05000289/LER-1978-019-03, /03L-0:on 780605,while Performing Procedure Sp 1303-5,control Fuse Opened & Valve RB-V-7 Did Not Operate.Caused by Failure of Voltage Spike Suppressor Across Coil of Auxiliary Relay,Causing Short Circuit

From kanterella
(Redirected from ML19261F189)
Jump to navigation Jump to search
/03L-0:on 780605,while Performing Procedure Sp 1303-5,control Fuse Opened & Valve RB-V-7 Did Not Operate.Caused by Failure of Voltage Spike Suppressor Across Coil of Auxiliary Relay,Causing Short Circuit
ML19261F189
Person / Time
Site: Crane Constellation icon.png
Issue date: 06/22/1978
From:
METROPOLITAN EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19261F187 List:
References
LER-78-019-03L, LER-78-19-3L, NUDOCS 7910250609
Download: ML19261F189 (1)


LER-1978-019, /03L-0:on 780605,while Performing Procedure Sp 1303-5,control Fuse Opened & Valve RB-V-7 Did Not Operate.Caused by Failure of Voltage Spike Suppressor Across Coil of Auxiliary Relay,Causing Short Circuit
Event date:
Report date:
2891978019R03 - NRC Website

text

m.

.,o LICCNSEE EVENT REPORT s

CO t:T C.

3 L OC K: l l

l l

l l

l (PLE ASE PRINT OR TYPE ALL REDVIRED INFORMATIONI I

t 0

0 l0

- l0 l 0 l@lh 1 l1 l1 l1 l@l l

l@

]lPlA[TlMj!l1 @]Ol0l-l0l0 E 9 Lit NSEE CODE 14

!b LICENSE NWSEM 23 2E LICENSE TYPE JJ 57 GAT 56 T

{

3 gay lLlgl0l5l0l0l0l2l6l9l@l0l6l0 5[7l8l@l0l6l2l2l7lSj@

a 8

60 61 OCCKET NUVBER 68 69 EV ENT D ATE 74 75 REPCRT CATE 80 EVENT DESCRIPTION A NO PRCB ABLE CONSECUENCES h D lWhile performing S? 1303-3.1 "Eeactor Building Coolan', and Isolaticn System Icgic j

The j

g l Channel & Cc=penent Test", the control fuse opened and F3-V-7 did not operate.

g Peactcr Eldg. Cooling System is a closed syste= inside the Eeactor 31dg. thus no 1

g l threat to the health and safety of the puolic existed for the short period of time

[

s] l the valve was out of service.

.:is eve t is reportable.per T.S. 6.9 2.3.(2) and i

g l represents a degraded mode under T.S. 3.6.6. LER 77-14 reported a similar event.

[

I OI 80 8 9 SYSTEM

CAUSE

CAUSE COMP.

VALVE COCE CODE SUBCODE COMPONENT CCDE SUSCODE SUSCCDE

@ l Xl@ { g A [g {@ l Alg lE lE l L l A j Y X

A

{

8 9

10 11 12 13 18 19 20 SE QUE NTI A L OCCURAENCE REPORT R EV f SiON LE A RO EVENT YE AR REPORT NO.

CODE TYPE N O.

@,aga; IvIal 1-1 nI, o

d in I,j Lg_j I-1 La_]

_.21 22 23 24 26 47 23 29 JO 31 32 ACTION. FUTURE EFFECT SHuTcOwN ATT ACHV ENT NPRO 4 PP'ME COYP.

COYPONENT TAKEN ACTION ON PLANT METHCD HOURS 22 SUBMITTED FORMbuB.

SUPPLIER MANUFACTURER 0

l ?T @

l !I lh I X h X l9 Io o'h lA l@l Zl@

[1)@

l Z lh l,0 l 0 l 0 33 34 35 36 3<

40 41 4;

43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h B I"'he valve failed due to a blev - fusa i- + % ner+ rn' r4 r, u d +.

a va' + qa 4 '.r a l

] Isur ressien (thv ectcr). acrcss the m47 oc-a v4'4o-v -a7e r hoA #e 4 7 aA -o + g I

] la short circuit. The thvrector was rerlaced and the valve fu-etic-ed as desi --ad.

I B 13e valve was retun.ed to full crerability within 2h heu s.

l I

5 80 e 9 METHOO CF F ACILITY STATUS

% POWER OTHER STATUS

  • DISCOVE RY DISCOVERY OESCRiPitCN

.a C Wh l0 lo l8 lhl Ti/A l3lhl Surveillance l

8

'l 10 12 11 44 45 46 80 A C Tiv t TY CCNTENT mELEASE3 CF RE LE ASE AMOUNT CF ACTIVITY LOCATION OF RELE ASE D 12 l @ L11@l tr /A I

I tt / A I

8 9 10 11 44 45 80 PERSCNNEL EXPOSURES

'n0I rh lli hGh {Qt! !i'L U!!!! 9'.i!ld l

NUv9E R Tv P ".

O E SC RIPTION

! O l 0 lhdhl

?I/A l

1 80 PERSCNNE L N tu iES NuvSER CESCR;PTION D i-1010 l@l ruA 8 3 11

'2 L As CF OR Da.v AGE TO FACILITY

=

l *

  • vPE CE SCRIPTICN B: I@I i

80 8 9 10 PUB L ICITY NRC USE ONLY 45 r:S;.,E D DE SC RIPTION l

Weekly ?IeVS 3elease l

llllllllll ll l 7910250[O7