ML18153B881

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Insp Repts 50-280/89-21 & 50-281/89-21 on 890702-29. Violations Noted.Major Areas Inspected:Plant Operations, Plant Maint,Plant Surveillance,Ler Review,Followup on Inspector Identified Items & Plant Startup from Refueling
ML18153B881
Person / Time
Site: Surry  Dominion icon.png
Issue date: 09/01/1989
From: Fredrickson P, Holland W, Larry Nicholson, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18153B879 List:
References
50-280-89-21, 50-281-89-21, NUDOCS 8909140004
Download: ML18153B881 (26)


See also: IR 05000280/1989021

Text

,,

Report Nos. :

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION 11

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

50~280/89-21 and 50-281/89-21

Licensee:

Virginia Electric and Power Company

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

Inspection Conducted:

July 2-29, 1989

License Nos.: DPR-32 and DPR-37

<*~ ~~//

Inspectors:

~)?/.

~~

W. * E. Ho 11 ang:sei, o.rResi dent Inspector

J. W~Re~~r --~

L. E.3ifichoison, Resident Inspector

Accompanying I~

7: _t_Bre~ au, Be actor Engineer

Approved by: C.,--! I (]~'1,.-,VI/Vr:?J,/~

P. E. Fredrickson, Section Chief

Division of Reactor Projects

SUMMARY

Scope:

Date Signed

1/11~~1

Date Signed

1/i/Y2

Date'Signed

7/t/P}

Daite Signed

This routine resident inspection was conducted on site in the areas of plant

operations, p 1 ant maintenance, p 1 ant survei 11 ance, 1 i censee event report

review, followup on inspector identified items, and plant startup from

refueling.

Certain tours were conducted on backshifts or weekends.

The resident staff

maintained 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> coverage of the Unit 1 startup beginning on July 2 and

continuing through the return to power operations on July 7.

In addition,

backshift or weekend tours were conducted on July 8, 9, 15, 16, 17, 18, 19, 20,

23, and 29.

Results:

During this inspection period, three violations were identified for:

failure

to provide adequate procedures and/or instructions for calibration of the power

range nuclear instrumentation as required by Technical Specification 6.4

390':/ 140004

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2

(paragraph 3.a); failure to place an inoperable canal level instrument in trip

within one hour as required by Technical Specification Table 3.7-2, Item 5.a

  • (paragraph 3.g); and failure to maintain the condensate storage tank level at

or above the limit specified in Technical Specification 3.6.B.2 (pargraph 3.g).

Two unresolved items *were identified:

one regarding the reportability in

accordance-with 10 CFR 50.72 of two events which resulted in the tripping of

safety-re 1 ated chi 11 ers and charging pump service water pumps (paragraph 3. g),

and the other involving the licensee's program to effectively implement

requirements that are invoked by amendments to the technical specifications

(paragraph 6.h).

-

In addition, a weakness was identified during the Unit 1 restart with regards

to multiple procedure concurrent usage and a lack of sensitivity to initial

conditions in procedure (paragraph 3.a).

Also, a weakness was identified

regarding.the transmittal of data used by operations for reactivity calcula-

tions (paragraph 6.g) .

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

2 .

W. Benthall, Supervisor, Licensing

R. Bilyeu, Licensing Engineer

R. Blount, Superintendent of Technical Services

D. Christian, Assistant Station Manager

D. Erickson, Superintendent ot Health Physics

  • E. Grecheck, Assistant Station Manager
  • M. Kansler, Station Manager

T. Kendzia, Supervisor, Safety Engineering

  • J. McCarthy, Superintendent of Operations
  • G. Miller, Licensing Coordinator, Surry

J. Ogren, Superintendent of Maintenance

T. Sowers, Superintendent of Engineering

A. Price, Site Quality Assurance Manager

Other licensee employees contacted included control room operators, shift

technical advisors, shift supervisors and other plant personnel.

  • Attended exit interview

On July 24, i989, one of the Commissioners of the Nuclear Regulatory

Commission, James R. Curtiss, visited the Surry Power Station for a

familiarization tour, to meet with licensee management and staff, and to

review the current status of the station.

Commissioner Curtiss was

accompanied by the following personnel:

A. Gibson, Director, DRS, Region II

K. Connaughton, Technical Assistant to the Commissioner

M. Sinkule, Branch Chief, DRP, Region II

NRC Resident Inspectors

The Commissioner attended the morning management meeting, met with the

resident inspectors, was given a presentation on the status of the station

by licensee management, and was taken on a tour of the station including

the turbine building, control room, emergency diesel generator rooms, and

the independent spent fuel storage installation.

Acronyms and intialisms used throughout this report are listed in the last

paragraph.

Plant Status

Unit 1 began the reporting period in intermediate shutdown with a slow

heat up in progress.

The unit reached hot shutdown on July 4, and the


2

reactor was taken critical on July 5, 1989.

Physics testing commenced the

same day and was completed on July 6.

The unit was operating at 63% power

when an automatic reactor trip occurred at 0643 hours0.00744 days <br />0.179 hours <br />0.00106 weeks <br />2.446615e-4 months <br /> on July 9, 1989r

The trip, which is discussed in paragraph 3.~, was appropriately reviewed

and the unit was returned to criticality at 2353 hours0.0272 days <br />0.654 hours <br />0.00389 weeks <br />8.953165e-4 months <br /> on the same day.

The unit recommenced power operation on July 10 and remained at power for

the remainder of th~ period.

Unit 2 began the reporting period in cold shutdown.

The unit remained in

cold shutdown for the duration of the inspection period while substantial

operational reviews and maintenance activities were being conducted.

During the period, the hydrostatic testing of the S/G feedwater 1 i ne

repairs was accomplished.

3.

Operational Safety Verification (71707)

a.

Daily Inspections

The inspectors conducted daily* inspections in the following areas:

control room staffing, access, and operator behavior; operator

adherence to approved procedures, techni ca 1 speci fi cat i ans, and

limiting conditions for operations; examination of panels containing

instrumentation and other re~ctor protection system elements to

determine that required channels are operable; and review of control

room operator logs, operating orders, plant deviation reports, tagout

1 ogs, jumper 1 ogs, and tags *on components to verify compliance with

approved procedures. *

The inspectors specifically focused on Unit 1 restart activities

during the earlier part of the inspection period.

Twenty-four hour

monitoring coverage of the Unit 1 restart activities by the resident

inspector staff continued from the l_ast inspection period until

July 7, 1989.

During the monitoring of the Unit 1 startup, the inspectors noted

that the controlling procedures were not coordinated in a manner such

that one procedure would be completed prior to the next sequential

procedure being started.

One example was identified when OP-1.3,

Unit Startup Operation (350/450 to HSD), was not completed and

OP-1.4, Unit Startup Operation -

HSD to 2% Power, was being

accomplished at step 5.22 in the performance section.

Of special

concern was the fact that O.P-1.4, initial condition 3.2, required

that OP-1.3 be complete, yet the operators appeared to be comfortable

in OP-1. 4 without * a 11 initial conditions being verified and *

documented.

