ML18152A229

From kanterella
Jump to navigation Jump to search
Insp Repts 50-280/89-31 & 50-281/89-31 on 891001-28.No Violations Noted.Major Areas Inspected:Plant Operations, Plant Maint,Plant Surveillance,Info Meetings W/Local Officials & LER Review
ML18152A229
Person / Time
Site: Surry  Dominion icon.png
Issue date: 11/28/1989
From: Fredrickson P, Holland W, Larry Nicholson, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A230 List:
References
50-280-89-31, 50-281-89-31, NUDOCS 8912130192
Download: ML18152A229 (19)


See also: IR 05000280/1989031

Text

.. ,/*

  • 'I ****

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W .

ATLANTA, GEORGIA 30323

Report Nos.:

50-280/89-31 and 50-281/89-31

Licensee:

Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.:

DPR-32 and* DPR-37

Inspection Conduct.ed:

October 1 - 28, 1989

Inspectors:

~;:f?;7. ~

4

. W. 'E. Ho 11 and, Senior sldent Inspector

Approved

Scope:

~~/L-/ifs

J. W. York, Resident nspector

L.

InspecY,J

'lr~~

Fredrickson, Section Chief

Division of Reactor Projects

SUMMARY

Date Signed

Date Signed

Date Signed

11/-:>-1-f P'I

Dlte s, gned

This routine resident inspection was conducted on site in the areas of plant

operations, plant maintenance, plant surveillance, information meetings with

local officials, and licensee event report review.

Certain tours were conducted on backshifts or weekends.

Backshift or weekend

tours.were conducted on October 9, 11, 12, 19, 21, 22, and 25.

Results:

During this inspection period, one violation with two examples was identified

regarding licensed operators failure to follow procedures and/or instructions

(paragraph 3.a).

One unresolved item was identified regarding followup on

material problems associated with safety-related check valve maintenance

(paragraph 4.c).

In addition, seven non-cited violations were identified

during closeout of licensee event reports (paragraph 7) ..

These violations

involved personnel errors, procedural inadequacies and failure to perform

required samples .

8912130192 891128

PDR

ADOCK 05000280

Q

PDC

..

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer

R. Blount, Superintendent of Technical Services

D. Christian, Assistant Station Manager

D. Erickson, Superintendent of Health Physics

  • E. Grecheck, Assistant Station Manager

M. Kansler, Station Manager

T. Kendzia, Supervisor, Safety Engineering

  • J. McCarthy, Superintendent of Operations

G. Miller, Licensing Coordinator, Surry

J. Ogren, Superintendent of Maintenance

  • T. Sowers, Superintendent of Engineering
  • E. Smith, Site Quality Assurance Manager
  • Attended exit interview.

Other licensee employees contacted included control room operators, shift

technical advisors, shift supervisors and other plant personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Unit 1 began the reporting period at power.

The unit operated at power

for the duration of the inspection period.

Unit 2 began the reporting period with the unit increasing power after

turbine balancing evolutions had been completed.

The unit reached full

power on October 8, 1989, and operated at power until October 12, 1989,

when identification of leakage past a pressurizer safety valve required

that the unit be shut down for repairs. The unit was subcritical at 1116

hours on October 12, and reached the cold shutdown condition on October

13.

The unit remained in cold shutdown for the duration of the inspection

period.

3.

Operational Safety Verification (71707 & 42700)

a.

Daily Inspections

Inspections were conducted daily in the following areas:

control

room staffing, access, and operator behavior; operator adherence to

approved procedures, TS, and LCOs; examination of panels containing

2

instrumentation and other RPS elements to determine that required

channels are operable; and review of control room operator logs,

operating orders, plant deviation reports, tagout logs, jumper logs,

and tags on components to verify ~ompliance with approved procedures.

(1)

During this inspection period, the inspectors reviewed an

operational event associated with the incorrect system alignment

of a Unit 2 AFW pump during performance of the monthly TS

operability test.

The event sequence was as follows:

On October 8, 1989, a licensed operator on the midnight shift

was directed to conduct the monthly surveillance tests for* the

Unit 1 and 2 B train AFW pumps in accordance with procedures

1-PT-15.lB and 2-PT-15.lB, respectively.

The operator obtained

copies of each approved test procedure, other support equipment,

and went to the Unit 1 safeguards area to conduct the test on

the Unit 1 B pump (l-FW-P-38) in accordance with l-PT-15.lB.

After conducting all necessary prestart" alignments, the operator

requested the Unit 1 CRO to start the B pump as required by

procedure.

At this time the shift supervisor (a licensed SRO)

reported to the pump location and conducted a material condition

check of l-FW-P-3B prior to pump start. The PT for the Unit 1

pump was completed satisfactorily and the system was returned to

its

normal

operational

lineup.

The

procedure

required

independent verification for returning the system to normal

lineup.

The operator then preceded to the Unit 2 safeguards

area to conduct the same test on the Unit 2 B *pump (2-FW-P-3B)

in accordance with 2-PT-15.lB.

However, the operator performed

the re qui red a 1 i gnments on the Unit 2 A pump in stead of the

Unit 2 B pump as required by procedure.

These alignments

include shutting of the discharge isolation valves for the pump

to be tested. After completion of the alignments and a similar

verification of the material condition of the pump by the shift

supervisor, the Unit 2 CRO started the B pump as required by

procedure and noted flow to the steam generators (this condition

was not expected).

