ML18152A259

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Insp Repts 50-280/94-28 & 50-281/94-28 on 941002-1105. Violations Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Maint & Surveillance Insp, Plant Support,Ler follow-up & Action on Previous Insp Items
ML18152A259
Person / Time
Site: Surry  Dominion icon.png
Issue date: 12/02/1994
From: Belisle G, Branch M, David Kern, Tingen S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A260 List:
References
50-280-94-28, 50-281-94-28, NUDOCS 9412130095
Download: ML18152A259 (19)


See also: IR 05000280/1994028

Text

Report Nos. :

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/94-28 and 50-281/94-28

Licensee:

Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

October 2 through November 5, 1994

Inspectors:

Approved by:

Scope:

M. W. Branch, Senior Resident Inspector

G. Tingen, Resident Inspector

D. M. Kern, Resident Inspector

J~

~.A.

React r Projects Section 2A

Division of Reactor Projects

SUMMARY

11-1-rr-

Date Signed

I).- /-fy.

Date Signed

/ 7--/-9'-f

Date Signed

/l. *i- ttcf

Date Signed

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance and surveillance

inspections, plant support, Licensee Event Report followup, and action on

previous inspection items.

Inspections of backshift and weekend activities

were conducted on October 3, 6, 7, 12, 27, 28, 29, 31 and November 4, 1994 .

9412130095 941202

PDR

ADOCK 05000280

O

PDR

....

2

Results:

Plant Operations

The Unit 1 charging pump A cubicle was recently decontaminated and equipment

and housekeeping in the cubicle were good.

Housekeeping in the Unit 1

B charging pump cubicle was poor (paragraph 3.1.2).

Recurring annunciation of several control room alarms and C Steam

Generator (SG) level oscillations placed a heightened demand on operator

attentiveness.

Operators took appropriate action and effectively maintained a

safe operating environment.

The decision to reduce reactor power to control

SG level oscillations demonstrated a good safety perspective (paragraph 3.3).

On October 27, the 2A station battery was declared inoperable and on

October 28 the licensee requested and was granted enforcement discretion to

complete on-line repair.

Station Nuclear Safety and Operating Committee

review of this request was thorough and technically sound.

Licensed personnel

implemented appropriate operator actions while the 2A station battery was

inoperable (paragraph 3.4).

Maintenance

A violation was identified for failure to stop work and revise or obtain a new

procedure when the instructions in the design change to modify the charging

pump temperature control valve positioners could not be followed

(paragraph 4.2).

Operations, maintenance, and engineering personnel coordinated efficiently and

minimized the amount of time that the 2A station battery was out of service to

complete repairs.

Management oversight was evident and the temporary

modification was performed in a quality manner (paragraph 4.3).

Engineering

System engineer trending and evaluation of Unit 1 steam generator oscillations

was comprehensive.

Engineering technical support was timely and provided

valuable information to operations personnel for safe power operation

(paragraph 5.1).

An engineering evaluation of proposed modification to the 2A station battery

was sound (paragraph 5.2).

The charging pump lube oil temperature control systems in both units have a

history of operational difficulties.

Short term corrective actions were good

in that system operability was promptly evaluated and deviation reports

initiated when problems occurred.

However, the long term corrective actions

were not fully effective in that operational problems continue to occur

(paragraph 5.3) .

3

Plant Support

The general material condition and housekeeping within the turbine, security,

auxiliary, and safeguard buildings were good.

Minor discrepancies were

promptly corrected.

Radiological personnel were pro-active in establishing

measures to reduce the potential for spread of contamination during

preservation activities within the auxiliary building (paragraph 6.1) .

  • .

REPORT DETAILS

1.

Persons Contacted

1.1

Licensee Employees

  • W. Benthall, Supervisor, Licensing
  • M. Biron, Supervisor, Radiological Engineering
  • H. Blake, Jr., Superintendent of Nuclear Site Services
  • R. Blount, Superintendent of Maintenance
  • R. Cherry, Licensing, Corporate
  • D. Christian, Station Manager
  • R. Cross, Coordinator of Station Procedures

J. Costello, Station Coordinator, Emergency Preparedness

  • J. Downs, Superintendent of Outage and Planning

D. Erickson, Superintendent of Radiation Protection

  • A. Friedman, Superintendent of Nuclear Training

B. Garber, Licensing

B. Hayes, Supervisor, Quality Assurance

  • D. Hayes, Superintendent of Administrative Services
  • A. Keagy, Superintendent, Nuclear Materials
  • J. Kilmer, Licensing
  • C. Luffman, Superintendent, Security
  • R. MacManus, Supervisor, System Engineering
  • J. McCarthy, Assistant Station Manager
  • W. Miles, Supervisor, Quality Assurance

D. Miller, Radiation Protection

  • A. Price, Assistant Station Manager
  • R. Saunders, Vice President, Nuclear Operations

K. Sloane, Operations

E. Smith, Site Quality Assurance Manager

  • D. Sommers, Supervisor, Licensing, Corporate

T. Sowers, Superintendent of Engineering

B. Stanley, Station Procedures

  • J. Swientoniewski, Supervisor, Station Nuclear Safety

G. Thompson, Supervisor, Maintenance Engineering

E. Turko, Engineering

G. Woodzell, Nuclear Training

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics, security

force members, and office personnel.