The inspector did verify, that the intent of OP-1.3 had

been *completed and that the operators were in proper control of the

startup; however, multiple procedures were unnecessarily being

performed concurrently and a lack of sensitivity to initial

conditions was apparent .

3

On July 9, 1989 at 0643 hours0.00744 days <br />0.179 hours <br />0.00106 weeks <br />2.446615e-4 months <br />, Unit 1 experienced an automatic reactor trip from approximately 63% reactor power.

The reactor trip

was caused by a turbine trip which was initiated by a high level in

SIG B.

The high level in S/G B was caused by a transient

(approximately 30% turbine runback in about 9 seconds) due to the

protect ion circuitry sensing a rod drop condition on power range

channel N41.

The unit did not ride out the transient due in part to

B S/G .feedwater regulating valve being in manual control, rod control

being in manual, and an inadvertent operator action in closing the

main steam dump valves.

The operator actions were due to

misdiagnosis of the transient.

All safety systems functioned as

required during and after the reactor trip.

However, source range

channel N31 failed to reinstate automatically after the reactor trip

due to improper compensation of intermediate range channel N35.

Operators took the necessary actions to reinstate source range

channel N31.

After the trip, the plant was stabilized in the hot shutdown

condition.

The licensee held a post trip review meeting with those

operators involved in the trip,to review the sequence of events.

The

inspectors attended that meeting and with the information provided

from the meeting and other charts provided from computer printouts

determined the sequence of events as follows:

T0 minus 162 seconds - initiation of turbine runback signal

T minus 157 seconds - all steam dumps receive open signal

0

T

mi nus 153 seconds - turbine runback stops (approx. 50% load

r2duction)

T0 minus 145 seconds - all steam dumps open

T0 minus 120 seconds - S/G A, Band C level at 25%

T0 minus 96 seconds - S/G A, B, and C level at 32%

T0 minus 48 seconds - S/G A and C level at 44%; S/G B level at 55%

T minus 40 seconds - steam dumps receive close signal by operator

aetion

T0 minus 24 seconds - S/G A and C level at 50%; S/G B level at 68%

T0 minus 5 seconds - steam dumps start to close

T minus 2 seconds - S/G A and C level at 54%; S/G B level at 75%;

tSrbine trip

T0 - reactor trip

4

T plus 12 seconds -

steam dumps receive open signal based on

oSerator action and Tave-Tref mismatch

-

T0 plus 20 seconds - steam dumRs full open

T0 plus 50 seconds - steam dumps mostly closed due to Tave-Tref match

As shown above, the initial transient caused the S/G to decrease in

level (shrink).

Steam generators A and C were in automatic feed

control and were maintained in a band which would not have resulted

in a turbine/reactor trip.

However, B S/G feed control was in manual

due to the automatic control experiencing some electrical problems

earlier.

Operator action was required to maintain the proper SIG

level during the transient.

Due to an apparent overfeeding of the B

S/G during the early part of the transient to compensate for shrink,

the B S/G level increased to the turbine trip setpoint (75% level)

~pproximately 2 minutes and 40 seconds after the transient began,

resulting in the turbine trip/reactor trip.

After evaluation of the transient, the inspectors focused

specifically on the cause of the turbine runback.

During the

licensee's post trip review meeting with the operators, the licensee

determined that the cause of the transient was due to a blown control

fuse in NI cabinet N41.

The bl own fuse was caused by the I&C

technicians use of an ungrounded volt meter during recalibration of

the NI flux setpoints.

It was also noted that several discussions

had been held between the I&C technicians and their supervisor on

~hether to use a grounded or an ungrounded meter during the calibra-

tion.

However, no clear resolution was provided to this concern

prior to the mistake being made.

Also, the procedure used for the

calibration did not specify the type of meter to use.

The inspectors, after hearing the discussions above, concluded that

the I&C shop sensitivity to resolving problems prior to them becoming

a significant event was not what is required to ensure that safety

systems would not be unnecessarily challenged.

The inspectors

discussed this concern with station management and were reassured

that ensuring that the job is correctly performed each time is a

requirement.

This assurance was confirmed by aggressive management

actions with regard to changes in the shop supervision along with

other personnel actions.

The licensee also instituted a performance

improvement program in the I&C area.

After reviewing *all the above, the inspectors concluded that

appropriate corrective actions were being implemented; however, the

above event was a result of a failure to provide adequate procedure

and/or instructions for calibration of components involving the

nuclear safety of the station. Technical Specification 6.4 requires

that detailed written procedures with appropriate*check-off lists and

5

instruct ions be provided for calibration of instruments, components,

and systems involving the nuclear safety of the station.

Failure to

provide an,adequate procedure and/or instruction for calibration of

the power range nuclear instrumentation is a violation of TS 6.4

(280/89-21-01).

b.

Weekly Inspections

The inspectors conducted weekly inspections in the following areas:

verification of operability of selected ESF systems by valve

alignment, breaker positions, condition of equipment or component(s),

and operability of instrumentation and support items essential to

system actuation or performance.

Plant tours were

conducted which

included observation of general plant/equipment conditions,* fire

protection and preventative measures, control of activities in

progress, radiation protection controls, physical security controls,

plant housekeeping conditions/cleanliness, and missile hazards.

The

inspectors routinely monitored the temperature of the auxiliary

feedwater pump discharge piping to ensure steam binding is prevented.

  • c.

Biweekly Inspections

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagout(s) in

effect; review of sampling program (e.g., primary and secondary

coolant samples, boric acid tank samples, plant liquid and gaseous

samples); observation of control room shift turnover; review of

implementation of the plant problem identification system; verifica-

tion of selected portions of containment isolation lineup(s); and

verification that notices to workers are posted as required by

10 CFR 19.

-

d.

Areas Inspected

Inspections included areas in the Units 1 and 2 cable vaults, vital

battery rooms, steam safeguards areas, emergency switchgear rooms,

diesel generator rooms, control room, auxiliary building, Unit 2

containment, cable penetration areas, independent spent fuel storage

facility, low level intake structure, and the safeguards valve pit

and pump pit areas. Reactor coolant system leak rates were reviewed

to ensure that detected or suspected 1 eakage from the system was

recorded, investigated, and evaluated; and that appropriate actions

were taken, if required.

The inspectors routinely independently

calculated RCS leak*rates using the NRC Independent Measurements Leak

Rate Program (RCSLK9).

On a regular basis, RWPs were reviewed and

specific work activities were monitored to assure they were being

conducted per the RWPs.

Selected radiation protection instruments

were periodically checked, and equipment operability and calibration

frequenci were verified.

6

The residents observed chemical analyses being performed for boron

concentrations in the hot laboratory.

These analyses were for

operations information and to support certain parameter requirements

being used in physics testing.

On July 7, 1989, the inspectors

discussed with chemistry personnel a reactor power level hold at 30

percent because chlorides on the secondary side were 34 ppb.

Chemistry limits are 20 ppb chlorides.

The chloride level was

lowered by using S/G blowdown and adding clean makeup water.

The

licensee

1 s chemist stated that it is not unusual to have chloride

spikes after having a unit down for such a long period of time

(Unit 1 had been down 10 months).

A 11 actions appeared to be

conservative.

e.