The C"RO immediately secured the B AFW pump

and the operator and shift supervisor at the pump 1 ocat ion

determined that *the wrong pump *had been a 1 i gned for testing

(i.e. the A pump discharge valves had been closed instead of the

B pump discharge valves). The operator immediately opened the A

pump discharge valves after the mistake was realized.

The B

pump was then aligned for testing in accordance with 2~PT-15.1B

and the test was satisfactorily completed.

After learning about the above event, station management

reviewed the event with those individuals involved and concluded

the following:

The operator did not strictly follow procedure during

performance of the PT.

This fact was obvious when the

    • <

3

field copies were reviewed and very few signature blocks

were initialed as indicating performance of required.steps .

. The relative room location of the Unit 2 pumps are reversed

from the Unit 1 location. However, the pumps in the Unit 2

safeguards area were clearly labeled.

Immediate corrective actions were taken by station management to

include stern re,nstruction of all operating shifts with regards

to the requirement for strict procedure adherence and attention

to detail.

In addition, the operators involved in the event

were taken off shift and disciplinary actions were taken.

The inspector was present during the management review with the

involved individuals and concluded that the station upper- and

mid-level

management considered the performance of these

operators as unsatisfactory and that procedure adherence was

mandatory in the future.

The inspector agrees with licensee

management's assessment of the event; however, he also considers

that the lack of procedure adherence and attention to detail is

a lingering weakness which needs continued aggressive reinforce-

ment in order to eliminate the problem.

The inspect9r reviewed

the procedure for performance of the test and noted that strict

procedure adherence would have prevented this everit.

Failure to

follow procedure 2-PT-15.lB is identified as a violation of

TS 6.4 (VIO 280, 281/89-31-01).

.

(2) A second operational event occurred on October 25 that involved

a dilution of the Unit 2 RCS.

The unit was in cold shutdown in

a reduced inventory condition for repair of leaking SI check

valves.

Maintenance had completed the va,lve repair and the

opera tors were f i 11 i ng the RCS when the di 1 ut ion occurred.

Adequate shutdown margin was maintained during the event with no

increase in count rate on the source range nuclear instrumenta-

tion.

Containment integrity was not established during this

dilution event.

TS 3.8.A.6 requires that a boron dilution shall

not be made unless containment intergrity is intact.

The RO initiated filling the RCS from a standpipe level o~ 13.6

feet at 0120 hours0.00139 days <br />0.0333 hours <br />1.984127e-4 weeks <br />4.566e-5 months <br /> tin October 25.

Initial RCS boron concentra-

tion was listed as 2130 ppm.

Samples taken during the initial

phase of *the fill indicated that the makeup blend was resulting

in a slight boration (2300 ppm at 0320 hours0.0037 days <br />0.0889 hours <br />5.291005e-4 weeks <br />1.2176e-4 months <br />).

In addition to

correcting this bl end, the RO a 1 s'o increased the fi 11 rate by

placing the boric acid valve controller in manual and opening

the acid valve to fully open._ This action resulted in the boron

flow rate indication available to the RO going offscale high.

An adjustment of the pure water valve was al so made in an

attempt to maintain the same mixture.

. '

4

The RO secured the filling evolution at 0455 hours0.00527 days <br />0.126 hours <br />7.523148e-4 weeks <br />1.731275e-4 months <br /> to allow

transfer of inventory between boric acid tanks.

The RCS fill

was resumed at 0548 hours0.00634 days <br />0.152 hours <br />9.060847e-4 weeks <br />2.08514e-4 months <br />. It appears that at this time the RO

returned the boric acid valve controller to the automatic mode.

This action caused the controller to take control and close the

acid valve from the approximately 17 gpm full open flow rate

down to the 9. 5 gpm -that had been previously set on the

controller.

The reactor operator did not verify that the blend

settings were correct when he resumed the RCS fi 11 and did not

realize that this action resulted in a dilution of the makeup

blend.

The RCS fill was completed at 0752 hours0.0087 days <br />0.209 hours <br />0.00124 weeks <br />2.86136e-4 months <br /> with a boron

concentration of approximately 2065 ppm.

Although the oncoming dayshift operators recognized .that a

dilution had occurred and submitted a station deviition, they

did not determine the cause of the event.

Consequently, at 1052

hours the operators initiated a makeup to the RCS to increase

primary pressure without verifying the proper blender setting.

This resulted in a second unplanned dilution from approximately

2065 ppm to 1996 ppm at 1340 hours0.0155 days <br />0.372 hours <br />0.00222 weeks <br />5.0987e-4 months <br />.

The operators discovered

the error and performed a borat ion that resulted in an RCS

concentration of 2110 ppm at 1505 hours0.0174 days <br />0.418 hours <br />0.00249 weeks <br />5.726525e-4 months <br />.

Filling of the RCS is specified per operations procedure

2-0P-5.1.L

Step 5.10 requires that boric acid and primary_

grade water flow rates be in accordance with the blended flow

nomograph in the station curve book.

In addition, the licensee

has considered operation of the blender system as

11 skill of the

craft

11 *

This philosophy was defined by the Superintendent of

Operations as a task that is so routine that it could be

performed -by a licensed operator without the use of deta i 1 ed

procedures.

The

licensee also stated that training and

instructions direct that the boric acid and pure water flow

rates be verified in accordance with the blended flow nomograph

whenever an RCS makeup is initiated.

Contrary to these instructions, the operator initiated an RCS

fill after performing* a boric ac*id transfer without verifying

the correct fl ow rates.

In addition, the operators on the

following shift reinitiated RCS fill without verifying that the

flow rates were in accordance with the proper nomograph.

