ML18153B314

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Initial SALP Rept 50-280/93-16 & 50-281/93-16 for Period from 920405-930703
ML18153B314
Person / Time
Site: Surry  Dominion icon.png
Issue date: 09/01/1993
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18153B313 List:
References
50-280-93-16, 50-281-93-16, NUDOCS 9309140254
Download: ML18153B314 (24)


See also: IR 05000280/1993016

Text

ENCLOSURE

INITIAL SALP REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT NUMBER

50-280, 281/93-16

VIRGINIA ELECTRIC AND POWER COMPANY

SURRY UNITS 1 AND 2

FROM APRIL 5, 1992 THROUGH JULY 3, 1993

9309140254 930901

~

DR

ADOCK 0500~fi~O t~

TABLE OF CONTENTS

I.

INTRODUCTION ............................................... 1

I I.

SUMMARY OF RESULTS ......................................... 1

Overview ................................................... 2

I I I.

CRITERIA .....*.............................................. 2

IV.

PERFORMANCE ANALYSIS ....................................... 3

A.

Plant Operations ..................................... 3

B.

Radiological Controls ................................ 6

C.

Maintenance/Surveillance ............................. 8

D.

Emergency Preparedness ............................... 10

E.

Security ............................................. 12

F.

Engineering/Technical Support ........................ 14

G.

Safety Assessment/Quality Verification ............... 15

V.

SUPPORTING DATA AND SUMMARIES ............................ .. 18

A.

Major Licensee Activities ............................ 18

B.

Major Direct Inspection and Review Activities ........ 20

C.

Escalated Enforcement Action ......................... 20

D.

Licensee Conferences Held During Appraisal Period .... 20

E.

Confirmation of Action Letters ....................... 21

F.

Review of Licensee Event Reports ..................... 21

G.

Licensing Activities ................................. 21

H.

Enforcement Activity ................................. 22

I.

Reactor Trips ........................................ 22

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated Nuclear Regulatory Commission (NRC) staff effort to collect

available observations and data on a periodic basis and to evaluate licensee

performance on the basis of this information.

The SALP program is

supplemental to normal regulatory processes used to ensure compliance with NRC

rules and regulations. It is intended to be sufficiently diagnostic to

provide a rational basis for allocation of NRC resources and to provide

meaningful feedback to the licensee's management regarding the NRC assessment

of their facility's performance in each functional area.

An NRC SALP Board, composed of the staff members listed below, met on

August 9, 1993, to review the observations and data on performance and to

assess licensee performance in accordance with NRC Manual Chapter 0516,

"Systematic Assessment of Licensee Performance."

This report is the NRC's assessment of the licensee's safety performance at

Surry for the period April 5, 1992 through July 3, 1993.

The SALP Board for Surry Units I and 2 was composed of:

J. P. Jaudon, Deputy Director, Division of Reactor Safety, Region II (RII}

(Chairman}

J. R. Johnson, Deputy Director, Division of Reactor Projects (DRP}, RII

B. S. Mallett, Deputy Director, Division of Radiation Safety and Safeguards,

RII

M. V. Sinkule,,Chief, Reactor Projects Branch 2, DRP, RII

M. W. Branch, Senior Resident Inspector, Surry, DRP, RII

H. N; Berkow, Director, Project Directorate II-2, Office of Nuclear Reactor

Regulation (NRR}

B. C. Buckley, Senior Project Manager, Surry, Project Directorate II-2, NRR

Attendees at SALP Board Meeting:

G. A. Belisle, Chief, Reactor Projects Section 2A, DRP, RII

L. W. Garner, Project Engineer, Projects Section 2A, DRP, RII

J. W. York, Acting Senior Resident Inspector, North Anna, DRP, RII

II.

SUMMARY OF RESULTS

Performance in the Operations area was excellent. Unit I generally operated

well and Unit 2 had an excellent operating record. Management's attention to

and involvement in operations was effective. Operator responses to events

continued to be excellent. Operations management was sensitive to the safety

of shutdown operations.

Management's attention and involvement in radiation protection was observed to

be strong.

The licensee continued to maintain an effective internal and

external exposure control program.

The licensee's control of contamination at

the source has been aggressive.

1

Overall plant material condition was good.

Improvements in maintenance

procedure quality were noted. Surveillance program implementation

improvements were noted.

The flow-assisted corrosion program was well

implemented.

Risk management, especially during outages, was strong.

Management support and involvement in the emergency preparedness program was

evident.

The licensee maintained emergency facilities, equipment,

instrumentation, supplies, and individuals in a state of readiness as

demonstrated during the annual exercise.

The licensee continued to refine and enhance security program effectiveness.

The security training program was well planned and executed.

The security

force continued to track and trend safeguards events.

The licensee's performance in providing engineering and technical support was

generally good.

Support for plant modifications was excellent. Support to

operations and maintenance activities was generally good; resolution of

chronic equipment issues needs to be pursued as does resolution of the issues

arising from setpoint calculation control.

An excellent initial licensed

operator training program was demonstrated.

In the Safety Assessment/Quality Verification area, management demonstrated a

strong commitment in identifying problems.

Self-assessments were effective in

the areas of root cause evaluation and quality assurance assessments.

Responses to safety initiatives were, in most cases, technically complete and

thorough.

Overview

Performance ratings assigned for the last assessment period and the current

period are shown below.

