ML18348A255

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License Event Report 1977-010-00 Re Four PCP Loss of Flow
ML18348A255
Person / Time
Site: Palisades Entergy icon.png
Issue date: 02/14/1977
From: Hoffman D
Consumers Power Co
To: James Keppler
NRC/RGN-III
References
LER 1977-010-00
Download: ML18348A255 (2)


Text

consumers

  • Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
  • Area Code 517 788-0550 February 14, 1977 Mr James G Keppler Office of Inspection & Enforcement Region III US Nuclear RegulatorY Commission 799 Roosevelt Road Glen Ellyn, IL 60137
COCKET 50-255, LICENSE DPR PALISADES PLANT - ER-77 FOUR PCP LOSS OF FLOW Rf6Ui.11
  • YDOClffT FILE CP1>11 On February 1, 1977, we notified the IE staff of increased icing on the~~Jhs mission towers and lines between the Palisades Plant and the 345 kV switchyard.
  • The consequences of a complete tower failure could result in a condition not specifically considered in the FSAR Section 14.7. We, therefore, initiated analysis to determine the structural adequacy of the towers and lines as well as a 4-pump loss of flow without steam generator coastdown. The 4-pump loss of flow analysis has been completed and transmitted to the NRC staff for review.

The results indicated the transient to be less severe than others presented in Section 14.7 of the FSAR. PreliminarY analyses of the transmission towers and lines have been completed which indicate that a margin of safety exists for observed ice loadings. Additional evaluations are being made to 'determine if any modifications to the towers or lines are required.

David P Hoffman Assistant Nuclear Licensing Administrator FEB 1 7 1977

, - LICENSEE EVENT REPORT- Palisades CONTROL BLOCK: I I I I I *' I (PLEASE PAINT ALL REQUIRED INFORMATION) 1 6 LICENSE EVENT LICENSE NUMBER TYPE TYPE I ol ol-lol ol ol ol ol-1 ol ol 1411l1l1l 1I Io 11 I 15 25 26 30 31 32 REPORT REPORT TYPE. SOURCE OOCKET NUMBER EVENT DATE REPORT DATE 7

@El CON'T T*. ] .* I 8 57 58 w59 llJ 60 lo 61 15 lo I-lo .1215151 68 I69o I 1 I 3 I 1. I 1 I 174I lol2!1141117.I 75 80 EVENT DESCRIPTION lol2I I On Januarv 31, 1977, ice loading on the 345 kV bus tie and station nower lines between I 7 8 9 80 lol3I I the Palisades Plant and the switchyard were observed to be greater than normally ex- I 7 8 9 80 lol41 I pected due to the cooling tower plume passing the lines .. Plant power level was held I

7. 8 9 80 lo151 I at 60% until 4 PCP loss of flow without turbine generator coastdown could be analyzed I 7 8 9 80 lfilID I and proper operation of both diesel generators verified. (ER-77-10) 1 7 8 9 PRIME 80 SYSTEM CAUSE COMPONENT COMPONENT CODE CODE COMPONENT CODE SUPPUER MANUFACTURER VIOLATION 7

@El I El GI L£J 8 9 10 11 I z I z I z I zl zl z I 12 17 w 43 Iz Iz Iz Iz I 44 47 L~J' 48 CAUSE DESCRIPTION

@:@ I Abnormal icing is due to enviromnental conditions and operation of the cooling towers. I.

7 8 9 80 lolsl I FSAR .l'.ccident Analysis (Sec 14. 7) does not consider 4 pump loss of flow incident I 80 l8j j without turbine generator assist as. credible. I

~9 FACILITY METHOD OF 80 OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION w

STATUS  % POWER EEI8 LE..I I oI 6 I o I NA I Visual Obs of Towers & Lines 7 9 10 12 13 44 45 46 80 FORM OF ACTIVITY CONTENT 7

rn w 8 RELEASED 9

OF RELEASE

~

10 11 AMOUNT OF ACTIVITY

_ j_ _ _ _ _ NA____--~

44 45 LOCATION OF RELEASE NA 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION IT@] I ol oI ol LIJ NA 7 8 9 11 12 13 80 PERS"ONNEL INJURIES NUMBER DESCRIPTION B:Eilololol NA 7 8 9 11 12 80 PROBABLE CONSEQUENCES lTifil I None; loss of 4 PCP analysis indicates adequate MDNBR.

7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION QEW 7 8 9 10 NA 80 PUBLICITY NA I@fil

oomoNAL FACTORS NA 80 7 8 9 BO

[iliJ NA 7 8 9 BO