LER-1979-064, /03L:on 790906,during Startup,Motor Failed on Condensate Storage Tank Suction Valve.Replacement Valve Mistakenly Left Closed.Caused by Communications Breakdown. Upon Discovery,Valve Opened & Position Logged Daily |
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POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT DOCKET NO. 50-333 ATTACHMENT TO LER 79-064/03L-0 Page 1
of 1 During normal startup operations, while ccnducting Operations Surveillance Test F-ST-4E titled "HPCI Sub-sys tem Logic Funct ional Tes t," which was being conducted to satisfy the requirements of Technical Speci fications Appendix A, Table 3.2-2, the motor on the systems Condensate Storaga Tank suction valve failed. At this time reactor pressure was between 100-1f0 psig.
After extensive review by the Plant Operating Revier Commi ttee (PORC), i t was determined that the failed motor should be replaced by an identical motor f rom the system's torus suction valve (23-MOV-57).
This latter suction valve provides an alternate and secondary source of water to the HPCI system.
It was further directed by the PORC that 23-MOV-57 be p! aced in the open position in orcer to allow the HPCI system to take suction from the torus if required.
In addition, the other torus suction valve (23-MOV-58) was to be veri fied closed to satisfy primary containment isolation requirements contained in Technical Specifications Aopendix A, Paragraph 3.7.1.
Subsequently, the motor was removed from 23-M0V-57 as directed by the PORC, however, the valve was not placed in the open position.
This condition was discovered approximately five hours af ter reactor pressure was increased above 150 psig, thus, the torus wa, not automat ically available to the HPCI system for a five-hour period during which systuu operability was required Sy Technical Specifications.
Since the condensate storage tank suction valve to the HPCI system we in its normal open position, and both condensate storage tanks were nearly full, some 30C,000 gallons of water was available to the HPCI system in the event its operation was requi red.
In view of this large reserve of water in the condensate storage tanks, the HPCI system would have operated normally.
Minimal safety sign
- f i cance occurred from this event since the system would have operated automatically for a period of more than one hour before manual opening of the torus suction valve would have been requi red.
As soon as the condition was discovered, 23-MOV-57 was pla'ed in the open position and the position was logged oa a daily basis until 1.ie motor was re-placed and proper operation was demonstrated. The motor was replaced on S eptembe r 14, 1979 and found acceptable by completion of Operations Surveillance Test F-ST-4D ti tled "HPCI MOV Operabili ty Test."
Investigation into the cause of not opening the valve at the proper time revealed the plant's management did not adequately communicate to the plant's Operations and Maintenance personnel the importance of placing the valve in the open posi tion prior to the commencement of the repai r.
This point was brought to the attention of the Shift Supervisor and the significance of this event has been discussed with the Operations Department.
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| 05000333/LER-1979-001-03, /03L-0 on 790105:failure to Perform Core Performance Surveillance on 781210 & 781223.Currently Developing Surveillance Test Checkoff List,To Ensure That Test Is Not Overlooked Again | /03L-0 on 790105:failure to Perform Core Performance Surveillance on 781210 & 781223.Currently Developing Surveillance Test Checkoff List,To Ensure That Test Is Not Overlooked Again | | | 05000333/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000333/LER-1979-002-03, /03L-0 on 790108:flow Biased Portion of Average Power Range Monitor B Inoperable.Caused