LER-1979-023, /03L-0:on 791016,level Switch LIS 2-263-72A Failed to Trip During Calibr.Caused by Failure of One Mercury Wetted Magnetic Switch Encl in Level Indicator.New Switch Installed & Tested Satisfactorily |
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2 ! While performing the Reactor Low-Low Water Level Calibration, procedure QlS 11-1, l
level switch LIS 2-263-72A failed to trip when given a low-low reactor water signal l
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LER NUMBER:
LER/R0 79-23/03L-0 II.
LICENSEE NAME: Commonwealth Edison Compsav Quad-Cities Nuclear Power Station 111.
FACILITY NAME: Unit Two IV.
DOCKET NUMBER: 050-265 V.
EVENT DESCRIPTION
At 11:00 AM on October 16, 1979, while performing the Reactor Low-Low Water Level Calibration, procedure QlS 11-1, level switch LIS-2-263-72A failed to trip when given a low-low reactor water level signal.
VI.
PROBABLE CONSEQUENCES OF THE OCCURRENCE:
Level switch LIS 2-263-72A is one of four low-low level switches which initiate the Emergency Core Cooling System (ECCS) Logic.
The other three switches were tested during the same calibration and were found to be fully operable. These switches are arranged in a one-out-of-two-twice logic.
The other three operable switches would have given the proper ECCS initiation signal had a low-low reactor water level occurred. Subsequently the automatic initiation capability of ECCS was always operable and safe reactor operation was not af' ;ted by this occurrence.
Vll.
CAUSE
The level indicating switch that failed, LIS-2-263-72A, is one of four mercury wetted magnetic switches enclosed in the Yarway level indicator. A magnet moves on the arm of the level indicator causing each of these switches to close.
The switch that failed was the one that closes on low-low reactor water level. There was no observed physical damage to the switch.
Vill.
CORRECTIVE ACTION
Corrective action taken was to replace the switch with a like switch. The new switch was installed and tested satisfactorily on October 16, 1979 144lf'081
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