Functional Area

Rating Last

Period

Plant Operations

I

Radiological Controls

I

Maintenance/Surveillance

2

Emergency Preparedness

I

Security

I

Engineering/Technical Support

2

Safety Assessment/Quality Verification 2

III.

CRITERIA

Rating This

Period

I

I

2 Improving

I

I

2

I

The evaluation criteria which were used, as applicable, to assess each

functional area are described in detail in NRC Manual Chapter 0516.

This

chapter is in the Public Document Room files. Therefore, these criteria are

not repeated here, but will be discussed in detail at the public meeting held

with the licensee management.

2

IV.

PERFORMANCE ANALYSIS

A.

Plant Operations

1.

Analysis

This functional area addresses the control and performance of

activities directly related to operating the units, as well as

fire protection.

Unit 1 generally operated well during the assessment period but

was challenged by several equipment-related problems.

Three trips

occurred, one because of a contractor's error and two because of

degraded or failed relays. Several power reductions were

necessary to repair balance of plant equipment including main

feedwater pumps and electrical distribution equipment.

Unit 2 had an excellent operating record during the assessment

period.

Late in the period, the reactor tripped when a main

feedwater pump failed.

Early in the assessment period, after

being on line for approximately seven months, leaking pressurizer

safety valves forced a controlled shutdown for repairs. Toward

the end of the assessment period, a 61-day refueling outage was

completed.

However, the return to power was delayed, and the unit

was operated for the remainder of the period at a reduced reactor

coolant pressure because of pressurizer safety valve leakage.

Management's attention to and involvement in operations were

effective.

Command and control of evolutions was evident, and

shift turnovers and event briefings were effective in

communicating management's expectations. However, early in the

assessment period, operations established an electrical

configuration lineup that resulted in an unacceptable high head

safety injection/charging pump alignment which required additional

management corrective action. Further assessment of this event is

discussed in the Safety Assessment/Quality Verification section of

this assessment.

The licensee's management maintained a low

threshold for identifying problems, and they became aware of an

increasing trend in operator errors. Examples included valve

mispositions, incorrect tagging, and procedural adherence.

None

of these errors caused serious safety incidents but attracted

increased management attention. Corrective actions directed by

management resulted in a significant reversal in the error trend.

Op~rator responses to events continued to be excellent. Operators

were required to respond to four automatic reactor trips during

this period. During one of these trips, a rapid cooldown was in

progress because of a partia~ly opened main steam valve. The

3

operators diagnosed the event and took immediate corrective action

in accordance with the emergency procedures, thereby preventing an

excessive plant cooldown.

When a fitting on a reactor coolant

system letdown line failed, the operators reacted effectively to

isolate the line and minimize coolant loss.

Licensed operator staffing levels were a continuing strength.

Overtime was minimal except during outage periods.

The five

operating shifts had a minimum of four senior reactor operators

and an average of six reactor operators. This staffing level was

more than required by the station Technical Specifications and the

regulations.

In addition, non-shift senior reactor operators were

effectively utilized during refueling outages for oversight and

support of various outage activities. This support lessened the

administrative burden on the shift operating crew, which allowed

them to concentrate on maintaining plant parameters within safe

1 imits.

The fire protection program continued to be well implemented.

Fire brigade members and operators performed well during drills.

Control of ignition sources and combustible materials was

effective. The diesel generator rooms were kept clean, and oil

leaks from the engines were minimized.

With the exception of a

few minor deficiencies, the fire protection system material

condition was very good.

Housekeeping throughout the plant was good during the assessment

period and continued management commitment in this area was

evident.

Improvements in floor, wall, and equipment coatings were

noted.

Roof and ground water leakage continued during this

period.

Some roofing has been replaced, and further repairs are

continuing under a long-term program.

An enhanced ground water

_program was put in place during this period.

The long-term

results have yet to be realized.

Management support of innovative programs and policies

demonstrated a strong conunitment for safe operation of the plants.

These included the areas of decision making, minimizing the number

of alarmed control room annunciators, plant component labeling,

upgraded procedures, excellent outage planning/scheduling methods,

and implementing procedures and methods for expanding the

operations staff capabilities. These are more fully explained

below.

The plant component labeling program resulted in improved labels

and was close to completion during this assessment period.

The

program has progressed to a point where approximately 90 percent

of the labels have been placed on the individual components.

In

order to maintain relabeling program effectiveness, an

administrative procedure was developed and implemented near the

end of the assessment period for maintaining component labeling

and resolving labeling discrepancies.

4

The operations portion of procedures completed in the Technical

Procedures Upgrade Program was slightly less than the program

goal.

However, the updated procedures were generally of good

quality and, when used, required only one-third the number of

changes as compared to non-upgraded procedures.

Part of this

increased quality has been brought about by assigning a senior

licensed operator as operations coordinator and validating these

upgraded procedures by personnel from other operating shifts.

Operations management was sensitive to the safety of shutdown

operations when in the refueling and cold shutdown modes.

A

detailed daily schedule was developed based on outage activities

and included required surveillances and relevant items associated

with the other unit. This schedule listed suggested times and

priorities for activities and gave operations management an in-

depth picture of day-to-day outage activities, thereby improving

safety awareness.

Several methods were used to expand capabilities and broaden the

experience base for operations personnel.

An Operations Review

Board was formed.

It was chaired by the Operations Manager and

included non-licensed and licensed operators. Their functions

were to review and coordinate deviations, commitment tracking,

quality assurance responses and corrective action items, and

requests for engineering assistance projects assigned to the

Operations Department.

