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LER-1979-075, /01T-0:790907,w/reactor Critical,Rhr Svc Water Pumps A-D Would Not Pump Rated Flow at Rated Discharge Pressure.Caused by Incorrected Formulas for Calculated Inlet & Discharge Pressures.Pumps Retested |
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| 3211979075R01 - NRC Website |
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io i2 1 I that the RHR service water pumps "A", "C" and "D" would not nump_ rated flow at rated I
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I di_scharce orcSlur_e_as_p_er HNP-1-3167. "P&_S_crv_i ce__'sta ter Pugp Goerabi_l i ty f o la Since I tesL__Later, the__"B" pu p was also diacnosed to have the same urablem.
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li i I l The RHR serv _i_ce water pumn nperabill rv test contained formulas for calcula tire Inlet The archi-r tm) LPressure end the discharce_aressure which were determined to be incorrect.
J l tect encineer was consulted about the ecuations, their succestions were then iralem-l I i j -)
I ented in e revision to HNP-1-3167 and a Document Chance to the Tech Snecs lim j
is-!
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Coggin, Supt. P 1 L. r.qq. sqrv.,,,, g. g.
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Georgia Power Company
'....v. Plant E. I. Hatch Caxley, Georgia 31513 s
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.f;f Event Description and Probable Consequencesoperability test is a repetitive occur :nce for the RHR service water pumps; reference License Event Report No. 50-321/1979-063.
Cause Description and Corrective ActionsThe pumps were then successfully retested.
The Unit 1 & 2 plant service water, RHR service water and standby plant service water pump procedures were all reviewed and found to contain the same formulas as mentioned before.
All the procedures were revised prior to Unit startups.
A further review of the procedure formulas revealed that the original " Delta P" formula was cor-
- - rect, only the required RHR service water pump Total Dynamic Head in feet needed to be changed.
1060 010 W
SUPPLEMENT TO LER 50 7?1/1970-075 1
On September 7,
- 1979, with the reactor critical at 2304 megawatts, while performing the RHR service water pump operability procedure (HNP-1-3167),
RHR sortice water pumps E11-C001A, C,
and D would not pump rated flow (4000 GPMT a t, rated pressure as required by H"P-1-3167 and Tech.
.3 0 e c.
section 4.5.C.1.b.
The 1E11-C001A pump had a flou of
'! O / '4 GPM at 35S DSIG; the 1E11-C001C p u rr n had a flow of 4024 GPV at 179 PSIG, and the 1E11-C001D pump had a flow of h024 G P
at 173 PSIG.
After the discharge pressu"e gages
/1E11-R00hA-Di were recalibrated, it was d e t e r". i n e d that 1E11-C0014 had a:so failed to meet the flow and pressure requi-e v nts; the p u r. ?
had a flow of 4156 GPM at 405 PSIG.
At this time the "eactor was brought to cold shutdown as per Tech. Spec. sect!on 0.5.r.
Due to the inherent problem of the ptmps failing to p u r.o rated flow at rated pressure when the river water level is
- low, engineering services was consulted to review the pump pressure formulas in HNP-1-3167.
The initial review i nd i c a '.e d that the formulas for inlet
- pressure, discharge
- pressure, and differential pressure were incorrect.
The A"chitect 7.n rz i n e e r s submitted neu formulas which were incornorated into the Unit 1 and 2
operability procedures for RHR service water olant service water, and the standby plant service water ounns.
On 9-9 74, the Unit 1 RHR service water oumos we c "etested using the new formulas clus the corrected " Total P/nanic Headd for the pumos granted by the Tech Soecs c h a n :* e.
s.11 the nu.o s passed their operability test so new reference data was taken and the Unit started up.
A later review of the new roanulas revealed that the original differential pressure formula was correct.
Thus, the original
" Delta P"
formulas were reinserted i n t.o their respective operabisity procedures.
As far as the RHR service water procedure is concerned the valves derived from the new " Delta P"
formula are very close (within a few PSI) and in a conse"vative direction to those valves derived from the old " Delta P"
fornula with the new total dynamic head valve.
