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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20024J2471994-10-0606 October 1994 LER 94-009-00:on 940909,EDG G-02 Inadvertently Started & Station Battery Charger D-08 Tripped Off Due to Blown Fuse. Caused by Inadequate Procedure.Blown Fuse Replaced & Electrical Distribution Sys Restored to normal.W/941006 Ltr ML20029C8511994-04-22022 April 1994 LER 94-001-00:on 940323,identified That Feedwater Flow May Have Been Underestimated Since Beginning of Operating Cycle. Caused by Degradation of Signals from Transducers.Transducer replaced.W/940422 Ltr ML20044E5571993-05-17017 May 1993 LER 92-009-01:on 921012,identified That Ccws Surge Tank Vent Valves Outside Design Basis Due to Oversight During Original Design of CCW Sys.Proposes to Replace Radiation Detector & Associated Circuitry W/Dedicated safety-related Sys ML20044E6221993-05-17017 May 1993 LER 93-006-00:on 930416,discovered That Outside CIV Not Leak Tested,Per TS 15.4.4.III.D Requirements Due to Review on 840202,recommending That Valve Be Tested During RHR Hydrostatic Testing.Subj Valve replaced.W/930517 Ltr ML20044D8811993-05-14014 May 1993 LER 93-005-00:on 930415,containment Accident Fan Time Delay Relay 1-TDR-26 (Turbine Bldg Cooler Svc Water Inlet Valve 1SW-2880) Unexpectedly Closed.Caused by Failure to Recognize Presence of Relay in Contact.Function Changed ML20044D2061993-05-10010 May 1993 LER 93-003-00:on 930328,Point Beach Unit 2 Tripped Due to Surveillance Testing Problems.Test Procedures Can Trip Unit Due to Equipment or Human Failure.Failure Tests Delayed Until Unit 1 & Knpp Restored to power.W/930510 Ltr ML20024H2151991-05-21021 May 1991 LER 91-003-00:on 910429,charging Sys Check Valve 1-370 Discovered W/Leakage in Excess of Limits Due to Worn Disc Arm Bushing Steps.Worn Disc Arm Bushing Steps Cladded W/ E308 Weld Matl & Hand Filed to Design contour.W/910521 Ltr ML20029C2101991-03-20020 March 1991 LER 91-002-01:on 901009,inadvertent Start of Auxiliary Feedwater Pump Occurred.Caused by Inadequate Test Procedures.Auxiliary Feedwater Pump Secured & Maint Work Request Mwr 904517 initiated.W/910320 Ltr ML20029C1141991-03-12012 March 1991 LER 91-010-01:on 900816,axial Flux Differential Outside Tech Specs Limits Due to Malfunction of Turbine Electrohydraulic Governor Control.Operator Training Revised. W/910319 Ltr ML20028H0321990-09-27027 September 1990 LER 90-011-00:on 900829,low Net Positive Suction Head to Containment Spray Pumps W/Eccs in Recirculation Mode Occurred.Caused by Procedural Deficiency.Temporary Procedure Changes initiated.W/900927 Ltr ML20043G2011990-06-0808 June 1990 LER 90-005-00:on 900510,steam Generator lo-lo Level Reactor Trip Occurred During Cold Shutdown.Caused by Inadequate Warning Sign Posting.Nonconformance Rept Written to Document Event & Recommend evaluation.W/900608 Ltr ML20042G7761990-05-0909 May 1990 LER 90-003-00:on 900409,determined That Piping & Supports in Fuel Oil Pumphouse Could Not Be Demonstrated to Perform Support Functions.Caused by Design Base Not Sufficiently Documented.Mod Performed to Support Fuel Oil Piping ML20042G7791990-05-0808 May 1990 LER 90-004-00:on 900404,single Failure Potential in Safeguards Switchgear B03/B04 Tie Breaker Discovered & Could Have Resulted in Failure of Diesel Generator.Control Power Fuses for Tie Breakers Removed ML20042F5361990-05-0404 May 1990 LER 90-001-00:on 900405,auxiliary Feed Pump Inadvertently Started.Caused by Inadequate Design.Schematic Push to Test Lamp Circuitry Will Be Added to Elementary Wiring Diagrams & Personnel Briefed on Potential circuitry.W/900504 Ltr ML20042F1971990-05-0202 May 1990 LER 90-002-00:on 900402,main Steam Safety Valve 1-MS-2013 Failed to Relieve Setpoint During Tech Spec Testing.Caused by Personnel Error During Setpoint Adjustment.Safety Valves 1-MS-2011,1-MS-2006 & 1-MS-2008 restored.W/900502 Ltr ML20011D5131989-12-19019 December 1989 LER 89-010-00:on 891120,auxiliary Feedwater Flow Transmitters Inadvertently Isolated.Caused by Error in Approved Procedure & Personnel Cognitive Error.Unit 1 Transmitters Valved Back Into Svc immediately.W/891219 Ltr ML19351A6721989-12-15015 December 1989 LER 89-009-00:on 891115,unexpected Steam Generator a lo-lo Level & Steam Generator B lo-lo Level Reactor Trip Signals Experienced.Caused by Installation of Analog Signal Generator.Procedures revised.W/891215 Ltr ML19332F7011989-12-11011 December 1989 LER 89-008-01:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power.Caused by Less than Adequate Tech Spec Change.Power Descension to 38% initiated.W/891211 Ltr ML19332E7221989-12-0707 December 1989 LER 89-009-00:on 891107,D05 & D06 Station Batteries Declared Inoperable.Caused by Original Design Deficiency.Mod Completed to Restore Battery D05 to Operable Status by Replacing Eight nonsafety-related breakers.W/891207 Ltr ML19332E8921989-12-0404 December 1989 LER 89-008-00:on 891103,during Refueling,Contractor Personnel Generated False Trip Signal While Investigating Wiring Discrepancy in Reactor Protection Sys Instrument Racks.Caused by Labeling Error.Supply changed.W/891204 Ltr ML19332F0901989-11-28028 November 1989 LER 89-003-01:on 890712,tank B Level Channel 2LE-934 Began to Indicate Spuriously.Caused by Moisture Intrusion Between Halar Insulator & Sensing Rod.Level Detector Replaced & Channel Reestablished for Accumulator Tank B.W/891128 Ltr ML19332C8411989-11-22022 November 1989 LER 89-007-00:on 891027,Train a Safety Injection Signal Generated During Installation of Mod in Containment High Pressure Circuit.Caused by Inadequate Installation Procedure.Procedure changed.W/891122 Ltr ML19327C2001989-11-14014 November 1989 LER 89-006-01:on 891015,steam Generator