05000321/LER-1979-009-03, /03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line

From kanterella
(Redirected from ML19270F542)
Jump to navigation Jump to search
/03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line
ML19270F542
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 02/07/1979
From: Rogers W
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19270F540 List:
References
LER-79-009-03L, LER-79-9-3L, NUDOCS 7902150412
Download: ML19270F542 (1)


LER-1979-009, /03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line
Event date:
Report date:
3211979009R03 - NRC Website

text

...

LICENSEE EVENT REPORT CoS %cl BLCCK: l l

l l }

l l

(PLEASE PRINT OR TYPE ALL REOUinED INFORMATION) l 6

l Gl Al El Il HI 1l@! 0 l 0 Ol 010l 0 0l0l0l0l0j@l4 1l1l1l1 @l l

l@

e i

14 15 LICENSE NUYUER 25 26 LIC E *.SE T YPE J3 Si CAT Ld 8 9 LIC E '.S E E. CC G E,

con'T 3%,"c,' lL l@l 0l S l 0l 0 l 0 l 3l 21 1 @l 0 l 112 l 3 l 7 l 9 @l 01210 l 7 l 7 l 91@

o i

S tid til CCCKETNUV3EH (W

t,J kVENT DATE 74 h

REPCH T D A TE EJ EVENT DESCRIPTICN AND PROBAELE CONSECUENCES h o

2 1 Durinq norral operation, while oerformina unscheduled maintenance on both R'.lCU pumos, I o

3 I the laboratory p.

.unnel were unable to sample primary coolant as required by l

1 Technical Scecification 4.6.F.2.a.l. of cnce every 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> when the primary coolant 1

o o s I continuous conductivity monitor is out of service. The public health and safety l

das not affected by this event.

0 6

0l7 l l

0 18 l l

8 3 80 SYSTE" CAUS E

CAUSE

CCV8 VALVE CCCE CCCE SUGCCCE CCVPONENT CODE SUBCODE SueCOOE lP lB l@ lB l@ l Al@ l P l I l P l E1X l X l@ W@ y @

o 9

6 9

10 11 12 13 18 19 20 S E CU E NTI A L CCCURRENCE REPCHT REVISION LE i;q VENTYEAR REPCRT NO.

CODE WPE N O.

@ g".3,3 17 l 9 l l-l l 0IOf 9l l/l 1013 l lL l l-l 10l L2,

__n u

3, n

u n

u 26 n

n n'3 MYN cVRNT SunW lF l-@34[Aj@

l Z l@

l Z l@

l 0 l 0 l 0 @l 0 l

^WWFP 0%",t'u.

'"#4 Sir J 0'ifN"n'ER SOURS s

l Nl@

lNl@

lN l@

l X I 9 l 9 l 9 l@

33 Ob 26 31 40 4

42 43 44 47 CAUSE DESCRIPTION AND CORRECT!VE ACTIONS h Tf511 Before cerformina maintenance on the RWCU pumos, the 2 pumos were isolated from serge i which in turn isolated the continuous conductivity monitor sample line.

The redundanj i

i i samole line oroved to be stopped up.

Efforts were made to find a third sample point,;

i 2

i j 31 l without success.

A maintenance request has been written to unstop the redundant samp]e i

1 I line.

l 3 9 83 ST A

% POWER OTHER STATUS DISCov RY DISCCVERY DESCR'PTION W@ l 01619l@l NA l

l C l@l Personnel Observation l

i s

ACTIVtTY Cor TENT RELEASED OF RELE ASE AMOUNT OF ACTIVITY LCCATION OF RELEASE i ie LZJ @ LZJ@l "A

I I

NA I

8 3 13 It 44 45 83 PE A 'ONNEL EXFOSURES N U.V8 E R TYPE E,E SCRI P TIC N 1010101@l Z i@L_ __

  • l NA l

i P E R SON'. LINJUHIES NUveER CESCRIPTION f

10l010l@l M

I i

2 8 9 11 17 80 LOSS CF CH CAY AGE TO FACILITY l

TYPE C E sc;N8TtCN

[

[,7j@l NA I

t 3

d 3 13 80 E CmPr'CN

'SSUEf81 L1 NA I

IIllilillil'll 2

o g 3 to 63 63 83 E NAME OF PPEPARER PHONE:

I maa mem s t