The "eason the old formula was reinserted is because the new formula did not take into account the Hydraulic Institute Standards for t. h e pumps.
o pJ di) i 1060 011
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| 05000366/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000366/LER-1979-001-03, /03L-0 on 781229:in Cold Shutdown While Performing HNP-2-3154,reactor Water Level Instrument Switch 1 Was Found Inoperative Due to Broken Foot, & Switch 3 Actuated at 122.2 in H2O Input | /03L-0 on 781229:in Cold Shutdown While Performing HNP-2-3154,reactor Water Level Instrument Switch 1 Was Found Inoperative Due to Broken Foot, & Switch 3 Actuated at 122.2 in H2O Input | | | 05000321/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000321/LER-1979-001-03, /03L-0 on 790109:during Steady State Power at 2400 Mwt,Plant Personnel Inadvertently Opened Both Doors of Reactor Bldg 130-ft Airlock R106.For Reasons Unknown,Switch Which Allows Defeat of Interlock Was Operated | /03L-0 on 790109:during Steady State Power at 2400 Mwt,Plant Personnel Inadvertently Opened Both Doors of Reactor Bldg 130-ft Airlock R106.For Reasons Unknown,Switch Which Allows Defeat of Interlock Was Operated | | | 05000321/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000321/LER-1979-002-03, /03L-0 on 790111:during Normal Operation,Hpci Steam Supply valves,E41-F002 & E41-F003,automatically Isolated Due to Equipment Room High Differential Temp & Cold Outside Air Flowing Across Inlet Air Temp Elements | /03L-0 on 790111:during Normal Operation,Hpci Steam Supply valves,E41-F002 & E41-F003,automatically Isolated Due to Equipment Room High Differential Temp & Cold Outside Air Flowing Across Inlet Air Temp Elements | | | 05000366/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000366/LER-1979-002-03, /03L-0 on 791231:in Cold Shutdown While Performing HNP-2-3456,overvoltage Trip Setpoint for Reactor Protection Sys Motor Generator Set B Was Found at 133.5 Volts Alternating Current.Caused by Setpoint Drift | /03L-0 on 791231:in Cold Shutdown While Performing HNP-2-3456,overvoltage Trip Setpoint for Reactor Protection Sys Motor Generator Set B Was Found at 133.5 Volts Alternating Current.Caused by Setpoint Drift | | | 05000321/LER-1979-003-03, /03L-0 on 790114:during Normal operation,hi-flow Alarm Occurred on Stack Effluent Radiation Monitor.Sample Pump Was Found Not Running.Restart Failed,As Did Spare Pump. Caused by Failure of Operating Pump Carbon Valves | /03L-0 on 790114:during Normal operation,hi-flow Alarm Occurred on Stack Effluent Radiation Monitor.Sample Pump Was Found Not Running.Restart Failed,As Did Spare Pump. Caused by Failure of Operating Pump Carbon Valves | | | 05000321/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000366/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000366/LER-1979-003-03, /03L-0 on 790102:in Cold Shutdown While Performing HNP-2-3173 on Reactor Pressure Switch 2B21-N021C,setpoint Found Above 600 Psig for Switch No 2.Caused by Switch Setpoint Drift | /03L-0 on 790102:in Cold Shutdown While Performing HNP-2-3173 on Reactor Pressure Switch 2B21-N021C,setpoint Found Above 600 Psig for Switch No 2.Caused by Switch Setpoint Drift | | | 05000321/LER-1979-004-03, /03L-0 on 790119:during Performance of Procedure HNP-1-3302,armature Winding of HPCI Injecting Valve Motor (E41-F006) Burned When Valve Was Opening.Minor Internal Disorder Probably Led to Overheat | /03L-0 on 790119:during Performance of Procedure HNP-1-3302,armature Winding of HPCI Injecting Valve Motor (E41-F006) Burned When Valve Was Opening.Minor Internal Disorder Probably Led to Overheat | | | 05000366/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000366/LER-1979-004-03, /03L-0 on 790104:review of HNP-2-3610-0 (RHR Pump Operability) Data Sheet Revealed Pump Delta Requirements Not Met.Caused by Personnel