Physical Security Program Inspections

In the course of monthly activities, the inspectors included a review

of the licensee

I s physical security program.

The performance of

various shifts of the security force was observed in the conduct of

daily activities to include:

protected and vital areas access

controls; searching of personnel, packages and vehicles; badge

issuance and retrieval; escorting of visitors; and patrols and

compensatory posts.

f.

Licensee 10 CFR 50.72 Reports

(1)

On July 9, 1989, the licensee made a report in accordance with

10 CFR 50. 72 with regards to an automatic reactor trip/turbine

trip on Unit 1.

Details of this event are discussed in

paragraph 3.a.

(2)

On July 9, 1989, the licensee made a report in accordance with

10 CFR 50. 72 with regards to degradation of the emergency

assessment capability in that the SPDS displays from the ERF

computer were not functioning properly.

This condition occurred

during downloading of data from the Unit 1 reactor trip that

occurred earlier that day.

The licensee diagnosed the problem

as SPDS hardware related.

The problem was corrected and the

unit returned to power.

g.

Operations Related Problems

The inspectors expressed concern regarding i ndi cat ions of poor

operator performance that surfaced during the latter part of the

inspection period.

Discussions were held with appropriate levels of

station and corporate management with everyone in agreement that

operator performance warranted corrective actions.

Specific examples

of the problems included the following:

(1)

7

Intake Canal Level Instrumentation

  • On July 14, 1989, the licensee identified via stati~n deviation

S2-89-610 that an inoperable intake canal level channel was not

placed in the tripped condition within one hour as required by

TS Table 3.7-2, Item 5.a.

Channei III of the intake canal level

instrumentation system was rendered inoperable when stop logs

were installed in accordance with TM S2-89-76 at 1210 hours0.014 days <br />0.336 hours <br />0.002 weeks <br />4.60405e-4 months <br /> on

July 14, 1989.

The channel was not placed into a tripped

condition until 1910 hours0.0221 days <br />0.531 hours <br />0.00316 weeks <br />7.26755e-4 months <br /> that day.

Further evaluation of this

event by the licensee revealed that a similar event occurred

when Unit 1 exceeded the 350 DEGF/450 PSIG 1 imitations on

July 2, 1989, and ~ont i nued ope rat ion with an inoperable level

channel until July 5, 1989, without placing the channel in the

tripped condition.

The safety consequence during these two

evolutions were minimal, however, due to the waterbox being

dewatered and therefore causing the level channel to

automatically go to the trip condition.

Previous SSFI issues required the installation of four

independent level indicators at the high level intake structure

that provide input to a 3 out of 4 logic circuit for initiation

of non-essential SW isolation.

The four level sensors. are

located in the i ndi vi dual high level intake screenwe 11 bays

(Unit 1-bays

18

1 and

1D

1

, Unit 2-bays

1A

1 and

1C1 ), between the

rotating screens and trash bar racks.

This is a shared system

that provides input to both units ESF logics.

The stop logs are

essentially large plates that are installed in the canal at the

intake structure and a 11 ow dewateri ng of the pl ant systems

downstream of the intake structure.

The installation of stop

logs on the bays that contain the level instrumentation isolates

the level sensors from the actual canal.

The operators failed to realize that installation of stop logs

on certain Unit 2 intake structures rendered the downstream

level . indicators inoperable that were required for Unit 1

operation.

The affected channel automatically goes to the

tripped position, however, when the waterbox is dewatered below

the actuation setpoi nt.

A review of the sequence of events

revealed that the licensee operated for approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />

with a less conservative 3 out of 3 logic instead of the

required 3 out of 4.

A sequence of events is summarized as follows (times indicated

in parentheses):

6/14/89

6/23

New level system placed in service.

Technical Specification amended requiring system

operability.

...

. ..,-:.*

6/25

7/2 (2200)

7/5

(2100)

7/14 (1210)

7/14 (1521)

7/14 (1910)

7/17 (1157)

8

Stop log installed & unit 2-A waterbox dewatered.

Unit 1 enters mode requiring operable level

instrumentation.

Unit 2-A waterbox refilled and stop logs removed.

Unit 2-A stop logs installed.

Unit 2-A waterbox dewatered.

Canal level channel III placed in trip.

Unit 2-A stop logs removed.

The stop logs were installed and removed using the station TM

system as prescribed in stat ion admi ni strati ve procedure

SUADM-0-11.

The station does not have a specific procedure

outlining the method and precautions involved with stop log

installations.

The inspectors reviewed the TM log sheets for

the installations noted above and concluded that an inadequate

review and analysis were performed prior to authorization by the

shift supervisor for stop lo~ installation.

Paragraph C.2 of

the subject TM logs was marked

11 N/A

11 , therefore deleting any

need for a safety analysis or 10 CFR 50.59 review for the impact

on the UFSAR or TS requirements.

In addition, subsequent

review of this TM by both the Superintendent of Operations and

the SNSOC failed to identify and correct the 1 ack of a review or

analysis on the initial TM stop log installation.

The inspectors reviewed th~ training lesson plans given to all

licensed operators regarding the installation of the new canal

level instrumentation.

Three separate lesson plans contained

information on the location and function of the* new sensofs.

Although the fact that the stop log installation would interfere

with the level sensors was not specifically detailed in the

lesson plans, the inspector concluded that sufficient training

was conducted.

-

The licensee performed a human performance evaluation of this

event and presented the preliminary findings to the resident

inspector staff on July 24 and 25.

A general conclusion was

given that this problem was essentially a human performance

problem with a lack of attention to detail.

In addition,

several weaknesses were identified that contributed to the TS

violation.

The inspectors reviewed the licensee 1s evaluation of

this situation and agreed with the following conclusions:

No procedures existed for the installation and removal of

stop logs.

This work was performed under a TM with no

formal procedure in place.

(2)

9

The closeout process for the design change package that

installed the new level system. failed to adequately

identify the need for revision of applicable procedures.

The review and safety analysis of the TM that installed and

removed the stop logs*were inadequate.

Technical Specification Table 3. 7-2, Item 5. a, requires that

i noperab 1 e 1 ow intake cana 1 1 eve 1 channe 1 s be p 1 aced in a

tripped condition within one hour.

failure to place the low

intake canal level channel III in a tripped condition when it

became inoperable on July 14, 1989, is a violation of the TS

(280/89-21-02).

Corrective actions were being evaluated by the licensee as the

inspection period ended.

A standing order (S.O. 10) was issued

on July 27 that * requires the Superintendent of Operations

approval prior to installation of stop logs.

Service Water Cooling

On July 18, 1989, a total Joss of SW cooling to the Units 1 and

2 charging pumps occurred apparently due to the operation of an

adjacent MOV and therefore connecting an empty line to the SW

flowpath.

A six hour LCO to place the unit in .hot shutdown was

initiated after both SW pumps to the charging pumps became

airbound.

In addition, since the Unit 2 SW pumps also became

ai rbound, -a seven day LCO was entered due to the 1 oss of

crosstie charging capability.

A report of this event was being

p*repared in accordance with 10 CFR 50. 73.

