05000321/LER-1979-018-03, /03L-0 on 790310:plant Svc Water Not Valved in to 1B Diesel Generator.Caused by Plant Svc Water Maint Procedure HNP-2-6200 Not Specifying Correct Valve Alignment. Temporary Procedure Change Made

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/03L-0 on 790310:plant Svc Water Not Valved in to 1B Diesel Generator.Caused by Plant Svc Water Maint Procedure HNP-2-6200 Not Specifying Correct Valve Alignment. Temporary Procedure Change Made
ML19282C520
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 03/23/1979
From: Baxley S
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19282C516 List:
References
LER-79-018-03L, LER-79-18-3L, NUDOCS 7903300274
Download: ML19282C520 (1)


LER-1979-018, /03L-0 on 790310:plant Svc Water Not Valved in to 1B Diesel Generator.Caused by Plant Svc Water Maint Procedure HNP-2-6200 Not Specifying Correct Valve Alignment. Temporary Procedure Change Made
Event date:
Report date:
3211979018R03 - NRC Website

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Ri#CRT D. ATE EQ EVENT DESCRIPTION AND FROB ASLE CONSEQUENCES h o 2i l Durina normal oneration of Unit 1. at 1100 CST it was discovered that Plant Service I

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4 Surveillance was in prooress per Tech. Specs. 4.5.J.2. A when at 1100 CST the Standby I

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Service Water pump was returned to coerable status.

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