Tubes Found Degraded,W/Undefined Signal & W/Axial Indications in Tubesheet Area.Degradation Caused by Time.Affected Tubes Plugged or Preventively sleeved.W/891114 Ltr ML19327C0651989-11-0606 November 1989 LER 89-005-00:on 891006,intermediate Range High Level Trip Signal Unexpectedly Generated During Course of Routine Source Range Channel Calibr.Caused by Loose Connection of Input/Output Cable.Connection tightened.W/891106 Ltr ML19327B3061989-10-19019 October 1989 LER 89-008-00:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power, Disenabling Sys.Caused by High Tech Spec Setpoint.Enable/ Disable Setpoint Reset to 30%.W/891019 Ltr ML18041A1611987-11-16016 November 1987 LER 87-004-01:on 870515,voltage Lost on Red Instrument Bus Resulting in Reactor Protection Sys Actuation.Caused by Excessive Current Demand by ferro-resonant Circuit.Plant Mods to Load Bank Proposed ML18041A1341986-07-0303 July 1986 LER 86-003-00:on 860603,reactor Trip Occurred Due to Loss of Power on White Instrument Bus.Caused by Trip of White Inverter Output Breaker.Procedures for Placing Inverter on Line Will Be revised.W/860703 Ltr ML20028E3551983-01-13013 January 1983 LER 82-029/03L-0:on 821216,automatic Monitoring & Alarm Program Constant Found Incorrect.Caused by Unknown Personnel W/Access to on-line Computer.Value of Constant Restored & Control Rods Alignment Verified ML20028E2381983-01-13013 January 1983 LER 82-028/03L-0:on 821215,routine Test on Fire Detection Sys Found Panel D407 Which Monitors Unit 1 Rod Drive Room Inoperable.Caused by Blown Fuse.Fuse & Indication Lights Replaced on 821215.Detection Sys Undergoing Design Review ML20028E1791983-01-13013 January 1983 Updated LER 82-020/01X-1:on 821102,while Performing Type B & C Leakage Tests of Containment Penetrations & Isolation Valves,One Valve Had Leakage Exceeding Limit.Cause Not Stated.Valve Clapper & Seat Lapped ML20028E3031983-01-11011 January 1983 LER 82-027/03L-0:on 821211,operator Noted That Steam Generator Pressure Transmitter 1PT-469 Indicated Higher than Other Channels.Caused by Frozen Sensing Line Due to Inadequate Interim Piping Insulation ML20028E3211983-01-10010 January 1983 Updated LER 82-017/01X-2:on 821030,w/unit Shut Down for Refueling,Eddy Current Exam of Steam Generator Tubes Indicated Four Tubes in Steam Generator a & Three Tubes in Steam Generator B Exceeded Plugging Limit.Caused by Caustic ML20028C2431982-12-27027 December 1982 LER 82-020/01T-0:on 821103,following Type B & C Leak Rate Tests,Total as-measured Leakage Exceeded Tech Spec Limit, Causing Reactor Coolant Pump Component Cooling Water to Have Excessive Leakage.Cause Not Stated.Clapper & Seat Lapped ML20023B3251982-12-10010 December 1982 Updated LER 82-017/01T-1:on 821030,verified That Indications for Four Steam Generator a Tubes & Three Steam Generator B Tubes Exceeded 40% Plugging Limit During Eddy Current Exam on 821026-30.Cause Not Stated.Tubes Mechanically Plugged ML20028B4151982-11-15015 November 1982 LER 82-017/01T-0:on 821030,four Tubes in Steam Generator a & Three Tubes in Steam Generator B Indicated Degradation Greater than 40% Plugging Limit.Caused by Intergranular Attack.Tubes Mechanically Plugged ML20028A0371982-11-0505 November 1982 LER 82-008/03L-0:on 821006,low Steam Line Pressure Setting for Pressure Instrument 2PT-478 Found Lower than Allowed by Tech Specs.Caused by Bumping of Setpoint Adjustment Knob.Instrument Tested & Realigned ML20027D6821982-11-0303 November 1982 LER 82-018/01T-0:on 821015,incorrect Instrument Bus Supply Shifted to Alternate Supply Following Rept of Fire in Supply Breaker for 1GYO4 Motor Generator Set,Causing Loss of Redundancy on Containment Pressure Indicator 1PT-950 ML20052G4501982-05-12012 May 1982 LER 82-002/01T-0:on 820428,during Eddy Current Exam, Discovered Abnormal Degradation in Fuel Cladding,Rcpb & Primary Containment.Seludge Lancing Will Be Performed ML20052G3701982-05-0707 May 1982 LER 82-009/03L-0:on 820408,4.16-kV Safeguards Undervoltage Relays Did Not Meet 0-volt Time Delay Spec.Caused by Manufacturer Characteristic Curves.Relays Not Capable of Less than 0.38-s.Tech Spec Change Requested on 820427 ML20052G3831982-05-0707 May 1982 LER 82-011/03L-0:on 820415,during Biweekly Calibr Check ICP 2.1 of Reactor Protective Sys Functions,Overpower Delta T Setpoint 2 for Channel 2 Found Less Conservative than Tech Spec Limit.Caused by Setpoint Drift in Impulse Summer Unit ML20052G6331982-05-0707 May 1982 LER 82-010/03L-0:on 820414,ICP 2.9 Found Not to Provide for Proper Unblocking of Source Range High Flux Reactor Trip Over Small Range of Instrument Readings.Caused by Failure to Identify Subtle Procedural Flow.Procedure to Be Revised ML20052B4521982-04-23023 April 1982 LER 82-008/03L-0:on 820323,minor Installation Defects Noted on Four of Six Containment Pressure Transmitters Installed as TMI Response Mod.Caused by Backfit Contractor QC Program Breakdown ML20050B2661982-03-25025 March 1982 LER 82-006/01T-0:on 820311,type B & C Valve Leakage Tests Exceeded Tech Spec Limits.Caused by Corrosion.Svc Air Check Valves Disc Replaced & Valve Cover Remachined ML20041F4861982-03-0808 March 1982 LER 82-005/01T-01:on 820222,poison Test Samples & Two Fuel Assemblies W/Less than 1-yr Cooling Period Found Placed Next to Divider Wall in Spent Fuel Pool.Caused by Tech Spec Misinterpretation ML20041E4911982-03-0404 March 1982 LER 82-004/03L-0:on 820206,during Inservice Testing, Differential Pressure Instrument 4007 for Auxiliary Feed Pump P38A Found Isolated.Probably Caused by Failure to Return Instrument to Svc Following Calibr ML20041E6131982-03-0202 March 1982 LER 82-003/01T-0:on 820217,during Surveillance Testing, Emergency Diesel Generator 3D Failed to Operate.Caused