Found Routed Thru Div 11 Riser Under Panel 9-3.Caused by Personnel Error During Constr.Redundant Sys Were Operable | | | 05000298/LER-1978-034-03, /03L-0 on 781111:during S.P.6.4.1.2. (Withdrawn Control Rod Operability), Control Rod 30-31 Was Found Uncoupled from Its Control Rod Drive. Cause Cannot Be Determined Until Control Rod Drive Is Removed & Examined | /03L-0 on 781111:during S.P.6.4.1.2. (Withdrawn Control Rod Operability), Control Rod 30-31 Was Found Uncoupled from Its Control Rod Drive. Cause Cannot Be Determined Until Control Rod Drive Is Removed & Examined | | | 05000298/LER-1978-034, Forwards LER 78-034/03L-0 | Forwards LER 78-034/03L-0 | | | 05000298/LER-1978-035-01, /01T-0 on 781124:while Checking RR MG Set 1B Speed control,1 Amp fuse(F2) in Drive Amplifier Circuit Was Pulled Out & Checked.Caused Rapid Increase in Pwr Level,Tripping RR MG Set 1B | /01T-0 on 781124:while Checking RR MG Set 1B Speed control,1 Amp fuse(F2) in Drive Amplifier Circuit Was Pulled Out & Checked.Caused Rapid Increase in Pwr Level,Tripping RR MG Set 1B | | | 05000298/LER-1978-035, Forwards LER 78-035/01T-0 | Forwards LER 78-035/01T-0 | | | 05000298/LER-1978-036, Forwards LER 78-036/04T-0 | Forwards LER 78-036/04T-0 | | | 05000298/LER-1978-036-04, /04T-0 on 781212:discharge of Floor Drain Sample Tank Was Made W/O Effluent Monitoring Required by Tech Specs,Because Flushing Valve of Radwaste Effluent Monitor Was Inadvertently Left Open | /04T-0 on 781212:discharge of Floor Drain Sample Tank Was Made W/O Effluent Monitoring Required by Tech Specs,Because Flushing Valve of Radwaste Effluent Monitor Was Inadvertently Left Open | | | 05000298/LER-1978-037, Forwards LER 78-037/03L-0 | Forwards LER 78-037/03L-0 | | | 05000298/LER-1978-037-03, /03L-0 on 781201:during Normal Operation,Pressure Recorder PC-PR-512A Was Found Reading Full Scale & Declared Inoperable.Cause Was Isolated to a Bad Amplifier Circuit Board | /03L-0 on 781201:during Normal Operation,Pressure Recorder PC-PR-512A Was Found Reading Full Scale & Declared Inoperable.Cause Was Isolated to a Bad Amplifier Circuit Board | | | 05000298/LER-1978-038-03, /03L-0 on 781208:during Normal Operation,One Struthers Wells Cross Connect Valve Failed to Open During Surveillance Procedure.Caused by Mfg Error | /03L-0 on 781208:during Normal Operation,One Struthers Wells Cross Connect Valve Failed to Open During Surveillance Procedure.Caused by Mfg Error | | | 05000298/LER-1978-038, Forwards LER 78-038/03L-0 | Forwards LER 78-038/03L-0 | | | 05000298/LER-1978-039-03, /03L-0 on 781206:while Performing Surveillance Test After No 1 Diesel Generator Was Out of Svc for Maint,Diesel Engine Failed to Reach Full Speed.Caused by Reduced Air Pressure | /03L-0 on 781206:while Performing Surveillance Test After No 1 Diesel Generator Was Out of Svc for Maint,Diesel Engine Failed to Reach Full Speed.Caused by Reduced Air Pressure | | | 05000298/LER-1978-039, Forwards LER 78-039/03L-0 | Forwards LER 78-039/03L-0 | | | 05000298/LER-1978-040-03, /03L-0 on 781227:during Normal Operation,While Doing Special Test of Drywell Purging Techniques,Primary Containment Vent Valve PC-246AV Leaked Excessively & Was Inoperable Due to Incomplete Valve Closure.Valve Replaced | /03L-0 on 781227:during Normal Operation,While Doing Special Test of Drywell Purging Techniques,Primary Containment Vent Valve PC-246AV Leaked Excessively & Was Inoperable Due to Incomplete Valve Closure.Valve Replaced | |
|