LER-1979-056, /01X-1:on 790926,cabling Associated W/Hpci Sys Inboard Steam Supply Isolation Valve & Automatic Depressurization Sys (ADS) Did Not Meet NRC Separation Criteria.Caused by Proximity of HPCI & ADS Cables |
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POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR 00WER PLANT u
DOCKET N0. 50-333 ATTACHMENT TO LER 79-056/01X-1 Page 1 of 1 During normal operation, the plant staff was informed by the Architect-Engineer that certain cabling associated with the High Pressure Coolant Injection (HPCI) System inboard steam supply isolation valve and the Auto-matic Depressurization System (ADS) did not meet the separation criteria required by the Nuclear Regulatory Commission.
This discovery was made as a result of the Fire Hazard Analyses being conducted by the Architect-Engineer.
The six,(6) caQles in question which could affect the control of the inboard isolation valve for the HPCI System steam supply (23-MOV-15) are located in the same cable tray as some ADS cables.
Discovery of this condition is considered a reportable event under the circumstances described in Technical Specifications Appendix A, Paragraph 6.9.A.4.1.
The only manner in which improper operation or an undesired situation could result is an event which could cause simultaneous failure of both ADS and HPCI cables to the extent that both systems would be inoperable.
Initial corrective action (taken on September 26,1979) to preclude spuridus closure of 23-MOV-15, de-energized the vahe by racking out of the breaker.
In addition, to satisfy the requirements of primary con-tainment isolation, the outside isolation valve for the HPCI system (23-M0V-16) was maintained. in its normal closed position and checked daily as required by Technical Specifications Appendix A, Paragraph 3.7.1.
In addition, the Architect-Engineer informed the plant that other (third party) cables could affect the operation of 23-MOV-15 due to their proximity to both HPCI and ADS cables.
There are two alternate solutions to correct both cf the problems set forth above. One solution is to re-route the cables while the second solution is to install a redundant ADS control system. As a result of a detailed review of the alternatives, the cable re-routing option was selected and a preliminary design modification to re-route the cables of concern was completed during the week of November 12, 1979.
Further, the plant staff has also re-evaluated the initial corrective action takpn.
This re-evaluation indicated the preferred method of assuring operability of the systems ECCS and primary containment isolation functions would be to pro, vide augmented protection against a fire which might involve cables of both the s9 stems. Accordingly, the FitzPatrick Plant Staff initiated, on November 16, 1979, an hourly patrolling fire watch in those areas in which cabling for the HPCI and ADS are in proximity to each other and restored 23-MOV-15 to a fully operable condition.
This action of establishing an hourly patrolling fire watch parallels that required by Technical Specifications, Appendix A, Paragraph 3.12.E.1.b. when early warning protection against a potential fire must be taken due to inadequate or inoperable fixed detection systems.
With respect to the proposed design modification which will re-route certain cables associated with the HPCI system to provide diverse physical separation, the FitzPatrick Plant anticipates that implementation of the modifications will be completed as originally stated, during the forthcoming refueling outage.
In view of the actions noted above, the event does not represent a significant hazard to the public health and safety.