1.2

NRC Personnel

  • M. Branch, Senior Resident Inspector
  • D. Kern, Resident Inspector

S. Tingen, Resident Inspector

  • Attended Exit Interview

Acronyms and initial isms used throughout this report are listed in the

last paragraph.

  • .

2.

2

Plant Status

Units 1 and 2 operated at power for the entire inspection period.

Reactor power on Unit 1 was reduced to 97 percent on October 15 to

reduce SG level oscillations (paragraph 3.3) and remained at this power

level through the end of the inspection period.

3.

Operational Safety Verification (71707)

3.1

Biweekly ESF Inspections

3.1.1 RSHX SW Supply/Discharge Piping

The inspectors walked down the RSHX SW supply and discharge

piping located in the Unit 1 and 2 safeguards buildings.

Proper containment isolation and SW radiation monitor and

SW flow instrument valve alignments were verified.

Equipment was in good overall condition and housekeeping was

adequate.

Housekeeping in these areas was recently improved

by cleaning the sumps and maintaining them in a dry

condition in lieu of being full of water.

3.1.2 Unit 1 Charging Pump Cubicles

On November 4, the inspectors walked down the Unit 1

charging pump cubicles.

Items inspected were charging pump

lube oil system, lube oil temperature control system,

charging pump seal cooling system and general equipment

condition.

Lube oil was present on the base plates of all

three charging pumps which indicated that there were minor

lube oil leaks.

Charging pump A had been decontaminated and

equipment and housekeeping was good.

Charging pump B had a

large quantity of boric acid on the base plate which was

considered contaminated.

The boric acid appeared to be from

RCS leakage past the pump outboard seal.

Also boric acid

was present at the outboard seal cooler mechanical joints

which indicated that the joints were leaking.

It appeared

that SW was leaking from the capped joint downstream of

valve l-SW-183.

Debris was present on the pump base plate

and on the cubicle floor.

The inspectors concluded that

housekeeping in charging pump B cubicle was poor.

Although

leaking joints were identified, the leakage did not appear

to be serious.

The overall condition of the equipment in

the cubicle was considered satisfactory.

Charging pump C

seal cooler mechanical joints had some boric acid present

but overall housekeeping and equipment condition was good in

the cubicle.

The above observations were presented to

maintenance management for evaluation and correction.

  • .

3.2

3.3

3

RCP lC Seal Degradation

Prior to the 1994 Unit 1 RFO, the #1 seal leakoff for RCP lC was

approximately 1.25 gpm.

After seal maintenance during the RFO,

the measured seal leakoff was approximately 1 gpm.

The design

flow rate through the #1 seal is approximately 3 gpm.

Westinghouse Product Update S-009, issued in March 1988, specifies

the normal operating range for #1 seal leakoff flow at NOP to be

from 1.0 to 5.0 gpm.

Current leakoff flows on the three Unit 2

RCPs was approximately 2.5 gpm.

Beginning in July, 1994, the #1 seal leakoff flow for RCP lC

slowly trended down from the 1 gpm value.

The licensee's

operating and abnormal procedures cautioned against continued RCP

operation with a low seal leakoff condition.

The technical

information provided to the licensee indicated that seal leakoff

values between 1 gpm and 0.8 gpm indicated a degraded RCP seal

which should be closely monitored, and at a value below 0.8 the

pump should be secured.

The licensee's monitoring of seal leakoff included validation of

control room flow indication by performing what the licensee

termed as a "bucket check".

This involved sending personnel into

containment to operate several local valves in order to divert and

collect the #1 seal leakoff in a graduated container.

Several

"bucket checks" were performed which determined that indicated

flow was approximately 0.2 gpm less than actual measured leakoff

fl ow.

At the inspection period's end the licensee continued to closely

monitor RCP seal leakoff flow.

A 21-day maintenance outage that

includes repair/replacing the RCP lC seal has been scheduled to

commence on November 27, 1994.

Unit 1 Operator Response to Control Room Alarms and Indications

Recurring annunciation of several control room alarms and C SG

level oscillations placed a heightened demand on operator

attentiveness early in this report period.

Degraded RCP seal

leakoff (paragraph 3.2) necessitated frequent reliance on abnormal

operating procedures and multiple containment entries to confirm

control room indication.

On October 10, operators observed five

percent peak-to-peak C SG level oscillations.

The magnitude of

the level oscillations increased slowly over the next several

days.

On October 12, the PZR Relief Valve Low Air Pressure alarm

locked in indicating that the backup actuating air supply to the

PZR PORVs was degraded.