Maintenance was

performing stroke testing on

a

MOV

(2-SW-MOV-201A) that supplies water to the Unit 2 bearing

cooling water heat exchangers when the event occurred.

The six

inch SW supply to the subject pumps taps off a thirty-six inch

supply line to the bearing ~oolers.

The perturbation occurred

when the large MOV was cycled open.

The licensee stated at the

time that air in the large bearing cooling line was drawn into

the suction of the safety-related SW lines .and resulted in the

air binding.

Station engineering later stated, after the

July 23 event, {see next paragraph), that the SW discharging to

a basically empty Unit 2 discharge tunnel could have contributed

to pulling air back up into the system.

The system configura-

tion contributes to the problem in that the SW charging pumps

for both units (1 & 2- SW-P-10 A & B) and all three main control

room envelope chillers take SW suction off a common header.

Air

entrainment into this common header results in a loss of both

trains of equipment for both units.

10

On July 23, 1989, operation of the SW system again resulted in a

total loss of SW to mechanical equipment room #3, which resulted

in a loss of main control room envelope chillers and cooling

water to the charging pumps.

This event was similar to that

discussed above in that it was initiated by the operation of a

SW valve (2-SW-MOV-2018) to the Unit 2 bearing cooling water

heat exchanger.

Although system engineering could not identify

the exact cause of this pertubation, it does indicate that the

operation of the SW system is extremely sensitive to pertuba-

t ions in thfs area.

The ope rat ions staff was aware of the

previous event and was prepared to close the bearing cooling

valve upon indications of air binding.

It became apparent

following this event that the full implications of discharging

to an empty un*it 2 discharge tunnel was not understood.

The

1 i censee is prepa*ri_ng a report to the NRC on this event in

accordance with 10 CFR 50.73.

During the event on July 23, the inspector was in the control

room during part of the recovery of some of the components.

The

inspector observed that the operators were fo 11 owing the

required procedures; however, with the loss of multiple

components, it was noted that 1 imited guidance was provided

regarding the appropriate sequence of recovery for components.

Also, the.inspector observed recovery operations at the location

of most of the components (MER3) and again concluded that

procedural . guidance regarding the appropriate venting of the

system was not available to the operators.

These areas are

under review by the licensee for possible enhancements.

The inspectors questioned the licensee with regards to

reportability of the two above events as required by

10 CFR 50. 72.

The licensee stated that although there is no

formal analysis documenting an acceptable dufation of operation

without SW cooling, they have historically been able to vent the

air from the system and restore flow prior to any adverse

effects on the charging pumps.

A review of the Unit 2 charging

pump data during the 47 minute duration that the SW was

inoperable indicated that the thrust bearing temperature

increased over that period.

The inspection period ended prior to reso 1 ut ion of the

reportability of these events~

This issue is identified as an

unresolved item (280/89-21-03) pending additional

NRC and

licensee review of reportability and appropriate classification

of charging pump operability.

(3)

Component Cooling Water Perturbation

On July 26, 1989 at 2119 hours0.0245 days <br />0.589 hours <br />0.0035 weeks <br />8.062795e-4 months <br />, operators were attempting to

refill a CCW heat exchanger (1-CC~E-18) and caused a rapid level

_)

11

drop in the CCW head tank that resulted in low CCW pump

discharge header pressure and an automatic start of a standby

pump.

The motor amperage *for the running CCW pumps fluctuated,

but th~ reactor coolant* pump parameters remained stable during

this transient.

The procedure used to return the heat exchanger

to service, MOP-1.6, Return To Service Of Safety Related Heat

Exchangers (Generic), is a generic procedure with no instruc-

tions pertaining to the CCW heat exchangers.

The inspectors reviewed this event and discussed the facts with

station management.

The transient was formally identified on

station deviation Sl-89-1752 that was submitted on July 27.

The

immediate safety consequence of this event is a loss of cooling

to the reactor coolant pumps on Unit 1.

Component cooling also

provides cooling to the RHR system and various primary heat

exchangers.

The licensee stated that this event was caused by a

lack of adequate supervision of an inexperienced auxiliary

operator.

Corrective act i ans were being developed as the

inspection period ended.

Although this event was not considered to be a violation of

regulatory requirements, the inspector agree with licensee

managements assessment that proper overview and ctintrol of an

evolution which could affect the safe operation of the station

must be maintained.

(4)

Emergency Condensate Storage Tank Level Drop

On July 27, 1989, operators allowed the level in the Unit 2

emergency condensate storage tank (2-CN-TK-1) to fall

approximately 10,000 gallons below the TS limit while trans-

ferring water to fill the underground condensate tank.

This

condition is 1n violation of TS 3.6.B.2 that requires a minimum

of 60,000 galloni of water be available from the opposite ~nit

to supply the auxiliary feedwater crossconneGt.

The transfer of water was being performed in accordance with

operating procedure 2-0P-31.2.5,

Filling The

Emergency

Condensate Makeup Tank, 2-CN-TK-3.

Section 4.0 of this

procedure references a requirement to maintain greater than

60,000 ga 11 ons in tank 2-CN-TK-1.

A review of the reactor

operator logs indicated that the level was adequate at 1000

hours and had fallen to 44 percent (50,000 gal) at 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br />.

The operator 16gged this level without realizing that the level

was in.violation of TS.

The problem was detected at 1822 hours0.0211 days <br />0.506 hours <br />0.00301 weeks <br />6.93271e-4 months <br />

and the tank level ~as refilled to greater than 60w000 gall~ns

by i844 hours.

Technical Specification 3.6.B.2 requires that a minimum of

60,000 gallons of water shall be available in the tornado

protected condensate storage tank of the opposite unit to supply

12

emergency water to the auxiliary feedwater pump suction of that

unit.

Failure to maintain greater than 60,000 gallons of water

in tank 2-CN-TK-l on July 27, 1989, is a.violation of TS

(280/89-21-04).

The above problems indicate a lack of attention to detail.

Two of the

events, i.e. stop 1 og and condensate l eve 1, are related in that the

operators for Unit 2 ~ere not sensitive to the effects of their action on

the opposite unit at power.

The SW events indicate that the performance

of this system is very sensitive to inappropriate operation.

Within the areas inspected, three violations and one unresolved item were

identified.

4.

Operational Readiness Program Review - Unit 2 (71710)

The inspectors reviewed the Unit 2 restart action items list.

Currently

75 of 211 items still remain open.

All of these items and any additional

items added to the list will be resol.ved before Unit 2 is restarted.

Items will be added as a result of the system walkdowns.

The licensee has

completed 100 percent of the system walkdowns in Unit 2 containment and is

evaluating the results.

A review of the containment charging and

ventilation systems revealed that six items would be added to the restart

list for the ventilation system and two would be added for the charging

system.

In the case of the six items, three involved cleaning filters and

three involved repairing or evaluating a valve.

In the case of the two

  • items for the charging systems, one involved a missing flow transmitter

(the transmitter had been removed to repair one on Unit 1) and the second

item involved the necessity to add several supports for a charging line.

The inspectors reviewed selected findings from the system engineering

walkdown of the Unit 2 SI system.

A problem was identified (station

deviation S2-89-682) pertaining to the labeling of certain .valves and

instrumentation in the hot leg SI lines.

