Similar Documents at Hatch |
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LER-1979-104, /03L-0:on 791216,w/reactor in Shutdown Mode, Standby Diesel Svc Water Pump Motor 2P41-C002 Tripped.Caused by Mechanical Overload.Bolts Associated W/Pump Had Broken Loose Causing Misalignment of Pump Shaft.Pump Rebuilt |
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| 3211979104R03 - NRC Website |
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8 60 68 OOCKET NUYDER od 63 EVENT DATE 74 JS REPORT DATE 80 EVENT DESCRIPTION AND PROCABLE CONSEcuENCES h 10121 l With the reactor in the shutdown mode, while performinq procedure HNP-1-3301, Diesel I
- O l3l [. Generator Manual Start, 2P41-C002, Standby Diesel Service Water Pump, tripped.
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[ Technical Specification 3.5.J.2 was not reouired due to the plant being shutdown 1
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Public health and safety were not affected by this incident.
This l [O lc l l was not a repetitive occurrence.
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40 46 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l The cause of the 2P41-C00? motor trip was due to a mechanical overload.
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Georgia Pcwcr Company Plant E. I. Hatch Baxley, Georgia 31513 Reportable Occurrence Report No. 50-321/1979-104.
Cause Description and Corrective Actions (cont)
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have been caused by the misalignment of the pump shaft. The direct cause of the deterioration of bolts _ is not known at this time.
The deterioration, of the bolts, appears to have been caused by electrolysis. An analysis is ting made to determine the direct cause of deterioration. Aa update report will follow when an analysis is determined. The 2P41-C002 is a standby service water pump, shared by both units, and the only pump of its type at Plant Hatch.
The pump stages bolts, bowl bearings, lower seal ring and the pump shaft were replaced and the pump returned to service.
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NARRATIVE
REPORT Georgia Power Company Dhh D []@{ff
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Baxley, Georgia 31513 Reportable Occurrence Report No. 50-321/1979-104.
~ - On December 16, 1979, with the reactor in the shutdown node, the 2P41-C002, Standby Diesel Service Water Pump, motor tripped. 'The c.iuse of the motor
. tripping was due to a mechanical overload.
Upon investigation of the problem, it was discovered that a number of the bolts used to assemble the suction bell, internediate bowls and discharge case of the pump 1.'d deteriorated and broken loose causing misalignment of the pump shaft.
There was also evidence of wear to the seal rings, bowl bearings and the pump shaft.
The direct cause of the deterioration of the bolts is net known at this time.
The deterioration, of the bolts, appears to have been ceased by electrolysis.
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An analysis is being made to determine the cause of deterioration. The cause of wear to the pump shaf t, seal rings amd bowl bearings was due to pump shaft misalignment.
The pump was rebuilt, meeting all operating requirements and returned to service.
There are other pumps of a similar design located in the general area with this pump'.
There has not been a similar problem with any of these pumps.
This was not a repetitive occurrence. The 2P41-C002 is the standby service water pump, shared by both units, and the only pump of its type at the plant site.
A follow-up report will be submitted when the cause of the bolt deterioration is determined.
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| 05000366/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000366/LER-1979-001-03, /03L-0 on 781229:in Cold Shutdown While Performing HNP-2-3154,reactor Water Level Instrument Switch 1 Was Found Inoperative Due to Broken Foot, & Switch 3 Actuated at 122.2 in H2O Input | /03L-0 on 781229:in Cold Shutdown While Performing HNP-2-3154,reactor Water Level Instrument Switch 1 Was Found Inoperative Due to Broken Foot, & Switch 3 Actuated at 122.2 in H2O Input | | | 05000321/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000321/LER-1979-001-03, /03L-0 on 790109:during Steady State Power at 2400 Mwt,Plant Personnel Inadvertently Opened Both Doors of Reactor Bldg 130-ft Airlock R106.For Reasons Unknown,Switch Which Allows Defeat of Interlock Was Operated | /03L-0 on 790109:during Steady State Power at 2400 Mwt,Plant Personnel Inadvertently Opened Both Doors of Reactor Bldg 130-ft Airlock R106.For Reasons Unknown,Switch Which Allows Defeat of Interlock Was Operated | | | 05000321/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000321/LER-1979-002-03, /03L-0 on 790111:during Normal Operation,Hpci Steam Supply valves,E41-F002 & E41-F003,automatically Isolated Due to Equipment Room High Differential Temp & Cold Outside Air Flowing Across Inlet Air Temp Elements | /03L-0 on 790111:during Normal Operation,Hpci Steam Supply valves,E41-F002 & E41-F003,automatically Isolated Due to Equipment Room High Differential Temp & Cold Outside Air Flowing Across Inlet Air Temp Elements | | | 05000366/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000366/LER-1979-002-03, /03L-0 on 791231:in Cold Shutdown While Performing HNP-2-3456,overvoltage Trip Setpoint for Reactor Protection Sys Motor Generator Set B Was Found at 133.5 Volts Alternating Current.Caused by Setpoint Drift | /03L-0 on 791231:in Cold Shutdown While Performing HNP-2-3456,overvoltage Trip Setpoint for Reactor Protection Sys Motor Generator Set B Was Found at 133.5 Volts Alternating Current.Caused by Setpoint Drift | | | 05000321/LER-1979-003-03, /03L-0 on 790114:during Normal operation,hi-flow Alarm Occurred on Stack Effluent Radiation Monitor.Sample Pump Was Found Not Running.Restart Failed,As Did Spare Pump. Caused by Failure of Operating Pump Carbon Valves | /03L-0 on 790114:during Normal operation,hi-flow Alarm Occurred on Stack Effluent Radiation Monitor.Sample Pump Was Found Not Running.Restart Failed,As Did Spare Pump. Caused by Failure of Operating Pump Carbon Valves | | | 05000321/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000366/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000366/LER-1979-003-03, /03L-0 on 790102:in Cold Shutdown While Performing HNP-2-3173 on Reactor Pressure Switch 2B21-N021C,setpoint Found Above 600 Psig for Switch No 2.Caused by Switch Setpoint Drift | /03L-0 on 790102:in Cold Shutdown While Performing HNP-2-3173 on Reactor Pressure Switch 2B21-N021C,setpoint Found Above 600 Psig for Switch No 2.Caused by Switch Setpoint Drift | | | 05000321/LER-1979-004-03, /03L-0 on 790119:during Performance of Procedure HNP-1-3302,armature Winding of HPCI Injecting Valve Motor (E41-F006) Burned When Valve Was Opening.Minor Internal Disorder Probably Led to Overheat | /03L-0 on 790119:during Performance of Procedure HNP-1-3302,armature Winding of HPCI Injecting Valve Motor (E41-F006) Burned When Valve Was Opening.Minor Internal Disorder Probably Led to Overheat | | | 05000366/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000366/LER-1979-004-03, /03L-0 on 790104:review of HNP-2-3610-0 (RHR Pump Operability) Data Sheet Revealed Pump Delta Requirements Not Met.Caused by Personnel Error Resulting from New Procedures | /03L-0 on 790104:review of HNP-2-3610-0 (RHR Pump Operability) Data Sheet Revealed Pump Delta Requirements Not Met.Caused by Personnel Error Resulting from New Procedures | | | 05000321/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000366/LER-1979-005-03, /03L-0 on 790103:under Frequency Trip Setpoint Found at 54.1HZ for Motor Generator Set A.Caused by pre-op Test on Sys.Surveillance Test HNP-2-3456 Contains Setpoint More Conservative than Tech Specs | /03L-0 on 790103:under Frequency Trip Setpoint Found at 54.1HZ for Motor Generator Set A.Caused by pre-op Test on Sys.Surveillance Test HNP-2-3456 Contains Setpoint More Conservative than Tech Specs | | | 05000366/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000321/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000321/LER-1979-005-03, /03L-0 on 790118:while Performing HNP-1-350-M,TDR G31-R616D Failed to Actuate at Its Setting of 15-s.Two-h Time Limit Exceeded W/Sys Down for Repair.Caused by Loose Screw on Diaphragm,Resulting in Component Failure | /03L-0 on 790118:while Performing HNP-1-350-M,TDR G31-R616D Failed to Actuate at Its Setting of 15-s.Two-h Time Limit Exceeded W/Sys Down for Repair.Caused by Loose Screw on Diaphragm,Resulting in Component Failure | | | 05000366/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000366/LER-1979-006-03, /03L-0 on 790102:reactor Pressure Instrument Ft&C, Relay 2B21-K34A Failed to Operate W/Actuation of 2B21-N021A. Caused by Open Coil | /03L-0 on 790102:reactor Pressure Instrument Ft&C, Relay 2B21-K34A Failed to Operate W/Actuation of 2B21-N021A. Caused by Open Coil | | | 05000321/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000321/LER-1979-006-03, /03L-0 on 790122:during Normal Startup,Reactor Operated Above 1% for Over 24-h W/O Critical Mass Peaking Factor Being Calculated.Caused by Computer Limitations for Low Power Operation | /03L-0 on 790122:during Normal Startup,Reactor Operated Above 1% for Over 24-h W/O Critical Mass Peaking Factor Being Calculated.Caused by Computer Limitations for Low Power Operation | | | 05000321/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000321/LER-1979-007-03, /03L-0 on 790120:reactor Core Isolation Cooling Min Flow Valve (E51-F019) Failed to Close Automatically. Caused by Failure of Open Limit Switch,Resulting in Damage to Valve Operator & Torque Switch | /03L-0 on 790120:reactor Core Isolation Cooling Min Flow Valve (E51-F019) Failed to Close Automatically. Caused by Failure of Open Limit Switch,Resulting in Damage to Valve Operator & Torque Switch | | | 05000321/LER-1979-008-03, /03L-0 on 790121:reactor Max Cooling Rate Exceeded Due to