The

iispectors discussed this event with various licensed operators

and noticed an attitude that a dilution to recover from an

unplanned boration was not considered significant and did not

require the establishment of containment integrity.

The

licensee management expressed concern over this attitude and was

initiating actions to reinstruct all licensed operators as the

.,**

5

inspection period ended.

This failure to follow instructions,

which also resulted in a violation of TS 3.8.A.6, is a second

example of Violation 280, 281/89-31-01.

b.

Weekly Inspections

The inspectofs conducted weekly inspections in the following areas:

verification of operability of selected ESF

systems by

valve

alignment, breaker positions, condition of equipment or component,

and operability of instrumentation and support jtems essential to-

system actuation or performance.

Plant tours were conducted which

included observation of* general plant/equipment conditions, fire

protection and preventative measures, control of activities in

progress, radiation protection controls, physical security controls,

plant housekeeping conditions/cleanliness, and missile hazards.

The

inspectors routinely monitored the temperature of the AFW pump

discharge piping to ensure increases in temperature were being

properly monitored and evaluated by the licensee.

c.

Biweekly Inspections

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagouts in effect;

review of sampling program (e.g., primary and secondary coolant

samples, boric acid tank samples, plant liquid and gaseous samples);

observation of control room shift turnover; review of implementation

of the plant problem identification system; verification of selected

portions of containment isolation lineups; and verification that

notices to workers are posted as required by 10 CFR 19.

d.

Other Inspection Activities

Inspections included areas in the Units 1 and 2 cable vaults, vital

battery rooms, steam safeguards areas, emergency switchgear rooms,

diesel generator rooms, control room, auxiliary building, Unit 2

containment, cable penetration areas, independent spent fuer storage

facility, low-level intake structure, and the safeguards valve pit

and pump pit areas. RCS 1-eak rates were reviewed to ensure that

detected or suspected leakage from

the system was

recorded,

investigated, and evaluated; and that appropriate actions were taken,

if required.

The inspectors routinely* independently calculated RCS

leak rates using the ~RC Independent Measurements Leak Rate Program

(RCSLK9).

On a regular basis, RWPs were reviewed and specific work

activ1ties were monitored to assure they were being conducted per the

RWPs.

Selected radiation protection instruments were periodically-

checked, and equipment operability and ca 1 i brat ion frequency were

verified .

6 -

e.

Physical Security Program Inspections

In the course of monthly activities, the inspectors included a review

of the li.censee's physical security program.

The performance of

various shifts of the security force was observed in the conduct of

daily activities to include: protected and vital areas access*

controls;

searching of personnel, packages and vehicles; badge

issuance and retrieval; escorting of visitors; and patrols and

compensatory posts.

Within the areas inspected, one violation was identified.

4.

Maintenance Inspections (62703 & 42700) -

During the reporting period, the inspectors reviewed maintenance '

activities to

assure

compliance with

the appropriate procedures.

Inspection areas included the following:

a.

Modification to Service Water Piping to MER3

During this i-nspection period, the licensee continued with modifica-

tions to the service-water piping which supplies flow to the safety-

related components (MCR chillers and charging pump SW pumps) in MER 3

and 4.

This modification was being accomplished in accordance with

Design Change 87-34-3, Servic~ Water Pipe Replacement /Surr~/1 & 2.

The inspector noted the periods in which the licensee entered TS LCOs

in order to complete required connections to portions of the existing

system.

In order to accomplish these hookups, the licensee had

installed and placed in service a temporary SW supply line, as

allowed by TS Amendment No. 134 dated October 5, 1989.

This LCO was

entered twice in accordance with the modification schedule.

The inspectors reviewed the licensee work package for this modifica-

tion, frequently visited the jobsite to observe work in progress and

specifically reviewed the TS requirements associated with LCO entry.

The licensee had prepared special procedures to insure that LCO entry

was well coordinated and that all actions required by the TS was

implemented as necessary. *No discrep~ncies were noted.

b.

Repair of Unit 2 Pressurizer Safety Valve (2-SV-2251B)

On October 11,* 1989, at 2230 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.48515e-4 months <br />, Surry Unit 2 received a

pressurizer safety valve open alarm while.operating at 100% power.

The

CR operators *noted that the primary relief tank level and

pressure were increasing.

The alarm cleared approximately I-hour

later but then came back in several times during the next hour.

The

iicensee commenced an orderly shutdown of the unit at 0355 hours0.00411 days <br />0.0986 hours <br />5.869709e-4 weeks <br />1.350775e-4 months <br /> on

  • -**

7

October 12.

All three pressurizer safety valves were subsequently

removed and transported to the Westinghouse Western Service Center

for testing and repair.

Surry has three (3) Crosby style 6xK2x6 self-actuated relief valves

that are mounted downstream of hpt loop seals (water) on top of the

pressurizer. A recent design change added mirrored insulation to the

loop seals in order to maintain the seals at an elevated temperature.

The seals have thermocouples installed that facilitate a local

temperature reading of the seal piping.

In addition, safety valve

tailpipe temperature and acoustic monitors are provided to alert the

CR of safety valve problems.

A review of the data following the

ab_ove event indicated that the B safety valve (2-RC-SV-2551B) was

leaking.

It was also noted that the inlet flange studs on the B

valve were discolored blue, indicating an abnormally high pipe

temperature.

The as-found test results of the three valves substantiates the

conclusion that" valve piping temperature effects the safety valve

lift setpoint as stated by Westinghouse in their informal memorandum

to Virginia

Power

on

October 12,

1989.

The

licensee

has

traditionally used steam with no loop seal (water seal) to set and/or

verify the valve lift setpoints.