Administrative burdens on management were

decreased by the Review Board's establishment. Rotational

assignments to this Board gave participants experience in

resolving problems and interfacing with other departments.

Assignments on this Board also provided valuable training for

current and future operators. Operations management also created

three new positions for senior reactor operators and implemented

rotational assignments in these positions.

One position was as a

member of operations management staff; another was as a shift

maintenance advisor; and the third was assigned special projects,

such as labeling and procedures.

By these innovative programs,

management developed personnel with a broader experience base.

No violations were identified during the assessment period.

2.

Performance Rating

Category:

1

3.

Board Recommendations

None

5

B.

Radiological Controls

I.

Analysis

This functional area addresses those activities related to

radiological controls, radioactive waste management, environmental

monitoring, water chemistry and transportation of radioactive

material.

Management involvement in radiation protection was observed to be

strong. This was evidenced by appropriate staffing levels with

well trained and experienced radiation protection personnel, a

strong as 1 ow as reasonably achievable (ALARA) awareness program,

and management support for proactive dose reduction initiatives

and goals.

Licensee management closely monitored radiation

protection performance through quality assurance based assessments

and ensured effective adherence to radiation protection

procedures. Also, throughout the assessment period, the licensee

took the initiative to involve engineering in radiological

problems.

During the assessment period, the licensee maintained effective

internal and external exposure control programs.

One personnel

exposure in excess of administrative limits occurred during the

period; it was attributed to an isolated case of ineffective

communications and poor procedural adherence. A review of

external exposure controls showed that effective use of alarming

dosimetry prevented exposures in excess of regulatory limits.

The licensee's control of contamination at its source continued to

be aggressive.

The reduction of contaminated areas in the plant

to about one percent of the radiologically controlled area has

contributed to improved equipment access and less personnel

exposure.

Personnel contamination events were commensurate with

the licensee's scope of work and were reduced from 164 during the

previous assessment period to 140 during this assessment period.

During this assessment period, the licensee's program to reduce

out-of-core source term and collective dose continued to be

excellent. Through the effective use of mockup training, close

management of realistic collective dose goals, effective

involvement of coordinators, maximum utilization of the enhanced

surrogate tour for pre-job briefings, and hot spot reduction

efforts, the licensee continued to reduce collective dose.

The

licensee's three-year collective dose average for 1989-1991 was

330 person-rem per unit.

The dose average for 1990-1992 was 289

person-rem per unit. The average dose was reduced even though the

licensee continued to be challenged with potentially significant

dose work such as the removal of resistance temperature detectors.

6

The licensee's program to control quantities of radioactive

material in liquid and gaseous effluents was effective. The

licensee has taken significant steps to control the quantities of

radioactive material released in liquid effluents from the

station. The quantities of radioactive materials released in the

liquid waste stream in 1992 were approximately one-seventh of

those released in the previous year. This significant reduction

was attributed to improved fuel integrity, as well as, the more

efficient treatment and cleanup system in the new Surry Radwaste

Facility, which became operational in November 1991 .. The

significant decrease in radioactive materials in gaseous effluents

in 1992 was also attributed to improved fuel integrity. There

were no unplanned liquid or gaseous radioactive releases during

this assessment period.

The estimated potential doses to the

public resulting from the rele~se of liquid and gaseous effluents

for calendar year 1992 were well below the dose limits specified

by the Technical Specifications and were less than one percent of

the environmental dose limits specified in the regulations.

The licensee experienced operability problems with some effluent

monitors.

The cumulative out-of-service time and extensive

maintenance on the Waste Gas Holdup System Hydrogen Monitoring

Instrumentation System eventually resulted in the system being

inoperable for greater than 30 consecutive days.

During this

assessment period, there were continuing short-term operability

problems with both units' Circulating Water Discharge Radiation

Monitors because of electronic spiking, water/moisture intrusion,

and high radiation alarm setpoint problems.

In addition, the

licensee experienced electronic spiking and automatic flow control

problems with the stack radiation monitors and moisture intrusion

problems in the sampling lines of the Process Vent monitors.

These problems indicate a need for increased attention to these

radiation monitors.

During this assessment period, the licensee performed audits of

radiological effluents, the Offsite Dose Calculation Manual, the

Process Control Manual, environmental monitoring, and radioactive

materials management.

The audits were technically sound and well

documented.

The problems identified were of low safety

significance and were adequately addressed.

The licensee's program for processing, packaging, storing and

shipping radioactive solid wastes was effective. The technicians

who performed radioactive waste shipments were adequately trained

and performed their duties competently. Daily solid waste

generation has been reduced through aggressive management

attention, information campaigns, minimizing the use of herculite,

recycling tent enclosure materials, preventing equipment packing

material from entering containment, and use of a radiological

waste inventory tracking program.

One violation was identified-during the assessment period.

7

2.

Performance Rating

Category:

I

3.

Board Recommendations

None

C.

Maintenance/Surveillance

1.

Analysis

This functional area addresses those activities related to

equipment condition, maintenance, surveillance performance, and

equipment testing.

Overall plant material condition was good.

Significant

improvements included modifications to remove the resistance

temperature detector bypass lines, repairs and modifications to

the containment ventilation system, and extensive repairs to the

Unit 2 containment airlock. Although not complete, improvements

were noted for several other degraded material conditions being

addressed as part of a five-year plan. These included ground

water and roof leaks and service water intake structure

degradation.