by Operational Amplifier Failure.Circuit Board Replaced | /03L-0 on 790108:flow Biased Portion of Average Power Range Monitor B Inoperable.Caused by Operational Amplifier Failure.Circuit Board Replaced | | | 05000333/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000333/LER-1979-003-03, /03L-0 on 790115:during Mainsteam Flow, Surveillance Procedure Instrument 02-DPIS-116B Found Set at 110 psid,2 Psid Above Tech Spec Max Due to Drift in Differential Pressure Switch | /03L-0 on 790115:during Mainsteam Flow, Surveillance Procedure Instrument 02-DPIS-116B Found Set at 110 psid,2 Psid Above Tech Spec Max Due to Drift in Differential Pressure Switch | | | 05000333/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000333/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000333/LER-1979-004-03, /03L-0 on 790119:while Performing Operations Surveillance Test F-St-76D,water Leak Noted on Post Indicator Valve 76-FPS-30 & Discovered Water Leaking from Lubrication Line.Caused by Shovel Cut During Snow Removal | /03L-0 on 790119:while Performing Operations Surveillance Test F-St-76D,water Leak Noted on Post Indicator Valve 76-FPS-30 & Discovered Water Leaking from Lubrication Line.Caused by Shovel Cut During Snow Removal | | | 05000333/LER-1979-005-04, /04L-0 on 790124: Apparent Excessive Solution Release from Makeup Water Treatment Waste Neutralizer Tanks to Circulating Water Discharge Tunnel Noted.Calculations Show Tech Specs Not Exceeded | /04L-0 on 790124: Apparent Excessive Solution Release from Makeup Water Treatment Waste Neutralizer Tanks to Circulating Water Discharge Tunnel Noted.Calculations Show Tech Specs Not Exceeded | | | 05000333/LER-1979-005, Forwards LER 79-005/04L-0 | Forwards LER 79-005/04L-0 | | | 05000333/LER-1979-006, Forwards LER 79-006/03X-1 | Forwards LER 79-006/03X-1 | | | 05000333/LER-1979-006-03, /03X-1:on 790124,during Normal Operations,Ground Fault on 125 Station Battery a Noted.Caused by Bellows Failure on Pressure Switch Circuit safety-relief Valve 02-RV-71J.Ground Cleared.Valve Restored to Operation | /03X-1:on 790124,during Normal Operations,Ground Fault on 125 Station Battery a Noted.Caused by Bellows Failure on Pressure Switch Circuit safety-relief Valve 02-RV-71J.Ground Cleared.Valve Restored to Operation | | | 05000333/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000333/LER-1979-007-03, /03L-0 on 790125:jet Pump Operability Surveillance Had Not Been Conducted on 790123-24 as Required.Procedures Subsequently Revised | /03L-0 on 790125:jet Pump Operability Surveillance Had Not Been Conducted on 790123-24 as Required.Procedures Subsequently Revised | | | 05000333/LER-1979-008-03, /03L-0 on 790125:core Performance Surveillance Not Done on 790120-22.Operations Surveillance Test for Daily Checks Was Being Developed to Include check-off of Surveillance Requirements.Caused by Operator Error | /03L-0 on 790125:core Performance Surveillance Not Done on 790120-22.Operations Surveillance Test for Daily Checks Was Being Developed to Include check-off of Surveillance Requirements.Caused by Operator Error | | | 05000333/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000333/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000333/LER-1979-009-03, /03L-0 on 790205:rod Control Drive Rendered Inoperable in Order to Repair Leak in Control Rod Drive Sys Hydraulic Control Unit.Upon Completion of Repair,All Components Returned to Svc | /03L-0 on 790205:rod Control Drive Rendered Inoperable in Order to Repair Leak in Control Rod Drive Sys Hydraulic Control Unit.Upon Completion of Repair,All Components Returned to Svc | | | 05000333/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000333/LER-1979-010-03, /03L-0 on 790202:step Increase in Indicated Core Flow.Caused by Earlier Failure of Square Root Computation Module for Jet Pump.Square Root Computation