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| 05000333/LER-1979-001-03, /03L-0 on 790105:failure to Perform Core Performance Surveillance on 781210 & 781223.Currently Developing Surveillance Test Checkoff List,To Ensure That Test Is Not Overlooked Again | /03L-0 on 790105:failure to Perform Core Performance Surveillance on 781210 & 781223.Currently Developing Surveillance Test Checkoff List,To Ensure That Test Is Not Overlooked Again | | | 05000333/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000333/LER-1979-002-03, /03L-0 on 790108:flow Biased Portion of Average Power Range Monitor B Inoperable.Caused by Operational Amplifier Failure.Circuit Board Replaced | /03L-0 on 790108:flow Biased Portion of Average Power Range Monitor B Inoperable.Caused by Operational Amplifier Failure.Circuit Board Replaced | | | 05000333/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000333/LER-1979-003-03, /03L-0 on 790115:during Mainsteam Flow, Surveillance Procedure Instrument 02-DPIS-116B Found Set at 110 psid,2 Psid Above Tech Spec Max Due to Drift in Differential Pressure Switch | /03L-0 on 790115:during Mainsteam Flow, Surveillance Procedure Instrument 02-DPIS-116B Found Set at 110 psid,2 Psid Above Tech Spec Max Due to Drift in Differential Pressure Switch | | | 05000333/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000333/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000333/LER-1979-004-03, /03L-0 on 790119:while Performing Operations Surveillance Test F-St-76D,water Leak Noted on Post Indicator Valve 76-FPS-30 & Discovered Water Leaking from Lubrication Line.Caused by Shovel Cut During Snow Removal | /03L-0 on 790119:while Performing Operations Surveillance Test F-St-76D,water Leak Noted on Post Indicator Valve 76-FPS-30 & Discovered Water Leaking from Lubrication Line.Caused by Shovel Cut During Snow Removal | | | 05000333/LER-1979-005-04, /04L-0 on 790124: Apparent Excessive Solution Release from Makeup Water Treatment Waste Neutralizer Tanks to Circulating Water Discharge Tunnel Noted.Calculations Show Tech Specs Not Exceeded | /04L-0 on 790124: Apparent Excessive Solution Release from Makeup Water Treatment Waste Neutralizer Tanks to Circulating Water Discharge Tunnel Noted.Calculations Show Tech Specs Not Exceeded | | | 05000333/LER-1979-005, Forwards LER 79-005/04L-0 | Forwards LER 79-005/04L-0 | | | 05000333/LER-1979-006, Forwards LER 79-006/03X-1 | Forwards LER 79-006/03X-1 | | | 05000333/LER-1979-006-03, /03X-1:on 790124,during Normal Operations,Ground Fault on 125 Station Battery a Noted.Caused by Bellows Failure on Pressure Switch Circuit safety-relief Valve 02-RV-71J.Ground Cleared.Valve Restored to Operation | /03X-1:on 790124,during Normal Operations,Ground Fault on 125 Station Battery a Noted.Caused by Bellows Failure on Pressure Switch Circuit safety-relief Valve 02-RV-71J.Ground Cleared.Valve Restored to Operation | | | 05000333/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000333/LER-1979-007-03, /03L-0 on 790125:jet Pump Operability Surveillance Had Not Been Conducted on 790123-24 as Required.Procedures Subsequently Revised | /03L-0 on 790125:jet Pump Operability Surveillance Had Not Been Conducted on 790123-24 as Required.Procedures Subsequently Revised | | | 05000333/LER-1979-008-03, /03L-0 on 790125:core Performance Surveillance Not Done on 790120-22.Operations Surveillance Test for Daily Checks Was Being Developed to Include check-off of Surveillance Requirements.Caused by Operator Error | /03L-0 on 790125:core Performance Surveillance Not Done on 790120-22.Operations Surveillance Test for Daily Checks Was Being Developed to Include check-off of Surveillance Requirements.Caused by Operator Error | | | 05000333/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000333/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000333/LER-1979-009-03, /03L-0 on 790205:rod Control Drive Rendered Inoperable in Order to Repair Leak in Control Rod Drive Sys Hydraulic Control Unit.Upon Completion of Repair,All Components Returned to Svc | /03L-0 