The availability and reliabi.lity of the control room

and emergency switchgear room cooling system continued to be

impacted by the material condition of the service water supply

strainers and the chiller units. Modifications to add two more

chiller units and implementation of recent Technical Specification

changes that provide greater operational flexibility for the

service water system to allow needed maintenance, are two of the

improvements currently being implemented to resolve this issue.

Additionally, material condition problems with radiation monitor

failures and pressurizer safety valve leakage continued to

challenge the operators.

An upward trend in relay failures was

noted, and several of these failures resulted in two Unit I

reactor trips in 1993.

The single point failure analysis and

preventive maintenance review commissioned by the licensee were

two actions initiated to facilitate early correction of this

degrading material condition trend. Furthermore, management's

commitment to improvements in all areas of plant material

condition was demonstrated by their policy to restore or repair,

during outages, balance of plant components that were temporarily

repaired while operating.

Staffing levels in the Maintenance Department were adequate

throughout the assessment period. Maintenance engineering

staffing was adjusted to reduce the backlog of Cause Determination

Evaluations that was noted in the previous assessment.

At the end

of the assessment period th~ backlog had been reduced from 400

8

to 21, indicating management focus and attention to this area.

The evaluation quality remained good.

Although the maintenance qualification and training program

continued to produce knowledgeable and skilled craftsmen, several

performance problems that involved failure to adhere to

administrative procedures were noted.

Examples included: failure

to verify independently the placing of danger tags and lifting a

wrong lead that caused the isolation of component cooling to the

residual heat removal heat exchanger during system operation.

Post maintenance testing program problems noted in the previous

assessment were not apparent during this period.

Instrumentation

and control equipment that was previously not included in the

program was gradually being added to the data base.

Improvements in the quality of maintenance procedures that were

upgraded through the technical procedure upgrade program were

noted.

The program was proceeding on schedule, but the

instrumentation and control effort was somewhat behind schedule

because of a lack of engineering support in providing the

instrument scaling factors and setpoints necessary for procedure

upgrade.

Management recognized these obstacles to meeting program

goals and made necessary adjustments by assigning additional

procedure writers. Engineering priorities were modified to

provide scaling factors and setpoints in a manner that would

complement the procedure upgrade efforts. There were craft

performance problems noted that were sometimes related to the

quality of non-upgraded procedures.

For example, the positioner

feedback bracket for the main steam power operated relief valve

was not reconnected and the stroke adjustment instructions

conflicted with the vendor's manual.

The backlog of non-outage-related corrective maintenance work

orders was reduced by approximately one-half during this

assessment period, and the average age of the outstanding work

orders was also reduced by approximately one-half. Problems

associated with availability of parts and lack of planning support

that were noted in previous assessments were not major

contributors to the backlog.

Improvements were noted in the Outage Planning and Scheduling

Department's performance during refueling outages. The Unit I and

Unit 2 refuelings were accomplished on time without the need to

operate in reduced inventory conditions with fuel in the reactor

vessel.

An innovative outage scheduling method was developed that

assigned a risk rating factor to work activities being planned.

This method provided a visual display of risk parameters and was

modeled to allow the planner to see the impact of planned

maintenance or modifications on critical outage plant parameters

such as electrical distribution, containment integrity and heat

removal.

For example, all maintenance items that required reduced

9

D.

inventory were rated as red and were scheduled when fuel was

removed from the reactor vessel, thereby reducing risk.

Surveillance program implementation improved from the previous

assessment period. Several technically inadequate procedures,

used to satisfy Technical Specification requirements, were

identified by the licensee through their on-going program and

reported as missed surveillances.

Each time surveillances were

determined to be inadequate they were modified and appropriate

retesting was performed.

Strengths were noted in the non-

intrusive testing of check valves connected to the reactor coolant

system.

Use of this new method resulted in reducing radiation

exposure and the need for a reduced inventory evolution.

Good implementation of the inservice inspection program was noted

during this assessment period.

The procedures, examination

techniques, and documentation of examination results were good.

Supervisors, engineers, and non-destructive examination examiners

were knowledgeable in their respective areas. Only a few minor

problems were identified and they were associated with procedural

adherence during piping examinations.

The flow-assisted corrosion program was proactive and well

implemented.

Industry developed computerized programs, CHECMATE

and CHEC-NDE, were being used.

Over 5000 components per unit were

included in the program.

The program has strong corporate and

site support with dedicated resources and was well documented in

corporate standards and site procedures. Degraded piping has been

routinely identified and replaced with upgraded materials.

One violation was identified during the assessment period.

2.

Performance Rating

Category:

2 Improving

3.

Board Recommendations

None

Emergency Preparedness

1.

Analysis

This functional area addresses activities related to the execution

of the Emergency Plan and its implementing procedures, including

licensee performance during emergency exercises and actual events,

interactions between onsite and offsite emergency response

organizations during exercises and actual events, and support and

training of emergency response personnel.

10


Management support and involvement in the emergency preparedness

program were evident by the variety of drills conducted and the

emergency facility and equipment improvements made during the

assessment period.

The licensee continued to maintain emergency

response capability in a state of operational readiness. Staffing

of the emergency preparedness function continued as a program

strength because an effective base of expertise was maintained

intact at the station and at corporate headquarters.

The

licensee's corrective action program for resolving emergency

preparedness issues and inspection findings was very thorough and

effective. Other identified program strengths included a

comprehensive independent audit function and a thorough system of

surveillances of emergency response facilities and equipment.