Components indicated on station

drawing 11548-FM-0898, sheet 4 of 4, as injection lines to the hot leg of

the reactor coo 1 ant loop 1 are actually associated with the hot leg

loop 3, and vice-versa.

The problem was limited to components downstream

of any MOVs or components requiring operator actions.

The Operations

Superintendent reviewed the situation and concluded that the problem would

not have an adverse effect on operation during any accident scenario.

The

inspectors reviewed the evaluations and concurred with the findings.

On July 22, 1989, the inspectors observed a Unit 2 containment walkdown

for parts of the auxiliary feedwater system and SIG blowdown system by

systems engineers. The methods used for the evaluation and the findings

appeared to be acceptable.

Within the areas inspected, no violations or deviations were identified .

,.,,"_ -

13

5.

Maintenante In~pections (62703 & 42700)

During the reporting period, the inspectors reviewed maintenance

activities to assure compliance with the appropriate procedures.

Inspection areas included the following:

'

a.

Pressurizer Power Oper~ted Relief Valve

b.

The inspectors reviewed the repair of the pressurizer PORV

2-RC-PCV-2455C following the valve failure that occurred on June 21,

1989.

The RCS was being maintained in a reduced inventory condition

with the PORVs open and vented to the primary relief tank.

The

control room operator n~ticed that the subject valve went from open

to close when the II Lo Air Bottle Press ure

11 annunciator came on.

The

operator attempted unsuccessfully to reopen the valve.

Field

inspections revealed that the valve actuator had cocked and several

cap screws within the actuator had sheared.

The backup air b'ott l es

had depressurized.

The inspectors observed certain failed parts from this valve and

reviewed the corrective actions and failure analysis associated with

this _event.

It appears that the regulator in the backup air bottle

supply failed and allowed the full 2400 psig pressure to be applied

  • to the valve actuator.

The licensee performed an evaluation of the

failure as documented in EWR 89-499, dated July 8, 1989.

The results

of this evaluation concluded that this event did not constitute an

unreviewed safety question.

The inspectors reviewed the evaluations

and documentation pertaining to this event and agreed with the

licensee's assessment.

No discrepancies were identified.

Feedwater Regulating Valve

On July 14; 1989, the inspectors observed the repair on the Vnit 1

feedwater regulating valve 1-FW-FCV-1488.

This valve is the main

feedwater regulating valve for the B S/G.

The valve was sticking in

certain positions making it more difficult to control the water level

of the S/G.

In order to make the repair, the licensee reduced power

on Unit 1 to 19 percent, isolated the valve, and used the feedwater

bypass line to supply feedwater to the S/G .. The inspector observed

replacement of the valve cage and the double plug and stem. The

internal part of the valve and adjacent piping were inspected for

cleanliness and foreign objects.

The torquing technique for the cage

and some o*f the bolts was observed. The inspectors examined the

procedure being used, Procedure No.

MMP-C-FW-145, Disassembly,

Repair, Reassembly, and Testing of Feedwater Regulating Valve.

The

torquing values being used were in accordance with the procedure and

14

the appropriate steps were being initialed.

A later evaluation by

the 1 i censee showed that the va 1 ve externa 1 spring was rubbing

against one side of the yoke inhibiting it 1 s feedwater control

function.

No discrepancies were identified.

Within the areas inspected, no violations or deviations were identified.

6.

Surveillance Inspections (61726 & 42700)

During the reporting period, the inspectors reviewed various surveillance

activities to assure comp 1 i ance with the appropriate procedures as

follows:

Test prerequisites were met.

Tests were performed in accordance with approved procedures.

  • Test procedures appeared to perform their intended function.

Adequate coordination existed among' personnel involved in the test.

Test data was properly collected and recorded.

Inspection areas included the following:

a.

Containment Spray System

On July 2, 1989, the inspector reviewed test documentation for

periodic test l-PT-17.1, Containment Spray System, for spray pumps

l-CS-P-18, tested on June 3, 1989 and both 1-CS-P-lA and 1-CS-P-18,

tested on June 12, 1989.

Documentation was complete; the test

results indicated that satisfactory performance was obtained, with

the exception that pump 18 was placed in an alert status due to high

axial vibration from the inboard bearing.

The licensee issued.EWR 89-433 to eva 1 uate the results, and subsequently determined and

approved on June 20, 1989, new reference va 1 ues based on prior

performances of the pumps.

These new values permitted the licensee

to remove pump 18 from an alert status.

No discrepancies were noted.

b.

Charging Pump Operability Test

On July 2, 1989, the inspector reviewed test documentation for

periodic test 1-PT-.18.7, Charging Pump Operability and Performance

Test, for charging pumps: 1-CH-P-lA, tested June 4, 1989, 1-CH-P-18,

tested June 18, 1989, and 1-CH-P-lC, tested June 27, 1989.

Documentation

was

complete;

results indicated satisfactory

performance with the exception of pump 18.

Pump 18 was placed in an

alert status due to a high axial vibration on the inboard bearing .

. -_ .. :-.--

15

The licensee had several !SI pumps listed in the alert status in June

due to high vibration measurements as compared to their respective

reference va 1 ues.

The 1 i censee issued EWR-89-445 to eva 1 uate the

existing base 1 i ne va 1 ues, which were es tab 1 i shed using computer

generated reference values taken by the predictive analysis group

over the last year.

It was determined that these values were not

reflective of actua 1 component operating conditions.

The 1 i censee

establish new reference values using the actual data from the last

two tests; these values were approved by SNSOC on June 27, 1989.

Based on these hew values, pump l-CH-P-18 was not ~onsidered as being

.in an alert status.

No discrepancies were noted.

c.

Motor Driven Auxiliary F~edwater Pumps

On July 3, .1989, the inspector reviewed periodic test l-PT-15.lA,

Motor Driven Auxiliary Feedwater Pump, for pumps l-FW-P-3A, tested on

June 9, 1989 and l-FW-P-38, tested on June 15, .1989.

Test results

indicated that both pumps were in an a 1 ert status due to high

vertical vibration on the outboard pump bearing.

The test critique

. sheet for pump 3A did not correctly reflect this condition however,

and the licensee was informed of this error *in documentation.

The

licensee promptly corrected the documentation discrepancy.

Based on

the new reference values noted in EWR 89-445, both pumps were removed

from an alert status by the licensee.

No further discrepancies were

noted.

d.

Containment Inside Recirculation Spray System

On July 3, 1989, the inspector reviewed periodic test l-PT-17.2,

Containment Inside Recirculation Spray, for pumps 1-RS-P-lA and

l-RS-P-18, tested on June 21, 1989.

Documentation was complete; test

results indicated that pump lA was satisfactory and 18 was unsatis-

factory because the ERFSC failed to display the required information.

The 1 i censee adjusted the ERFCS and retested pump 1B on June 23,

1989.

The test results indicated that pump 18 performance was

satisfactory.

No discrepancies were noted.

e.

Containment Outside Recirculation Spray System

On July 4, 1989, the -inspector reviewed periodic test-l-PT-17.3,

Containment Outside Recirculation Spray, for pump l-RS-P-2A, tested*

on June .16, 1989.