A containment entry was required to

investigate the cause.

On October 13-14, the PZR PORV/SV Open

alarm annunciated approximately twenty times.

Initial

investigation verified that none of the PZR PORV/SVs had opened .

However, the alarm continued to recur whil~ technicians worked to

identify the cause of the erroneous alarm.

The inspectors

  • .

3.4

4

observed that control room operators responded appropriately to

each of the above alarms and effectively maintained a safe

operating environment.

The inspectors expressed concern that operators could become

unnecessarily challenged if additional alarms or further increases

in SG level oscillations occurred.

Station management was

sensitive to this concern and discussed potential compensatory

actions such as staffing an additional control room operator in

the event that the control room tempo further increased.

On

October 15, SG level oscillations increased to twenty percent

peak-to-peak.

The Shift Supervisor directed that reactor power be

reduced, which eliminated the SG level oscillations.

The

Operations Superintendent issued an operations standing order

which instructed operators to maintain reduced power levels to

minimize SG level oscillations until plant shutdown for SG

chemical cleaning (paragraph 5.1).

The decision to lower reactor

power significantly reduced the level of demand placed upon

operators in the control room by reducing the need to devote

special attention to steam generator levels.

Technicians subsequently repaired the circuit which had caused the

false PZR PORV/SV Open alarms.

The inspectors noted good system

engineer involvement in the evaluation and repair of this alarm.

On October 19, operators entered containment, identified an air

fitting leak which had caused the PZR Relief Valve Low Air

Pressure alarm, and placed the standby air bottles in service.

The inspectors concluded that licensee response to the elevated

control room tempo was appropriate.

Power reduction to reduce SG

level oscillations demonstrated a good safety perspective.

Management has scheduled a 21-day maintenance outage commencing

November 27, 1994, to repair/replace the RCP IC seal and

chemically clean the Unit 1 SGs.

Request for Enforcement Discretion

At 11:00 am on October 27, the licensee declared the Unit 2

120 vdc 2A station battery inoperable when a battery cell failed

the monthly surveillance test (paragraph 4.3).

The licensee

appropriately entered a 24-hour LCO shutdown action statement as

required by TS 3.16.B.3.

The inspectors observed station

management's discussion of corrective options and SNSOC's review

of the resulting corrective action plan.

The proposed plan

involved jumpering a degraded battery cell to restore the

operating integrity of the 2A station battery.

The engineering

basis for modifying the station battery and status of corrective

action planning was presented for SNSOC review.

On October 28,

the licensee concluded that evaluation and corrective maintenance

would not be complete within the TS permitted 24-hour period.

SNSOC subsequently approved a justification for continued Unit 2

operation at power for an additional 24-hour period to complete

corrective maintenance to the 2A station battery.

The inspectors

5

concluded that SNSOC adequately addressed pertinent safety

concerns to support the licensee's request for enforcement

discretion.

The licensee verbally requested NRC enforcement discretion via a

telephone conference call at 7:45 am on October 28.

Specifically,

the licensee requested enforcement discretion from TS 3.16.B.3 to

permit continued power operation for an additional 24-hour period.

NRC Region II and NRR representatives listened to the licensee's

request and asked questions concerning the current condition of

the station battery, safety aspects of continued power operation

in this condition for an additional 24-hours, and design

capability of the intended battery modification.

The licensee

responded that the remaining 59 battery cells showed no sign of

degradation, operational experience from a similar power plant

would be used for the battery modification, and that continued

operation did not create a significant hazards consideration as

defined in 10 CFR 50.92.

System engineers further described the

mechanism which had degraded the single battery cell and indicated

that the condition was unlikely to significantly worsen in the

next 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Subsequent to the conference call, the inspectors requested

further information regarding the relative risk of continued

operation for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> for on-line repairs as compared to

performing the corrective repair while shutdown.

Station

management determin~d that the likelihood of occurrence for the

most challenging station battery significant event was on the

order of IOE-7.

SNSOC further determined that the inherent risk

associated with the battery jumper installation process was not

sign~ficantly altered by maintaining the plant at power.

The NRC

further internally reviewed the technical aspects and safety

significance of the request.

The NRC concluded that exercise of

enforcement discretion was appropriate to minimize the potential

safety consequences of unnecessary plant transients and the

accompanying operational risks and impacts.

At approximately

9:30 am, the NRC verbally granted the licensee enforcement

discretion from TS 3.16.B.3, extending the LCO action statement

for an additional 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The licensee promptly submitted a written request for enforcement

discretion to follow-up the conference call. The inspectors

observed that the document did not directly discuss the projected

condition of the degraded cell or its affect on the 2A station

battery during the additional 24-hour period.

However, this

information was provided during the conference call in appropriate

detail.

In addition the licensee stated that a TS amendment

request to clarify the narrative description of the station

battery in TS 4.6.C.l would be submitted.

