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LER-1977-007, Forwards LER 77-007/01T.Provides Supplemental Info |
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NRC eonu 195 u.s. NUCLii An nECULATonY CF NIS3loN DOC V T *W M ef,p 5C-489 (2 7e1 N
NRC DISTRIBUTION con PART 50 DOCKET MATERIAL
'"'IgNE!;"TREPORT TO:
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FROM:
oATE oF oCCUMENT Metropolitan Edison Comm ny 5/23/77 Mr. J. P. O' Reilly Reading, Pa.
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3 / (o A,) h DESCniPTION ENCLoSunE Licensee Event Report (R0 50-289/77-07/1T) on 5/9/77 concerning both doors of the reactor building. emergency personnel access hatch 6
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ACKNOWLEDGED PLANT NAME:
(3-P: (1-P)
Three Mile. Island Unit No 1 NOTE:
IF PERSONNEL EXPOSURE IS INVOLVED RJL SEND DIRECTLY TO KREGER/J. COLLINS EOR ACTION /INFORMATION 4
BRANCH CHIEF:
(ti i W/3 CYS FOR ACTION I
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._.,r METROPOLIIAN EDISON COMPANY POST OFFICE BOX 542 READING PENNSYLVANI A 19603 TELEPWCNE 215 - 9294M1 c,
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May 23,197; i.
Regulatory Docket File C ' J 0 :z Mr. J. P. O'Reilly, Director 7'
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Office of Inspection and Enforcement, Region 1
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U. S. Nuclear Regulatory Cor:=ission
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631 Park Avenue C'4
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ing of Prussia, Pennsylvania 19406
Dear Sir:
Decket No. 50-289 Operating License No. DPR-50 In accordance with the Technical Specifications of our Three Mile Island Nuclear Statien Unit 1 (TMI-1), we are reporting the following reportable occurrence:
(1) 2.eport Number:
77-07/1T (2a) Required Report Date:
5-23-77 (2b) Date of Occurrence: 5-09-77 (3) Facility: Three Mile Island Nuclear Station - Unit 1 (b) Identificaticn o f Occurrence:
Title : Ecth dccrs of the reactor building emergency personnel access hatch were cpen at the same time.
Type :
A reportable occurrence as defined by Technical Specification 6 9 2.a. (2) in that both doors of the reactor building emergency personnel access hatch were open at the same time, thus leading to a loss of containment integrity as stated in section 17 when the ecnditions were as stated in section 3.6.1 of the Technical Specifications.
M76 M2 771520006
Sh'. J. P. O' Reilly, Director May 23, 1977 Office of Inspection and Enforce =ent, Region 1 GQL 070L (5) Ccnditions Prior to occurrence:
Power:
Core: 0 Elec. 0 6 RC Flcw:
102 x 10 lb/hr RC Pressure:
L90 psig RC Temp:
300 F PR2R Level:
100 inches PR2R Temp:
465 F (6) Description of Occurrence:
A maintenance man, while opening the inner dcor of the reactor building e=ergency perconnel access hatch, noticed that the cuter door was also partially open. He i==ediately re-closed the inner door and notified the Shift Foreman who investigated and returned the outer door in its closed pocition.
(7) Apparent Cause of Occurrence:
The cause of this occurrence has been determined to be both desien and personnel in that :
- 1) Attempting to clcse the decrs against an obstruction or too rapidly swinging the decr open and closed can cause excessive stress en the upper hinge shift extension causing it to bend, and thereby creating excessive door free-travel. The free-travel then allows violation of the door techanical interlock.
- 2) The upper hinge chaft extencion =ay not be adequately suppcrted (to take the strain frc= occasional dcor =isuse).
The manufacturer has propcsed an additional bearing be installed to provide additional support.
(8) Analysis of Occurrence:
Perscnnel at the scene i=nediately re-established containment integrity therefore, both decrs were open for less than ene minute.
The inner door seals were tight thus the occurrence did not constitute a threat to the health and safety of the public.
