ML19282C563

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Util Determined Certain stem-mounted Limit Switches on safety-related Valves May Not Be Suitable for Svc in LOCA Containment.Forwards List of Specific Switch Types & Valves on Which Switches Are Installed
ML19282C563
Person / Time
Site: Millstone Dominion icon.png
Issue date: 03/23/1979
From: Counsil W
NORTHEAST UTILITIES
To: Reid R
Office of Nuclear Reactor Regulation
References
TAC-46174, NUDOCS 7903300339
Download: ML19282C563 (2)


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;'"=;02"l l=l March 23,1979 Docket No. 50-336 Director of Nuclear Reactor Regulation Attn

Mr. R. Reid, Chief Operating Reactors Branch #4 U. S. Nuclear Regulatory Commission Washington, D. C.

20555 Refe ance:

(1)

B. H. Grier letter to W. G. Counsil dated February 8,1979, forwarding I&E Bulletin 79-01.

Gentlemen:

Millstone Nuclear Power Station, Unit No. 2 I&E Bulletin 79-01 Environmental Qualification of Class lE Equipment In accordance with the reporting requirements of Reference (1), Northeast Nuclear Energy Company (NNECO) is advising the NRC Staff that it has been determined that certain stem-mounted limit switches (SMLS) on safety-related valves in the Millstone Unit No. 2 containment may not be suitable for service in the LOCA environment.

A list of the specitic SMLS types and the valves on which they are installed is attached. Discussions with the manufacturer and evaluations by NNECO and NUSCO have revealed that environmental qualification documentation for the SMLS's identified on the attached page cannot be produced. Further investi-gations are in progress to ascertain the currently qualified capability of these components.

NNECO will address specific corrective actions and a schedule for completion in the detailed written report which will follow in 14 days in accordance with the Reference (1) request. Millstone Unit No. 2 is currently in its second refueling outage and is scheduled to start Cycle 3 operation in May, 1979.

Therefore, justification for continued operation is not applicabic.

Very truly yours, NORTHEAST NUCLEAR ENERGY 0MPANY 7

/

/

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0h0lA W. G. Counsil Vice President Attachment 790330033%

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STEM-M0UNTED LIMIT SWITCHES r

VALVE L.S. TYPE QUAN.

RC-001 HV-1064 (SL3C-82) 2 RC-002 HV-1062 (SL3C-B2) 2 RC-003 HV-1060 (SL3C-B2) 2 CH-506 (SL3C-B2) 2 SSP-16 1 HV-9151 (SL3C-B2) 2 LRR-43 1 HV-9015 (SL3C-B2) 2 GR-ll-1 HV-9125 (SL3C-B2) 2 CH-515 EA170-11302 2

CH-516 EA170-11302 2

CH-517 D-2400X 2

CH-518 EA170-11302 2

CH-519 EA170-11302 2

SI-614 EA700-20,000 1

SI-624 EA700-20,000 1

SI-634 EA700-20,000 1

SI-644 EA700-20,000 1

SI-618 D-2400X 2

SI-628 D-2400X 2

SI-638 D-2400X 2

SI-648 D-2400X 2

SI-651 D-2400X 2

SI-652 D-2400X 2

AC-5 HV-8082 EA170-3202 2

AC-6 HV-8125 EA170-3202 2

EB-91 HV-8380 EA740-50,000 2

EA740-60,000 1

EB-100 HV-8378 EA740-50,000 2

EA740-60,000 1