Documentation was adequate; test results indicated

that the pump was satisfactory but placed on the alert status due to

high axial vibration on the inboard bearing.

The new reference

values, which were subsequently determined by EWR 89-445, permitted

pump 2A to be removed from an alert status.

No discrepancies were

noted .

f.

16

Emergency Service Water Pumps

On July 4, 1989, the inspector reviewed periodic tests l-PT-25.3A,

- .38, and .3C, Emergency Service Water Pump, for pumps 1-SW-P-lA,

tested on June 20, 1989; and 1-SW-P-lB and 1-SW-P-lC, tested on

February 15, 1989.

Documentation was adequate and test results

  • indicated that the pumps performed as desired.

No discrepancies were

noted.

g.

Control Rods

On July 4, 1989, the inspector witnessed hot rod testing of the

Unit 1 rods in accordance with periodic test 1-PT-7.2, Hot Rod Drops,

dated January 29, 1989.

This test measured the drop time for each of

the 48 control rods from fully withdrawn to dashpot entry.

The

inspector reviewed se 1 ected timing traces to independently verify

. that the drop time was within the 2.4 seconds allowed by TS.

Step 3.1 of the above test procedure requires the calculation of the

shutdown margin prior to changing core reactivity.

The inspector

reviewed the calculated shutdown margin and noted that the data used

(i.e. critical boron, rod worth, etc.) was supplied by the reactor

engineer in lieu of the curve book.

Although the procedure _that

performs this ca lcul at ion, OP-lF, specifies that approved data may be

supp 1 i ed by the reactor engineer, the data used for the above

calculation was obtained from a single sheet of paper marked

11 for

reference only

11 , with no revi'eW or approval process evident.

The

i nspec*tor revi e.wed the data and concluded that the figures used were

more conservative; however,

the use of the substitute data

constituted a revision to the station curve book without a comparable

review process.

The 1 i censee concurred that this is an apparent

weakness and plans to revise their method for supplying engineering

data regarding reactor startup.

The inspector reviewed a station

memorandum, dated July 24, 1989, that addressed this weakness and

out 1 i ned the need for improvement.

This i tern is i dent i fi ed as a

weakness with the control of data used for reactivity calculations.

h.

Reactor Trip Bypass Breaker

The inspectors reviewed the details regarding the inability to test

the automatic shunt trip feature on the reactor trip bypass breakers

as required by TS Table 4.1-1. This condition was identified by the

licensee (station deviation Sl-89-1646) dur1ng a review of the TS.

Because Surry does *not have automatic shunt trips on their reactor

trip bypass breakers, the licensee could not comply with the TS.

Amendment 117 to the TS, issued in 1987, required that the reactor

trip bypass breaker local manual undervoltage trip be tested prior to

placing the breaker in service and the automatic shunt trip be tested

17

every refueling.

A local manual undervoltage trip and an automatic

shunt trip feature do not exist at Surry.

The inspectors discussed

the existing breaker features with NRC regional management and NRR,

and ascertained that the existing condition is acceptab 1 e for

continu~d operations.

The .licensee is planning to submit a TS change

for this compliance issue.

The above discrepancy indicates a potent i a 1 weakness in the

licensee's program that implements TS requirements and assures that

compliance is achieved.

The fact that a specific requirement was

added in 1987 and the normal implementation and review/audit

functions did not identify that compliance was impossible until 1989

raises questions regarding the effectiveness of the programs.

This

item is identified as an unresolved item (280,281/89-21-05) pending a

more thorough review of the licensee 1 s program that implements TS

requirements.

Within the areas inspected, one unresolved item was identified.

7.

Licensee Event Report Review (92700)

The inspectors reviewed the LER's listed below to ascertain whether NRC

reporting requirements were being met and to determine appropriateness of

the corrective actions. The inspector's review also included followup on

implementation of corrective action and review of licensee documentation

that all required corrective actions were complete.

LERs that identify violations of regulations and that meet the criteria of

10 CFR, Part 2, Appendix C,Section V shall be identified as NCV in the

following closeout paragraphs.

NCVs are considered first-time occurrence

violations which meet the NRC Enforcement Policy for exemption from

issuance of a Notice of Violation.

These items are identified to allow

for proper evaluations.of corrective actions in the event that similar

events occur in the future.

(Closed) LER 280/88-021, Lifting of PORV Due to Overly Conservative

Setpoint:

This event was initiated with Unit 1 in cold shutdown, and was

caused by a pressure transient during a start of the RCP with a solid

plant.

The licensee

1s corrective actions, which included increasing the

PORV lift pressure setpoi nt by 10 lbs. to account for instrument

inaccuracies and revising operating procedure OP-5.1.2 to reflect the

desired RCP operations during solid water plant conditions appeared to be

adequate.

This LER is c~osed.

(Closed) LER 280/88-023,

11C

11 S/G Steam Flow Channel IV Failed Low Due to

Failed Mult.iplier/Divider.

The licensee was not able to determine the

cause for the fai 1 ed multiplier/divider power supply transformer.

However, corrective actions were routine, e.g., replaced failed component

and conducted logic circuit tests.

Since the reactor protection and SI

instrumentation is periodically tested and calibrated, no additional

corrective actions are necessary.

This LER is closed.

18

(Closed) LER 280/88-025, Control/Relay Room Chillers Inoperable Due to

Inadequate Service Water Flow.

The licensee believed that the cause of

the event was due to inadequate SW flow to the chiller condensers as a

result of the method used to start/stop the chillers.

The licensee's

corrective action consisted of developing a procedure for starting/

stopping,control room chillers.

The inspector determined from a review of

operating procedure OP-21.4, dated September 20, 1988, that the procedure

provides adequate details to operate the control room chillers.

This LER

is closed.

(Closed) LER 280/88-028, Spent Fuel Assembly Placed in Wrong Location Due

To Inadequate Procedure.

The licensee determined that the cause of this

event was due to deficiencies in the methods used when spent fuel movement

was initiated and directed by on-site personnel.

The licensee revised

procedure OP-4.22, dated May 9, 1989, to include a verification that

Region I spent fuel pool area contains only Region I applicable fuel

assemblies prior to moving a dry storage cask into the fuel building.

The

inspector I s review of this procedure indicated that the procedure is

adequate to prevent recurrence of this event.

This LER is closed.

(Closed) LER 280/88-034, Control Room Chiller Tripped Due to Inadequate

Service Water Flow.

This event was caused by pressure control valves

being incorrectly adjusted.

The licensee's corrective action of

overhauling and setting the pressure control valves to their correct

setting is similar to the corrective actions of LER 88-007, which is a

similar event.

The corrective actions for LER 88-007 included a design

review to upgrade the SW supply to the control room and relay room

chillers; this review is not complete.

The inspector believes that the

licensee I s actions for LER 88-034 are adequate, but wi 11 continue to

monitor the status of the design work to upgrade the SW supply to the

chillers.

This LER is closed.

(Closed) LER 280/88-035, Iodine Spike.

This event is suspected to have

been caused by fuel element defects.

