05000298/LER-1979-009-03, /03L-0 on 790430:four Penetrations Found Leaking Excessively During Local Leak Rate Test.Caused by Defects in Limitorque Operator Torque Switch,Seal Rings & Check Valves. All Defects Repaired

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/03L-0 on 790430:four Penetrations Found Leaking Excessively During Local Leak Rate Test.Caused by Defects in Limitorque Operator Torque Switch,Seal Rings & Check Valves. All Defects Repaired
ML19274F048
Person / Time
Site: Cooper Entergy icon.png
Issue date: 05/22/1979
From: Phillips D
NEBRASKA PUBLIC POWER DISTRICT
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19274F047 List:
References
LER-79-009-03L, LER-79-9-3L, NUDOCS 7906080256
Download: ML19274F048 (1)


LER-1979-009, /03L-0 on 790430:four Penetrations Found Leaking Excessively During Local Leak Rate Test.Caused by Defects in Limitorque Operator Torque Switch,Seal Rings & Check Valves. All Defects Repaired
Event date:
Report date:
2981979009R03 - NRC Website

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8 60 61 COCKET NUMB EM 68 69 EVENT DATE 74 75 REPORT OATE 80 EVENT OESCRIPTION AND PROBA8LE CONSEQUENCES h o

2 Phile performing local leak rate test procedure 6.3.1.1.

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i Limitoroue operator torcue switch. two were 24" Allia N 1-a-a h m en-

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