LER-1979-004, /03L-0 on 790211:suction Isolation Valve Mo 2-1001-50 Failed to Close from Control Room.Caused by Failed Circuit Breaker in Valve Motor Control Center. Valve Taken Out of Svc for Repair During Outages |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2651979004R03 - NRC Website |
|
text
o -
u-c CONTi10t. ULOCK- (
l l
l l
l lh
. (P. :ASE PRlr.T OR TYPE ALL REQUIRCD INFORMNilON)
I ti iTTil I il L I o I ^ l o i 2 Igi O ! O i 01-101010l-10 10 10 I@[4lilililiI@l l
Ig 8 9 LICEN3EE COCL 14 15 LICENSE NUVtiER 25 26 LICENSE 1YPE J3 b7CATb0 "oN'T m
4 3c.nlA 7 l 9_.h M.
-$ I Li@l0l5!0 I0 10 I2 b 5 bl 012 ! 1 I 1 I 7 l 9 h nl I
I
~ m
..a u
_:m
~
E '. '
2'.
'T' 37; nAOLE~ """ ~ ' ':; g
-! L While the shutdown coolino mode of RHRS was being taken off. suct'nn i nnlation I
J!
valve MO 2-1001-50 failed to clo_se from the control room.
The safety implications i
m _0 2-1001-47J 9 L of this occurrence are minimal due to the fact the second isolation _ valve M
- -- 1 ;
in the shutdown cooling line is fully operable.
Bacause the requirements _of j
,; g Technical Specification 3 7.D.3 have been met, reactor power operation will be 1
continued.
[
' l __.
__ Ja a3 c6 cc..e
- < S7" Cur
C' Ci "L.:,.E CC ":;NE' ? CC CI c.3C-Q-h !A'C Z g I S ' O ' h dj h I A!b I V'A I L'V 0 P i
3 m
m m
3 m
- Ecfic'iTI AL
- CCu * ' '.%E ntP* R T M PT D g i m po
- VEN T YE 2 A REFOe4T NO.
.C0e Tv*E 4C.
OU Pig
!7 l9 l l-l l0 l0 l4 l l/l l0 l3 l lL l i- _j l0 l u
_ 21 21 23 24 26 21 28 23 JO 31 32 AC11Cl4 FUTUHE EFFECT SHUT DOWN ATTACHVENT APRO 4 FRlY2 COMP.
CC' tPONE N T TAKEf4 ACTION ON PL ANT METHOD HOURS SUBMITTED FOHM bvH.
SUPPU ER MANUFACTURER Wgl34B [g l Z lg Zl@
l 0l 0l 0 l
lY lg lY lg lNl@
lLl2 l0 [0 [g 33 3
36 3
40 41 42 43 44 47 CAUSE DESCRIPTION AND COR'1ECTIVE ACTIONS l, j o j l An initial investigation indicated a component failure of the circuit breaker in l
the valve's motor control center.
The MO 2-1001-50 valve was electrically taken l
l,y,yl
~
out-of-service, closing the valve.
During an outage when the valve can be appropriately
,,y operated and tested, the necessary repairs will be made.
,, y 1
4 80 7
8 9 F ACILITY METHOD OF STATUS
% POWER OTHER STATUS DISCOVEHY DISCOVEHY DESCniPTicN l
NA l
lAlh!
Ope ra t iona l Event Ic l @ 10 10 10 l@l li s
7 8 9 to 12 13 44 45 46 80 ACTIVI TY CONTENT FIELE AsEn OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RELEASE NA l
HA l
W @ Zlgl li c
7 b 9 10 13 44 45 60 PERSONNEL EXPOSUPES [tjij j 0 ] 0 [ 0 l@l ZTYPL @lDESCTil* TION l
NUMBER NA 7
J 9 11 17 13 60 PE nSONNE L INJURIE S NuYHE R DE5CHiPilON NA' l
13 ; [0l0l0lgl 00 7
8 9 11 12 L OSS OF OR C A'.' A GE TO F ACILIT Y TY E Oc CC HIP IIGN
"^
TITl L_J81 60 T
15 3 10
'7 9 0 3 2 9 0 0 M '
7171 b 8)lCRiPT.ON@
- - NA nnC usc onty tl; m
o l
lllllllll [
CB 63 E0*.
a 8 9 to G. Tietz 309-654-2241, ext. 247 NAYF Cr PHEPANEn rHONE-
/
l.
LEL NUMBER:
LER/R0 79-04/03L-0 11.
LICENSEE NAME: Commonwealth Edison Company Quad-Cities Nuclear Power Station Ill.
FACILITY NAME: Unit Two IV.
DOCKET NUMBER: 050-265 V.