During the annual emergency response exercise in November 1992,

the licensee demonstrated a capability to effectively implement

the Emergency Plan in response to the simulated accident scenario.

The scenario appropriately challenged the licensee's emergency

response organization. The licensee demonstrated the ability to

identify emergency conditions, to make correct classifications in

accordance with Emergency Plan implementing procedures, and to

take appropriate measures to mitigate the adverse consequences of

degraded plant conditions. Timely activation and capable support

operations were observed at each of the emergency response

facilities. The licensee had two procedures for making Protection

Action Recommendations which were not internally consistent.

Additionally, the licensee did not always follow these procedures

for developing the recommendations.

The licensee made extensive

procedural improvements following a review of the methodology for

deriving protective action recommendations.

This issue was

resolved prior to the end of the current appraisal period.

The licensee maintained emergency facilities, equipment,

instrumentation and supplies in a state of readiness with thorough

equipment inventories, and adequate surveillances and functional

tests. A new, more suitable location for the alternate

Operational Support Center was identified and established,

resulting in a significant improvement in this capability. During

the previous appraisal p~riod, the licensee fully implemented an

upgrade of the offsite siren system through the addition of a

computerized feedback capability to monitor each siren's operation

during any mode of testing or activation. The siren availability

factor was in excess of 99 percent during 1992, a condition

attributed to the feedback system.

During this appraisal period, no emergency declarations were made,

and no violations or exercise weaknesses were identified.

2.

Performance Rating

Category: 1

11

3.

Board Recommendations

None

E.

Security

1.

Analysis

This functional area addresses those safeguards activities

associated with the plant's safety-related vital equipment, the

accountability of special nuclear material, and the effectiveness

of the licensee's Fitness-For-Duty Program.

The licensee's enhancement of security facilities and equipment

and the effective utilization of security resources contributed

significantly to the security force's capability to protect the

station's vital resources, to respond to unscheduled contingencies

and to have a low incidence of safeguards events.

Staffing of the security organization remained at sufficient

levels during this assessment period. The security force

continued to perform in a professional manner and was provided

dedicated support by site and corporate management.

The continued

low turnover rate of the security force was attributed to

management support and effective supervision.

During this assessment period, the licensee continued to refine

and enhance the effectiveness of the security program through

employment of progressive and innovative techniques to improve

personnel and system performance. These actions included

establishment of a computerized tracking program for maintenance

of security systems and equipment and the installation of vehicle

barriers at the two vehicle gates in the protected area barriers.

A Backup Central Processing Unit was acquired to serve as a

training simulator for new alarm station operators and as a backup

to the operational security computer system in the event of

failure or malfunction.

The barriers installed at the vehicle

gates, designed by the security force, consisted of aircraft

arresting cable, uniquely installed in a manner to preclude or

delay unauthorized vehicle entry.

Installation of the barriers at

the vehicle gates completed establishment of vehicle barriers at

all approachable areas of the protected area perimeter.

In the

area of personnel performance enhancement, several recognition

programs were established including: High Academic Achievement,

High Tactical Achievement and Semi-Annual Security Shift Awards"

The security training program was well planned and executed.

Continued site and corporate management support was evident as

demonstrated by the new training facility. A major strength of

the security training program was the realistic, contingency

tactical drills utilizing Multiple Integrated Laser Engagement

equipment.

Recent drill scenarios were developed and exercised

12

based on information from industry lessons learned contained in

NUREG-1485, "Unauthorized Forced Entry into the Protected Area at

Three Mile Island." Security personnel were provided Basic and

Fundamental System Training to enhance their knowledge and assist

in applying protection strategies. Of specific significance was

the ongoing joint operations/security training scenarios developed

and conducted in the station's training simulator to focus on

communications and developing cohesive relationships in

identifying weaknesses and responding to threats.

The licensee's corporate quality assurance organization continued

to conduct aggressive audits of the security program.

In

addition; internal audits of security programs and security force

activities were conducted by station personnel to evaluate

performance effectiveness, compliance, and site-specific

requirements.

The security organization developed and implemented

an Internal Safeguards Information Audit Program to examine and

evaluate on an annual basis, the handling, control and storage of

Safeguards Information.

As a result of the audit the volume of

safeguards material at the station was reduced by approximately 40

percent.

The licensee's programs continued to be effective in meeting

objectives for Fitness-For-Duty, access authorization and the

prevention of the introduction of contraband items into the

protected area. Reportable events were thoroughly addressed and

reported in a timely manner.

The security force continued to .track and trend safeguards events,

maintenance and priority projects utilizing a computerized data

base.

The licensee did not experience any I-hour reportable

Safeguards Events during the assessment period. A total of 19

Loggable Safeguards Events were documented for the second quarter

of calendar year 1993. Several of these events, related to access

control equipment failure, were attributed to aging of the

existing security access control system.

However, the number of

loggable events remained low.

No violations were identified during the assessment period.

2.

Performance Rating

Category:

1

3.

Board Recommendations

None

13

F.

Engineering/Technical Support

I.

Analysis

This functional area addresses activities associated with the

design of plant modifications, and technical support for

operations, outages, maintenance, and licensed operator training.

The licensee's performance in providing engineering and technical

support was generally good during this assessment period, but some

weaknesses were identified in the Engineering Department's support

of operations and maintenance activities.