on 790205:rod Control Drive Rendered Inoperable in Order to Repair Leak in Control Rod Drive Sys Hydraulic Control Unit.Upon Completion of Repair,All Components Returned to Svc | | | 05000333/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000333/LER-1979-010-03, /03L-0 on 790202:step Increase in Indicated Core Flow.Caused by Earlier Failure of Square Root Computation Module for Jet Pump.Square Root Computation Module Replaced W/Identical Unit & Core Flow Evaluation Test Completed | /03L-0 on 790202:step Increase in Indicated Core Flow.Caused by Earlier Failure of Square Root Computation Module for Jet Pump.Square Root Computation Module Replaced W/Identical Unit & Core Flow Evaluation Test Completed | | | 05000333/LER-1979-011-03, /03L-0 on 790214:drywell Atmospheric Sample Isolation Valve 27-SOV-123B Blew a Fuse.Caused by Shorted Valve Solenoid.Incident Recurred 790306.Will Submit Followup Rept When Valve Replacement Is Completed | /03L-0 on 790214:drywell Atmospheric Sample Isolation Valve 27-SOV-123B Blew a Fuse.Caused by Shorted Valve Solenoid.Incident Recurred 790306.Will Submit Followup Rept When Valve Replacement Is Completed | | | 05000333/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000333/LER-1979-014, Forwards LER 79-014/01T-0 | Forwards LER 79-014/01T-0 | | | 05000333/LER-1979-014-01, /01T-0 on 790312:calculations in Piping Stress Analysis Are Being Redone on Accelerated Basis by Architect/Engineer.Shutdown Will Continue Until All Problems Are Resolved.Final Rept on Matter Is Forthcoming | /01T-0 on 790312:calculations in Piping Stress Analysis Are Being Redone on Accelerated Basis by Architect/Engineer.Shutdown Will Continue Until All Problems Are Resolved.Final Rept on Matter Is Forthcoming | | | 05000333/LER-1979-015, Forwards LER 79-015/03X-1 | Forwards LER 79-015/03X-1 | | | 05000333/LER-1979-015-03, /03X-1:on 790315,during Load Reduction & Shutdown, Rod Sequence Control Sys Failed to Pass Operations Surveillance Test F-ST-23A.Cause Unstated.Mode Switch Moved from Shutdown Position.Sys Repaired | /03X-1:on 790315,during Load Reduction & Shutdown, Rod Sequence Control Sys Failed to Pass Operations Surveillance Test F-ST-23A.Cause Unstated.Mode Switch Moved from Shutdown Position.Sys Repaired | | | 05000333/LER-1979-020, Forwards Revised LER 79-020/03X-1 | Forwards Revised LER 79-020/03X-1 | | | 05000333/LER-1979-020-03, During Normal Cold Shutdown,Operations Surveillance Testing Revealed That Emergency Diesel Generator Starting Air Compressor 93-AC-B1 Did Not Load Properly.Caused by Dirt in Unloader | During Normal Cold Shutdown,Operations Surveillance Testing Revealed That Emergency Diesel Generator Starting Air Compressor 93-AC-B1 Did Not Load Properly.Caused by Dirt in Unloader | | | 05000333/LER-1979-023-99, Fire Protection Piping Associated W/Hpci Maint Intentionally to Permit Required HPCI Maint.Partial Disassembly of Fire Protection Piping Required.Following Maint,Piping Restored | Fire Protection Piping Associated W/Hpci Maint Intentionally to Permit Required HPCI Maint.Partial Disassembly of Fire Protection Piping Required.Following Maint,Piping Restored | | | 05000333/LER-1979-023, Forwards Revised LER 79-023/99X-1 | Forwards Revised LER 79-023/99X-1 | | | 05000333/LER-1979-024, Forwards Revised LER 79-024/03X-1 | Forwards Revised LER 79-024/03X-1 | | | 05000333/LER-1979-024-03, Emergency Svc Water Pump Failed to Meet Shutoff Head Requirements of Tech Spec. Caused by Normal Wear.Overhaul & Minor Mod of Impeller by Manufacturer Restored Shutoff Head to within Tech Specs | Emergency Svc Water Pump Failed to Meet Shutoff Head Requirements of Tech Spec. Caused by Normal Wear.Overhaul & Minor Mod of Impeller by Manufacturer Restored Shutoff Head to within Tech Specs | | | 05000333/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000333/LER-1979-026-03, /03L-0 on 790507:radwaste Bldg Exhaust Fan 69-FN-8A Did Not Trip Per Hi-Hi Radiation Signal.Caused by Misadjusted Position Switch Associated W/Discharge Damper. Switch Linkage Adjusted | /03L-0 