The licensee I s corrective actions

consisted of inspecting the fuel assemblies during their outage coupled

with subsequent shipment of fuel assemblies.

The inspector noted during

this review that one leaking assembly was identified during the

inspections.

The licensee replaced the defective assembly and removed

debris from 10 other assemb 1 i es.

The i rispector considers the licensee

I s

corrective actions as adequate.

This LER is closed.

(Closed) LER 280/88-036, Charging Pump Component Cooling Pumps Inoperable

Due To Air Binding.

Thi~ event was caused by an inadequate system design

in that the system does not allow for adequate venting of the CCW side of

the intermediate seal coolers, without air binding of the pumps, after the

system has been opened for maintenance.

The licensee's corrective action

consisted of performing an engineering review to resolve system design

inadequacies.

The inspector determined that the licensee has installed

high point vents to mitigate future air binding problems and that related

__ ., _.-.- ... -~,>-_

., --------

~~-.-,....:~.--.;-ro..,;..

19

drawings and procedures have been adequately updated to reflect these

changes.

This LER is closed.

(Closed) LER 280/88-037, Fire Watch Not Posted at Improperly Sealed

Pe net rat ion Within One Hour Due to Personnel Error.

The cause of this

event was attributed to the failure of a* QA inspector in promptly

reporting the unsealed penetration to the control room.

Also, operations

personnel, once notified, failed to post a fire watch within one hour.

The licensee

1s corrective actions consisted of personnel being counseled

on the need to take prompt corrective act ions when discovering or

receiving reports of any abnormal plant conditions.

The inspector

believes these actions are aqequate to prevent recurrence.

This LER is

closed.

~

(Closed)

LER 280/88-039, Control/Relay Room Chillers Trip Due To

Inadequate SW Flow.

This event was cause by a small refrigerant leak in

combination with insufficient SW cooling.

SW flow was being controlled

manually because normal pressure control valves were out of service, thus

preventing automatic increase in SW flow when higher demand was required.

The lice~see

1s corrective action was to overhaul the pressure control

valves * and recharge the refrigerant.

The inspector I s review of the

licensee

1 s corrective action indicated that these actions were adequate.

This LER is similar to LERs88-007 and 88-034, which substantiates the

need for the licensee to resolve SW flow design problems with this system.

The actions of this LER are adequate, but as noted above, the inspector

will monitor the licensee

1s design review to resolve SW flow problems.

This LER is closed.

(Closed) LER 280/88-042, Process Ventilation System Hi-Range Radiation

Monitors Out of Service Due to Failed Circuit Board.

The licensee 1s

corrective action consisted of replacing the failed circuit board, and is

considered adequate.

This LER is closed.

(Closed) LER 280/88-043, RSHX SW MOVs Discovered With Wrong Size Torque

Motors.

This event was

noted during the 1 i censee I s engineering

evaluation, conducted in response to IE Bulletin 85-b3.

The above MOVs

were noted as having undersized motors.

The licensee

1 s corrective actions

included replacing the undersized motors with the required 5 ft-lb torque

motors and expanding the MOV program to include all safety-related MOVs.

The inspector determined that the correct motors were installed and that

the licensee expanded its MOV program.

The MOV program is tracked as part

of commitment 89-0101-001 in response to NRC Inspection Report 280,281/88-45.

The licensee

1s corrective actions are adequate.

This LER is closed.

(Closed) LER 280/88-044, Unplanned Actuation of ESF Components, TV-DG-108A

and SOV-VS-101A.

This LER is germane to both units.

The event was

presumed to occur due to personnel in the area of the SOV disturbing it,

resulting in its actuation.

No conclusive evidence for the cause of this

20

event was determined in the ensuing investigation.

The licensee's actions

included normal refueling SI functional testing during the outage to

ensure operability.

This testing will be completed prior unit startup.

The inspector's review concluded that successful SI testing was completed

for Unit 1.

This corrective action is considered adequate.

This LER is

closed.

(Closed) LER 280/88-046, Operating MCR/ESGR Chi 11 er Turned Off Due To

Personnel Error.

The cause of this event was attributed to the control

room shift supervisor incorrectly assuming that only one chiller was in

operation, therefore, when l-SW-263 closed, the shift supervisor

incorrectly assumed all SW to the chillers had been isolated.

The shift

supervisor thus directed a control room operator to stop the

11C

11 chiller.

The licensee's corrective action consisted of counselling the shift

supervisor concerning his responsibility to maintain an accurate status of

plant components and systems.

The inspectors review determined that the

corrective actions are adequate.

This LER is closed.

(Closed)

LER 280/88-048, Diesel Fire Pump Batteries Not Seismically

Qualified.

This event was due to the failure in identifying the

operability concern of the* system when the deficiency was noted in

Jun~ 1986.

The licensee's corrective action consisted of re-em~hasizing

the policy of prompt reporting of discrepant conditions and to upgrade the

battery racks to meet seismic qualifications.

The inspector reviewed

these actions and determined that the battery racks meet seismic

~ualifications.

This LER is closed.

8.

Plant Startup from Refueling (71711)

During this inspection period, the inspectors witnessed selected portions

of the Unit 1 restart special testing as follows:

The inspectors witnessed testing and monitored activities associated with

periodic test l-PT-28.11, Startup Physics Testing.

This procedure was the

controlling procedure for several of the tests that were required to be

performed at low power. levels following refueling.

The inspectors

witnessed pre-test briefings, verified that specified conditions were met,

and witnessed selected portions of the following tests:

Reactivity Computer Accuracy Determination

This test determines the reliability range of the reactivity computer that

is used in subsequent testing by inserting and withdrawing control rods to

subtract or add react i vfty.

The computer was determined to be accurate

within plus or minus 30 pcm.

No discrepancies were noted.

Isothermal Temperature Coefficient

This test involves measuring the moderator temperature coefficient by

determining the effects of plant temperature changes on reactivity while

21

maintaining constant rod position and boron concentration.

The MTC was

determined to be -3.61 pcm/°F.

No discrepancies were noted.

Rod Swap Reference Bank Measurement

This test allows for measurement of rod worth (pcm) of the reference bank

(Cqntrol Bank 8) when fully inserted from 225 steps to O steps.

No

discrepancies were noted.

Integral Rod Worth Measurements Using the Rod Swap Technique

This test allows for determination of the differential rod worth of the

reference bank (Control Bank B) when each of the remaining rod banks is

fully inserted from 225 to O steps.

The* inspector witnessed se 1 ected

portions of this test when control banks C and D were the test banks.

During this testing, several urgent rod* control failure alarms were

received.

The operators were able to immediately clear the alarms.

The

cause of the a 1 arms was determined to be the rod bank se 1 ector switch.

Several times when the selector switch passed through the C control bank

position to another bahk position, the alarm would come in.

A deviation

report was written to identify the prob 1 em.

However, the 1 i censee

determined that the problem did not affect proper operation of the rod

control system and testing was completed. satisfactorily.

No other

discrepancies were notedr

In the areas inspected, no violations or deviations were noted.

9.

Allegation Case No. RI! 89-A-0010

a.

