05000289/LER-1978-006-03, /03L-0:on 780124,during Normal Operation,Reactor Coolant Sample Isolation Valve CA-V13 Failed to Close When Actuated by Remote Signal.Caused by Valve Stem Thread Wear. Containment Isolation Valve CA-V2 Closed

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/03L-0:on 780124,during Normal Operation,Reactor Coolant Sample Isolation Valve CA-V13 Failed to Close When Actuated by Remote Signal.Caused by Valve Stem Thread Wear. Containment Isolation Valve CA-V2 Closed
ML19261F257
Person / Time
Site: Crane 
Issue date: 02/21/1978
From: Stevens R
METROPOLITAN EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19261F255 List:
References
LER-78-006-03L, LER-78-6-3L, NUDOCS 7910250693
Download: ML19261F257 (1)


LER-1978-006, /03L-0:on 780124,during Normal Operation,Reactor Coolant Sample Isolation Valve CA-V13 Failed to Close When Actuated by Remote Signal.Caused by Valve Stem Thread Wear. Containment Isolation Valve CA-V2 Closed
Event date:
Report date:
2891978006R03 - NRC Website

text

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6 60 61 OOCKET NUMB ER 68 69 EV ENT C ATE 74 75 REPORT D ATE 80 EVENT DESCRIPTION ANO PROB ABLE CONSECUENCES h oi2 l During nor=al operation, RC Letdevn 3a=ple Isolation Valve CA-713 failed to close i

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l vhen actuated by a re=cte signal. The valve was being closed upon ec=pletic: cf the i l routine RC sa:pling. Sis event is reportable per Technical Specification 6.9.2.3(2).1 o

oi5 lContain=ent Isolaticn Valve CA-V2 was prc=ptly closed thus preventing m y threat to I

o,6 l the health a=d safety of the public. Similar Events: 77-28/3L.

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, ; sampling schedule has been medified to reduce valve cycling._The valve vill be over ;

l. auled during the 1978 refueli=g. Data: Maxi== diffe ential pressure : 2500 psi; j

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AS"4 A-132, F216; Tri=:

A-132, F6; Seats: Stellite,

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