05000333/LER-1979-092-03, /03L-0:on 791013,during Normal Operation,Noted Intermittent Isolation Signal to HPCI Sys Steam Supply Inside Isolation Valve 23-MOV-15,indicating High Ambient Temp.Caused by Loose Lead to HPCI Switch.Lead Tightened

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/03L-0:on 791013,during Normal Operation,Noted Intermittent Isolation Signal to HPCI Sys Steam Supply Inside Isolation Valve 23-MOV-15,indicating High Ambient Temp.Caused by Loose Lead to HPCI Switch.Lead Tightened
ML19210C500
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 11/07/1979
From: W. Verne Childs
POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19210C497 List:
References
LER-79-092-03L, LER-79-92-3L, NUDOCS 7911140349
Download: ML19210C500 (2)


LER-1979-092, /03L-0:on 791013,during Normal Operation,Noted Intermittent Isolation Signal to HPCI Sys Steam Supply Inside Isolation Valve 23-MOV-15,indicating High Ambient Temp.Caused by Loose Lead to HPCI Switch.Lead Tightened
Event date:
Report date:
3331979092R03 - NRC Website

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