The as-found data supports the conclusion that this technique results

in an actual lift setpoint, after installation with a loop seal,

somewhat higher than the plus or minus one percent allowed by the TS.

The worst case data from the three unit 2 safety valves are given

below.

The numbers in parenthesis represent the amount the setpoint

was above the allowable 2485 psig.

Vave

2-RC-2551A

2-RC-25518

2-RC-2551C

As-Found/Water Seal

2566 psig (3.25%)

2563.8 psig (3.2%)

2589 psig (4.2%)

As-Found/Steam

2433 psig

2462 psig

2497 psig

The inspectors closely followed the issues concerning safety valve

performance both at Surry and industry-wide as they developed.

The

licensee responded appropriately regarding the generic increased

setpoint concern by removing all three valves from Unit 2 and testing

the setpoints in an as-installed condition (with loop seal).

A

conference call on October 19, 1989, between the licensee and the NRC

identified that the as-found setpoints were below the 2635 psig

maximum pressure (105.4% of nominal) that analysis determined was

necessary to maintain the peak RCS pressure below the 110% design

overpressure limit.

The results did indicate, however, that the

actual lift setpo1nts were above the 2485 plus or minus 6ne percent

psig allowed by TS.

8

The licensee submitted the safety valve test results for Unit 2 with

a Justification for .Continued Operation for Unit 1 in a request for

Discretionary Enforcement dated October 23, 1989.

This letter

acknowledged that the potential exists for the Unit 1 valves to

exceed the one percent TS to 1 erance . and requested Di scret i ona ry

Enforcement until December l, 1989, to allow time for resolution of

this generic issue.

A separate issue developed from the generic concern above was the

premature. leaking that occurred on October 11.

The inspectors

discussed with the licensee the concern that the temperature of the

loop seal can affect the lift setpoint.

The drain valve under the B

valve loop seal (2~RC-136) was found to have a broken packing flange.

The licensee has postulated that the loop seal inventory could have

been lost through the broken drain valve and therefore allowed the

inlet piping temperature to increase to a point that safety valve

leakage occurred.

The inspectors reviewed all work. involving the

above valves.

No discrepancies were identified.

c.

Safety Injection Check Valve Repair

The inspectors reviewed the repair of SI* check valve 2-SI-79 as

authorized by work order 3800086812 and in accordance with procedure

MCM-0417-1.

The six inch Velan check valve exhibited excessive

backleakage into the cold leg SI piping.

This same valve was

disassembled and overhauled during the previous Unit 2 outage.

Inspection of the valve internals indicated severe damage to the

body/bonnet gasket which appears to have been caused by an incorrect

size gasket and/or improper gasket alignment with respect to the

valve body.

The bonnet sheared a portion of the

11 Flexitallicll gasket

which caused the spiral ribbon construction of the gasket to unwind.

EWR 89~684 was issued detailing the problems and d~termined that the

four to six feet of 304 stainless steel ribbon and the carbon filler

material that was removed from the valve had prevented the valve

disc from fully seating.

The valve was reassembled using the correct

gasket and returned to operations.

The inspector reviewed the

documentation and discussed with the* station staff the following

con c 1 u s i on s-:

An incorrect size gasket had been installed during the previous

valve maintenance.

Correct replacement parts have not been maintained in spare

parts inventory.

Adherence to an established foreign material exclusion program

was evident .

9

Adherence to procedure was evident.

The procedure had been

upgraded to the new format with clear, concise instructions and

useful diagrams.

The licensee adequately evaluated the implications of the above

failure on the. remaining check valves that had been worked.

The licensee was continuing an investigation of the above failure as

. the inspection period ended.

Plans were being made to open two

additional check valves that records indicate may have a gasket

material problem.

This item is identified as an unresolved item

(280, 281/89-31-02) pending final determination of the cause of the

check valve maierial discrepancies.

Within the areas inspected, no violations were identified.

5.

Surveillance Inspections

(61726 & 42700)

During the reporting period, the inspectors reviewed various

surveillance activities to assure compliance with

the appropriate

procedures as follows:

Test prerequisites were met.

Tests *were performed in accordance with approved procedures.

Test procedures appeared to perform their intended function.

Adequate coordination existed among pe~sonnel involved in the test.

Test data was properly collected and recorded.

Inspection areas included the following:

a.

Heat Tracing

b.

On October 11, 1989, selected portions bf periodic test l-PT-27H,

Heat Tracing (Panels 2Al, Bl, and 5-Thermon and Strip Heaters), were

witnessed.

The

inspector observed the recording of amperage,

voltage, and temperature niea surements of several channels. in panel

2Bl.

The test procedure was reviewed to ensure that initial

conditions and test steps had been performed.

No discrepancies were

noted.

Safety Injection Control Isolation Logic

On October 13, 1989, selected portions of periodic test l-PT-8.3A,

Safety Injection and

Feedwater Control

Isolation

Logic,

were

witnessed.

The .inspector observed the pretest briefing, the

determination of the condition (energized or not) of certain relays

10

on

both train A and train B, and the activation of -certain

annunciators in Unit 1 CR when cert~in test switches were activated

in the relay cabinets. The procedur~ was reviewed and the inspector

observed the signing and accomplishment of certain steps during the

testing.

No discrepancies were noted.

Within the areas inspected, no violations or deviations were

identified.

6.

Information Meetings with Local Officials

(94600)

On October 26 and 27, 1989, the Senior Resident Inspector, accompanied by

the Section Chief from the Region II office responsible for the -Virginia

Power plants, conducted meetings with local officials in the surrounding

counties and cities. The counties visited included York, Surry and James

City County. The city visited was Newport News.