Engineering support for plant modifications was excellent; the

quality and technical content of temporary and minor modifications

were generally good.

An example of strong engineering support to

modifications was DCP 91-12, RSHX Service Water Flow Element

Modifications, Units 1 and 2.

Another example of proactive

engineering involvement was demonstrated by the Engineering Work

Request program and the Design Change Package backlog reduction

program.

The licensee implemented a Level I Project Modification

Package Backlog Reduction program designed to reduce the backlog

from the 333 in August 1992 to 150 by June 1993.

The backlog

reduction was on schedule as of April 1993 with 172 packages

remaining in the backlog population.

However, a problem was

identified with updating design drawings within the required time

period following the implementation of two design changes.

Engineering and technical support to operations and maintenance

activities were generally good during this assessment period.

Examples of good engineering support included the timely and

effective engineering support provided to assess the pressurizer

safety relief valve issue and in resolving and reducing both

deviation reports and requests for engineering assistance. The

various engineering groups worked well together to resolve complex

problems that could have potentially affected plant operations.

However, some examples of weak engineering support were also

identified. One included an engineering personnel error which

subsequently led to a safety injection because of a spurious

signal generated after replacing a defective relay during the

return of a high consequence limiting safeguards circuit to

normal. Another included a failure during the Unit 2 refueling

outage to control motor operated valve setpoints adequately. A

significant example of weak engineering support was demonstrated

by the licensee's failure to correct weaknesses in setpoint

control identified during the last SALP assessment period.

Inconsistencies between plant instrumentation and channel

statistical allowance calculations continued during this

assessment period. Also a loss of coolant accident reanalysis was

required during this assessment period because of NRC-identified

14

G.

inadequate acceptance criteria for a shortfall of required flow

from one low head safety injection pump.

From January 1992 to May 1993, a total of 654 deviation reports

were assigned to station engineering to resolve.

Engineering was

overdue in responding to 16 deviation reports in 1992.

There have

been no late responses for 1993 through the end of the assessment

period. System engineering involvement was instrumental in

reducing the numbers of deviation reports and requests for

engineering assistance. Satisfactory engineering training was

also demonstrated by the performance levels obtained during this

assessment period.

The licensee's Self-assessment Program included appraising

engineering programs during this assessment period.

Licensee

quality assurance audits of engineering activities verified that

the conduct of these activities demonstrated the licensee's

commitment to improving the quality and effectiveness of

engineering support provided to the plant.

An excellent initial licensed operator training program was

demonstrated during the assessment period as evidenced by the fact

that all candidates passed the Generic Fundamental Examination

Section and initial licensing examination.

The NRC also

administered requalification examinations to 15 operators.

Fourteen of fifteen operators passed the examination. There was

an improvement in administering the process compared to previous

requalification examinations.

The simulator was used effectively

for training. The licensee's simulator instructors were

knowledgeable of the simulator and plant operations. The

simulator adequately modeled scenario events.

One violation was identified during the assessment period.

2.

Performance Rating

Category:

2

3.

Board Recommendations

None

Safety Assessment/Quality Verification

I.

Analysis

This functional area addresses those activities related to

licensee implementation of safety policies; amendments, exemptions

and relief requests; response to Generic Letters, Bulletins, and

Information Notices; resolution of safety issues; safety review

committee activities; and the use of feedback from self-assessment.

programs and activities.

15

A multi-tiered program consisting of both corporate and station

resources was effectively utilized to accomplish safety assessment

and quality verification activities. The Nuclear Business Plan,

Nuclear Oversight Board, Management Safety Review Committee,

Corporate Nuclear Safety, Nuclear Quality Assurance, Management

Review Board, Station Nuclear Safety and Operating Conunittee, and

Station Nuclear Safety incorporated all levels of corporate and

station management in ensuring safe operation. Corporate Nuclear

Safety Integrated Trend Reports, quality assurance assessments,

Management Review Board Performance Annunciator Windows, and the

Station Nuclear Station Deviation Trend and Nuclear Safety

Assessment Reports were examples of self-assessment activities

that were effective in monitoring and evaluating plant performance

and following up with corrective action recommendations when

prriblems were identified.

Human performance problems in the areas

of tagging components, work practices, and recurring equipment

problems, including those associated with radiation monitors and

control room chillers, were identified by these self-assessment

programs.

Staffing and training of self-assessment programs were

superior. These self-assessment programs significantly exceeded

technical specification requirements, and management encouraged

employees to visit counterparts at other nuclear plants to compare

programs and identify possible improvements.

In general, management demonstrated a strong commitment in

identifying problems, but in some instances such as ground water

intrusion, radiation monitor failures, control room chiller

failures, and pressurizer safety valve seat leakage, permanent

corrective actions entailed long-term program commitments.

Therefore, these problems continued to occur throughout the

assessment period, carrying over from previous periods.

Long-term

corrective actions associated with other problems such as the

resistance temperature detector bypass manifold, instrument air

system, containment ventilation system and containment personnel

access hatch were effective once they were fully implemented.

Deviation report trending and the Integrated Trend Report improved

identification of recurring problems. Corrective actions

implemented to verify proper operation of steam traps in the steam

supply lines to the turbine-driven auxiliary feed pumps and

replacing injection/charging pump lube oil temperature control

valves were examples of recurring problems that were adequately

resolved. It was noted during the last assessment period that

Corporate Nuclear Safety recommendations from older event reviews

had not been verified as being completed. This area was reviewed

during this assessment period and considered acceptable.