Background:

An individual, herein after referred to as the alleger, contacted

Region II staff and reported that a worker modified a cable tray

label (identification) to match the tray identification entered for

the cable on the pull ticket.

b.

Allegation Inspection:

The inspectors had discussions with two of the licensee 1 s engineers

concerning the marking and identification of electrical cable trays.

The engineers stated that the letter designations were the most

important part of the marking because these letters determine the

type of cable that will go into that tray. The designations are as

follows:

A- instrumentation cables

8- power cables

C- control cables plus power cables for up to 60 h.p. motors or 60

amperes .

22

The engineers stated that a 1 was added in front of the letter

designation, and was not important to the cable tray designation.

During an

NRC electrical inspection conducted May 10-12, 1989,

violation 280/89-12-01, failure to maintain cable tray covers in

place as required by Appendix R, was issued. As a result of this

violation, the licensee has agreed to walk down the cable trays,*

making sure that the cable trays are properly marked, and issue new

drawings as necessary.

The electrical engineer performing the walk down under EWR 89-283

found trays with numbers pee 1 ed off, trays with added numbers

(numbers added with ink markers), and trays that had the wrong color

code. The new markings will be of a standard height and stenciled

onto the cable tray.

All of the trays in Unit 1 containment were

walked down before startup.

Unit 2 containment will be walked down

before startup.

c.

Conclusions

Visual inspection of the electrical cable tray in question from

approximately 20 feet below appears to substantiate the allegation,

however, this marking of a 1 in front of a letter had no safety

significance.

As discussed previously, all safety-related electrical

cable trays will be walked down and properly identified.

10. Action on Previous Inspection Findings

(92701, 92702)

(Closed) VIO 280,281/87-32-01, Inadequate Emergency Operating Procedure

for Natural Circulation Cooldown, e.g., Cooldown Curves Exceed Those in

the Technical Specifications.

The inspector determined from a review of

the licensee's corrective actions that a TS change request was submitted

which indicates the cooldown curve, Figure 3.1-1, is based on RCS cold leg

temperature .. The inspector also noted that emergency procedures EP-1.02A

and EP-l.02B, reflect the corrected TS cooldown curve.

The licensee

1s

corrective actions are adequate; this item is considered closed.

11.

Exit Interview

The inspection scope and fi.ndings were summarized on August 2, 1989, with

those individuals identified by an asterisk in paragraph 1.

The following

new items were identified by the inspectors during this exit:

One violation was identified (paragraph 3.a) for failure to provide

adequate

procedures

for

the

calibration

of

instrumentation

(280,/89-21-01).

One violation was identified (paragraph 3.g) for failure to place an

inoperable low intake canal level channel in trip as required by TS

Table 3.7-2, Item 5.a (280/89-21-02)

23

One violation was identified (paragraph 3.g) for failure to maintain

greater than 60,000 gallons of water in 2-CN-TK-1 as required by

TS 3.6.B.2 (280/89-21-04).

.

One unresolved item was identified (paragraph 3.g) for additional NRC and

1 icensee review of reportabil ity in accordance with 10 CFR 50. 72 of two .

events which resulted in the tripping of safety-related chillers and

charging pump service water pumps (280/89-21-03).

One unresolved* item was identified (paragraph 6.h) for additional

inspections of the licensee

1s program for implementing TS requirements

(280,281/89-21-05).

.

In addition, a weakness was identified (paragraph 3.a) during the Unit 1

restart with regards to multiple procedure concurrent usage and a lack of

sensitivity to initial conditions in procedures.

Also, a weakness was

identified (paragraph 6.g) regarding the transmittal of data used by

operations for reactivity calculations.

The licensee acknowledged the inspection findings with no dissenting

comments.

The licensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

12.

INDEX OF ACRONYMS AND INITIALISMS

AP

ccw

cm

cw

DEGF

DR

DRP

DRS

ERF

ERFSC

ESF

ESGR

EWR

ft-lb

GAL

GPM

HPSI

HSD

IA

I&C

I FI

!SI

LCO

LER

ABNORMAL OPERATING PROCEDURE

COMPONENT COOLING WATER

CODE OF FEDERAL REGULATIONS

CIRCULATING WATE~

DEGREE FAHRENHEIT

DEVIATION* REPORT

DIVISION.OF REACTOR PROJECTS

DIVISION OF REACTOR SAFETY

EMERGENCY RESPONSE FACILITY

EMERGENCY RESPONSE FACILITY STATUS COMPUTER

ENGINEERED SAFETY FEATURE

EMERGENCY SWITCHGEAR ROOM

ENGINEERING WORK REQUEST

FOOT-POUND

.

GALLONS

GALLONS PER MINUTE

HIGH PRESSURE SAFETY INJECTION

HOT SHUTDOWN

INSTRUMENT AIR

INSTRUMENTATION AND CONTROL

INSPECTOR FOLLOWUP ITEM

INSERVICE INSPECTION

LIMITING CONDITION FOR OPERATION

LICENSEE EVENT REPORT

' '

MER3

MOV .

MCR

MTC

NCV

NI

NRC

NRR

OP

PCM

PM

PORV

ppb

PSI

PSIG

PT

QA

QC

SNSOC

SPDS

SW

RCS

RHR

RAI

RCP

RO

RPS

RSHX

RSS

RWP

SER

S/G

SI

SNSOC

sov

SPDS

SRO

ssn

SW

Tave

Tref

TM

TS

UFSAR

URI

VIO

24

MECHANICAL EQUIPMENT ROOM 3

MOTOR OPERATED VALVE

MAIN CONTROL ROOM

MODERATOR TEMPERATURE-COEFFICIENT

NON-CITED VIOLATION

NUCLEAR INSTRUMENTATION

NUCLEAR REGULATORY COMMISSION

NUCLEAR REACTOR REGULATION

OPERATING PROCEDURE

PERCENT MILLIRHO

PREVENTATIVE MAINTENANCE

POWER OPERATED RELIEF VALVE

PARTS PER BILLION

POUNDS PER SQUARE INCH

POUNDS PER SQUARE INCH GAUGE

PERIODIC TEST

QUALITY ASSURANCE

QUAL ITV CONTROL

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SAFETY PARAMETER DISPLAY SYSTEM

SERVICE WATER

REACTOR COOLANT SYSTEM

RESIDUAL HEAT REMOVAL

RESIDENT ACTION ITEM

REACTOR COOLANT PUMP

REACTOR OPERATOR

REACTOR PROTECTION SYSTEM

RECIRCULATION SPRAY HEAT EXCHANGER*

RECIRCULATION SPRAY SYSTEM

RADIATION WORK PERMIT

SAFETY EVALUATION REPORT

STEAM GENERATOR

SAFETY. INJECTION

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SOLENOID OPERATED VALVE .

SAFETY PARAMETER DISPLAY SYSTEM

SENIOR REACTOR OPERATOR

SAFETY SYSTEM FUNCTION INSPECTION

SERVICE WATER

AVERAGE TEMPERATURE

REFERENCE TEMPERATURE.

TEMPORARY MODIFICATION

TECHNICAL* SPECIFICATIONS

UPDATED FINAL SAFETY ANALYSIS REPORT

UNRESOLVED ITEM

VIOLATION