P.r. J. P. O'Reilly, Director May 23,1977 Office of Inspection and Enforcement, Region 1 GQL 070L (9) Corrective Acticn:
IMEDIATE:
1.
Returned the dcors to their closed positicn.
2.
Verified that the Control Rocm alar s for the reacter building doors functioned prcperly.
3 Restricted use of thie decr tc emergency use only.
k.
Performed dcor seal leakage test-satis factory.
LONG TERM:
A design change is being evaluated to install additional shaft support bearings and to provide an additional interlock device.
The Plant Operations Review Cor:mittee and Unit Superintendent have reviewed and approved the above corrective action and have taken steps to assure its completion.
(10) Failure Data:
Manufacturer - Chicago Bridge & Iron Cc.
Contract No. 2631U Gilbert Associates Hinged Shaft Extensicn - 2" steel shaft is part of hinge assembly.
Similar G.
74-11 7k-32 Sincerely, h '
J. G.
L rtein Vice President JGH:LGM:rk Attachment. Licensee Event Eeport 1476 G4
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| 05000289/LER-1977-001, Forwards LER 77-001/01T.Provides Supplemental Info | Forwards LER 77-001/01T.Provides Supplemental Info | | | 05000289/LER-1977-001-01, /01T:on 770203,w/diesel Generator B Out of Svc,A Generator Was Lost,Causing Operation at Limiting Condition Less Conservative than Tech Specs.Generator a Out of Svc Due to Binding of Oil Pressure Low Speed Switch | /01T:on 770203,w/diesel Generator B Out of Svc,A Generator Was Lost,Causing Operation at Limiting Condition Less Conservative than Tech Specs.Generator a Out of Svc Due to Binding of Oil Pressure Low Speed Switch | | | 05000289/LER-1977-002-04, /04T-0:on 770304,river Water Discharge Exceeded Inlet River Water Temp by 14 F,Violating 12 F Limit During Normal Operation.Caused by Atmospheric Conditions & Personnel Error.Standby Decay Heat Water Pump Reduced Temp | /04T-0:on 770304,river Water Discharge Exceeded Inlet River Water Temp by 14 F,Violating 12 F Limit During Normal Operation.Caused by Atmospheric Conditions & Personnel Error.Standby Decay Heat Water Pump Reduced Temp | | | 05000289/LER-1977-003-03, /03L:on 770309,reactor Bldg Spray Pump Suction Isolation Valve Motor Failed.Caused by Excessive Grease in Operators Spring Pack Which Stopped Normal Compression of Spring,Preventing Torque Switch Sensing Force to Be Applied | /03L:on 770309,reactor Bldg Spray Pump Suction Isolation Valve Motor Failed.Caused by Excessive Grease in Operators Spring Pack Which Stopped Normal Compression of Spring,Preventing Torque Switch Sensing Force to Be Applied | | | 05000289/LER-1977-003, Forwards LER 77-003/03L.Provides Supplemental Info | Forwards LER 77-003/03L.Provides Supplemental Info | | | 05000289/LER-1977-004-01, /01T:on 770415,error in Safety Analysis Discovered.Caused by Personnel Using Erroneous Combined Relief Valve Capacity Figures from Vendor Valve Drawing in Safety Analysis | /01T:on 770415,error in Safety Analysis Discovered.Caused by Personnel Using Erroneous Combined Relief Valve Capacity Figures from Vendor Valve Drawing in Safety Analysis | | | 05000289/LER-1977-004, Forwards LER 77-004/01T.Provides Supplemental Info | Forwards LER 77-004/01T.Provides Supplemental Info | | | 05000289/LER-1977-005, Forwards LER 77-005/04T.Provides Supplemental Info | Forwards LER 77-005/04T.Provides Supplemental Info | | | 05000289/LER-1977-005-04, /04t on 770319,change in River Water Discharge Temp More than 2 Degrees in Hour Period Violated Ets.Caused