Similar Documents at Hatch |
|---|
|
LER-1979-098, /01T-0:on 791210,HPCI Sys Not Proven Inoperable as Required by Tech Specs.Caused by Failure of Personnel to Consider Reactor Core Isolation Cooling Sys Inoperable After Trip on High Turbine Exhaust Pressure |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 3211979098R01 - NRC Website |
|
text
Hb
- 7 77)
LICENSEE EVENT REPORT COmROt stoCu i I
l l
l l
g (PLE ASE PRINT OH TYPE ALL REQUIRED INFORMAT40*H lGlAlEJI H l1 l@l0 10 l0 l0 l0 10 01010 l010 @l 4 l 1l 1l ll 11@l l
l@
a i
8 9 LICE %EE CODE 14 1S LICENSE NL YdEH 22 26 l.lCENSE TYPE JO
$ 1 C A T $8
'T
_. W S$ "E lLl@ 0l5 0 l0 10 l3 12 l1 }@l1 12 1 10 ]7 l9 }@l 1 l 2 l 1 l 9 l 7 l 9 @
8 60 61 DOCK ET NuvaER tA 6J EVENT DATE 14 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBA8LE CONSEQUENCES h IFailure to consider RCIC system inoperable af ter a trip on high turbine exhaust pres-j O
2 [sure on 12-8-79.
Therefore, the HPCI system was not proven operable as required by
[
O 3
l Tech Specs 4.5.E.2.
Also, Tech Specs section 3.5.E.3 was not complied with.
A 1
. _10 4
grevious event of this nature was reported on LER 50-321/1979-066.
,iO s
I IO is 1 l
I O ' 7_] I l
_IO 8
60 7
8 3 0
CODE SUBCO E COMPONEtrCODE SO9C DE SU OE l C ] E j@ l A l@ l Al@ Liz z i z i z i z ig gg g g
- O 9
B 9
10 11 12 i3 18 19 20 SECU E NTI AL OCCURRENCE REPORT REVISION
- - EVENT YEAR REPORT NO CODE TYPE NO.
LER RO 7 9l
[---J l 0l 9l 8l l/]
l0l1l l Tl
[-j [0 j O,aj,gg l21 22 2J 24 26 27 28 23 30 31 J2,
S IT ED FOR LS.
SUPPLIE MAP F HER TAKEf ACT ON O PL T
P/ I t
HCURS
(([J@lz l@
Ez_jg iz j@
l O i 01 O i 6 1 ty g. inig izig lzl9l9l9]@
33 34 33 3G 3'
40 48 42 4J 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1The cause of the event was due to an oversight by operating personnel on shif t to dec-;
i o
_ li li l 1lare RCIC system inoperable when the system tripped on high turbine exhaust pressure.
l i 121, l The personnel involved in the occurrence were administratively relieved of their
[
l licensed duties and were evaluated at the~ conpletion of a training and self-study pro-j l i l 3j i
4 1 gram. They were returned to licensed duties based on successfuli 89 7
8 9 STA 5
% POV.ER OTHER STATUS SCO RY DISCOVEHY DESCRIPTION
[,CJ@ l 0l 8l 0l@l NA j
lAl@l Personnel i
s AC TIVI TY CONTENT RE LE ASE D OF RE LE ASE AVOUN1 OF ACTitlTY LO" ATION OF RELE ASE i
c NA l
NA l
7 8 9 10 11 44 45 80 PE F' SONNE L E XPOSURES NUYBEH
DESCRIPTION
1010 01@ TYPFzl@l NA
~
l i
7 PmSO,.N Er,Nas 1644 328
- - e DESCR,PnON@
li l-1 I 010101@l h9 l N u,.
R NA 60 1
8 9 11 12 LOSS OF OR DAYAGE TO F ACILITY 7
l TYPE DESCHIP TION i > R Lzj@
NA 7
60 7
8 9 to NRC USE ONL Y ISSU E SC RIP TIOrd lihlLSESI NA j ~ -[]
lll lltj;I~
68 69 30 ['
F 8 9 10
$. X. 8axley, $uDt. Onerations PsoNs 912-367-7781 2
NAVE OF PREPARER
Georgia Power Company Plant E. I. Hatch Baxley, Georgia 31513 Cause Description and Corrective Actionscompletion of their evaluation.
I e
1644 329
LER #:
50-321/1979-098 Licensee:
Georgia Power Company Facility Name:
Edwin I.
Hatch Docket Number 50-321
Narrative
Report On 12-8-79, at 0940 RCIC system tripped on high turbine exhaust pressure.