The inspectors

determined that the document accurately recorded the safety basis

for the request.

3.5

6

At 11:00 am on October 28, operators entered TS 3.0.l which is a

six-hour shutdown LCO action statement.

Earlier, operators had

been informed that the NRC had tentatively, verbally granted the

requested enforcement discretion, but were awaiting confirmation

from the corporate staff.

The corporate staff confirmed NRC

approval at 1:30 pm and the licensee promptly exited TS 3.0.1.

Corrective maintenance was performed (paragraph 4.3) and the

licensee exited the exited TS 3.16.B.3 at 6:15 pm, thereby

terminating the NRC enforcement discretion.

Monthly Verification of Containment Isolation Valve Lineups

The inspectors walked down containment penetrations and verified

that the containment isolation valves were properly aligned,

vent/drain connections were capped, and that there was no leakage

from the piping.

Unit 1 exterior containment penetrations 79

through 86 were inspected.

These penetrations contain the SW

supply and discharge piping to the RSHXs.

The inspectors verified

locally that the air operated containment isolation valve in each

line was shut and verified that the control room indications also

indicated shut.

Unit 2 exterior containment penetrations 79

through 86 were also inspected. These penetrations provide the

same function as the Unit 1 penetrations and the containment

isolation valve in each line was verified to be shut in the same

manner as the Unit 1 valves.

3.6

Monthly Review of Safety-Related Tagouts

The inspectors reviewed the following safety-related tagouts and

verified that the tagouts were prepared and implemented in

accordance with OPAP-0010, Tagouts, revision 4, and that the

tagged components were in the required position:

Tagging Record No.: l-94-EP-0116, Replace l-VS~E-48 Normal

Supply Breaker.

Tagging Record No.: 2-93-EP-0050, Issue to shift supervisor

(emergency bus cross-tie breaker).

Within the areas inspected, no violations or deviations were identified.

4.

Maintenance and Surveillance Inspections (62703, 61726, TI 2515/125)

The inspectors observed various maintenance and surveillance activities

to verify proper calibration of test instrumentation, use of approved

procedures, performance of work by qualified personnel, conformance to

LCOs, and correct system restoration following the completion of

maintenance and post maintenance .

4.1

7

FME Controls (TI 2515/125)

The inspectors reviewed VPAP-1302, FME Program, rev1s1on 6, and

concluded that provisions for material, parts, and tool

accountability to ensure loose items are not inadvertently left

inside structures, systems, or components after the completion of

work activities were properly addressed.

Work activities

involving entry into SGs, reactor cavity when the reactor vessel

head is removed, fuel pool, containment sump and SI, RHR, AFW and

RC system openings were examples where FME controls were invoked.

Methods for maintaining FME include establishing an FME controlled

work area where items entering and exiting the work area are

logged in and out, covering system openings when work is not being

done, maintaining cleanliness when the work is performed and

performing closeout inspections after completion of the work to

ensure that all FM was removed.

In June 1994, the licensee noted an increasing trend in deviations

associated with FME controls. A task team was assembled to review

recent FME events and to evaluate the overall effectiveness of the

program and its requirements.

The task team concluded that the

station FME program was adequate and that the increasing trend in

deviations was primarily due to a lack of awareness of FME

standards on the part of individuals not directly involved in the

implementation of FME controls. Also in June 1994, Violation

50-280, 281/94-17-02 was issued for failure to prop~rly install

FME covers over RCS maintenance openings and the failure to remove

scaffold material after cleaning a CCW heat exchanger.

The

inspectors reviewed the licensee's response to the violation and

considered that it was adequate.

The inspectors also reviewed the

corrective actions recommended by the task team to improve station

awareness of FME controls and considered them to be adequate.

The

inspectors will review implementation of these as part of the

violation closure.

During monthly maintenance observations the inspectors routinely

checked for proper FME controls.

FME controls were observed to

have been properly implemented during the recent maintenance

activities associated with cleaning CC heat exchanger 1-CC-E-lD,

overhaul of EOG fuel oil transfer pump 1-EE-P-lD and replacement

of the AVEF train A charcoal filter media.

FME controls have improved.

FME covers were installed over the

  1. 1 EOG air intake filters for welding and grinding activities;

however, the same level of protection was not provided for the air

cooling louvers for the electrical generator.

During grinding and

weld activities, the inspectors noted that metal grinding material

was entering the electrical generator housing.

The inspectors

questioned the craft personnel about FME controls and was told

that grinding was now complete and that they had not considered

the air louvers as an area needing protection.

The inspector

notified the SE who exhibited a great deal of concern with metal

4.2

8

material entering the electrical generator.

The SE directed

electrical maintenance to remove the generator covers and vacuum

out the metal grinding material. Additionally, procedural

controls for work on the other two EDGs was modified to specify

more complete FME controls.

Modification To Charging Pump SW TCV Positioners

On October 23 and 24, the inspectors witnessed the modification of

the positioner to A charging pump TCV, l-SW-TCV-108A.