Self-assessments were effective in the areas of root cause

evaluation, quality assurance assessments and methodologies and

approaches for assessing quality assurance and station

performance, Startup Assessment Program, shutdown management,

post-trip review, operationa~ and event review, and Level I

16

Project Tracking.

During the assessment period, the quality of

licensing basis documents improved.

The Updated Final Safety

Analysis Report and Design Basis Document improvement programs

continued to progress and a Technical Specification review program

was implemented.

Weaknesses were identified in the areas of long-

term corrective actions for improper high head safety

injection/charging pump configuration, safety evaluation screening

and commitment tracking system.

Improper high head safety

injection/charging pump configuration resulted in degraded safety

system capability. During the previous assessment period,

enforcement action was taken for a similar occurrence. Although

the impact of these events was similar, they had different root

causes.

The problem was attributed to inadequate change control,

and the licensee implemented appropriate corrective action.

Deficiencies were noted with safety evaluations for certain

procedures that were used to operate plant systems differently

than described in the Updated Final Safety Analysis Report, and

several commitments were closed without performing the required

actions.

Throughout the period, management continued to maintain a low

threshold for identifying problems.

Station deviations were

written by station personnel whenever they perceived that a

problem existed. The improper high head safety injection/charging

pump configuration was identified by the licensee. Station

deviations provided a major input to the licensee's self-

assessment programs.

The details and quality of the safety reviews conducted by the

Management Safety Review Committee and Station Nuclear Safety and

Operating Committee in this assessment period were good.

The

Management Safety Review Committee was sensitive to operator

errors and members were objective in evaluating Technical

Specification changes.

The Station Nuclear Safety and Operating

Committee effectively monitored proper implementation of the

corrective actions associated with deviation reports as well as

evaluating substitution of manual manipulation for automatic

actions.

During the assessment period, a significant effort was expended in

the licensing area in which the licensee was aggressive in

providing the necessary information to resolve issues effectively.

Frequent meetings and discussions between licensee and staff were

also held to address licensing and other technical issues. The

licensee's submittals continued to be timely and of high quality,

reflecting an in-depth understanding of the technical issues and

regulatory requirements as well as an effective oversight review

process.

Examples of high quality submittals were amendments

relating to upgrading of Section 4.0 of the Technical

Specifications, non-essential service water isolation actuation

logic, and changes in acceptance criteria for mechanical snubbers.

Another example of a high quality submittal was the May 10, 1993,

17

request to change a prior commitment relating to the station

blackout rule. This submittal was clear, accurate and of

sufficient detail to allow the NRC staff to make an evaluation

without a request for additional information.

The continued use of the "top 10" licensing issues management

scheme was a very effective tracking system which focused

attention on those issues judged to be of high priority to both

the licensee and the NRC staff. The "top 10" list appropriately

balanced safety significance and cost benefit considerations. The

"top 10" list was continually updated, in coordination with the

staff, as issues were brought to closure and new issues arose.

Safety reviews by on-site and off-site safety groups continued to

be accomplished in a manner that provided assurance that the

proposed activities were properly analyzed and did not compromise

the safe operation of the plant.

Responses to NRC Bulletins, Generic Letters, and other regulatory

requests were, in most cases, technically complete, and thorough.

The quality and the timeliness of Licensee Event Reports were very

good during this assessment period.

The reports were well written

and provided objective assessments of the root causes of events,

their safety significance, and corrective actions.

Two violations were identified during the assessment period.

2 *.

Performance Rating

Category:

1

3.

None

Board Recommendations

V.

SUPPORTING DATA AND SUMMARIES

A.

Major Licensee Activities

Unit 1 began the assessment period, April 5, 1992, in a refueling

outage.

The outage was completed in May and the unit returned to

service at that time. Operation of the unit was inconsistent and

resulted in three reactor trips, caused respectively by personnel error

and degraded relays, and balance of plant equipment problems including

main feedwater pumps and electrical distribution equipment.

At the end

of the assessment period, July 3, 1993, the unit was in service.

Unit 2 began the assessment period, April 5, 1992, in service. In

February 1993 a coastdown for a refueling outage started, and after 230

consecutive days of being in service, the unit shut down for refueling

in March 1993.

The outage was completed in May 1993 and the unit

returned to service. The unit ha~ one reactor trip on June 20, 1993

18

resulting from the failure of a main feedwater pump.

The unit returned

to service the same day and operated at reduced power for the remainder

of the assessment period while repairs were being made to the main

feedwater pump.

Management and/or organizational changes instituted by the licensee

during the assessment period:

September 1992 - L. M. Girvin became the Vice President, Nuclear

Services.

September 1992 - E.W. Harrell became Vice President, Nuclear

Engineering Services.

September 1992 - F. K. Moore became Vice President, Procurement.

January 1993

- T. E. Capps became Chairman of the Board of

Dami nion Resources.

The following major activities and modifications of both units were

completed during this assessment period:

Construction continued on a new mechanical equipment room to*

accommodate two new control room and emergency chillers.

New design rotating screens were installed in the high and low

level intake structures.

The resistance temperature detector bypass loops were removed.

Replacement of the roofs on the auxiliary building, Unit 2 valve

pit and fire pump building continued in an effort to minimize

rainwater and groundwater leakage into the facility on safety-

related components.

The containment ventilation systems were modified to reduce the

likelihood of control rod drive failures due to overheating.