The RCIC system was being used to maintain RPV water level during startup until the reactor feed pump was placed in service.
When the RCIC system tripped the RFP was placed in service and startup continued.
The licensed personnel on shift did not declare RCIC inoperable, only resct RCIC and placed in standby conditions on 12-9-79, at 1015 the RCIC system was started to demonstrate operability as required by normal surveillance as indicated by Tech Specs.
The RCIC system again tripped on high turbine exhaust pressure.
The system was declared inoperable and all requirements of Tech Specs performed.
The
cause
of the RCIC system trip was investigated and found that the manual stop check
- valve, E51-F001 was closed.
The lock had broken and chain then came off handwheel, and valve vibrated closed.
The E51-F001 valve was immediately opened and the chain installed with a new lock.
Engineering is evaluating a
different type looking device for valves of this type.
The exhaust valve on HPCI Units 1 and 2 and also the exhaust valve of Unit 2 RCIC was checked to ensure they were locked in the open position.
Better type locks have been ordered and will be replacing the type Yale lock that was used on the E51-F001 valve The personnel involved in the occurrence were administratively relieved of their licensed duties and were evaluated at the completion of a training and self-study program.
They were returned to licensed duties based on their successful completion of their evaluation.
The training and self-study program included the following:
1.
Tech Specs review for LCOs 2.
Tech Specs Surveillance Requirements 3
Procedure HNP-425 4.
Procedure HNP-17 5.
Tech Specs Sections on ECCS systems 1644 330
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000366/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000366/LER-1979-001-03, /03L-0 on 781229:in Cold Shutdown While Performing HNP-2-3154,reactor Water Level Instrument Switch 1 Was Found Inoperative Due to Broken Foot, & Switch 3 Actuated at 122.2 in H2O Input | /03L-0 on 781229:in Cold Shutdown While Performing HNP-2-3154,reactor Water Level Instrument Switch 1 Was Found Inoperative Due to Broken Foot, & Switch 3 Actuated at 122.2 in H2O Input | | | 05000321/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000321/LER-1979-001-03, /03L-0 on 790109:during Steady State Power at 2400 Mwt,Plant Personnel Inadvertently Opened Both Doors of Reactor Bldg 130-ft Airlock R106.For Reasons Unknown,Switch Which Allows Defeat of Interlock Was Operated | /03L-0 on 790109:during Steady State Power at 2400 Mwt,Plant Personnel Inadvertently Opened Both Doors of Reactor Bldg 130-ft Airlock R106.For Reasons Unknown,Switch Which Allows Defeat of Interlock Was Operated | | | 05000321/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000321/LER-1979-002-03, /03L-0 on 790111:during Normal Operation,Hpci Steam Supply valves,E41-F002 & E41-F003,automatically Isolated Due to Equipment Room High Differential Temp & Cold Outside Air Flowing Across Inlet Air Temp Elements | /03L-0 on 790111:during Normal Operation,Hpci Steam Supply valves,E41-F002 & E41-F003,automatically Isolated Due to Equipment Room High Differential Temp & Cold Outside Air Flowing Across Inlet Air Temp Elements | | | 05000366/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000366/LER-1979-002-03, /03L-0 on 791231:in Cold Shutdown While Performing HNP-2-3456,overvoltage Trip Setpoint for Reactor Protection Sys Motor Generator Set B Was Found at 133.5 Volts Alternating Current.Caused by Setpoint Drift | /03L-0 on 791231:in Cold Shutdown While Performing HNP-2-3456,overvoltage Trip Setpoint for Reactor Protection Sys Motor Generator Set B Was Found at 133.5 Volts Alternating Current.Caused by Setpoint Drift | | | 05000321/LER-1979-003-03, /03L-0 on 790114:during Normal operation,hi-flow Alarm Occurred on Stack Effluent Radiation Monitor.Sample Pump Was Found Not Running.Restart Failed,As Did Spare Pump. Caused by Failure of Operating Pump Carbon Valves | /03L-0 on 790114:during Normal operation,hi-flow Alarm Occurred on Stack Effluent Radiation Monitor.Sample Pump Was Found Not Running.Restart Failed,As Did Spare Pump. Caused by Failure of Operating Pump Carbon Valves | | | 05000321/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000366/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000366/LER-1979-003-03, /03L-0 