The meetings were held to

update the officials on the current NRC organization, provide.appropriate

business telephone numbers and points of contact, and to discuss the

status of Surry Power Station and related community concerns with the

local officials. The meetings were held with appropriate people including

the 1 oca 1 government coordinators, county -administrators, and other

government offic'ial s.

The meetings were constructive with no major

concerns identified. The inspectors also left a standing invitation for

additional meetings with interested parties and/or city/county officials

to discuss matters of mutual interest.

7.

Licensee Event Report Review

(92700)

The inspectors reviewed the LER's listed below to ascertain whether NRC

reporting requirements were being met and to determine appropriateness of

the corrective actions. The inspector's review also included followup on

. implementation of corrective action and review of licensee documentation

that all required corrective actions were complete.

LERs that identify violations of regulations and that meet the criteria of

10 CFR, Part*2, Appendix C,Section V shall be identified.as NCV in the

following closeout paragraphs.

NCVs are considered first-time occurrence

violations which meet the* NRC* Enforcemen-t Policy for exemption from

_ issuance of a Notice of Violation.

These items are identified to allow

for proper evaluations of corrective actions in the event that similar

events occur in the future .

.

(Closed) LER 280/89-01, Unplanned Auto Start of No. 3 EOG Due to Failed

Diode.

The issue involved an automatic start of the subject EOG due .to a

failed diode in the engine control circuit.

Corrective action included

replacement of the diode and proper testing of the- engine control circuit

after repairs were made.

This LER is closed.

(Closed) LER 280/89-03, Degraded IRSP Motor Power Feeder Cables and Motor

Leads.

The issue involved identification of damage to the subject pump

11

motor cables during reinstallation of one of the pump motors.

Corrective

actions included shipping the motors to the vendors* for corrective

actions.

This issue was inspected by region based inspectors and was

addressed in NRC Inspection Report 280, 281/89-03.

This LER is closed.

(Closed) LER 280/89-04, Cable Tray Covers Not Properly Installed for

Compliance with 10 CFR 50, Appendix R.

The issue involved the identifica-

tion of: a condition where cable tray cover installation was not in

compliance with Appendix R commitments.

This issue was ins-pected by

region based inspectors and was addressed in NRC Inspection Report 280,

281/89-12.

This LER is closed.

(Closed) LER 280/89-05, Auto Start of No. 1 and No. 3 EDGs Upon Loss ~f F

Transfer Bus.

The issue involved the subject ESF actuations due to the

failure of a 4160 volt breaker to close.

Correct"ive actions inclu_ded

refurbishment of all 4160 volt safety-related circuit breakers prior to

unit restart.

This issue was closely followed by both region based and

resident inspectors and is addressed in NRC Inspection Reports

280,

281/89-06 and 89-12.

This LER is closed.

(Closed)

LER 280/89-06, Spu*rious Safety Injection Due to Inadequate

Special Test Procedure.

The issue involved various ESF actuations which

occurred during testing due to an inadequate procedure.

CorrectiVe action

_included

changing

the test procedure

to

prevent recurrence

and

satisfactorily completing the test.

This issue was addressed in NRC

Inspection Report 280, 281/89-06.

This LER is closed.

(Closed)

LER 280/89-07,

Failure to Initiate Alternate Radiological

Sampling of Ventilation Vent Due to Personnel Error.

The issue tnvolv~~ a

failure to initiate alternate sampling of ventilation flowpath within

one-hour after loss of normal sampling as required by TS 3.7-5(b).

The

alternate sampling was not initiated because operators thought that they

could restore normal *sampling within the one-hour period.

Corrective

actions included reinstruction of all operati_ons and health physics

personnel.

The inspecto.r reviewed the LER and corrective actions.

This

issue is identified as a NCV 280/89-31-03 for failure to commence

alternate sampling in accordance with TS.

This LER is closed.

(Closed)

LER 280/89-08, A and B Inside Recirculation Spray Pumps

Inoperable Due to Replicator Shaft Sleeves.

The issue involved identifica-

tion of replicator parts which had been installed in several safety-

related pumps.

Corrective actions included purchase order review to

identify the scope of the problem and replacement of all identified

replicas in safety-related applications. This issue was closely monitored

by the resident inspectors and was addressed in NRC Inspection Reports

280, 281/88-51, 89-06, 89-13, and 89-17.

This LER is closed,

(Closed) LER 280/89-09, Inadvertent Isolation of Component Cooling Watef

to Operating RHR Heat Exchanger Due to Inadequate Awareness of System

12

Configuration.

The issue involved improper alignment of the subject heat

exchanger due to operator error. This issue was closely monitored by the

resident inspectors and was addressed in NRC Inspection Report * 280,

281/89-08.

This LER is closed.

(Closed)

LER 280/89-10, Lockout of No.2 Auto-tie Transformer Due to

Failure of Lighting Arrestor and Subsequent De-energization of lH and 2J

Emergency Buses.

The issue involved the subject failure and resultant ESF

actuations due to undervoltage conditions sensed on emergertcy buses.

The

event evaluation was closely monitored by the residents and was addressed

in NRC Inspection Report 280, 281/89-13.

This LER is closed.

(Closed) LER 280/89-11, TS Required Fire Watch* Patrol Not Maintained While

Containment *smoke Detectors Were Inoperable.

The issue involved a failure

to have a continuous firewatch patrol in the Unit 1 containment when smoke

detectors were inoperable. The firewatch exited the containment without

proper relief.