by Failure of Mechanical Cooling Tower C Fan.Fan to Be Repaired During Current Refueling Outage | /04t on 770319,change in River Water Discharge Temp More than 2 Degrees in Hour Period Violated Ets.Caused by Failure of Mechanical Cooling Tower C Fan.Fan to Be Repaired During Current Refueling Outage | | | 05000289/LER-1977-006-01, /01T:on 770324,during Reactor Refueling,Tech Specs for Leakage of Valves & Penetrations Were Exceeded. Caused by Inability of Carbon Steel Gate Valves in Cooling Water Sys to Keep Tight Seals Between Tests | /01T:on 770324,during Reactor Refueling,Tech Specs for Leakage of Valves & Penetrations Were Exceeded. Caused by Inability of Carbon Steel Gate Valves in Cooling Water Sys to Keep Tight Seals Between Tests | | | 05000289/LER-1977-006, Forwards LER 77-006/01T-0 | Forwards LER 77-006/01T-0 | | | 05000289/LER-1977-007, Forwards LER 77-007/01T.Provides Supplemental Info | Forwards LER 77-007/01T.Provides Supplemental Info | | | 05000289/LER-1977-007-01, /01T:on 770509,both Doors of Reactor Bldg Emergency Personnel Access Hatch Open at Same Time,Violating Tech Specs.Caused by Door Design Flaw Allowing Free Travel If Closed Against Obstruction,Causing Interlock Stress | /01T:on 770509,both Doors of Reactor Bldg Emergency Personnel Access Hatch Open at Same Time,Violating Tech Specs.Caused by Door Design Flaw Allowing Free Travel If Closed Against Obstruction,Causing Interlock Stress | | | 05000289/LER-1977-008-03, /03L:on 770504 Snubbers Failed to Perform within Acceptable Criteria,Resulting in Operation in Degraded Mode. Caused by Improperly Adjusted Locking Devices & O-ring Seal Leaks.Cause of Failure of Eight Snubbers Unknown | /03L:on 770504 Snubbers Failed to Perform within Acceptable Criteria,Resulting in Operation in Degraded Mode. Caused by Improperly Adjusted Locking Devices & O-ring Seal Leaks.Cause of Failure of Eight Snubbers Unknown | | | 05000289/LER-1977-008, Forwards LER 77-008/03L.Provides Supplemental Info | Forwards LER 77-008/03L.Provides Supplemental Info | | | 05000289/LER-1977-009-01, /01T:on 770512,loose Steam Generator LOCA Restraint Bolt Found.Caused Either by Improper Tightening During Installation or Loosening Due to Thermal Cycling & Bolt Relaxation in Svc | /01T:on 770512,loose Steam Generator LOCA Restraint Bolt Found.Caused Either by Improper Tightening During Installation or Loosening Due to Thermal Cycling & Bolt Relaxation in Svc | | | 05000289/LER-1977-009, Forwards LER 77-009/01T.Provides Supplemental Info | Forwards LER 77-009/01T.Provides Supplemental Info | | | 05000289/LER-1977-010, Forwards LER 77-010/01T.Provides Supplemental Info | Forwards LER 77-010/01T.Provides Supplemental Info | | | 05000289/LER-1977-011, Forwards LER 77-011/01T.Provides Supplemental Info | Forwards LER 77-011/01T.Provides Supplemental Info | | | 05000289/LER-1977-011-01, T:On 770519,engineered Safeguards Motor Control Center Tripped During Power Operation.Caused by Binding of a Phase Overload Device Tripping Stem.Preventive Maint Will Be Modified to Check for Tripping Stem Resetting | T:On 770519,engineered Safeguards Motor Control Center Tripped During Power Operation.Caused by Binding of a Phase Overload Device Tripping Stem.Preventive Maint Will Be Modified to Check for Tripping Stem Resetting | | | 05000289/LER-1977-012, RO 77-12/3L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Operability of Redundant Pump.Caused by Personnel Error.Redundant Pump Tested