by Sticking Shutdown Solenoid Plunger on Woodward Type UG8 Governor.Solenoid Cleaned,Checked & Generator Tested ML20049H6981982-02-23023 February 1982 LER 82-001/03L-0:on 820203,boric Acid Heat Tracing Circuit P-42 Found Inoperable.Caused by Failed Thermon Type 4 Circuit Controller.Circuit Controller Replaced ML20040G6811982-02-0505 February 1982 LER 82-001/03L-0:on 820107,steam Generator Pressure Sensing Lines Discovered Frozen on a Steam Generator.Caused by Inadequate Freeze Protection & Extremely Cold Weather.Addl Heat Lamps Installed ML20040G5801982-02-0505 February 1982 LER 82-002/03L-0:on 820112,during Hot shutdown,1PT-469 Steam Generator Pressure Transmitter Isolated by Maint Personnel Due to Leaking Coupling.Pressure Sensing Tubing Showed Signs of Steam Leak Due to Freezing ML20040D3791982-01-18018 January 1982 LER 81-020/03L-0:on 811219,frozen Sensing Line Caused High Indication of Steam Generator Pressure Instrument 1PT-482. Caused by Incomplete Insulation of Line & by Cold Weather. Instrument Placed in Tripped Position & Tubing Thawed 1994-04-22
[Table view] Category:RO)
MONTHYEARML20024J2471994-10-0606 October 1994 LER 94-009-00:on 940909,EDG G-02 Inadvertently Started & Station Battery Charger D-08 Tripped Off Due to Blown Fuse. Caused by Inadequate Procedure.Blown Fuse Replaced & Electrical Distribution Sys Restored to normal.W/941006 Ltr ML20029C8511994-04-22022 April 1994 LER 94-001-00:on 940323,identified That Feedwater Flow May Have Been Underestimated Since Beginning of Operating Cycle. Caused by Degradation of Signals from Transducers.Transducer replaced.W/940422 Ltr ML20044E5571993-05-17017 May 1993 LER 92-009-01:on 921012,identified That Ccws Surge Tank Vent Valves Outside Design Basis Due to Oversight During Original Design of CCW Sys.Proposes to Replace Radiation Detector & Associated Circuitry W/Dedicated safety-related Sys ML20044E6221993-05-17017 May 1993 LER 93-006-00:on 930416,discovered That Outside CIV Not Leak Tested,Per TS 15.4.4.III.D Requirements Due to Review on 840202,recommending That Valve Be Tested During RHR Hydrostatic Testing.Subj Valve replaced.W/930517 Ltr ML20044D8811993-05-14014 May 1993 LER 93-005-00:on 930415,containment Accident Fan Time Delay Relay 1-TDR-26 (Turbine Bldg Cooler Svc Water Inlet Valve 1SW-2880) Unexpectedly Closed.Caused by Failure to Recognize Presence of Relay in Contact.Function Changed ML20044D2061993-05-10010 May 1993 LER 93-003-00:on 930328,Point Beach Unit 2 Tripped Due to Surveillance Testing Problems.Test Procedures Can Trip Unit Due to Equipment or Human Failure.Failure Tests Delayed Until Unit 1 & Knpp Restored to power.W/930510 Ltr ML20024H2151991-05-21021 May 1991 LER 91-003-00:on 910429,charging Sys Check Valve 1-370 Discovered W/Leakage in Excess of Limits Due to Worn Disc Arm Bushing Steps.Worn Disc Arm Bushing Steps Cladded W/ E308 Weld Matl & Hand Filed to Design contour.W/910521 Ltr ML20029C2101991-03-20020 March 1991 LER 91-002-01:on 901009,inadvertent Start of Auxiliary Feedwater Pump Occurred.Caused by Inadequate Test Procedures.Auxiliary Feedwater Pump Secured & Maint Work Request Mwr 904517 initiated.W/910320 Ltr ML20029C1141991-03-12012 March 1991 LER 91-010-01:on 900816,axial Flux Differential Outside Tech Specs Limits Due to Malfunction of Turbine Electrohydraulic Governor Control.Operator Training Revised. W/910319 Ltr ML20028H0321990-09-27027 September 1990 LER 90-011-00:on 900829,low Net Positive Suction Head to Containment Spray Pumps W/Eccs in Recirculation Mode Occurred.Caused by Procedural Deficiency.Temporary Procedure Changes initiated.W/900927 Ltr ML20043G2011990-06-0808 June 1990 LER 90-005-00:on 900510,steam Generator lo-lo Level Reactor Trip Occurred During Cold Shutdown.Caused by Inadequate Warning Sign Posting.Nonconformance Rept Written to Document Event & Recommend evaluation.W/900608 Ltr ML20042G7761990-05-0909 May 1990 LER 90-003-00:on 900409,determined That Piping & Supports in Fuel Oil Pumphouse Could Not Be Demonstrated to Perform Support Functions.Caused by Design Base Not Sufficiently Documented.Mod Performed to Support Fuel Oil Piping ML20042G7791990-05-0808 May 1990 LER 90-004-00:on 900404,single Failure Potential in Safeguards Switchgear B03/B04 Tie Breaker Discovered & Could Have Resulted in Failure of Diesel Generator.Control Power Fuses for Tie Breakers Removed ML20042F5361990-05-0404 May 1990 LER 90-001-00:on 900405,auxiliary Feed Pump Inadvertently Started.Caused by Inadequate Design.Schematic Push to Test Lamp Circuitry Will Be Added to Elementary Wiring Diagrams & Personnel Briefed on Potential circuitry.W/900504 Ltr ML20042F1971990-05-0202 May 1990 LER 90-002-00:on 900402,main Steam Safety Valve 1-MS-2013 Failed to Relieve Setpoint During Tech Spec Testing.Caused by Personnel Error During Setpoint Adjustment.Safety Valves 1-MS-2011,1-MS-2006 & 1-MS-2008 restored.W/900502 Ltr ML20011D5131989-12-19019 December 1989 LER 89-010-00:on 891120,auxiliary Feedwater Flow Transmitters Inadvertently Isolated.Caused by Error in Approved Procedure & Personnel Cognitive Error.Unit 1 Transmitters Valved Back Into Svc immediately.W/891219 Ltr ML19351A6721989-12-15015 December 1989 LER 89-009-00:on 891115,unexpected Steam Generator a lo-lo Level & Steam Generator B lo-lo Level Reactor Trip Signals Experienced.Caused by Installation of Analog Signal Generator.Procedures revised.W/891215 Ltr ML19332F7011989-12-11011 December 1989 LER 89-008-01:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power.Caused by Less than Adequate Tech Spec Change.Power Descension to 38% initiated.W/891211 Ltr ML19332E7221989-12-0707 December 1989 LER 89-009-00:on 891107,D05 & D06 Station Batteries Declared Inoperable.Caused