Error Resulting from New Procedures | /03L-0 on 790104:review of HNP-2-3610-0 (RHR Pump Operability) Data Sheet Revealed Pump Delta Requirements Not Met.Caused by Personnel Error Resulting from New Procedures | | | 05000321/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000366/LER-1979-005-03, /03L-0 on 790103:under Frequency Trip Setpoint Found at 54.1HZ for Motor Generator Set A.Caused by pre-op Test on Sys.Surveillance Test HNP-2-3456 Contains Setpoint More Conservative than Tech Specs | /03L-0 on 790103:under Frequency Trip Setpoint Found at 54.1HZ for Motor Generator Set A.Caused by pre-op Test on Sys.Surveillance Test HNP-2-3456 Contains Setpoint More Conservative than Tech Specs | | | 05000366/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000321/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000321/LER-1979-005-03, /03L-0 on 790118:while Performing HNP-1-350-M,TDR G31-R616D Failed to Actuate at Its Setting of 15-s.Two-h Time Limit Exceeded W/Sys Down for Repair.Caused by Loose Screw on Diaphragm,Resulting in Component Failure | /03L-0 on 790118:while Performing HNP-1-350-M,TDR G31-R616D Failed to Actuate at Its Setting of 15-s.Two-h Time Limit Exceeded W/Sys Down for Repair.Caused by Loose Screw on Diaphragm,Resulting in Component Failure | | | 05000366/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000366/LER-1979-006-03, /03L-0 on 790102:reactor Pressure Instrument Ft&C, Relay 2B21-K34A Failed to Operate W/Actuation of 2B21-N021A. Caused by Open Coil | /03L-0 on 790102:reactor Pressure Instrument Ft&C, Relay 2B21-K34A Failed to Operate W/Actuation of 2B21-N021A. Caused by Open Coil | | | 05000321/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000321/LER-1979-006-03, /03L-0 on 790122:during Normal Startup,Reactor Operated Above 1% for Over 24-h W/O Critical Mass Peaking Factor Being Calculated.Caused by Computer Limitations for Low Power Operation | /03L-0 on 790122:during Normal Startup,Reactor Operated Above 1% for Over 24-h W/O Critical Mass Peaking Factor Being Calculated.Caused by Computer Limitations for Low Power Operation | | | 05000321/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000321/LER-1979-007-03, /03L-0 on 790120:reactor Core Isolation Cooling Min Flow Valve (E51-F019) Failed to Close Automatically. Caused by Failure of Open Limit Switch,Resulting in Damage to Valve Operator & Torque Switch | /03L-0 on 790120:reactor Core Isolation Cooling Min Flow Valve (E51-F019) Failed to Close Automatically. Caused by Failure of Open Limit Switch,Resulting in Damage to Valve Operator & Torque Switch | | | 05000321/LER-1979-008-03, /03L-0 on 790121:reactor Max Cooling Rate Exceeded Due to Injection of Condensate Feedwater Into Reactor Vessel During Slowdown.Caused by Pressure Decreasing Below Condensate Booster Pump Discharge Pressure | /03L-0 on 790121:reactor Max Cooling Rate Exceeded Due to Injection of Condensate Feedwater Into Reactor Vessel During Slowdown.Caused by Pressure Decreasing Below Condensate Booster Pump Discharge Pressure | | | 05000366/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000366/LER-1979-008-03, /03L-0 on 790110:reactor Core Isolation Cooling Steam Line Differential Pressure Low Switch Found to Actuate at 119 in H2O & High Switch at +122 in H2O.Caused by Switch Setpoint Drift | /03L-0 on 790110:reactor Core Isolation Cooling Steam Line Differential Pressure Low Switch Found to Actuate at 119 in H2O & High Switch at +122 in H2O.Caused by Switch Setpoint Drift | | | 05000321/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000366/LER-1979-009-03, /03L-0 on 790111:low Switch & High Switch of 2E51-NO18 Operated Contrary to Tech Specs.Caused by Switch Setpoint Drift.Corrected by Performance of HNP-2-5202 Procedure | /03L-0 on 790111:low Switch & High Switch of 2E51-NO18 Operated Contrary to Tech Specs.Caused