The failure to maintain .a required firewatch patrol was

attributed to poor communications.

The inspector reviewed the LER.

This

~ssue is identified as a NCV 280/89-31-04 for failure to maintain required

firewatches as required by TS.

This LER is closed.

(Closed) LER 280/89-12, Reanalysis of CR Dose Following OBA With Manual

Discharge of Air Bbttles Results in Exceeding GDC-19 Limits.

The issue

involved the subject reanalysis and the resulting conclusion that

automatic initiation of an air bottle dump was required to meet the new

analysis. Corrective action included redesign and installation of an auto

air bottle dump signal on SI initiation. The inspectors reviewed the LER

and verified that the auto-dump modification was implemented and tested

satisfactorily.

This LER is closed.

(Closed) LER 280/89-13, Lockout of 230 KV Bus No.3 Due to Personnel Error

and Subsequent De-energization of lH and 2J Emergency Buses.

The issue

involved loss of one source of offsite power to personnel error in the

switchyard.

Corrective actions included restoration of offsite power and

the placement of stricter controls-on workers in the switchyard.

The

resident inspectors monitored the licensee evaluation and reviewed the

operator actions during the event.

This effort was addressed in NRC

Inspection Report 280, 281/89-13.

This LER is clos~d.

(Closed) LER 280/89-14, Main Control Room Ve~tilation Isolation (Unplanned

ESF Actuation) Due to a Spurious Chlorine Gas Detector Alarm.

The issue

involved an ESF actuation due to a spurious signal from a detector which

is no longer required.

Corrective action included reioval of the detector

from service.

The inspector reviewed the LER and verified that chlorine

monitoring was no longer required by TS.

This LER is closed.

(Closed) LER 280/89-15, Setpoints Required for Auto Start of Fire Pumps Do

Not Correspond to TS Requirements.

The issue i nvo 1 ved auto start

setpoi nts for fire pumps that .were 1 ower than those specified in TS.

Corrective action included changing the auto start setpoint to comply with

the TS.

The inspector reviewed the LER.

This LER is closed.

.-.

13

(Closed) LER 280/89-16, Inadvertent Positive Reactivity Additton by Boron

Dilution Wi~hout Containment Integrity Intact Due to Leaking RCP Standpipe

Makeup Valve.

The issue involved an inleakage of water into the RCS which

slowly decreased boron

concentration.

Corrective action

included

identification of the leak point and corrective maintenance to the leaking

valve.

The inspector reviewed the LER and also the operator actions

during the leakage determination timeframe.

This LER is closed.

(Closed) LER 280/89-17, Failure to Sample CC Heat Exchangers Within 12

Hours Due to Personne 1 Error.

The issue i nvo 1 ved a vi o 1 at ion of TS

required sampling periodicity due to personnel error. The individual who

failed to properly evaluate the samples was reinstructed on TS require-

ments;

The inspector reviewed the LER.

This issue is identified as a NCV

280/89-31-05 fo*r fa i 1 ure to sample required systems in accordance with TS.

This LER is closed.

(Closed) LER 280/89-18, Failure to Obtain the WGDT Sample Within TS

Required 24 Hour Frequency Due to Personnel Error.

The issue involved a

violation of TS required sampling periodicity due to personnel error. The

error occurred due to an operator misreading the log for the time requi~ed

to take the sample.

Corrective actions included additional written

guidance to operators to insure that samples are obtained within the

required TS times.

The inspector reviewed the LER.

This issue i-s

identified as NCV 280/89-31-06 for failure to take a TS required sample .

This LER is closed.

(Closed) LER 280/89-19, Unplanned ESF Component Actuation (Auxiliary Vent

Fans Tripped Due to Test Rig Design).

The issue involved an inadvertent

ESF actuation due to a test rig that was

inadequately designed.

Corrective action included removal of the test rig and restarting of

required fans.

Additional actions included discussions with personnel

responsible for preparation and revision of special tests. The inspector

reviewed the LER.

This LER is ciosed.

(Closed) LER 280/89-20, Potentially Inoperable Reactor Protection Channel

Due to High Leakage Currents in Cable While in Harsh Containment.

The.

issue involved identification of the subject concern during review of a

similar problem at the Nor-th Al'lna Station.-

Corrective actions included

replacement of the suspect cables.

The resident inspectors monitored the

licensee 1 s evaluation and corrective actions for this issue. This LER is

closed.

(Closed) LER 280/89-21, Contra 1 /Re 1 ay Room Chi 11 ers I noperab 1 e Due to

Inadequate Service Water Flow.

The issue involved the tripping of the

operable control room chiller due to high condenser discharge pressure.

Corrective action

included restarting of the chiller.

Additional

corrective actions are underway to upgrade the capacity of service water

flow to the chillers.

The inspector reviewed the LER, the licensee

1 s

,.

14

corrective action, and monitored the Service Water System upgrades that

affect this area.

This LER is closed.

(Closed)

LER 281/88-09,

Inoperable

Component

Cooling

Water

Heat

Exchangers Due* to Vac~um Priming Seismic Restraints Not Installed.

The

issue involved impr*oper supporting of vacuum priming line due to the

missing restraints.

Corrective action included reinstallation of the

supports.

This issue was discussed in

NRC

Inspection Report 280,

281/88-14.

This LER is closed.

(Closed)

LER 281/88-11, Control/Relay Room Chiller Inoperable Due to

Fouled Fi 1 ter-Dryer Element.

The issue i nvo 1 ved the remova 1 of the

operating chiller from service in order to replace the filter/dryer

elements.