by Original Design Deficiency.Mod Completed to Restore Battery D05 to Operable Status by Replacing Eight nonsafety-related breakers.W/891207 Ltr ML19332E8921989-12-0404 December 1989 LER 89-008-00:on 891103,during Refueling,Contractor Personnel Generated False Trip Signal While Investigating Wiring Discrepancy in Reactor Protection Sys Instrument Racks.Caused by Labeling Error.Supply changed.W/891204 Ltr ML19332F0901989-11-28028 November 1989 LER 89-003-01:on 890712,tank B Level Channel 2LE-934 Began to Indicate Spuriously.Caused by Moisture Intrusion Between Halar Insulator & Sensing Rod.Level Detector Replaced & Channel Reestablished for Accumulator Tank B.W/891128 Ltr ML19332C8411989-11-22022 November 1989 LER 89-007-00:on 891027,Train a Safety Injection Signal Generated During Installation of Mod in Containment High Pressure Circuit.Caused by Inadequate Installation Procedure.Procedure changed.W/891122 Ltr ML19327C2001989-11-14014 November 1989 LER 89-006-01:on 891015,steam Generator Tubes Found Degraded,W/Undefined Signal & W/Axial Indications in Tubesheet Area.Degradation Caused by Time.Affected Tubes Plugged or Preventively sleeved.W/891114 Ltr ML19327C0651989-11-0606 November 1989 LER 89-005-00:on 891006,intermediate Range High Level Trip Signal Unexpectedly Generated During Course of Routine Source Range Channel Calibr.Caused by Loose Connection of Input/Output Cable.Connection tightened.W/891106 Ltr ML19327B3061989-10-19019 October 1989 LER 89-008-00:on 890910,ATWS Mitigating Actuation Circuitry Automatically Bypassed at About 42% Reactor Power, Disenabling Sys.Caused by High Tech Spec Setpoint.Enable/ Disable Setpoint Reset to 30%.W/891019 Ltr ML18041A1611987-11-16016 November 1987 LER 87-004-01:on 870515,voltage Lost on Red Instrument Bus Resulting in Reactor Protection Sys Actuation.Caused by Excessive Current Demand by ferro-resonant Circuit.Plant Mods to Load Bank Proposed ML18041A1341986-07-0303 July 1986 LER 86-003-00:on 860603,reactor Trip Occurred Due to Loss of Power on White Instrument Bus.Caused by Trip of White Inverter Output Breaker.Procedures for Placing Inverter on Line Will Be revised.W/860703 Ltr ML20028E3551983-01-13013 January 1983 LER 82-029/03L-0:on 821216,automatic Monitoring & Alarm Program Constant Found Incorrect.Caused by Unknown Personnel W/Access to on-line Computer.Value of Constant Restored & Control Rods Alignment Verified ML20028E2381983-01-13013 January 1983 LER 82-028/03L-0:on 821215,routine Test on Fire Detection Sys Found Panel D407 Which Monitors Unit 1 Rod Drive Room Inoperable.Caused by Blown Fuse.Fuse & Indication Lights Replaced on 821215.Detection Sys Undergoing Design Review ML20028E1791983-01-13013 January 1983 Updated LER 82-020/01X-1:on 821102,while Performing Type B & C Leakage Tests of Containment Penetrations & Isolation Valves,One Valve Had Leakage Exceeding Limit.Cause Not Stated.Valve Clapper & Seat Lapped ML20028E3031983-01-11011 January 1983 LER 82-027/03L-0:on 821211,operator Noted That Steam Generator Pressure Transmitter 1PT-469 Indicated Higher than Other Channels.Caused by Frozen Sensing Line Due to Inadequate Interim Piping Insulation ML20028E3211983-01-10010 January 1983 Updated LER 82-017/01X-2:on 821030,w/unit Shut Down for Refueling,Eddy Current Exam of Steam Generator Tubes Indicated Four Tubes in Steam Generator a & Three Tubes in Steam Generator B Exceeded Plugging Limit.Caused by Caustic ML20028C2431982-12-27027 December 1982 LER 82-020/01T-0:on 821103,following Type B & C Leak Rate Tests,Total as-measured Leakage Exceeded Tech Spec Limit, Causing Reactor Coolant Pump Component Cooling Water to Have Excessive Leakage.Cause Not Stated.Clapper & Seat Lapped ML20023B3251982-12-10010 December 1982 Updated LER 82-017/01T-1:on 821030,verified That Indications for Four Steam Generator a Tubes & Three Steam Generator B Tubes Exceeded 40% Plugging Limit During Eddy Current Exam on 821026-30.Cause Not Stated.Tubes Mechanically Plugged ML20028B4151982-11-15015 November 1982 LER 82-017/01T-0:on 821030,four Tubes in Steam Generator a & Three Tubes in Steam Generator B Indicated Degradation Greater than 40% Plugging Limit.Caused by Intergranular Attack.Tubes Mechanically Plugged ML20028A0371982-11-0505 November 1982 LER 82-008/03L-0:on 821006,low Steam Line Pressure Setting for Pressure Instrument 2PT-478 Found Lower than Allowed by Tech Specs.Caused by Bumping of Setpoint Adjustment Knob.Instrument Tested & Realigned ML20027D6821982-11-0303 November 1982 LER 82-018/01T-0:on 821015,incorrect Instrument Bus Supply Shifted to Alternate Supply Following Rept of Fire in Supply Breaker for 1GYO4 Motor Generator Set,Causing Loss of Redundancy on Containment Pressure Indicator 1PT-950 ML20052G4501982-05-12012 May 1982 LER 82-002/01T-0:on 820428,during Eddy Current Exam, Discovered Abnormal Degradation in Fuel Cladding,Rcpb & Primary Containment.Seludge Lancing Will Be Performed ML20052G3701982-05-0707 May 1982 LER 82-009/03L-0:on 820408,4.16-kV Safeguards Undervoltage Relays Did Not Meet 0-volt Time Delay Spec.Caused by Manufacturer Characteristic Curves.Relays Not Capable of Less than 0.38-s.Tech Spec Change Requested on 820427 ML20052G3831982-05-0707 May 1982 LER 82-011/03L-0:on 820415,during Biweekly Calibr Check ICP 2.1 of Reactor Protective Sys Functions,Overpower Delta T Setpoint 2 for Channel 2 Found Less Conservative than Tech Spec Limit.Caused by Setpoint Drift in Impulse Summer Unit ML20052G6331982-05-0707 May 1982 LER 82-010/03L-0:on 820414,ICP 2.9 Found Not to Provide for Proper Unblocking of Source Range High Flux Reactor Trip Over Small Range of Instrument Readings.Caused by Failure to Identify Subtle Procedural Flow.Procedure to Be Revised