by Switch Setpoint Drift.Corrected by Performance of HNP-2-5202 Procedure | | | 05000366/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000321/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000321/LER-1979-009-03, /03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line | /03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line | | | 05000321/LER-1979-010-03, /03L-0 on 790124:during Normal pre-conditional Ramp,Determined That a Reactor Coolant Chemistry Sample Could Not Be Obtained.Caused by Both Reactor Water Cleanup Pumps Being Inoperable & Primary Sample Line Clogged | /03L-0 on 790124:during Normal pre-conditional Ramp,Determined That a Reactor Coolant Chemistry Sample Could Not Be Obtained.Caused by Both Reactor Water Cleanup Pumps Being Inoperable & Primary Sample Line Clogged | | | 05000321/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000366/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000366/LER-1979-010-03, /03L-0 on 790117:in Cold Shutdown,While Performing HNP-2-3820,switches 2B21-N301 F,H & L Did Not Actuate.Caused by Switch Diaphragm Failure | /03L-0 on 790117:in Cold Shutdown,While Performing HNP-2-3820,switches 2B21-N301 F,H & L Did Not Actuate.Caused by Switch Diaphragm Failure | | | 05000321/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000366/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000366/LER-1979-011-03, /03L-0 on 790117:during Normal Startup Test & Reactor in Cold Shutdown,Review of HNP-2-3160 (RHR Pump Operability) Revealed Required Flow Not Being Met.Caused by Procedural Error by Personnel | /03L-0 on 790117:during Normal Startup Test & Reactor in Cold Shutdown,Review of HNP-2-3160 (RHR Pump Operability) Revealed Required Flow Not Being Met.Caused by Procedural Error by Personnel | | | 05000321/LER-1979-011-03, /03L-0 on 790124:while in Cold Shutdown,Both Doors of Reactor Bldg Were Opened,Violating Secondary Containment. Bracket Into Which Dead Bolt Projects Was Bent,Preventing Interlock from Functioning.Bracket Was Repaired | /03L-0 on 790124:while in Cold Shutdown,Both Doors of Reactor Bldg Were Opened,Violating Secondary Containment. Bracket Into Which Dead Bolt Projects Was Bent,Preventing Interlock from Functioning.Bracket Was Repaired | | | 05000366/LER-1979-012, Has Been Voided | Has Been Voided | | | 05000321/LER-1979-012-03, /03L-0 on 790124:during Shutdown,High Pressure of 200 to 300 Psig Existed in RHR Heat Exchangers.Caused by Slow Leak Past E11-F015A Valve | /03L-0 on 790124:during Shutdown,High Pressure of 200 to 300 Psig Existed in RHR Heat Exchangers.Caused by Slow Leak Past E11-F015A Valve | | | 05000321/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000366/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000321/LER-1979-013-01, /01X-1 on 790131:scram Received on Intermediate Range Monitor Hi-Hi Trip at Notch 26 of Rod 42-15.Caused by Notches Being Withdrawn Past Point Required to Achieve Criticality.Procedures Revised | /01X-1 on 790131:scram Received on Intermediate Range Monitor Hi-Hi Trip at Notch 26 of Rod 42-15.Caused by Notches Being Withdrawn Past Point Required to Achieve Criticality.Procedures Revised | | | 05000366/LER-1979-013-03, /03L-0 on 790125:while in Refuel Mode,Control Rod & Control Rod Drive Removal Was Begun Before Performing one- Rod Out Refueling Interlock Operability Test.Caused by Omission of This Step in Procedure.Procedure to Be Revised | /03L-0 on 790125:while in Refuel Mode,Control Rod & Control Rod Drive Removal Was Begun Before Performing one- Rod Out Refueling Interlock Operability Test.Caused by Omission of This Step in Procedure.Procedure to Be Revised | | | 05000321/LER-1979-013, Foward LER 79-013/01X-1 | Foward LER 79-013/01X-1 | | | 05000321/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | |
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