Satisfactorily on 770519.Forwards LER 77-12/03L | RO 77-12/3L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Operability of Redundant Pump.Caused by Personnel Error.Redundant Pump Tested Satisfactorily on 770519.Forwards LER 77-12/03L | | | 05000289/LER-1977-012-03, /03L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Redundant Pump. Caused by Personnel Error.Redundant Pump Tested Satisfactorily.Personnel Instructed in Procedures | /03L:on 770519,engineered Safeguard Pump MU-P-1A Was Removed from Svc Prior to Testing Redundant Pump. Caused by Personnel Error.Redundant Pump Tested Satisfactorily.Personnel Instructed in Procedures | | | 05000289/LER-1977-013-04, /04T:on 770523,during Normal Operation,Waste Concentration in River Water Discharge Found in Excess of Designated Max.Caused by Slug of Suspended Solids Breaking Loose During Sampling.Discharge Terminated | /04T:on 770523,during Normal Operation,Waste Concentration in River Water Discharge Found in Excess of Designated Max.Caused by Slug of Suspended Solids Breaking Loose During Sampling.Discharge Terminated | | | 05000289/LER-1977-014-03, /03L:on 770524,during Reactor Bldg Cooling & Isolation Sys Logic Channel & Component Test,Reactor Bldg Cooling Return Isolation Valve RB-V7 Failed to Close Upon Receipt of Signal.Caused by Dirt on Valve Diaphragm | /03L:on 770524,during Reactor Bldg Cooling & Isolation Sys Logic Channel & Component Test,Reactor Bldg Cooling Return Isolation Valve RB-V7 Failed to Close Upon Receipt of Signal.Caused by Dirt on Valve Diaphragm | | | 05000289/LER-1977-015, Notes Error in LER 77-15/3L Submitted 770628.Both Drawings in Section 9 Should Be Numbered 207-011 | Notes Error in LER 77-15/3L Submitted 770628.Both Drawings in Section 9 Should Be Numbered 207-011 | | | 05000289/LER-1977-015-03, /03L:on 770529,during Normal operation,230 Kv Substation Bus 4 Was de-energized by Differential Relay 87BB-1.Caused by Wiring Error on Auxiliary Transformer Due to Drawing Error.Bus & Transformer Returned to Svc | /03L:on 770529,during Normal operation,230 Kv Substation Bus 4 Was de-energized by Differential Relay 87BB-1.Caused by Wiring Error on Auxiliary Transformer Due to Drawing Error.Bus & Transformer Returned to Svc | | | 05000320/LER-1977-016, /01T-0 on 770924:half Trip of Steam & Feedwater Rupture Control Sys Resulted in Opening of Pressurizer Power Relief Valve.Possibly Caused by Loose Connections at Terminal Boards | /01T-0 on 770924:half Trip of Steam & Feedwater Rupture Control Sys Resulted in Opening of Pressurizer Power Relief Valve.Possibly Caused by Loose Connections at Terminal Boards | | | 05000289/LER-1977-016-01, /01T-0:on 770924,RCS Temp & Pressure Rose.Caused by Half Trip Condition from Steam & Feedwater Rupture Control Sys.Possible Cause of Half Trip Attributed to Loose Connection at Terminal Boards | /01T-0:on 770924,RCS Temp & Pressure Rose.Caused by Half Trip Condition from Steam & Feedwater Rupture Control Sys.Possible Cause of Half Trip Attributed to Loose Connection at Terminal Boards | | | 05000289/LER-1977-016, Forwards Supplemental Info to LER 77-016/01T-0 Re Half Trip in Steam Feedwater Rupture Control Sys | Forwards Supplemental Info to LER 77-016/01T-0 Re Half Trip in Steam Feedwater Rupture Control Sys | | | 05000289/LER-1977-017-03, /03L:on 770624,during Normal Operating & semi- Annual Leak Test,Leakage Observed Around Inner Door Seal of Personnel Accces Hatch of Reactor Bldg.Caused by