The purpose

of this modification was to change the positioner from reverse

acting to direct acting and was accomplished in accordance with

WO 271507-05 and portions of DCP 92-27-3, Charging Pump SW TCV

Replacement Surry Units 1 and 2, field change 3.

The inspectors witnessed the technicians removing the positioner

and modifying the positioner in the shop.

The instructions

required that the positioner be partially disassembled in order to

perform the modification.

The instructions specified that the set

screw be removed from one side of the disc assembly and installed

on the opposite side of the disc assembly.

The inspectors noted

that technicians removed and reversed the disc assembly in lieu of

removing and relocating the set screw.

The inspectors were

informed that the design did not lend itself to removing and

relocating the set screw.

The positioner was reassembled and

reinstalled.

During subsequent testing the positioner did not

properly operate.

The positioner was removed and disassembled.

Technicians concluded that the disc assembly was not properly

oriented during the initial modification attempt.

The assembly

was reoriented and the positioner reassembled and reinstalled.

During subsequent testing the positioner again failed to properly

operate.

During the third attempt to modify the posit i oner

technicians noted that other parts were not properly assembled in

the positioner.

The positioner was properly reassembled and

satisfactorily operated during subsequent testing.

Step 3.3.f of DCP 92-27-3 specified that the positioner be

modified in accordance with Appendix 4-12.

Following the

modification of the positioner for the Unit 1 A charging pump TCV,

the inspectors questioned if Appendix 4-12 needed to be revised to

provide correct instructions.

The DCP was subsequently revised.

This revision also ctarified how the positioner was to be

reassembled.

Subsequent investigation revealed that the licensee's controlled

vendor technical manual for the charging pump TCV positioners did

not provide instructions for modifying the positioner.

The

instructions in the DCP for modifying the positioner were provided

directly to station engineering by the vendor and incorporated

into DCP 92-27-3.

The vendor was contacted by the licensee and

questioned why these instructions would not work.

The licensee

was informed that the instructions were not applicable to the

...

9

licensee's TCV positioners and were provided in error.

The vendor

subsequently approved the licensee's method of modifying the

pas it i oner.

This same modification was previously performed on the positioner

for the Unit 2 B charging pump TCV, 2-SW-TCV-208B.

The inspectors

reviewed WO 272634-03 completed on September 2, 1994.

The WO

summary sheet completed by the technicians that performed the work

did not discuss that the instructions in the DCP could not be

followed.

A change to DCP 92-27-3 instructions was not issued

during that time.

The inspectors were informed that the

positioner for the Unit 2 B charging pump TCV was modified by

reversing the disc assembly in lieu of removing and relocating the

set screw as specified in the DCP.

Step 6.10.2.b of VPAP-0801, Maintenance Program, rev1s1on 4,

requires that when a work instruction cannot be followed the items

shall be placed in a safe condition, work stopped, and a new or

r~vised instiuction be prepared.

The failure to stop work after

it was identified that instructions for modifying Unit 1 A

charging pump and Unit 2 B charging pump TCV positioners could not

be followed was identified as VIO 50-280, 281/94-28-01, Failure to

Stop Work When Work Instructions Could Not Be Followed .

4.3

Unit 2 Online LCO Maintenance - Station Battery

On October 27, the 2A station battery cell 52 voltage was measured

at 2.067 volts and the 2A station battery was declared inoperable

(paragraph 3.4).

An event chronology and enforcement action

associated with this event are addressed in a special report,

NRC Inspection Report Nos. 50-280/94-32 and 50-281/94-32.

The licensee developed TM S2-94-15, Station Battery 2A Cell 52

Bypass Jumper, revision 0, and corrective maintenance procedure

2-ECM-0101-10, Cell 52 Of Main Station Battery 2A - Jumper Cable

Installation or Removal Provision, revision 0, to jumper out

cell 52 from the 2A station battery while the plant remained at

power.

Experience gained from similar maintenance at the North

Anna Power Station was effectively used.

The inspectors observed

SNSOC's review of the TM and installation procedure.

SNSOC

members demonstrated strong safety sensitivity to performing this

maintenance on-line and asked detailed questions which improved

the quality of procedure 2-ECM-0101-10.

The inspectors' questions

regarding procedural guidance to open circuit the battery were

appropriately addressed in the SNSOC review.

The inspectors attended the licensee's pre-brief for the

installation of TM S2-94-15.

The work plan (WO 302410) was

reviewed thoroughly by maintenance, operations, and management

personnel.

Specific precautions and preparations for a potential

loss of DC power were implemented in accordance with abnormal

procedure 2-AP-10.06, Loss of DC Power, revision 2.

The licensee

  • .... ~.

10

also implemented senior management oversight controls using

VPAP-0108, Infrequently Conducted or Complex Tests.