on 790102:in Cold Shutdown While Performing HNP-2-3173 on Reactor Pressure Switch 2B21-N021C,setpoint Found Above 600 Psig for Switch No 2.Caused by Switch Setpoint Drift | /03L-0 on 790102:in Cold Shutdown While Performing HNP-2-3173 on Reactor Pressure Switch 2B21-N021C,setpoint Found Above 600 Psig for Switch No 2.Caused by Switch Setpoint Drift | | | 05000321/LER-1979-004-03, /03L-0 on 790119:during Performance of Procedure HNP-1-3302,armature Winding of HPCI Injecting Valve Motor (E41-F006) Burned When Valve Was Opening.Minor Internal Disorder Probably Led to Overheat | /03L-0 on 790119:during Performance of Procedure HNP-1-3302,armature Winding of HPCI Injecting Valve Motor (E41-F006) Burned When Valve Was Opening.Minor Internal Disorder Probably Led to Overheat | | | 05000366/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000366/LER-1979-004-03, /03L-0 on 790104:review of HNP-2-3610-0 (RHR Pump Operability) Data Sheet Revealed Pump Delta Requirements Not Met.Caused by Personnel Error Resulting from New Procedures | /03L-0 on 790104:review of HNP-2-3610-0 (RHR Pump Operability) Data Sheet Revealed Pump Delta Requirements Not Met.Caused by Personnel Error Resulting from New Procedures | | | 05000321/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000366/LER-1979-005-03, /03L-0 on 790103:under Frequency Trip Setpoint Found at 54.1HZ for Motor Generator Set A.Caused by pre-op Test on Sys.Surveillance Test HNP-2-3456 Contains Setpoint More Conservative than Tech Specs | /03L-0 on 790103:under Frequency Trip Setpoint Found at 54.1HZ for Motor Generator Set A.Caused by pre-op Test on Sys.Surveillance Test HNP-2-3456 Contains Setpoint More Conservative than Tech Specs | | | 05000366/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000321/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000321/LER-1979-005-03, /03L-0 on 790118:while Performing HNP-1-350-M,TDR G31-R616D Failed to Actuate at Its Setting of 15-s.Two-h Time Limit Exceeded W/Sys Down for Repair.Caused by Loose Screw on Diaphragm,Resulting in Component Failure | /03L-0 on 790118:while Performing HNP-1-350-M,TDR G31-R616D Failed to Actuate at Its Setting of 15-s.Two-h Time Limit Exceeded W/Sys Down for Repair.Caused by Loose Screw on Diaphragm,Resulting in Component Failure | | | 05000366/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000366/LER-1979-006-03, /03L-0 on 790102:reactor Pressure Instrument Ft&C, Relay 2B21-K34A Failed to Operate W/Actuation of 2B21-N021A. Caused by Open Coil | /03L-0 on 790102:reactor Pressure Instrument Ft&C, Relay 2B21-K34A Failed to Operate W/Actuation of 2B21-N021A. Caused by Open Coil | | | 05000321/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000321/LER-1979-006-03, /03L-0 on 790122:during Normal Startup,Reactor Operated Above 1% for Over 24-h W/O Critical Mass Peaking Factor Being Calculated.Caused by Computer Limitations for Low Power Operation | /03L-0 on 790122:during Normal Startup,Reactor Operated Above 1% for Over 24-h W/O Critical Mass Peaking Factor Being Calculated.Caused by Computer Limitations for Low Power Operation | | | 05000321/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000321/LER-1979-007-03, /03L-0 on 790120:reactor Core Isolation Cooling Min Flow Valve (E51-F019) Failed to Close Automatically. Caused by Failure of Open Limit Switch,Resulting in Damage to Valve Operator & Torque Switch | /03L-0 on 790120:reactor Core Isolation Cooling Min Flow Valve (E51-F019) Failed to Close Automatically. Caused by Failure of Open Limit Switch,Resulting in Damage to Valve Operator & Torque Switch | | | 05000321/LER-1979-008-03, /03L-0 on 790121:reactor Max Cooling Rate Exceeded Due to Injection of Condensate Feedwater Into Reactor Vessel During Slowdown.Caused by Pressure Decreasing Below Condensate Booster Pump Discharge Pressure | /03L-0 on 790121:reactor Max Cooling Rate Exceeded Due to Injection of Condensate Feedwater Into Reactor Vessel During Slowdown.Caused by Pressure Decreasing Below Condensate Booster Pump Discharge Pressure | | | 05000366/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000366/LER-1979-008-03, /03L-0 on 790110:reactor Core Isolation Cooling Steam Line Differential Pressure Low Switch Found to Actuate at 119 in H2O & High Switch at +122 in H2O.Caused by Switch Setpoint