Procedural Inadequacies Causing Improper Installation of Door | /03L:on 770624,during Normal Operating & semi- Annual Leak Test,Leakage Observed Around Inner Door Seal of Personnel Accces Hatch of Reactor Bldg.Caused by Procedural Inadequacies Causing Improper Installation of Door | | | 05000289/LER-1977-018-03, /03L:on 770629,during Normal Operation,Nuclear Svcs River Water Pump NR-P1C Shaft Failed During Pump Operation.Caused by Mechanical & Procedural Problems.Pump Lined Up & Repaired within 4-h | /03L:on 770629,during Normal Operation,Nuclear Svcs River Water Pump NR-P1C Shaft Failed During Pump Operation.Caused by Mechanical & Procedural Problems.Pump Lined Up & Repaired within 4-h | | | 05000289/LER-1977-019-03, /03L:on 770713,during Normal Operation,Leak in Miscellaneous Waste Evaporator Feed Tank Immersion Heater Shorted Out Heater & Feed Pump.Caused by Leak in Temp Probe on Heater.Heater Replaced & Operating Procedure Modified | /03L:on 770713,during Normal Operation,Leak in Miscellaneous Waste Evaporator Feed Tank Immersion Heater Shorted Out Heater & Feed Pump.Caused by Leak in Temp Probe on Heater.Heater Replaced & Operating Procedure Modified | | | 05000289/LER-1977-020, Forwards LER 77-20/04T-0 | Forwards LER 77-20/04T-0 | | | 05000289/LER-1977-020-04, /4T:on 770719,during Passage of Storm Front,Station River Water Discharge Temp Fell to in Excess of 3 F Below Inlet Temp.Caused by Storm Front.A & B Mechanical Draft Cooling Fans Stopped | /4T:on 770719,during Passage of Storm Front,Station River Water Discharge Temp Fell to in Excess of 3 F Below Inlet Temp.Caused by Storm Front.A & B Mechanical Draft Cooling Fans Stopped | | | 05000289/LER-1977-021-01, /01T:on 770726,during Normal Operation,Radiation Monitor RM-A2 Failed & Atmosphere Sampling of Reactor Bldg Not Performed.Caused by Improper Reassembly Following 770725 Surveillance Test.Monitor Repaired.Procedure to Be Revi | /01T:on 770726,during Normal Operation,Radiation Monitor RM-A2 Failed & Atmosphere Sampling of Reactor Bldg Not Performed.Caused by Improper Reassembly Following 770725 Surveillance Test.Monitor Repaired.Procedure to Be Revised | | | 05000289/LER-1977-022-01, /01T:on 770825,during Normal Operation Restrictions Placed on Decay Heat Removal Pumps Found Contrary to Pump Operating Capability Per Fsar.Restrictions Placed on Pump by B&W Due to Pump Failure at Other Util | /01T:on 770825,during Normal Operation Restrictions Placed on Decay Heat Removal Pumps Found Contrary to Pump Operating Capability Per Fsar.Restrictions Placed on Pump by B&W Due to Pump Failure at Other Util | | | 05000289/LER-1977-023-01, /01T:on 770926,during Heatup Operation Both Doors of Reactor Bldg Emergency Personnel Access Hatch Open Simultaneously.Caused by Failure of Interlock,Poor Hatch Design & Operator Error.Addl Interlock to Be Added | /01T:on 770926,during Heatup Operation Both Doors of Reactor Bldg Emergency Personnel Access Hatch Open Simultaneously.Caused by Failure of Interlock,Poor Hatch Design & Operator Error.Addl Interlock to Be Added | | | 05000289/LER-1977-023, RO 77-23/1T:on 770920,both Doors of Reactor Bldg Emergency Personnel Access Hatch Open Simultaneously.Caused by Personnel Error.Doors Closed.Forwards LER 77-23/1T | RO 77-23/1T:on 770920,both Doors of Reactor Bldg Emergency Personnel Access Hatch Open Simultaneously.Caused by Personnel Error.Doors Closed.Forwards LER 77-23/1T | |
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