Maintenance

technicians observed that procedure 2-ECM-0101-10 provided

detailed instruction for the installation of a permanent jumper,

but did not specifically indicate that two permanent jumpers were

required to complete the TM.

Management personnel reviewed this

concern and confirmed with SNSOC that installation of the second

jumper was within the scope of the procedure.

Maintenance

personnel were directed to perform the TM using the procedure as

written.

The inspectors evaluated the increased safety risk of

delaying the TM for further refinement of the procedure and

concluded that the management decision was appropriate.

The pre-

brief for this safety related maintenance was excellent.

Maintenance personnel commenced WO 302410 at 3:21 pm on

October 28.

The inspectors observed maintenance activities in the

control room and in the battery room.

Communications were

effectively established and management oversight was appropriate.

The inspectors observed excellent second checking by electricians

while performing each step of the jumper installation procedure.

System engineers provided close technical support to technicians

in the battery room.

Materials were properly staged and access to

the work area was effectively controlled.

TM S2-94-15 was

completed, the 2A station battery was declared operable, and the

licensee exited TS 3.16.B.3 at 6:15 pm on October 28.

Operations,

maintenance, and engineering personnel coordinated efficiently to

minimize the amount of time that the 2A station battery was out of

service and to complete the TM in a quality controlled manner.

Constructive comments and lessons learned from this first

performance of 2-ECM-0101-10 were collected for incorporation into

a procedure revision.

Within the areas inspected, one violation was identified.

5.

Onsite Engineering Review (37551)

5.1

SG Level Oscillations

Unit 2 SG level oscillations had been observed as early as

May 1993.

The licensee evaluated the condition, modified plant

operations, and eventually resolved the issue by chemically

cleaning the SGs in June 1994.

Engineers determined that the

oscillations resulted from buildup of a hard iron-copper scale on

the SG tube support plates.

The blockage caused an increased

pressure drop in the two-phase flow zone which in turn resulted in

hydrodynamic instability (SG level oscillations).

Licensee root

cause evaluation determined that Unit 1 was susceptible to the

same problem.

Further assessment of Unit 2 identified several SG

water chemistry trends as precursors to the onset of SG level

oscillations.

The vendor performed a visual inspection of the

Unit 1 SG tube support region in March 1994 and identified

significant tube support plate blockage in the A and C SGs.

The

-.

11

licensee commenced monitoring SG chemistry following the restart

of Unit 1 and observed gradual development of the same trends

which had preceded oscillations on Unit 2.

The inspectors

discussed the SG inspection results and trend analysis with system

engineers and concluded that the licensee maintained a good

technical understanding of the SG level oscillation phenomenon.

On October 10, operators began to observe Unit 1 C SG level

oscillations (paragraph 3.3).

On October 15, operators reduced

reactor power to eliminate the oscillations as had been previously

recommended by engineering to address Unit 2 oscillations.

The

inspectors questioned whether continued operation with

oscillations, and thereby a reduced SG operating inventory, posed

an unreviewed safety question.

Engineering prepared Safety

Evaluation 94-183 and determined that continued operation with

oscillations did not present an unreviewed safety question.

Engineering Transmittal S-94-0171 was then developed to provide

interim operating guidance until the plant could be shut down for

SG cleaning.

Engineering recommended reactor power be limited to

98 percent to eliminate SG level oscillations.

Further power

reductions in one percent increments were projected as necessary

to compensate for continuing tube sheet blockage prior to plant

shutdown for SG cleaning.

The inspectors reviewed Safety

Evaluation 94-183 and Engineering Transmittal S-94-0171 and

determined them to be technically sound.

Use of previous

experience from Unit 2 and engineering support for continued power

operation was comprehensive.

5.2

Evaluation of Unit 2 Station Battery Temporary Modification

Safety Evaluation 94-185 and TM S2-94-15 were created to support

on-line modification of the 2A station battery.

The modification

was written to temporarily jumper out degraded cell 52, thereby

restoring integrity to the 2A station battery.

The inspectors

reviewed the documents and determined that they had been properly

prepared in accordance with VPAP-1403, Temporary Modifications.

SNSOC's evaluation of the TM was detailed.

The licensee developed Engineering Transmittal CEE-94-063 and

Calculation EE-0046 to evaluate the capability of the 2A station

battery to perform its design function with up to two of the

original 60 cells jumpered out of service.

Engineering determined

that the 2A station battery would remain operable with two cells

jumpered.

The inspectors concluded that the documents technically

justified the licensee's determination that the 2A station battery

was operable following the installation of TM S2-94-15.

5.3

Charging Pump Lube Oil Temperature Control System

The charging pump lube oil temperature control systems in both

units have had a history of operational difficulties.

In 1992,

the TCVs on all six charging pumps were replaced to improve system

~.

12

operation.

Prior to 1992, SW flow blockages in the system were a

major problem.

Replacement of the TCVs solved the blockage

problem but additional problems developed following the

installation of the new TCVs.