EVENT DESCRIPTION
On February 11, 1979, Unit Two was i ; the REFUEL mode and the shutdown cooling mode of RHRS was operating.
At 10: 30 a.m.,
the control room operator was taking shutdown cooling off when he discovered that the suction valve, M0 2-1001-50, would not close from the control room. Upon notifying the Shift Engineer, it was decided to take the valve out-of-service by tripping the breaker and thus closing the valve.
The second isolation valve, M0 2-1001-47 was also closed.
There has been no previous occurrences of this nature irvolving the M0 2-1001-50 valve.
VI.
PROBABLE CONSEQUENCES OF THE OCCURRENCE:
The safety implications of this occurrence are minimal due to the fact the second Isolation valve, M0 2-1001-47, in the shutdown cooling suctic, line was fully operable at all times.
Therefore, had a Group 11 isolation signal occurred the 47 valve would have isolated the line.
Vll.
CAUSE
The initial investigation indicated that equipment failure was the probable cause of this occurrence.
A contact in the valve breaker was not operating properly.
During a future maintenance outage, a full investigation of the problem and the necessary repairs will be completed.
Vill.
CORRECTIVE ACTION
The immediate corrective action was to take the valve out-of-service electrically, closing it.
During a maintenance outage, when the valve can be appropriately operateJ and tested, the necessary repairs will be completed.
Until that t ime, p ri ma ry containment isolation is assured by the closure of M0-2-1001-50, and the operabili ty of valve M0-2-1001-47
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000265/LER-1979-001-03, /03L-0 on 790104:during Monthly Operability Test, Inlet Air Heater on a Standby Gas Treatment Sys Was Found Inoperable.Caused by Setpoint Drift of Flow Switch 1/2-7541-8A | /03L-0 on 790104:during Monthly Operability Test, Inlet Air Heater on a Standby Gas Treatment Sys Was Found Inoperable.Caused by Setpoint Drift of Flow Switch 1/2-7541-8A | | | 05000254/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000265/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000254/LER-1979-001-03, /03L-0 on 790107:high Steam Line Flow Alarm & Automatic Isolation of Reactor Core Isolation Cooling Steam Supply Line Occurred.Caused by Failure of Micro Switch Inside Steam Line High Flow Differential Pressure Switch | /03L-0 on 790107:high Steam Line Flow Alarm & Automatic Isolation of Reactor Core Isolation Cooling Steam Supply Line Occurred.Caused by Failure of Micro Switch Inside Steam Line High Flow Differential Pressure Switch | | | 05000265/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000265/LER-1979-002-03, /03L-0 on 790110:during Routine Insp of Reactor Water Cleanup Pump Rooms,Small Leak Was Found on 2-1205B Cleanup Pump Suction Line.Cause Unknown.Leak Was Isolated & Linear Indication on Flange Ground Out | /03L-0 on 790110:during Routine Insp of Reactor Water Cleanup Pump Rooms,Small Leak Was Found on 2-1205B Cleanup Pump Suction Line.Cause Unknown.Leak Was Isolated & Linear Indication on Flange Ground Out | | | 05000254/LER-1979-002-03, /03L-0 on 790110:during Freon Test,Noted That Freon Penetration Through Charcoal Absorbers Exceeded Tech Spec Max.Caused by One of Charcoal Clamping Levers Not Being Fully Latched | /03L-0 on 790110:during Freon Test,Noted That Freon Penetration Through Charcoal Absorbers Exceeded Tech Spec Max.Caused by One of Charcoal Clamping Levers Not Being Fully Latched | | | 05000254/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000265/LER-1979-003-03, /03L-0 on 790214:during High Temp Isolation Calibr Procedure,Temp Switch TS 2-2373A Was Found to Trip in Excess of Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibrated & Retested | /03L-0 on 790214:during High Temp Isolation Calibr Procedure,Temp Switch TS 2-2373A Was Found to Trip in Excess of Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibrated & Retested | | | 05000254/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000265/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000254/LER-1979-003-03, /03L-1 on 790119:MSIV Local Leak Rate Showed Seven Valves Leaking Excessively.Causes Unspecified.Valve Stroke Adjusted,Certain Valves Dismantled,Discs & Seats Were Lapped & Machined | /03L-1 on 790119:MSIV Local Leak Rate Showed Seven Valves Leaking Excessively.Causes Unspecified.Valve Stroke Adjusted,Certain Valves Dismantled,Discs & Seats Were Lapped & Machined | | | 05000254/LER-1979-004, Forwards LER 79-004/01T-0 | Forwards LER 79-004/01T-0 | | | 05000254/LER-1979-004-01, /01T-0 on 790122:piece of Control Rod Drive Return Nozzle Thermal Sleeve Retaining Ring Was Missing.Cause Unknown | /01T-0 on 790122:piece of Control Rod Drive Return Nozzle Thermal Sleeve Retaining Ring Was Missing.Cause Unknown | | | 05000265/LER-1979-004-03, /03L-0 on 790211:suction Isolation Valve Mo 2-1001-50 Failed to Close from Control Room.Caused by Failed Circuit Breaker in Valve Motor Control Center. Valve Taken Out of Svc for Repair During Outages | /03L-0 on 790211:suction Isolation Valve Mo 2-1001-50 Failed to Close from Control Room.Caused by Failed Circuit Breaker in Valve Motor Control Center. Valve Taken Out of Svc for Repair During Outages | | | 05000265/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000254/LER-1979-005-03, /03L-0 on 790123:during Unit 1/2 Diesel Generator Monthly Load Test Qos 6600-1,pilot Solenoid Valve to Air Starting Motors Failed & Unit 1/2 Diesel Was Shutdown. Caused by Mechanical Failure of Valve.Valve Was Replaced | /03L-0 on 790123:during Unit 1/2 Diesel Generator Monthly Load Test Qos 6600-1,pilot Solenoid Valve to Air Starting Motors Failed & Unit 1/2 Diesel Was Shutdown. Caused by Mechanical Failure of Valve.Valve Was Replaced | | | 05000254/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000265/LER-1979-005-03, /03L-0 on 790223:2A Recirculation Motor Generator Field Breaker Opened,Causing Flow Mismatch.Caused by Loosening of Coupling Between Main Shaft & Recirculation Motor Generator Set Tachometer.Tachometer Coupling Reset | /03L-0 on 790223:2A Recirculation Motor Generator Field Breaker Opened,Causing Flow Mismatch.Caused by Loosening of Coupling Between Main Shaft & Recirculation Motor Generator Set Tachometer.Tachometer Coupling Reset | | | 05000265/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000254/LER-1979-006-03, /03L-0 on 790125:during Primary Containment Isolation Valve Closure Timing,Valve AO 1-1601-21 Failed to Close in 10 Seconds.Caused by Improper Adjustment of Valve Speed Control from Operational Wear.Control Was Readjusted | /03L-0 on 790125:during Primary Containment Isolation Valve Closure Timing,Valve AO 1-1601-21 Failed to Close in 10 Seconds.Caused by Improper Adjustment of Valve Speed Control from Operational Wear.Control Was Readjusted | | | 05000254/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000254/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000254/LER-1979-007-03, /03L-0 on 790201:main Steam Line Leak Detection Temp Switches TS 1-261-16A,MTS 1-261-18A & TS 1-261-15C Tripped in Excess of Setpoint.Caused by Instrument Setpoint Drift.Temp Switches Recalibrated | /03L-0 on 790201:main Steam Line Leak Detection Temp Switches TS 1-261-16A,MTS 1-261-18A & TS 1-261-15C Tripped in Excess of Setpoint.Caused by Instrument Setpoint Drift.Temp Switches Recalibrated | | | 05000254/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000254/LER-1979-008-03, /03L-0 on 790202:temp Switch TS-1-1360-15D Had Trip Setpoint in Excess of Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibrated & Satisfactorily Tested | /03L-0 on 790202:temp Switch TS-1-1360-15D Had Trip Setpoint in Excess of Tech Spec Limit.Caused by Setpoint Drift.Switch Recalibrated & Satisfactorily Tested | | | 05000254/LER-1979-009-03, /03L-0 on 790203:bed Plate Drain Valves AO 1-4999-57,58 & 60 Did Not Fully Close.Caused by Corrosion & Failure of Internal Return Springs.Springs Replaced & Valves Satisfactorily Retested | /03L-0 on 790203:bed Plate Drain Valves AO 1-4999-57,58 & 60 Did Not Fully Close.Caused by Corrosion & Failure of Internal Return Springs.Springs Replaced & Valves Satisfactorily Retested | | | 05000254/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000265/LER-1979-009, Forwards LER 79-009/03L-0.Corrects Docket Number of Original Forwarding Ltr | Forwards LER 79-009/03L-0.Corrects Docket Number of Original Forwarding Ltr | | | 05000265/LER-1979-009-03, /03L-0:on 790429,switch Trip Positions Found at Greater than 10% of MSIV Closure.Caused by Failure to Set Field Calibr for Switch Trip Point Limit.Switches Were Adjusted to 10% Closure or Less | /03L-0:on 790429,switch Trip Positions Found at Greater than 10% of MSIV Closure.Caused by Failure to Set Field Calibr for Switch Trip Point Limit.Switches Were Adjusted to 10% Closure or Less | | | 05000254/LER-1979-010-03, /03L-1 