Injection of Condensate Feedwater Into Reactor Vessel During Slowdown.Caused by Pressure Decreasing Below Condensate Booster Pump Discharge Pressure | /03L-0 on 790121:reactor Max Cooling Rate Exceeded Due to Injection of Condensate Feedwater Into Reactor Vessel During Slowdown.Caused by Pressure Decreasing Below Condensate Booster Pump Discharge Pressure | | | 05000366/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000366/LER-1979-008-03, /03L-0 on 790110:reactor Core Isolation Cooling Steam Line Differential Pressure Low Switch Found to Actuate at 119 in H2O & High Switch at +122 in H2O.Caused by Switch Setpoint Drift | /03L-0 on 790110:reactor Core Isolation Cooling Steam Line Differential Pressure Low Switch Found to Actuate at 119 in H2O & High Switch at +122 in H2O.Caused by Switch Setpoint Drift | | | 05000321/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000366/LER-1979-009-03, /03L-0 on 790111:low Switch & High Switch of 2E51-NO18 Operated Contrary to Tech Specs.Caused by Switch Setpoint Drift.Corrected by Performance of HNP-2-5202 Procedure | /03L-0 on 790111:low Switch & High Switch of 2E51-NO18 Operated Contrary to Tech Specs.Caused by Switch Setpoint Drift.Corrected by Performance of HNP-2-5202 Procedure | | | 05000366/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000321/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000321/LER-1979-009-03, /03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line | /03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line | | | 05000321/LER-1979-010-03, /03L-0 on 790124:during Normal pre-conditional Ramp,Determined That a Reactor Coolant Chemistry Sample Could Not Be Obtained.Caused by Both Reactor Water Cleanup Pumps Being Inoperable & Primary Sample Line Clogged | /03L-0 on 790124:during Normal pre-conditional Ramp,Determined That a Reactor Coolant Chemistry Sample Could Not Be Obtained.Caused by Both Reactor Water Cleanup Pumps Being Inoperable & Primary Sample Line Clogged | | | 05000321/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000366/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000366/LER-1979-010-03, /03L-0 on 790117:in Cold Shutdown,While Performing HNP-2-3820,switches 2B21-N301 F,H & L Did Not Actuate.Caused by Switch Diaphragm Failure | /03L-0 on 790117:in Cold Shutdown,While Performing HNP-2-3820,switches 2B21-N301 F,H & L Did Not Actuate.Caused by Switch Diaphragm Failure | | | 05000321/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000366/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000366/LER-1979-011-03, /03L-0 on 790117:during Normal Startup Test & Reactor in Cold Shutdown,Review of HNP-2-3160 (RHR Pump Operability) Revealed Required Flow Not Being Met.Caused by Procedural Error by Personnel | /03L-0 on 790117:during Normal Startup Test & Reactor in Cold Shutdown,Review of HNP-2-3160 (RHR Pump Operability) Revealed Required Flow Not Being Met.Caused by Procedural Error by Personnel | | | 05000321/LER-1979-011-03, /03L-0 on 790124:while in Cold Shutdown,Both Doors of Reactor Bldg Were Opened,Violating Secondary Containment. Bracket Into Which Dead Bolt Projects Was Bent,Preventing Interlock from Functioning.Bracket Was Repaired | /03L-0 on 790124:while in Cold Shutdown,Both Doors of Reactor Bldg Were Opened,Violating Secondary Containment. Bracket Into Which Dead Bolt Projects Was Bent,Preventing Interlock from Functioning.Bracket Was Repaired | | | 05000366/LER-1979-012, Has Been Voided | Has Been Voided | | | 05000321/LER-1979-012-03, /03L-0 on 790124:during Shutdown,High Pressure of 200 to 300 Psig Existed in RHR Heat Exchangers.Caused by Slow Leak Past E11-F015A Valve | /03L-0 on 790124:during Shutdown,High Pressure of 200 to 300 Psig Existed in RHR Heat Exchangers.Caused by Slow Leak Past E11-F015A Valve | | | 05000321/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000366/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000321/LER-1979-013-01, /01X-1 on 790131:scram Received on Intermediate Range Monitor Hi-Hi Trip at Notch 26 of Rod 42-15.Caused by Notches Being Withdrawn Past Point Required to Achieve Criticality.Procedures Revised | /01X-1 on 790131:scram Received on Intermediate Range Monitor Hi-Hi Trip at Notch 26 of Rod 42-15.Caused by Notches Being Withdrawn Past Point Required to Achieve Criticality.Procedures Revised | | | 05000366/LER-1979-013-03, /03L-0 on 790125:while in Refuel Mode,Control Rod & Control Rod Drive Removal Was Begun Before Performing one- Rod Out Refueling Interlock Operability Test.Caused by Omission of This Step in Procedure.Procedure to Be Revised | /03L-0 on 790125:while in Refuel Mode,Control Rod & Control Rod Drive Removal Was Begun Before Performing one- Rod Out Refueling Interlock Operability Test.Caused by Omission of This Step in Procedure.Procedure to Be Revised | | | 05000321/LER-1979-013, Foward LER 79-013/01X-1 | Foward LER 79-013/01X-1 | | | 05000321/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | |
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