ML20052B4521982-04-23023 April 1982 LER 82-008/03L-0:on 820323,minor Installation Defects Noted on Four of Six Containment Pressure Transmitters Installed as TMI Response Mod.Caused by Backfit Contractor QC Program Breakdown ML20050B2661982-03-25025 March 1982 LER 82-006/01T-0:on 820311,type B & C Valve Leakage Tests Exceeded Tech Spec Limits.Caused by Corrosion.Svc Air Check Valves Disc Replaced & Valve Cover Remachined ML20041F4861982-03-0808 March 1982 LER 82-005/01T-01:on 820222,poison Test Samples & Two Fuel Assemblies W/Less than 1-yr Cooling Period Found Placed Next to Divider Wall in Spent Fuel Pool.Caused by Tech Spec Misinterpretation ML20041E4911982-03-0404 March 1982 LER 82-004/03L-0:on 820206,during Inservice Testing, Differential Pressure Instrument 4007 for Auxiliary Feed Pump P38A Found Isolated.Probably Caused by Failure to Return Instrument to Svc Following Calibr ML20041E6131982-03-0202 March 1982 LER 82-003/01T-0:on 820217,during Surveillance Testing, Emergency Diesel Generator 3D Failed to Operate.Caused by Sticking Shutdown Solenoid Plunger on Woodward Type UG8 Governor.Solenoid Cleaned,Checked & Generator Tested ML20049H6981982-02-23023 February 1982 LER 82-001/03L-0:on 820203,boric Acid Heat Tracing Circuit P-42 Found Inoperable.Caused by Failed Thermon Type 4 Circuit Controller.Circuit Controller Replaced ML20040G6811982-02-0505 February 1982 LER 82-001/03L-0:on 820107,steam Generator Pressure Sensing Lines Discovered Frozen on a Steam Generator.Caused by Inadequate Freeze Protection & Extremely Cold Weather.Addl Heat Lamps Installed ML20040G5801982-02-0505 February 1982 LER 82-002/03L-0:on 820112,during Hot shutdown,1PT-469 Steam Generator Pressure Transmitter Isolated by Maint Personnel Due to Leaking Coupling.Pressure Sensing Tubing Showed Signs of Steam Leak Due to Freezing ML20040D3791982-01-18018 January 1982 LER 81-020/03L-0:on 811219,frozen Sensing Line Caused High Indication of Steam Generator Pressure Instrument 1PT-482. Caused by Incomplete Insulation of Line & by Cold Weather. Instrument Placed in Tripped Position & Tubing Thawed 1994-04-22
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARNPL-99-0569, Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pbnp,Units 1 & 2. with ML20212D5961999-09-15015 September 1999 Safety Evaluation Supporting Licensee IPEEE Process.Plant Has Met Intent of Suppl 4 to GL 88-20 NPL-99-0051, Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Pbnp,Units 1 & 2. with NPL-99-0449, Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pbnp,Units 1 & 2. with ML20196J4251999-06-30030 June 1999 Safety Evaluation Authorizing Proposed Alternatives Described in Relief Requests VRR-01,ROJ-16,PRR-01 & VRR-02 ML20209D2691999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pbnps,Units 1 & 2 ML20196F3341999-06-22022 June 1999 Safety Evaluation for Implementation of 422V+ Fuel Assemblies at Pbnp Units 1 & 2 ML20195F9781999-06-10010 June 1999 Unit 2 Refueling 23 Inservice Insp Summary Rept for Form NIS-1 ML20209D2751999-05-31031 May 1999 Revised MORs for May 1999 for Pbnps,Units 1 & 2 NPL-99-0328, Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pbnp,Units 1 & 2. with NPL-99-0273, Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Point Beach Nuclear Plant,Units 1 & 2.With ML20196F3521999-04-30030 April 1999 Non-proprietary WCAP-14788, W Revised Thermal Design Procedure Instrument Uncertainty Methodology for Wepc Point Beach Units 1 & 2 (Fuel Upgrade & Uprate to 1656 Mwt - NSSS Power) NPL-99-0193, Monthly Operating Repts for Mar 1999 for Pbnp,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pbnp,Units 1 & 2. with NPL-99-0134, Monthly Operating Repts for Feb 1999 for Pbnp,Units 1 & 2. with1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Pbnp,Units 1 & 2. with ML20207D6751999-02-22022 February 1999 Assessment of Design Info on Piping Restraints for Point Beach Nuclear Plant,Units 1 & 2.Staff Concludes That Licensee Unable to Retrieve Original Analyses That May Have Been Performed to Justify Removal of Shim Collars ML20206R9001999-01-13013 January 1999 SER Accepting Nuclear Quality Assurance Program Changes for Point Beach Nuclear Plant,Units 1 & 2 NPL-99-0008, Monthly Operating Repts for Dec 1998 for Pbnp,Units 1 & 2. with1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Pbnp,Units 1 & 2. with NPL-99-0091, 1998 Annual Results & Data Rept for Pbnps,Units 1 & 2. with1998-12-31031 December 1998 1998 Annual Results & Data Rept for Pbnps,Units 1 & 2. with ML20198C7671998-12-10010 December 1998 Safety Evaluation Accepting Licensee Proposed Alternative to ASME BPV Code,1986 Edition,Section XI Requirement IWA-2232, to Use Performance Demonstration Initiative Program During RPV Third 10-yr ISI for Plant,Unit 2 NPL-98-1006, Monthly Operating Repts for Nov 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Point Beach Nuclear Plant,Units 1 & 2.With ML20195J5101998-11-16016 November 1998 Proposed Revs to Section 1.3 of FSAR for Pbnp QA Program ML20198J5941998-11-0303 November 1998 1998 Graded Exercise,Conducted on 981103 NPL-98-0948, Monthly Operating Repts for Oct 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Point Beach Nuclear Plant,Units 1 & 2.With NPL-98-0880, Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored1998-10-21021 October 1998 Special Rept:On 980913,fire Alarm Control Panels Inoperable for More That Fourteen Days.Troubleshooting of D-401 Panel Following Installation of Replacement Batteries Revealed No Apparent Cause for Spurious Alarms.Panel D-401 Restored ML20154M9121998-10-14014 October 1998 Unit 1 Refueling 24 Repair/Replacement Summary Rept for Form NIS-2 ML20154L6751998-10-14014 October 1998 Unit 1 Refueling 24 ISI Summary