05000321/LER-1979-088-03, /03L-0:on 791101,HNP-1-3004 Scram Discharge Vol Water Level Function Test Not Performed on Time.Caused by Omission in List of Surveillance Procedures for That Date. Procedure Performed Immediately

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/03L-0:on 791101,HNP-1-3004 Scram Discharge Vol Water Level Function Test Not Performed on Time.Caused by Omission in List of Surveillance Procedures for That Date. Procedure Performed Immediately
ML19210D318
Person / Time
Site: Hatch 
Issue date: 11/17/1979
From: Coggin C
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19210D313 List:
References
LER-79-088-03L-01, LER-79-88-3L-1, NUDOCS 7911260295
Download: ML19210D318 (2)


LER-1979-088, /03L-0:on 791101,HNP-1-3004 Scram Discharge Vol Water Level Function Test Not Performed on Time.Caused by Omission in List of Surveillance Procedures for That Date. Procedure Performed Immediately
Event date:
Report date:
3211979088R03 - NRC Website

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U. S. NUCLE AR REGULATORY COMMISSION NRC F ORM 3GG P 7H LICENSEE EVENT REPORT CONTROL BLOCK: l l

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8 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121 lWith the unit in steady-state power operation',, a review of Surveillance requirements l l

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l0 l31 l per Technical Specifications revealed that HNP-1-3004, Scram Discharge Vo ume l Level Functional Test, had not been performed within its allotted time frequency (i.

0 4 its interval of once every 3 months plus the grace period of 3 weeks). As required l

101s1 10-21-79, and as of the morn-l lOgoj lby Tech Specs 4.1-1(7), it should have been performed by There were no effects on public health l

l ng of 11-1-79, it hao not been performed.

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7 and safety as a result of this event. This is a non-repetitive occurrence.

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Georgia Power Company Plant E. I. Hatch Baxley, Georgia 31513 Cause Description and Corrective Actionslike this. The unit is now in full compliance withthe requirements and no fur-ther reporting is required.

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