Drift | /03L-0 on 790110:reactor Core Isolation Cooling Steam Line Differential Pressure Low Switch Found to Actuate at 119 in H2O & High Switch at +122 in H2O.Caused by Switch Setpoint Drift | | | 05000321/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000366/LER-1979-009-03, /03L-0 on 790111:low Switch & High Switch of 2E51-NO18 Operated Contrary to Tech Specs.Caused by Switch Setpoint Drift.Corrected by Performance of HNP-2-5202 Procedure | /03L-0 on 790111:low Switch & High Switch of 2E51-NO18 Operated Contrary to Tech Specs.Caused by Switch Setpoint Drift.Corrected by Performance of HNP-2-5202 Procedure | | | 05000366/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000321/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000321/LER-1979-009-03, /03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line | /03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line | | | 05000321/LER-1979-010-03, /03L-0 on 790124:during Normal pre-conditional Ramp,Determined That a Reactor Coolant Chemistry Sample Could Not Be Obtained.Caused by Both Reactor Water Cleanup Pumps Being Inoperable & Primary Sample Line Clogged | /03L-0 on 790124:during Normal pre-conditional Ramp,Determined That a Reactor Coolant Chemistry Sample Could Not Be Obtained.Caused by Both Reactor Water Cleanup Pumps Being Inoperable & Primary Sample Line Clogged | | | 05000321/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000366/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000366/LER-1979-010-03, /03L-0 on 790117:in Cold Shutdown,While Performing HNP-2-3820,switches 2B21-N301 F,H & L Did Not Actuate.Caused by Switch Diaphragm Failure | /03L-0 on 790117:in Cold Shutdown,While Performing HNP-2-3820,switches 2B21-N301 F,H & L Did Not Actuate.Caused by Switch Diaphragm Failure | | | 05000321/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000366/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000366/LER-1979-011-03, /03L-0 on 790117:during Normal Startup Test & Reactor in Cold Shutdown,Review of HNP-2-3160 (RHR Pump Operability) Revealed Required Flow Not Being Met.Caused by Procedural Error by Personnel | /03L-0 on 790117:during Normal Startup Test & Reactor in Cold Shutdown,Review of HNP-2-3160 (RHR Pump Operability) Revealed Required Flow Not Being Met.Caused by Procedural Error by Personnel | | | 05000321/LER-1979-011-03, /03L-0 on 790124:while in Cold Shutdown,Both Doors of Reactor Bldg Were Opened,Violating Secondary Containment. Bracket Into Which Dead Bolt Projects Was Bent,Preventing Interlock from Functioning.Bracket Was Repaired | /03L-0 on 790124:while in Cold Shutdown,Both Doors of Reactor Bldg Were Opened,Violating Secondary Containment. Bracket Into Which Dead Bolt Projects Was Bent,Preventing Interlock from Functioning.Bracket Was Repaired | | | 05000366/LER-1979-012, Has Been Voided | Has Been Voided | | | 05000321/LER-1979-012-03, /03L-0 on 790124:during Shutdown,High Pressure of 200 to 300 Psig Existed in RHR Heat Exchangers.Caused by Slow Leak Past E11-F015A Valve | /03L-0 on 790124:during Shutdown,High Pressure of 200 to 300 Psig Existed in RHR Heat Exchangers.Caused by Slow Leak Past E11-F015A Valve | | | 05000321/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000366/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000321/LER-1979-013-01, /01X-1 on 790131:scram Received on Intermediate Range Monitor Hi-Hi Trip at Notch 26 of Rod 42-15.Caused by Notches Being Withdrawn Past Point Required to Achieve Criticality.Procedures Revised | /01X-1 on 790131:scram Received on Intermediate Range Monitor Hi-Hi Trip at Notch 26 of Rod 42-15.Caused by Notches Being Withdrawn Past Point Required to Achieve Criticality.Procedures Revised | | | 05000366/LER-1979-013-03, /03L-0 on 790125:while in Refuel Mode,Control Rod & Control Rod Drive Removal Was Begun Before Performing one- Rod Out Refueling Interlock Operability Test.Caused by Omission of This Step in Procedure.Procedure to Be Revised | /03L-0 on 790125:while in Refuel Mode,Control Rod & Control Rod Drive Removal Was Begun Before Performing one- Rod Out Refueling Interlock Operability Test.Caused by Omission of This Step in Procedure.Procedure to Be Revised | | | 05000321/LER-1979-013, Foward LER 79-013/01X-1 | Foward LER 79-013/01X-1 | | | 05000321/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | |
|