Module Replaced W/Identical Unit & Core Flow Evaluation Test Completed | /03L-0 on 790202:step Increase in Indicated Core Flow.Caused by Earlier Failure of Square Root Computation Module for Jet Pump.Square Root Computation Module Replaced W/Identical Unit & Core Flow Evaluation Test Completed | | | 05000333/LER-1979-011-03, /03L-0 on 790214:drywell Atmospheric Sample Isolation Valve 27-SOV-123B Blew a Fuse.Caused by Shorted Valve Solenoid.Incident Recurred 790306.Will Submit Followup Rept When Valve Replacement Is Completed | /03L-0 on 790214:drywell Atmospheric Sample Isolation Valve 27-SOV-123B Blew a Fuse.Caused by Shorted Valve Solenoid.Incident Recurred 790306.Will Submit Followup Rept When Valve Replacement Is Completed | | | 05000333/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000333/LER-1979-014, Forwards LER 79-014/01T-0 | Forwards LER 79-014/01T-0 | | | 05000333/LER-1979-014-01, /01T-0 on 790312:calculations in Piping Stress Analysis Are Being Redone on Accelerated Basis by Architect/Engineer.Shutdown Will Continue Until All Problems Are Resolved.Final Rept on Matter Is Forthcoming | /01T-0 on 790312:calculations in Piping Stress Analysis Are Being Redone on Accelerated Basis by Architect/Engineer.Shutdown Will Continue Until All Problems Are Resolved.Final Rept on Matter Is Forthcoming | | | 05000333/LER-1979-015, Forwards LER 79-015/03X-1 | Forwards LER 79-015/03X-1 | | | 05000333/LER-1979-015-03, /03X-1:on 790315,during Load Reduction & Shutdown, Rod Sequence Control Sys Failed to Pass Operations Surveillance Test F-ST-23A.Cause Unstated.Mode Switch Moved from Shutdown Position.Sys Repaired | /03X-1:on 790315,during Load Reduction & Shutdown, Rod Sequence Control Sys Failed to Pass Operations Surveillance Test F-ST-23A.Cause Unstated.Mode Switch Moved from Shutdown Position.Sys Repaired | | | 05000333/LER-1979-020, Forwards Revised LER 79-020/03X-1 | Forwards Revised LER 79-020/03X-1 | | | 05000333/LER-1979-020-03, During Normal Cold Shutdown,Operations Surveillance Testing Revealed That Emergency Diesel Generator Starting Air Compressor 93-AC-B1 Did Not Load Properly.Caused by Dirt in Unloader | During Normal Cold Shutdown,Operations Surveillance Testing Revealed That Emergency Diesel Generator Starting Air Compressor 93-AC-B1 Did Not Load Properly.Caused by Dirt in Unloader | | | 05000333/LER-1979-023-99, Fire Protection Piping Associated W/Hpci Maint Intentionally to Permit Required HPCI Maint.Partial Disassembly of Fire Protection Piping Required.Following Maint,Piping Restored | Fire Protection Piping Associated W/Hpci Maint Intentionally to Permit Required HPCI Maint.Partial Disassembly of Fire Protection Piping Required.Following Maint,Piping Restored | | | 05000333/LER-1979-023, Forwards Revised LER 79-023/99X-1 | Forwards Revised LER 79-023/99X-1 | | | 05000333/LER-1979-024, Forwards Revised LER 79-024/03X-1 | Forwards Revised LER 79-024/03X-1 | | | 05000333/LER-1979-024-03, Emergency Svc Water Pump Failed to Meet Shutoff Head Requirements of Tech Spec. Caused by Normal Wear.Overhaul & Minor Mod of Impeller by Manufacturer Restored Shutoff Head to within Tech Specs | Emergency Svc Water Pump Failed to Meet Shutoff Head Requirements of Tech Spec. Caused by Normal Wear.Overhaul & Minor Mod of Impeller by Manufacturer Restored Shutoff Head to within Tech Specs | | | 05000333/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000333/LER-1979-026-03, /03L-0 on 790507:radwaste Bldg Exhaust Fan 69-FN-8A Did Not Trip Per Hi-Hi Radiation Signal.Caused by Misadjusted Position Switch Associated W/Discharge Damper. Switch Linkage Adjusted | /03L-0 on 790507:radwaste Bldg Exhaust Fan 69-FN-8A Did Not Trip Per Hi-Hi Radiation Signal.Caused by Misadjusted Position Switch Associated W/Discharge Damper. Switch Linkage Adjusted | | | 05000333/LER-1979-027-03, /03L-0 on 