Rept for Form NIS-1 NPL-98-0826, Monthly Operating Repts for Sept 1998 for Point Beach Nuclear Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Point Beach Nuclear Plant,Units 1 & 2.With ML20151W3851998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Pbnp Units 1 & 2 NPL-98-0653, Monthly Operating Repts for July 1998 for Point Beach Nuclear Plant,Units 1 & 21998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W4471998-07-31031 July 1998 Corrected Page to MOR for July 1998 for Pbnp Unit 2 ML20151W4541998-07-31031 July 1998 Corrected Page to MOR for July 1998 for Pbnp Unit 1 ML20236Q3161998-07-10010 July 1998 Safety Evaluation Accepting Licensee Proposed Alternative to ASME Code Requirements PTP-3-01 & PTP-3-02 ML20236L6771998-07-0707 July 1998 Safety Evaluation Approving Wepco Implementation Program to Resolve USI A-46 at Point Beach NPP Units 1 & 2 NPL-98-0558, Monthly Operating Repts for June 1998 for Pbnp,Units 1 & 21998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Pbnp,Units 1 & 2 ML20151W4261998-06-30030 June 1998 Corrected Page to MOR for June 1998 for Pbnp Unit 2 ML20151W4221998-05-31031 May 1998 Corrected Page to MOR for May 1998 for Pbnp Unit 2 NPL-98-0481, Monthly Operating Repts for May 1998 for Point Beach Nuclear Plant,Units 1 & 21998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W4011998-04-30030 April 1998 Corrected Page to MOR for April 1998 for Pbnp Unit 2 NPL-98-0356, Monthly Operating Repts for April 1998 for Point Beach Nuclear Plant,Units 1 & 21998-04-30030 April 1998 Monthly Operating Repts for April 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20217F3131998-04-17017 April 1998 Safety Evaluation Accepting Proposed Alternative to ASME Code for Surface Exam of Nonstructural Seal Welds,For Plant, Unit 1 ML20216D7071998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W3981998-03-31031 March 1998 Corrected Page to MOR for March for Pbnp Unit 2 NPL-98-0209, Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable1998-03-30030 March 1998 Special Rept Re Fire Barrier Inoperable for Greater than Seven Days.Compensatory Measures Implemented in Accordance W/Fire Protection Program Requirements During Time That Barriers Were Inoperable ML20217A8501998-03-19019 March 1998 SER Accepting Proposed Changes Submitted on 980226 by Wiep to Pbnp Final SAR Section 1.8 Which Will Impact Commitments Made in Pbnp QA Program Description.Changes Concern Approval Authority for Procedures & Interviewing Authority ML20216J0101998-03-17017 March 1998 Safety Evaluation Accepting Third 10-yr Inservice Insp Interval Relief Request RR-1-18 for Plant NPL-98-0159, Monthly Operating Repts for Feb 1998 for Point Beach Nuclear Plant,Units 1 & 21998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20151W3891998-02-28028 February 1998 Corrected Page to MOR for Feb 1998 for Pbnp Unit 2 ML20216D7121998-02-28028 February 1998 Revised Corrected MOR for Feb 1998 for Point Beach Nuclear Plant,Unit 2 NPL-98-0084, Monthly Operating Repts for Jan 1998 for Point Beach Nuclear Plant,Units 1 & 21998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Point Beach Nuclear Plant,Units 1 & 2 ML20198L1151998-01-0808 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Point Beach Nuclear Plant,Units 1 & 2 1999-09-30
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NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION 87-7 M LICENSEE EVENT REPORT CONTROL BLOCK; l 6
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(PLE ASE PRINT OR TYPE ALL REQUIRED INFORMATION)
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DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h O 2 l Steam generator tube eddy current testing during refueling seven l gl and completed 11-3-79 revealed 69 defective tubes in the "A" steam l o A l generator and 62 defactive tubes in the "B". All but five of the l n s I defects were in the tubesheet crevice region and all were on the inlet l 1016l side. 100% of the inlet sides of the tubes in both generators were l l0 l7l j examined up to the first support by multifrequency eddy current l o a;; techniques. This event is reportable per T.S. 15.6.9.2.A.3 and similar to 7 8 9 prev 10uS Lt.KS . 80 SYSTEM CAUSE CAUSE COMP. VAtyg CODE CODE SU8 CODE COMPON ENT CODE SUSCODE SU8 CODE
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43 lWl1l2l0lg 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i o l Three inlet tubesheet samples of tubing were removed for metallurgical li til l evaluation. Plugs were welded in the three tubesheet holes. The
, 7 l defective tubes were explosively plugged. Also explosively plugged i 3 l after leak testing were two dripping tubes in the "B" steam generator ml and one in the "A" steam generator. l 7 8 9 80 SA S % POWER OTHER STATUS DIS O RY DISCOVERY DESCRIPTION i s
[H_J@ l1 l 0 l 0 l@l N/A l l C l@l Eddy current testing l ACTIVITY CO TENT RELE ASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELE ASE 1 6
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NAME OF PREPARER Sol Burstein PHONE:
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i ATTACHMENT TO LICENSEE EVENT REPORT NO. 79-017/OlT-0 Wisconsin Electric Power Company Point Beach Nuclear Plant Unit 1 Docket 50-266 Steam generator tube eddy current testing was conducted in both steam generators on October 16 and 18, 1979, for further evaluation of certain tubes examined during an outage in August 1979. A post outage review of the August 100% eddy current inspec-tion, a 400 KHz program, had raised questicus on a number of tubes which it was felt should be verified by an additional multifrequency inspection. Thirty-eight (38) tubes were inspected in the hot legs of both steam generators.