on 790507:radwaste Bldg Exhaust Fan 69-FN-8A Did Not Trip Per Hi-Hi Radiation Signal.Caused by Misadjusted Position Switch Associated W/Discharge Damper. Switch Linkage Adjusted | | | 05000333/LER-1979-027-03, /03L-0 on 790514:instrument 02-3-LIS-72D Tripped Minus 47.3 Inches.Instrument Recalibr,Then Replaced.Weekly Testing Will Continue to Assure Good Performance | /03L-0 on 790514:instrument 02-3-LIS-72D Tripped Minus 47.3 Inches.Instrument Recalibr,Then Replaced.Weekly Testing Will Continue to Assure Good Performance | | | 05000333/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000333/LER-1979-028-03, /03L-0 on 790517:during Cold Shutdown,Level Instrument of Carbon Dioxide Storage Sys Was Out of Calibr. Caused by Procedural Error.Instrument Racalibr & Satisfactorily Tested | /03L-0 on 790517:during Cold Shutdown,Level Instrument of Carbon Dioxide Storage Sys Was Out of Calibr. Caused by Procedural Error.Instrument Racalibr & Satisfactorily Tested | | | 05000333/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | | | 05000333/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000333/LER-1979-029-03, /03L-0 on 790518:during Snubber insp,14 Snubbers Required Some Work & Six Snubbers Were Determined to Be Potentially Inoperable.Snubbers Removed & Tested.Two Snubbers Failed Test & Were Declared Inoperable | /03L-0 on 790518:during Snubber insp,14 Snubbers Required Some Work & Six Snubbers Were Determined to Be Potentially Inoperable.Snubbers Removed & Tested.Two Snubbers Failed Test & Were Declared Inoperable | | | 05000333/LER-1979-030, Forwards LER 79-030/03L-0 | Forwards LER 79-030/03L-0 | | | 05000333/LER-1979-030-03, /03L-0 on 790518:during Cold Shutdown,Test Point Was Discovered in Error.Caused by Deviations in Conduction of Surveillance Test Procedures F-ISP-89.Procedure Was Immediately Correted & Surveillance Complete | /03L-0 on 790518:during Cold Shutdown,Test Point Was Discovered in Error.Caused by Deviations in Conduction of Surveillance Test Procedures F-ISP-89.Procedure Was Immediately Correted & Surveillance Complete | | | 05000333/LER-1979-031, Forwards LER 79-031/03L-0 | Forwards LER 79-031/03L-0 | | | 05000333/LER-1979-031-03, /03L-0 on 790519:fire Door Between North & South Emergency Switch Gear Rooms Failed to Close on Automatic Signal.Door & Closing Mechanism Lubricated & Adjusted | /03L-0 on 790519:fire Door Between North & South Emergency Switch Gear Rooms Failed to Close on Automatic Signal.Door & Closing Mechanism Lubricated & Adjusted | | | 05000333/LER-1979-032, Forwards LER 79-032/03L-0 | Forwards LER 79-032/03L-0 | | | 05000333/LER-1979-032-03, /03L-0 on 790519:sequencing Timer Associated W/Total Flooding Carbon Dioxide Sys Not Functioning Properly.Cause Not Stated.Sequencing Timer Cams Adjusted | /03L-0 on 790519:sequencing Timer Associated W/Total Flooding Carbon Dioxide Sys Not Functioning Properly.Cause Not Stated.Sequencing Timer Cams Adjusted | | | 05000333/LER-1979-033-03, /03L-0 on 790524:during Review of Plant Sys, Determined That Reactor Bldg Cooling Sys Supply & Return Lines to Drywell Equipment Drain Sump Did Not Have Seismic Stress Analysis Performed.Uncertain If It Is Required | /03L-0 on 790524:during Review of Plant Sys, Determined That Reactor Bldg Cooling Sys Supply & Return Lines to Drywell Equipment Drain Sump Did Not Have Seismic Stress Analysis Performed.Uncertain If It Is Required | | | 05000333/LER-1979-033, Forwards LER 79-033/03L-0 | Forwards LER 79-033/03L-0 | | | 05000333/LER-1979-034-03, /03L-0 on 790531:data Sheets Associated W/Instrument Surveillance Procedures F-ISP-4.5 Had Not Been Revised as Part of Procedure Revision Which Changed Instruments Calibr Range.Personnel Reinstructed | /03L-0 on 790531:data Sheets Associated W/Instrument Surveillance Procedures F-ISP-4.5 Had Not Been Revised as Part of Procedure Revision Which Changed Instruments Calibr Range.Personnel Reinstructed | | | 05000333/LER-1979-034, Forwards LER 79-034/03L-0 | Forwards LER 79-034/03L-0 | |
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