Through review of the DRs initiated

on the charging pump TCVs, the inspectors noted that 24 DRs were

initiated since 1993 due to operational problems.

On several

occasions charging pumps were rendered inoperable due to TCV

operational problems.

Sluggish operation of the TCV appeared to

be the problem in the majority of DRs submitted.

After the TCVs were replaced, a stem wiper ring was subsequently

installed on each TCV to prevent mud/silt from accumulating in the

packing.

In December 1993, field change 3 was issued to

DC 92-27-3 to implement additional changes in the charging pump

lube oil temperature control systems to reduce stem friction and

improve TCV operation.

Modifications to be implemented included

installation of differently designed TCV stem packing material and

modified wiper rings and increasing valve actuator air pressure

operating range.

These modifications have been recently

implemented on the Unit 2 B charging pump lube oil temperature

control system and these modifications are to be completed on the

remaining Unit 1 and 2 charging pump lube oil temperature control

systems.

However, sluggish operation of the Unit 2 B charging

pump TCV has been noted since completion of the DC 92-27-3

modifications.

Corrosion of the TCV guide bushings and packing follower has also

been identified as a cause of excessive valve stem friction.

The

licensee was developing a schedule to replace the packing follower

and guide bushings on all six charging pump TCVs with a less

corrosive material.

The licensee's 1994 third quarter DR trend report identified that

charging pump lube oil temperature control system problems were

recurring.

Also, the licensee has a Level I Project on this

issue.

The inspectors concluded that when charging pump lube oil

temperature control system problems occur, short term corrective

actions were good, in that, system operability was promptly

evaluated and DRs initiated.

However, the long term corrective

actions were not fully effective in that operational problems

continue to occur.

Within the areas inspected, no violations or deviations were identified.

6.

Plant Support (40500, 71707, 71750)

The inspectors conducted facility tours, work activities observations,

personnel interviews, and documentation reviews to determine whether

licensee programs were effectively implemented to comply with regulatory

requirements in the areas of radiological protection, security,

emergency preparedness, and fire protection.

13

6.1

Plant Tour Observations

The inspectors observed radiological control practices and

radiological conditions throughout the plant.

Portal and handheld

monitors were observed to be in good condition and within proper

calibration periodicities.

Radiological postings and control of

contaminated areas were good.

Workers complied with radiation

work permits and appropriately used required personnel monitoring

devices.

Plastic sheets were installed as a vertical extension of

the contaminated area boundary within portions of the auxiliary

building.

The inspectors determined this to be a pro-active

measure which reduced the potential for spread of contamination

during preservation activities within the auxiliary building.

The general material condition and housekeeping within the

turbine, security, auxiliary, and safeguard buildings were good.

Minor discrepancies such as improperly stored anticontamination

clothing were identified and reported to the shift supervisor.

The inspectors confirmed, on subsequent plant tours, that the

discrepancies had been corrected.

The inspectors observed that

some of the cable penetrations through the Unit 2 cable vault/pipe

tunnel wall were not sealed and questioned whether these

penetrations were credited as a fire barrier.

The licensee

presented controlled station drawings which showed that this wall

and penetrations were not credited as a fire barrier. A recent

design change package relocated the cable vault fire barrier to

the pipe tunnel/auxiliary building wall.

The inspectors reviewed

controlled station drawings and confirmed that penetrations in

question were not currently credited as a fire barrier.

No

discrepancies were identified.

Selected aspects of plant physical security were reviewed during

regular and backshift hours to verify controls were in accordance

with the security plan and implementing procedures.

This review

included security measures, vital and protected area barrier

integrity, maintenance of isolation zones, personnel access

control, searches of personnel, packages and vehicles, and

escorting of visitors.

No discrepancies were noted.

Use of

security cards for access to the Unit 2 battery room was relaxed

on October 28 to facilitate maintenance activities

(paragraph 4.3). A security guard was stationed to hold open the

door and verify that personnel entering the room had proper access

authorization.

The number of people involved in the maintenance

and turnover of guard personnel midway through the evolution posed

a challenge to access control.

The inspectors questioned the

stationed security personnel concerning their access control

responsibilities and actions to be taken in the event that the

battery room maintenance resulted in a fire.

Security personnel

were knowledgeable and performed their duties in an acceptable

manner .

  • ..

14

6.2

Management Safety Review Committee

The inspector reviewed the meeting minutes from MSRC meeting 94-08

and attended portions of the most recent MSRC meeting, convened on

October 4.

The committee is comprised of both licensee and

non-licensee personnel, who provide independent review and audit

of a wide variety of Surry Station activities.

Both Surry and

North Anna power station activities are reviewed at each MSRC

meeting.

The MSRC currently meets eight times per year, which is

more frequent than required by TS.

A quorum was properly

established on October 4, with fourteen of the seventeen committee

members present.

The committee reviewed current operating status,

NRC reportable events and violations since the last MSRC meeting,

key management personnel changes, and significant events including

the recent chemical contamination of the auxiliary ventilation

system charcoal filters discussed in NRC Inspection Report Nos.