on 790205:diesel Fire Pump 1/2A Out of Svc Beyond Tech Spec Limit.Caused by Personnel Error.Pump Returned to Svc | /03L-1 on 790205:diesel Fire Pump 1/2A Out of Svc Beyond Tech Spec Limit.Caused by Personnel Error.Pump Returned to Svc | | | 05000254/LER-1979-010, Forwards LER 79-010/03L-1 | Forwards LER 79-010/03L-1 | | | 05000265/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000265/LER-1979-010-03, /03L-0 on 790514:2A Fuel Pool Radiation Monitor Failed Upscale & Failed Again on 790601 & 02.Caused by Failure of GM-tube in Sensor Conventor Unit.Tube Finally Replaced W/Amperex 18529 | /03L-0 on 790514:2A Fuel Pool Radiation Monitor Failed Upscale & Failed Again on 790601 & 02.Caused by Failure of GM-tube in Sensor Conventor Unit.Tube Finally Replaced W/Amperex 18529 | | | 05000254/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000254/LER-1979-011-03, /03L-0 on 790202:drywell Vent Valve AO 1-1601-23 Closed in Excess of Tech Spec Max Time Limit.Caused by Worn & Leaking Seals on Air Operating pistons.U-cup Piston Seals Replaced | /03L-0 on 790202:drywell Vent Valve AO 1-1601-23 Closed in Excess of Tech Spec Max Time Limit.Caused by Worn & Leaking Seals on Air Operating pistons.U-cup Piston Seals Replaced | | | 05000265/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000265/LER-1979-011-03, /03L-0 on 790521:three Cables Not Installed in Accordance W/Drawings.Caused by Error in Cable Routing During Initial Const.Reroute of Cables Will Take Place During Nov 1979 Refueling Outage | /03L-0 on 790521:three Cables Not Installed in Accordance W/Drawings.Caused by Error in Cable Routing During Initial Const.Reroute of Cables Will Take Place During Nov 1979 Refueling Outage | | | 05000265/LER-1979-012-03, /03L-0 on 790622:nut Inadvertantly Droppoed Into Diesel Generator Winding During Preventive Maint.Outage Time of Generator Extended 20 Minutes Beyond 1.5-h Time Limit. Caused by Personnel Error | /03L-0 on 790622:nut Inadvertantly Droppoed Into Diesel Generator Winding During Preventive Maint.Outage Time of Generator Extended 20 Minutes Beyond 1.5-h Time Limit. Caused by Personnel Error | | | 05000265/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000254/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000254/LER-1979-012-03, /03L-0 on 790214:air Found Blowing Through Weld on 3/4 Inch Vent Line.Caused by Component Failure.Vent Line Inserted Into Sockolet & re-welded | /03L-0 on 790214:air Found Blowing Through Weld on 3/4 Inch Vent Line.Caused by Component Failure.Vent Line Inserted Into Sockolet & re-welded | | | 05000254/LER-1979-013-03, /03L-0 on 790217:check Valves 1-263-2-31B & 1-263-42A Failed to Check Flow Through Instrument Lines. Caused by Dirt in Valve Internals.Internals Removed,Cleaned & Reassembled | /03L-0 on 790217:check Valves 1-263-2-31B & 1-263-42A Failed to Check Flow Through Instrument Lines. Caused by Dirt in Valve Internals.Internals Removed,Cleaned & Reassembled | | | 05000254/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000265/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000265/LER-1979-013-03, /031-0 on 790712:while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for Pump Suction Valve 1C RHR Tripped & Could Not Be Reopened.Caused by Loose Electrical Connections at Breaker | /031-0 on 790712:while Performing Motor Operated Valve Operability Test,Thermal Overload Relay for Pump Suction Valve 1C RHR Tripped & Could Not Be Reopened.Caused by Loose Electrical Connections at Breaker | | | 05000254/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000265/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000265/LER-1979-014-03, /031-0 on 790723:steam Inlet Valve Mo 2-1301-16 Failed to Close During Reactor Core Isolation Cooling Monthly Valve Operability Test.Caused by Component Failure of Torque Switch on Valve Mo 2-1301-16.Switch Replaced | /031-0 on 790723:steam Inlet Valve Mo 2-1301-16 Failed to Close During Reactor Core Isolation Cooling Monthly Valve Operability Test.Caused by Component Failure of Torque Switch on Valve Mo 2-1301-16.Switch Replaced | | | 05000254/LER-1979-014-03, /03L-0 on 790214:automatic Blowdown Timers Exceeded Tech Spec Limits During Tests.Caused by Instrument Setpoint Drift.One Timer Readjusted,Another Replaced | /03L-0 on 790214:automatic Blowdown Timers Exceeded Tech Spec Limits During Tests.Caused by Instrument Setpoint Drift.One Timer Readjusted,Another Replaced | |
|