Of the 38 tubes inspected in the "A" steam generator, 12 tubes were found defective. Of the tubes inspected in the "B" steam generator, six tubes were found defective. All defects found were located in the tubesheet region.
The tube at position R15C45, one of the defective tubes in the "A" steam generator, was chosen to be removed for metallur-gical evaluation.
While doing profilometry inspections of the tubes adjacent to R15C45 prior to its removal, a defect was found in a tube which had not been part of the original sample program. Discovery of this additional defective tube required an expanded inspection program in accordance with Technical Specification Table 15.4.2-1.
Prior to commencing the expanded eddy current inspection, the tube at position R15C45 in the "A" hot leg was cut just below the second support plate and removal procedures began on October 20.
With pulling pressures up to 25,380 pounds and several equipment failures, five pieces of tube totalling approximately 21 inches in length were removed on October 21 and 22.
An examination of the tube portions, plus a later eddy current probe verification, indicated that the pulling operation had broken off the tube at a known defect, approximatel; one inch below the top of the tubesheet.
Following completion of the removal of the sections of tube from R15C45, a 2S (approximately 199) tube sample eddy current inspection was commenced in the "A" hot leg on October 23. The analysis of the 199 tubes determined that 28 of the tubes were defective. All defects in the tubes were located within the tube-sheet. The inspection program was again expanded in accordance with Technical Specification Table 15.4.2-1 to 100% of the tubes in the "A" inlet. This also required that an eddy current program be conducted in the "B" steam generator.
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The 100% multifrecuency eddy current inspection in the "A" inlet commenced on Octcaer 24 and was completed on October 27.
The analysis of the eddy current data showed 69 tubes with defects
>40% which would require plugging of the tubes. See Table 1 for details.
Following completion of eddy current testing in the "A" steam generator inlet, a decision was made to remove two additional tube samples from the generator. The first of the two tubes was chosen as a good tube from an area where no deep crevice tubesheet defects were evident. The tube at position R20C73 was cut just below the second support plate on October 28 and four pieces of tube totalling over 140 inches were removed on October 29. The breaking force for this tube was 10,400 pounds, the pulling force varied between 3,000 and 1,500 pounds.
The final tube to be removed was chosen as a good tube with no previous defects located in an area of the tube bundle where numerous deep crevice defects have been found. This tube at position R22C37 was cut just below the first support plate on October 29. The tube broke loose at a loading of 25,380 pounds on October 30 and three sections totalling 74 inches were removed on October 31. After breaking loose, the pulling force varied between 4,400 and 10,000 pounds during this operation.
The holes from which the three tubes were removed from the "A" inlet were weld repaired on November 2 and 3. Prior to the weld plugging of the hole at R15C45, a stabilizing rod was inserted 132 inches up into the tube to tie the tube which was cut just below the second support plate, but broken off one inch below the tubesheet top, to form a single member with the original tube and tubesheet hole.
The 2S (approximately 199 tube) multifrequency eddy current inspection of the "B" hot leg was commenced on October 29 and was completed on November 3. The analysis of the eddy current data showed 62 tubes with defects greater than 40%, which would reauire the tubes to be plugged. See Table 2 for details.
Prior to explosive plugging, an 800 psi secondary side leak test was performed on the "B" steam generator on November 5 to determine if any of the 90% (plus) defective tubes would leak or if other leaks could be generated by the test. Seven leaks were identified. Four of the leaks were leaking plugs in previously explosively plugged tubes, the other three being tube leaks. Of the tubes identified as leaking, one was previously identified as defective during the eddy current program; two tubes with extremely small leaks, in the range of one drip every ten seconds, were not identified as defective by the eddy current program.
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The four leaking plugs were weld repaired in the "B" inlet during the week of November 5. The defective tubes totalling 67 were explosively plugged during the period between November 6 and 8.
In summary, a total of 68 tubes were plugged in the "B" steam generator on the above dates: 62 tubes had defects greater than 40%; three tubes had defects less than 40%, but were plugged as a conservative measure; two tubes were found leaking during the leak test; and one tube, a sound tube, was plugged by mistake. See Table 2 for details.
An 800 psi secondary side leak test was scheduled to be performed in the "A" steam generator on November 7. Preparations for the leak test were terminated abruptly during the initial filling of the generator when water was found to be issuing from a tube directly over the cold leg manway and out the manway. It was immediately recognized that a scheduling error had been made in that the "A" steam generator should not have been filled prior to explosive plugging the outlet side of the tubes opened up ta the cold leg side by removal of the three sample tube lengths on the hot leg side. For further details, reference Licensee Event Report No. 79-019/0lT-0, " Inadvertent Reactor Coolant System Dilution During Refueling Shutdown". The outlet tube ends were explosively plugged on November 8.
The 800 psi secondary side leak test was performed in the "A" steam generator on November 9 prior to explosive plugging of the defective tubes. One leaking tube (R24C32) was noted which had been previously identified as having a 92% defect by eddy current testing.
Explosive plugging of the defective tubes in the "A" steam generator on November 12 revealed one additional leaking tube (one drip every 20 seconds), R29C25, with 0% defect indicated during the eddy current program. This final tube was plugged on November 12.