Recirculation spray heat exchanger service water V-cones were

installed to improve flow instrumentation readings.

Service water piping inspection and coating were completed.

The following major activities and modifications of Unit 2 were

completed during this assessment period:

A cold leg safety injection check valve was replaced without going

to reduced inventory when fuel was removed from the reactor

vessel.

Hinges on the containment personnel hatch outer door were replaced

along with the escape hatch und equalizing valves.

19

The five year main turbine overhaul was performed.

High head safety injection/charging pump under-voltage trip was

modified.

B.

Major Direct Inspection and Review Activities

During this assessment period 29 inspections were conducted by resident

and regional-based inspectors.

Nine meetings were held with licensee

management, including one Enforcement Conference.

C.

Escalated Enforcement Action

An Enforcement Conference was held in the Region II office on

June 10, 1992 associated with the electrical configuration lineup for

high head safety injection pumps such that Technical Specification

operability of the pumps in the automatic mode was defeated.

On

July 13, 1992, a Notice of Violation and a Proposed Imposition of Civil

Penalty was issued in the amount of $50,000.

The licensee acknowledged

the violation and paid the penalty on August 12, 1992.

D.

Licensee Conferences Held During Appraisal Period

July 31, 1992 - Meeting at Region II's office, Atlanta, Georgia, to

discuss several topics including operation and key indicators, the

surveillance and updated final safety analysis reviews, and the

precursor trending program.

The meeting was also used to introduce the

new Vice-President of Nuclear Services (Mr. L. M. Girvin).

August 5, 1992 - Meeting in Rockville, Maryland to discuss accumulation

of gas in low-head safety injection piping.

September 24, 1992 - A counterpart meeting at Virginia Electric and

Power Co.'s offices, Glen Allen, Virginia, to discuss current issues,

open enforcement conferences, ASME Code relief philosophy, licensing

activities overview, status of hydroid growth problems and Updated Final

Safety Analysis Report upgrade program.

December 7, 1992 - Meeting in Rockville, Maryland to discuss initiatives

for reducing regulatory requirements marginal to safety, optimization of

nuclear oversight activities and top ten licensing priorities.

March 24, 1993, Meeting at Region Il's office, Atlanta, Georgia, to

discuss the self-assessment results.

April 21, 1993 - Meeting at Rockville, Maryland to discuss reassessment

of the need for installing one, versus two, non-safety grade diesel

generators to mitigate the effects of a station blackout.

April 30, 1993 - Meeting at Rockville, Maryland to discuss the new

approved nuclear separate business unit and the initiative for reducing

regulatory requirements marginal to safety.

20

May 3, 1993 - Meeting at Region !I's office, Atlanta, Georgia, to

discuss the Design Basis Documentation Program and corrective actions on

identified findings.

E.

None

F.

Confirmation of Action Letters

Review of Licensee Event Reports

During the assessment period, a total of 21 Licensee Event Reports were

analyzed.

The distribution of these events by cause, as determined by

the NRC staffr is as follows:

G.

Cause

Unit I or Both

Unit 2 Totals

Component Failure

4

5

9

I

Design

I

Construction, Fabrication

or Installation

Personnel Error

Other

Total

- Operating Activity

2

- Maintenance Activity

1

- Test/Calibration

Activity

3

- Other

2

13

3

8

2

4

3

2

21

Note I: With regard to the area of "Personnel Error," the

NRC considers lack of procedures, inadequate procedures, and

erroneous procedures to be classified as personnel errors.

Note 2:

The "Other" category is comprised of Licensee Event

Reports where there was a spurious signal or a totally

unknown cause.

Note 3:

The above information was derived from a review of

Licensee Event Reports performed by the NRC staff and may

not completely coincide with the licensee's cause

assignments.

Licensing Activities

During the assessment period, a significant effort was expended in the

licensing area which resulted in the issuance of 23 license amendments,

15 reliefs, and 42 other licensing actions.

21

("* ... ,

  • .

H.

Enforcement Activity

FUNCTIONAL

AREA

NO. OF VIOLATIONS IN SEVERITY LEVEL

IV

III II I

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency Preparedness

Security

Engineering/Technical

Support

Safety Assessment/

Quality Verification

TOTAL

I.

Reactor Trips

I

I

I

1

4

1

I

May 7, 1992, Unit I Turbine Trip/Reactor Trip:

The unit had an automatic turbine trip followed by a reactor trip when

contractor maintenance personnel improperly attempted to stop an oil

leak on the thrust bearing test valve.

The unit was restarted the same

day.

January 8, 1993, Unit 1 Reactor Trip/Safety Injection:

While securing from a scheduled High Consequence Limiting Sequence on

Train A (degraded relay replacement), the unit tripped from 100% power

and a safety injection was initiated. A second safety injection was

initiated during the performance of corrective action for the first

event.

February 9, 1993, Unit 1 Reactor Trip:

During the process of securing from a monthly PT for testing reactor

trip breakers, a degraded relay caused the reactor to trip

automatically.

(The trip occurred simultaneously with the opening to

the '8' bypass breaker; the degraded relay was associated with the 'A'

reactor trip breaker train.)

June 20, 1993, Unit 2 Automatic Reactor Trip:

After loss of a main feedwater pump on an instantaneous ground, an

automatic reactor trip occurred on steam flow/feedwater flow mismatch in

coincidence with low steam generator water level in steam generator A.

22