One of the other chillers was inoperable due to being tagged

out for maintenance.

Corrective action included replacement of the

elements and returning the chiller to service.

Tbe inspector reviewed the

LER and the licensee's actions.

This LER is closed.

(Closed) LER 281/88-13,. Reactor Trip Breakers Opened Due to Inadequate

Procedure.

The issue involved an ESF actuation of reactor trip breakers

due to improper control of power supplies to simulated signals for S/G

level.

No immediate corrective action was required due to the reactor

being already shutdown and in a rnainten9-nce condition.

Additional

instruction was provided to personnel with regards to the need for clarity

when deviating procedures.

The inspector reviewed the LER.

This LER is

closed.

(Closed)

LER 281/88-14, Lifting of Power Operated Relief Valve Due to

Procedural Inadequacy.

The issue involved the lifti*ng and reclosing of a

PORV when an RCP was started.

The PORV 1 i fted due to the fa i 1 ure to

identify proper starting pressure when starting an RCP.

The inspector

reviewed the LER.

This issue is identified as NCV 281/89-31-07 for

failure to provide adequate procedure when starting RCPs for RCS venting.

This LER is closed.

(Closed)

LER 281/88-15, . Commencement of Shutdown Due to Rod Centro 1

Circuitry Failure.

The issue involved commencement of a TS

required

shutdown due to a rod control LCO.

After the shutdo~n was commenced, the

rod control problem* was corrected and properly tested.

Unit 2 then *

resumed normal operation.

The inspector reviewed the LER.

This LER is

closed.

(Closed) LER 281/88-18, * B S/G Stearn Flow Channel III Failed High Due To

Fail,ed Multiplier/Divider.

The issue involved a failure of the subject

component requiring that the unit enter TS 3.0.1.

Corrective action

included placing affected protection bistables in trip and replacing the

failed component.

After satisfactory testing of the replaced component,

the protection circuitry was returned to normal alignment and Unit 2

exited TS 3.0.1.

The inspector reviewed the LER.

This LER is closed .

15

(Closed)

LER 281/88-19, Unplanned Actuation of ESF Component, Inside

Containment Slowdown Trip Valve.

The issue involved the closure of the

inside containment A S/G blowdown isolation valve for an unknow~ reason.

Corrective action included a containment entry to correct the operability

condition.

After resetting of the high fl ow so 1 enoi d in containment,

proper valve operation was obtained and verified. The inspector reviewed

the LER.

This LER is closed.

(Closed) LER 281/88-21, B LHSI Pump Not Tested Within Required 8-Hour

Interval Due to Inoperable Test Equipment.

The issue involved the

required testing of the subject pump while the redundant pump was in a

maintenance condition.-

The test was not accomplished in the specified

timeframe due to equipment problems.

The inspector reviewed the LER.

This LER is closed.

(Closed) LER 281/88-22, Reactor T~ip by Turbine Trip Due to Inadequate

Procedure, Faulty Valve Position Limiter Indication and Response.

The

issue involved an unplanned reactor trip due to turbine trip.

No

immediate corrective actions were required other than to stabilize the

plant after the trip in accordance with procedure. This issue was closely

followed by the resident inspectors and was addressed in NRC Inspection

Report 280, 281/88-36.

This LER is closed.

(Closed)

LER 281/88-23, Inadvertent ESF Component Actuation Due to

Personnel Error.

The issue involved inadvertent closure of three contain-

ment trip valves associated with radiation monitoring and sampling due to

an electrician incorrectly li'fting leads to support maintenance activities

on another trip valve.

Corrective action included properly relanding of

the lead and appropriate testing of the affected components for

operability.

The inspector reviewed the LER.

This issue is identified ~s

an NCV (281/89-31-08) for failure to provide adequate instructions (proper

identification of leads to be lifted) for a maintenance activity which

affected operability of safety-related components.

This LER is closed.

(Closed) LER 281/89-01,

Loss of Containment Integrity During Refueling

Operations Due to Loss of Administrative Control.

The issue involved the

improper installation of a blank flange on one of the

11A

11 SG safety valve

openings

during refueling operations.

When

discovired,

refueling

evolutions were stopped and a proper blank was inst~lled.

In addition,

the b 1 an ks _ were tagged to prevent unauthori z'ed remova 1.

The in specter

reviewed the LER.

This issue is identified as an NCV (281/89-31-09) for

failure to provide for containment integrity as required* by TS during

refueling operations.

This LER is closed.

(Closed) LER 281/89-02,

Unplanned Auto-Start of EOG During Performance of

PT-22.6B Due to Previously Unrecognized EOG Control Circuit Logic.

The

issue involved the subject ESF actuation due to the failure to reset

appropriate relays prior to placing the EOG selector switches in AUTO.

This issue was discussed in NRC Inspection Report 280, 281/89-17.

In that

8.

16

  • report, this event and a similar earlier event were identified as a

weakness o: past corrective action problems.

No further enforcement

action is required.

This LER is closed.

Exit Interview*

The inspection scope and findings were summarized on October 31, 1989,

with those individuals identified by an asterisk in paragraph 1.

The

following new items were identified by the inspectors during this exit:

One violation with two examples was identified (paragraph 3.a) for failure

to follow procedures and/or instructions (281/89-31-01).

One unresolved item was identified (paragraph 4.c) regarding followup on

material problems associated with safety-related check valve maintenance

. (280, 281/89-31-02).

One non-cited violation was identified (paragraph 7) for falure to

initiate alternate radiological sampling of ventilation vents as required

by TS (280/89-31-03).