50-280/94-24 and 50-281/94-24.

Questions raised by committee

members were generally of an in-depth nature.

Station personnel

provided supplemental information when requested to clarify

actions which the station has taken to address both industry and

Surry specific issues.

The inspector concluded that MSRC

effectively performed review and audit of station activities.

Within the areas inspected, no violations or deviations were identified.

7.

Licensee Event Report Followup (92700)

The inspectors reviewed LERs submitted to the NRC to verify accuracy,

description of cause, previous similar occurrences, and effectiveness of

corrective actions.

The inspectors considered the need for further

information, possible generic implications, and whether the events

warranted further onsite follow-up.

The LERs were also reviewed with

respect to the requirements of 10 CFR 50.73 and the guidance provided in

NUREG 1022, Licensee Event Report System, and its associated

supplements.

(Closed) LER 50-280/94-004, Loop Isolation Valve Not Open Within TS

Limit Due to Personnel Error.

Violation 50-280/94-08-01, Failure to

Open the Unit 1 B Loop Hot Leg Stop Valve Within 2 Hours, was issued as

a result of this event.

Corrective actions for this event will be

reviewed during the closeout of Violation 50-280/94-08-01.

(Closed) LER 50-280, 281/94-008, Both Auxiliary Ventilation Fans

Inoperable Due to a Single Event.

Violation 50-280, 281/94-24-01,

Failure to Identify and Promptly Correct Conditions Adverse to Quality,

was issued as a result of this event.

Corrective actions will be

reviewed during the closeout of Violation 50-280, 281/94-24-01.

(Closed) LER 50-281/94-003, Failure to Isolate Primary Grade Water to

Blender.

Violation 50-281/94-17-01, Failure to Close Unit 2 Makeup

15

Water Isolation Valve Within Fifteen Minutes After Makeup, was issued as

a result of this event.

Corrective actions will be reviewed during the

closeout of Violation 50-281/94-17-01.

Within the areas inspected, no violations or deviations were identified.

8.

Exit Interview

The inspection scope and findings were summarized on November 8, 1994,

with those persons indicated in paragraph 1.

The inspectors described

the areas inspected and discussed in detail the inspection results

addressed in the Summary section and those listed below.

Item Number

VIO 50-280, 281/94-28-01

LER 50-281/94-003

LER 50-280/94-004

LER 50-280, 281/94-008

Status

Open

Closed

Closed

Closed

Description/(Paraqraph No.)

Failure to Stop Work When Work

Instructions Could Not be

Followed (paragraph 4.2).

Failure to Isolate Primary

Grade Water to Blender

(paragraph 7).

Loop Isolation Valve Not Open

Within TS Limit Due to

Personnel Error (paragraph 7).

Both Auxiliary Ventilation

Fans Inoperable Due to a

Single Event (paragraph 7).

Proprietary information is not contained in this report.

Dissenting

comments were not received from the licensee.

9.

Index of Acronyms and Initialisms

AFW

AUXILIARY FEEDWATER

AVEF

AUXILIARY VENTILATION EXHAUST FILTER

CCW

COMPONENT COOLING WATER

CFR

CODE OF FEDERAL REGULATIONS

DCP

DESIGN CHANGE PACKAGE

DR

DEVIATION REPORT

EOG

EMERGENCY DIESEL GENERATOR

EE

ENGINEERING EVALUATION

ESF

ENGINEERED SAFETY FEATURE

FME

FOREIGN MATERIAL EXCLUSION

GPM

GALLONS PER MINUTE

LCO

LIMITING CONDITIONS OF OPERATION

LER

LICENSEE EVENT REPORT

MSRC

MANAGEMENT SAFETY REVIEW COMMITTEE

NOED

NOTICE OF ENFORCEMENT DISCRETION

NOP

NORMAL OPERATING PRESSURE

..

NRC

NRR

PORV

PZR

RC

RCP

RCS

RFO

RHR

RSHX

SE

SG

SI

SNSOC

sv

SW

TCV

TI

TM

TS

voe

VIO

VPAP

WO 16

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

POWER OPERATED RELIEF VALVE

PRESSURIZER

REACTOR COOLANT

REACTOR COOLANT PUMP

REACTOR COOLANT SYSTEM

REFUELLING OUTAGE

RESIDUAL HEAT REMOVAL

RECIRCULATION SPRAY HEAT EXCHANGER

SYSTEM ENGINEER

STEAM GENERATOR

SAFETY INJECTION

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SAFETY VALVE

SERVICE WATER

TEMPERATURE CONTROL VALVE

TEMPORARY INSTRUCTION

TEMPORARY MODIFICATION

TECHNICAL SPECIFICATION

VOLTS DIRECT CURRENT

VIOLATION

VIRGINIA POWER ADMINISTRATIVE PROCEDURE

WORK ORDER