ML18348A200

From kanterella
Jump to navigation Jump to search
License Event Report 1977-062-00 Re Iodine Removal System Naoh Tank (T-103)
ML18348A200
Person / Time
Site: Palisades Entergy icon.png
Issue date: 01/06/1978
From: Hoffman D
Consumers Power Co
To: James Keppler
NRC/RGN-III
References
LER 1977-062-00
Download: ML18348A200 (2)


Text

consumers

  • Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
  • Area Code 517 788-0550 January 6, 1978 Mr James G Keppler Office of Inspection and Enforcement Region III US Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255 - LICENSE DPR PALISADES PLANT - ER-77-062 The reverse side describes a reportable occurrence for the Palisades Plant.

David P Hoffman Assistant Nuclear Licensing Administrator CC: ASchwencer, USNRC

  • 1 ~' :.;l r,t.i v ...

1 l 97 8

, e Palisades NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (7-771 LICENSEE EVENT REPORT CONTROL BLOCK: I I I I I I 1Q (PLEASE PR!NT OR TYPE ALL REQUIRED INFORMATION) 1 6 fil2J 7 8 lMlrJ~s!E~J~ I 1J0tO I 0 IO 1 I 0 L~lse~L~sJR 0 I 0 I 0 I ~J0l~ 11 J_:J -~ l_JG)I__ J_ J © CON'T IT:El  :~~~~~ ~0101 51010101215J5 IG)Jl J2101~7171©10111016171810 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES@

I While investigating a low level alarm in the iodine removal system NaOH

!Im 1

((ill J tank (T-103), nitrogen pressure was removed, rendering the tank inoperable I IIEJ I (TS 3 .19.1. b). The tank was restored to service within the time required l

[))))I by Technical Specifications. Loss of NaOH flow could adversely affect I

[)))) I ph control under postulated LOCA conditions. No effect on public 1

[§12] Lhealth or safety. Event similar to ER-77-53. I iI!Il 7 8 9

,oO SYSTEM CAUSE CAUSE COMP. VALVE COOE CODE SUBCODc COMPONENT CODE SUB'"'ODE SUl!,CODE W1J IS I HI@ L!.J@ ~@) IA I CJC I u IM JU I@ ~@ ~@

7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION*

LER/RO LVENT YEAR REPORT NO. CODE TYPE N8.

@ :j~~~~ 17 ILJ I23 I Io I 612 I 1,..,.1 I28 01 3 I L£j I31 I ~

21 2: 24 26 27 29 30 32 ACTION FUTURE EFFECT SHUTDOWN (22\ ATTACHMENT NPRD-4 PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS ~ SUBMITTED FORM :;us. SUPPLIER MANUFACTURER LJ:J@W@ ~@ ~@) 10 Io I 01 I lliJ@ LU§ ~@ I B15 12 I OJ@

33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORREC"rlVE ACTIONS @ ~ .

ITliJ I Pressure loss initially caused by opening tan.k and later by a de! ecti ve 1

[J]J] I gasket which apparently was damaged during removal of the tank cover. ,

I ITIIJ I Gasket was replaced and tank pressure restored .

..._~~~~~~~~~~~~~~~~~~~~~~~~~~~~~__JI

[ill]

[ill]

1 a ~9::~-:--~~~~~~~~~~~~~~~--::--~~~~~~~~~~-~~~~-~~~~~~~~~~....J F;CILITY ITITJ l.!J@ I Dlj<i2vj~

STATUS  % POWER OTHER STATUS METHOD OF 80 jO I 9 I 8 J@I N /A N/A DISCOVERY DESCRIPTION @

7 8 ACTIVITY 9 10 CONTENT 12 13 44. 45 . 0 ~465--------------------- 80

~ ~@~@IN/A r.-r;:-\RELEASED OF RELEASE AMOUNT OF ACTIVITY @ I N/A LOCATIONOFRELEASE~ (.;;;.,

7 8 9 10 11 . 'T_______________________ J 9

PERSONNEL EXPOSURES 44 45 r;-r:;-J NUMBER TY?E DESCRIPTION@ o L.!...J..?...J8 I9 0 I 010 11I@~@! 12 13 N/A '7"°"":..., 1 H:J1N~8

"-.C "0" '",....,"" r-JG ,.

~

7 PERSONNEL INJURIES E::ill I oNn)ro I@ DEir/~r!ON~ *'.~"C)

">._jvl.i\U...J-.) f1li'1..J.11.J1u.-..--..*1U

ll!i'i 80 7 89 1 LOSS OF OR DAMAGE

~12~::~--:::-::.::--~~~--~~~~-~~~-~-~--~~~~~~~-~-~~~-~-J

~

i*o FACILITY (';":;\ i"i**~ 11 1\!'**I:'*

r:;-r;;-i

~ ~@ TYPE DESCRjPTION N;A .-z.. on Ct' i\1* , ,~, nit"'

c'*!*

ao 7 8 9 ~10~~~~-::::-~---~~~~~-~-~~~~~~~-~~-~~~~~~~~~~~~~-~_JoO PUBLICITY Q.,

  • , NRC USE ONLY

~

1;:*J-j "j'.'"*:~1":**.

ITTIJ rwreeStlr!AION lHi'.-~'1boo'"JiX!j'j32-J II II IIII II III 8 9 10 68 69 80