05000333/LER-1979-085-01, /01T-0:on 791024,while Performing Pipe Stress Reanalysis,Pipe Support Found Inoperable.Cause Not Stated. Support Will Be Upgraded to Accept Increased Loading Resulting from SHOCK-III Analysis

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/01T-0:on 791024,while Performing Pipe Stress Reanalysis,Pipe Support Found Inoperable.Cause Not Stated. Support Will Be Upgraded to Accept Increased Loading Resulting from SHOCK-III Analysis
ML19254F453
Person / Time
Site: FitzPatrick 
Issue date: 11/06/1979
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19254F452 List:
References
LER-79-085-01T, LER-79-85-1T, NUDOCS 7911090460
Download: ML19254F453 (2)


LER-1979-085, /01T-0:on 791024,while Performing Pipe Stress Reanalysis,Pipe Support Found Inoperable.Cause Not Stated. Support Will Be Upgraded to Accept Increased Loading Resulting from SHOCK-III Analysis
Event date:
Report date:
3331979085R01 - NRC Website

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POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT DOCKET N0. 50-333 ATTACHMENT TO LER 79-085/01T-0 Page 1 of 1 The Architect-Engineer informed the plant staff that as the result of the Pipe Stress Reanalysis Program, pipe support BFSK-658(H-2) was inoperable.

Following the guidelines of the 14 August 1979 letter lifting the Show Cause Order, an analysis has been performed by the Architect-Engineer which demonstrates that the effected system (Fire Protection) remains operable following a Design Basis Earthquake, with this support removed. This support will be upgraded to accept the increased loading resulting from the Shock III analysis as part of our continuing program to correct pipe support deficiencies.

Because the system remains operable, this event is not considered to be a significant hazard to the public health and safety.

A follow up report will be submitted when modification of the support is completed.

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