ML19210D318

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LER 79-088/03L-0:on 791101,HNP-1-3004 Scram Discharge Vol Water Level Function Test Not Performed on Time.Caused by Omission in List of Surveillance Procedures for That Date. Procedure Performed Immediately
ML19210D318
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 11/17/1979
From: Coggin C
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19210D313 List:
References
LER-79-088-03L-01, LER-79-88-3L-1, NUDOCS 7911260295
Download: ML19210D318 (2)


Text

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U. S. NUCLE AR REGULATORY COMMISSION NRC F ORM 3GG P 7H LICENSEE EVENT REPORT CONTROL BLOCK: l l l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) e 1

6 o i lG l A l E lI lH l11GLo l o l o l o l o l o l o l o 25 lo 26 l o l o LICENSE l@lTYPE JO 411I I

ll 57 CAT ill@

$8 ll@l 14 lb LICENSE NUMBER 7 8 9 LICENSEE CODE CON'T

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8 OuRC l L ]@l0 l 5 l0 l010 l3 l211 l@l 1] 1l 0] 1] 7] 9]@l 111 11 l7 l7 60 6t DOCKET NUMBER 68 60 EVENT D ATE 74 75 HEPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121 lWith the unit in steady-state power operation',, a review of Surveillance requirements l l Water l l0 l31 l per Technical Specifications revealed that HNP-1-3004, Scram Discharge Vo ume 0 4 l Level Functional Test, had not been performed within its allotted time frequency (i.

its interval of once every 3 months plus the grace period of 3 weeks). As required l 101s1 10-21-79, and as of the morn-l lOgoj lby Tech Specs 4.1-1(7), it should have been performed by There were no effects on public health l O 7 l ng i of 11-1-79, it hao not been performed.

l O 3 and safety as a result of this event. This is a non-repetitive occurrence.

7 8 3 COMPONENT CODE SUBCOdE SU E DE CODE SUSC E l0l91 l RlB l@ l A l@ l Xl@ l Zl Zl Zl Zl Zl Zl@ W@ g @

f3 18 19 20 9 10 11 12 7 8 CCDE Y N REPORT O O ,R's" LE R/RO u

EVENT YE AR g l217l229 [--_j l0 l8 l8 26l y 27 l0 3l 28 29 lL l 30

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31 l0l 32 23 24 F0F B. 5 PPLI MAN FACTURER HOURS 22 S B IT D lZ l 9 l 9 9 [g KEN A O ON PLANT TH Lx__j@lZ l@ LZ_j@ U@

36 l0 l0 0 l0 l 31 40 l41 Yl@ lZl@ l Zl@

42 43 44 47 33 34 3d CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i O IThe procedure was not performed on time due to its being inadvertently left off of the i i l list of surveillance. procedures scheduled to be performed during the time period in i, i 7 i l question - it should have been scheduled for 9-30-79. The procedure was succ The Plant Hatch surveil- l li l 31 l performed immediately upon discovery of its being overdue.

l i 4 lance program was recently computerized to prevent recurrence of events (continued) 80 7 8 9 D SCO RY DISCOVERY DESCRIPTION

% POWER OTHER STATUS STA S .eview of Surveil 1ance l I115 l l El@ l0 l 9 l 5 l@l NA l lAl@l ACTIVITY CO TENT LOCATION OF RELEASE RELE ASED OF RELE ASE AYOUNT OF ACTIVITY l NA NA l l i e [ Zj @ [Z_j@l PERSONNEL EXPOS ES TYPE DE SCRIPTION NUP.'8 E R NA l 1 7 l 0l 0 l 0 l@l Z l@l l h d PERSONNE L INJU IES NUMaER oEscRiPriON@ j NA i a 8 9 l 0l 010[@l 11 12 80 7

L OSS OF OH DAMAGE TO FACILITY TYPE DESCHIPilON N^ l

' o LZJ@l 80 7 H ') 10 "" *

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'S *"'"'" NA 7911260 M , , , ,, , ,,

80 5 68 69 8 9 10 C. L Coogin, Supt. P1t. Enq. Serv, pgoys 912-367-7781 7

M- F PRFPAHEH

Georgia Power Company Plant E. I. Hatch Baxley, Georgia 31513 Cause Description and Corrective Actions (continued) like this. The unit is now in full compliance withthe requirements and no fur-ther reporting is required.

1390 249 O

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