05000321/LER-1979-072-03, /03L-0:on 790827,plant Svc Water Supply Isolation Valves for Standby Gas Treatment Charcoal Filter Fire Protection Deluge Valves Were in Closed Position.Caused by Low Svc Water Pressure and Very Sensitive Deluge Valves

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/03L-0:on 790827,plant Svc Water Supply Isolation Valves for Standby Gas Treatment Charcoal Filter Fire Protection Deluge Valves Were in Closed Position.Caused by Low Svc Water Pressure and Very Sensitive Deluge Valves
ML19208D449
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 09/21/1979
From: Coggin C
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19208D447 List:
References
LER-79-072-03L-01, LER-79-72-3L-1, NUDOCS 7909280440
Download: ML19208D449 (2)


LER-1979-072, /03L-0:on 790827,plant Svc Water Supply Isolation Valves for Standby Gas Treatment Charcoal Filter Fire Protection Deluge Valves Were in Closed Position.Caused by Low Svc Water Pressure and Very Sensitive Deluge Valves
Event date:
Report date:
3211979072R03 - NRC Website

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Caxley, Georgia 31513 Event Description and Probable Consequencesfeature of filter trains.

Similar event reported in LER 2-79-83.

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