In summary, a total of 77 tubes were explosively plugged in the "A" steam generator: 69 tubes had defects greater than 40%;
three tubes had defects less than 40%, but were plugged as a conser-vative measure; two tubee were plugged by mistake; one tube was identified as a leaker. Two good tubes were plugged because of the dbove described tube removal program. See Table 1 for details.
This event is reportable per Technical Specification 15.6.9.2.A.3.
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TABLE 1 Plugged Tubes with Defects $40%
Tube % Defect Location R18C24 84% 18" above tube end R24C32 91% 5" above tube end R09C24 93% 11" above tube end R10C41 94% 18" above tube end R10C42 95% 21" above tube end R22C41 87% 21", 15" and 5" above tube end R15C45 89% 20" above tube end R23C62 89% 7" above tube end R19C54 83% 20" above tube end R19C53 92% 20" above tube end R12C54 92% 20" above tube end R12C55 93% 18" above tube end R08C53 93% 20" above tube end R12C53 71% 17" above tube end R13C53 75% 20" above tube end R09C51 89% 20" above tube end R13C50 95% 20" above tube end R05C50 90% 11" above tube end R13C49 92% 20" above tube end R15C49 88% 21" above tube end R19C49 91% 20" above tube end R15C47 92% 20" above tube end R10C46 96% 20" above tube end R10C45 93% 20" above tube end R17C45 92% 20" above tube end R19C45 90%-81% 20", 21" above tube end R15C44 97% 21" above tube end R12C44 84% 12" above tube end R23C41 80% 6" above tube end R27C40 81% 20" above tube end R24C40 93% 4" to 12" above tube end R23C39 65% 5" above tube end R27C39 59% 21" above tube end R23C37 87% 10" above tube end R24C36 82% 6" above tube end R22C36 76% 11" above tube end R27C35 90% 21" above tube end R23C33 89% 3" to 8" above tube end R20C32 42% 20" above tube end R08C43 82% 15" above tube end RllC37 88% 17" above tube end R03C36 91% 10" above tube end R13C26 95% 16" above tube end RllC26 58% 19" above tube end R20C25 92% 17" above tube end R21C45 79% 21" above tube and R22C46 55% Top of tubesheet R29C46 84% 21" above tube end j437 320 Table 1 Page 2 Tube % Defect Location R20C40 99% 19" to 21" above tube end R30C53 65% 14" above tube end R17C53 73% 15" above tube end R15C51 81% 20" above tube end R05C56 87% 10" above tube end R30C57 80% Top of tubesheet R17C57 76% 8" above tube end R09C57 71% 20" above tube end R15C58 85% 18" above tube end R05C59 97% 10" above tube end R15C61 73% 17" above tube end R13C61 94% 19" above tube end R13062 81% 21" above tube end R14C62 95% 15" above tube end R13C63 96% 21" above tube end R12C63 76% 21" above tube end R13C64 91% 17" above tube end R23C64 72% 19" above tube end R13C65 92% 19" above tube end R05C76 85% 8" above tube end R15C62 94% 20" above tube end Tubes Plugged as Conservative Measure "A" Steam Generator R19C38 34% 8" above tube end R28C25 26% 14" above tube end R24C54 37% 21" above tube end Tubes Plugged by Mistake "A" St< tam Generator R24C30 R23C63 Tube Plugged - Leaker R29C25 i437 329
rY TABLE 2 Plugged Tubes with Defects >40%
Tube % Defect Location R14C61 86% 20" above tube end R14C48 86% 21" above tube end R23C43 63% 16" above tube end R24C30 90% 8", 14", 16" above tube end R06C39 90% 11" above tube end -
R06C35 87% 12" above tube end R22C31 90% 5" above tube end R20C32 89% 17" above tube end R23C32 94% 10" above tube end R22C33 78% 20" above tube end R25C38 90% 6" above tube end R23C41 87% 3" to 11" above tube end R12C43 91% 21" above tube end R24C45 84% 6" above tube end R23C45 73% 6" to 8" above tube end R22C45 92% 15" above tube end R14C46 93% 21" above tube end R24C46 75% 13" above tube end R26C54 93% 20" above tube end R09C16 83% 3" to 8" above tube end RllC18 83%, 92% 15" and 18" above tube end R04C19 77% 8" above tube end R11C24 73% 20" above tube end R17C27 78% 11" above tube end R12C27 72% 20" above tube end R06C27 64% 20" above tube end R11C29 85% 21" above tube end RllC30 92% 21" above tube end R13C30 53% 21" above tube end R13C31 92% 19" above tube end R04C32 76% 6" above tube end R09C33 86% 14" above tube end R27C36 95% 5" above tube end R04C37 90% 4" above tube end ..
R28C38 45% Top of tubesheet R09C39 62% 19" above tube end R08C39 95% 8" to 13" above tube end R32C42 61% " above tubesheet R29C44 65%, 50%, 20", 10", 5" above tube end 90%
R30C44 83% Top of tubesheet R31C44 90% 3" to 13" above tube end R29C45 77% 11" above tube end R10C46 87% 20" above tube end R27C50 89% 3" to 15" above tube end R22C56 91% 10" to 15" above tube end R20C57 82% 17" above tube end R21C57 83% 6" above tube end 1437 330
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Table 2 Page 2 Tube % Defect Location R20C58 93% 14" to 21" above tube end R03C58 90% 3" above tube end R06C59 90% 15" above tube end R15C59 84% 20" above tube end R08C60 89% 10" above tube end R21C61 94% 5" to 10" above tube end R23C62 96% 5" above tube end R13C62 61% 20" above tube end R03C62 48% 15" above tube end R21C64 76% 7" above tube end R08C65 64% 12" above tube end R10C66 40% 13" above tube end R01C68 95% 11" above tube end R24C71 93% 5" above tube end R02C77 95% 3" above tube end Tubes Plugged as Conservative Measure "B" Steam Generator R25C36 32% 21" above tube end R13C39 36% 15" above tube end R13C59 36% 20" above tube end Tube Plugged by Mistake "B" Steam Generator R09C32 Tubes Plugged - Leakers R23C47 R20C39 Leaking Plugs Weld Repaired "B" Steam Generator (Inlet) -.
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(RE: These plugs inserted during previous outages.)
R22C41 R23C31 R23C50 R21C26 1437 331