One non-cited violation was identified (paragraph 7) for failure to

maintain a TS required fire watch patrol while containment smoke detectors

were inoperable (280/89-31-04).

One non-cited violation was identified (paragraph 7) for failure to sampl*e

the component cooling heat exchangers within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> as required by TS

(280/89-31-05).

One non-cited violation was identified (paragraph 7) for failure to take a

TS required sample (280/89-31-06).

One

non-cited violation was

identified (paragraph 7) regarding an

inadequate procedure that resulted with the lifting of a power operated

relief valve (281/89-31-07).

One non-cited violation was identified (paragraph 7) for failure to

provide adequate instructions that resulted in an ESF component actuation

( 281/89-31-08). *

One non-cited violation was identified (paragraph 7) for failure to

provide con~ainment *integrity-as required by

TS

during refueling

opirations (281/89-31-09).

The licensee acknowledged the inspection findings with no dissenting comments.

The licensee did not identify as proprietary any of the materials provided to

or reviewed by the i_nspectors during this inspection.

. '

' '

17

9.

INDEX OF INITIALISMS

AFW

AUXILIARY FEEDWATER

ANSI

AMERICAN NATIONAL STANDARDS INSTITUTE

AP

.ABNORMAL OPERATING PROCEDURE

CAD

COMPUTER AIDED DESIGN

CAL

CONFIRMATION OF ACTION LETTER

CC

COMPONENT COOLING

CCW

COMPONENT COOLING WATER

  • CFR

CODE OF FEDERAL REGULATIONS

CLS

CONSEQUENCE LIMITING SAFEGUARD

CRO

. CONTROL ROOM OPERATOR

CW

CIRCULATING WATER

OBA

DESIGN BASES ACCIDENT

DPI

DELTA PRESSURE INDICATORS

DR

DEVIATION REPORT

EOG

EMERGENCY DIESEL GENERATOR

EHC

ELECTRO-HYDRAULIC CONTROL

EMP

ELECTRICAL MAINTENANCE PROCEDURE

ESF

ENGINEERED SAFETY FEATURE

ESW

EMERGENCY SERVICE WATER

EWR

ENGINEERING WORK REQUEST

GDC

GENERAL DESIGN CRITERIA

GPM

GALLONS PER MINUTE

HP

HEALTH PHYSICS

HX

HEAT EXCHANGER

HPSI

HIGH PRESSURE SAFETY INJECTION

IA

INSTRUMENT AIR

IE

INSPECTION AND ENFORCEMENT

IFI

INSPECTOR FOLLOWUP ITEM

IRSP

INSIDE RECIRCULATION SPRAY PUMP

IDER

INDEPENDENT OFFSITE EVALUATION REVIEW

IRPI

INDIVIDUAL ROD POSITION INDICATION

ISI

INSERVICE INSPECTION

KV

KILOVOLT

LER

LICENSEE EVENT REPORT

LCD

LIMITING CONDITIONS OF OPERATION

LHSI

LOW HEAD SAFETY INJECTION

LOCA

LOSS OF COOLANT ACCIDENT

LOOP

LOSS OF OFFSITE POWER

MER

MECHANICAL EQUIPMENT ROOM

MDV

MOTOR OPERATED VALVE

'MCR

MAIN CONTROL ROOM

NCV

NON-CITED VIOLATION

NRC

NUCLEAR REGULATORY COMMISSION

NRR

NUCLEAR REACTOR REGULATION

OP

OPERATING PROCEDURE

ORS

OUTSIDE RECIRCULATION SPRAY

. ,.

' . ,,

..

ti

, .,-

'I

PCV

PI

PM

PORV

PPM

PSI

PSIG

PT

QA

QC

RAI

RCP

RCS

RHR

RG

RO *

RPS

RSS

RWP

RWST

SCFM

SER

SG

SI

SNSOC

sov

SPOS

SRO

SW

TAVG

TI

TS

TSC

UFSAR

URI

UV

vs

WGOT

18

PNEUMATIC CONTROL VALVE

PRESSURE INDICATOR

PREVENTATIVE MAINTENANCE

.POWER AND OPERATED RELIEF VALVE

PARTS PER MILLION

POUNDS PER SQUARE INCH

POUNDS PER SQUARE INCH GAUGE

PERIODIC TEST

QUALITY ASSURANCE

QUALITY CONTROL

RESIDENT ACTION ITEM

REACTOR COOLANT PUMP .

REACTOR COOLANT SYSTEM

RESIDUAL HEAT REMOVAL

REGULATORY GUIDES

REACTOR OPERATOR.

REACTOR PROTECTION SYSTEM

RECIRCULATION SPRAY SYSTEM

RADIATION WORK PERMIT

REFUELING WATER STORAGE TANK

STANDARD CUBIC FEET PER MINUTE

SAFETY EVALUATION REPORT

STEAM GENERATOR

SAFETY INJECTION

STATION NUCLEAR SAFETY ANO OPERATING COMMITTEE

SOLENOID OPERATED VALVE

SAFETY PARAMETER DISPLAY SYSTEM

SENIOR REACTOR OPERATOR

SERVICE WATER

AVERAGE TEMPERATURE OF RCS

TEMPORARY INSTRUCTION

TECHNICAL SPECIFICATIONS

TECHNICAL SUPPORT CENTER

UPDATED FINAL SAFETY ANALYSIS REPORT

UNRESOLVED ITEM

UNDER VOLTAGE

VENTILATION SYSTEM

WASTE GAS OE{AY TANK