790514:instrument 02-3-LIS-72D Tripped Minus 47.3 Inches.Instrument Recalibr,Then Replaced.Weekly Testing Will Continue to Assure Good Performance | /03L-0 on 790514:instrument 02-3-LIS-72D Tripped Minus 47.3 Inches.Instrument Recalibr,Then Replaced.Weekly Testing Will Continue to Assure Good Performance | | | 05000333/LER-1979-027, Forwards LER 79-027/03L-0 | Forwards LER 79-027/03L-0 | | | 05000333/LER-1979-028-03, /03L-0 on 790517:during Cold Shutdown,Level Instrument of Carbon Dioxide Storage Sys Was Out of Calibr. Caused by Procedural Error.Instrument Racalibr & Satisfactorily Tested | /03L-0 on 790517:during Cold Shutdown,Level Instrument of Carbon Dioxide Storage Sys Was Out of Calibr. Caused by Procedural Error.Instrument Racalibr & Satisfactorily Tested | | | 05000333/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | | | 05000333/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000333/LER-1979-029-03, /03L-0 on 790518:during Snubber insp,14 Snubbers Required Some Work & Six Snubbers Were Determined to Be Potentially Inoperable.Snubbers Removed & Tested.Two Snubbers Failed Test & Were Declared Inoperable | /03L-0 on 790518:during Snubber insp,14 Snubbers Required Some Work & Six Snubbers Were Determined to Be Potentially Inoperable.Snubbers Removed & Tested.Two Snubbers Failed Test & Were Declared Inoperable | | | 05000333/LER-1979-030, Forwards LER 79-030/03L-0 | Forwards LER 79-030/03L-0 | | | 05000333/LER-1979-030-03, /03L-0 on 790518:during Cold Shutdown,Test Point Was Discovered in Error.Caused by Deviations in Conduction of Surveillance Test Procedures F-ISP-89.Procedure Was Immediately Correted & Surveillance Complete | /03L-0 on 790518:during Cold Shutdown,Test Point Was Discovered in Error.Caused by Deviations in Conduction of Surveillance Test Procedures F-ISP-89.Procedure Was Immediately Correted & Surveillance Complete | | | 05000333/LER-1979-031, Forwards LER 79-031/03L-0 | Forwards LER 79-031/03L-0 | | | 05000333/LER-1979-031-03, /03L-0 on 790519:fire Door Between North & South Emergency Switch Gear Rooms Failed to Close on Automatic Signal.Door & Closing Mechanism Lubricated & Adjusted | /03L-0 on 790519:fire Door Between North & South Emergency Switch Gear Rooms Failed to Close on Automatic Signal.Door & Closing Mechanism Lubricated & Adjusted | | | 05000333/LER-1979-032, Forwards LER 79-032/03L-0 | Forwards LER 79-032/03L-0 | | | 05000333/LER-1979-032-03, /03L-0 on 790519:sequencing Timer Associated W/Total Flooding Carbon Dioxide Sys Not Functioning Properly.Cause Not Stated.Sequencing Timer Cams Adjusted | /03L-0 on 790519:sequencing Timer Associated W/Total Flooding Carbon Dioxide Sys Not Functioning Properly.Cause Not Stated.Sequencing Timer Cams Adjusted | | | 05000333/LER-1979-033-03, /03L-0 on 790524:during Review of Plant Sys, Determined That Reactor Bldg Cooling Sys Supply & Return Lines to Drywell Equipment Drain Sump Did Not Have Seismic Stress Analysis Performed.Uncertain If It Is Required | /03L-0 on 790524:during Review of Plant Sys, Determined That Reactor Bldg Cooling Sys Supply & Return Lines to Drywell Equipment Drain Sump Did Not Have Seismic Stress Analysis Performed.Uncertain If It Is Required | | | 05000333/LER-1979-033, Forwards LER 79-033/03L-0 | Forwards LER 79-033/03L-0 | | | 05000333/LER-1979-034-03, /03L-0 on 790531:data Sheets Associated W/Instrument Surveillance Procedures F-ISP-4.5 Had Not Been Revised as Part of Procedure Revision Which Changed Instruments Calibr Range.Personnel Reinstructed | /03L-0 on 790531:data Sheets Associated W/Instrument Surveillance Procedures F-ISP-4.5 Had Not Been Revised as Part of Procedure Revision Which Changed Instruments Calibr Range.Personnel Reinstructed | | | 05000333/LER-1979-034, Forwards LER 79-034/03L-0 | Forwards LER 79-034/03L-0 | |
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