ML18152A225

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Insp Repts 50-280/89-13 & 50-281/89-13 on 890402-29.No Violations or Deviations Noted.Major Areas Inspected:Plant Operations,Plant Maint,Plant Surveillance,Ler Review & Followup on Inspector Identified Items
ML18152A225
Person / Time
Site: Surry  Dominion icon.png
Issue date: 05/30/1989
From: Fredrickson P, Holland W, Larry Nicholson, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A226 List:
References
50-280-89-13, 50-281-89-13, NUDOCS 8906190159
Download: ML18152A225 (19)


See also: IR 05000280/1989013

Text

.*.

Report Nos.:

50-280/89-13 and 50-281/89-13

Licensee:

Virginia Electric and Power Company

Glen Allen, VA

23060

Docket Nos.:

50-280 and 50-281

Facility Name:

Surry 1 and 2

License Nos.:

DPR-32 and DPR-37

Inspection Conducted:

April 2 - 29, 1989.

Inspectors: ~~

?'S(C

W. E. Holland, Seniorsidentlnspector

~~&~<<?

L. E. Nichols~Resident'nspector

Approved by:

V,,,.

~tJ,1~

a/

J. W. York, Resident Insp~

~~~-/b;

P. E. Fredrickson, Ac

ng Branch Chief

Division of Reactor

jects

SUMMARY

Scope:

§-2.1£-.P7

Date Signed

S*-..26-%7

Date Signed

s-2<!.'-57/

Date Signed

S"$cJ-8:9:

Date Signed

This routine resident inspection was conducted on site in the areas of plant

operations, plant maintenance, plant surveillance, licensee event report

review, and followup on inspector identified items.

A special evaluation of

the licensee's program which was used to walk down selected systems prior to

unit(s) restart was documented in the last three resident reports and this

inspection effort continues in this inspection report.

Certain tours were conducted on backshifts or weekends.

Backshift or weekend

tours were conducted on April 3, 9, 15, 23, and 26, 1989.

Results:

During this inspection period, no violations were identified. The licensee's

ongoing ope rational readiness p_rogram appears to be addressing a 11 necessary

items for Un:t 1 restart .

890~190159

PDR

ADOCK

G

890530

05000280

PNU

1.

Persons Contacted

Licensee Employees

REPORT DETAILS

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer
  • R. Blount, Superintendent of Technical Services

D. Christian, Assistant Station Manager

D. Erickson, Superintendent of Health Physics

  • E. Grecheck, Assistant Station Manager

M. Kansler, Station Manager

J. McCarthy, Superintendent of Operations

  • G. Miller, Licensing Coordinator, Surry

J. Ogren, Superintendent of Maintenance

A. Price, Site Quality Assurance Manager

  • T. Sowers, Superintendent of Engineering

Other licensee employees contacted included control room operators, shift

technical advisors, shift supervisors and other plant personnel.

  • Attended exit int.erview.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

Units 1 and 2 began the reporting period in cold shutdown.

The uni.ts

remained in cold shutdown for the duration of the inspection period while

substantial operational reviews and maintenance activities were being

conducted.

3.

Operational Safety Verification (71707)

a.

Daily Inspections

The inspectors conducted daily inspections in the following areas:

control room staffing, access, and operator behavior; operator

adherence to approved procedures, techni ca 1 speci fi cat i ans, and

limiting conditions for operations; examination of panels containing

instrumentation and other reactor protection system e 1 ements to

determine that required channels are operable; and review of control

room operator logs, operating orders, plant deviation reports, tagout

logs, jumper logs, and tags on components to verify compliance with

approved procedures .

. )

b.

2

Weekly Inspections

The inspectors conducted weekly inspections in the following areas:

verification of operability of selected ESF systems by valve

alignment, breaker positions, condition of equipment or components,

and operability of instrumentation and support items essential to

system actuation or performance. Plant tours were

conducted which

included observation of general plant/equipment conditions, fire

protection and preventative measures, control of activities in

progress, radiation protection controls, physical security controls,

plant housekeeping conditions/cleanliness, and missi"h:! hazards.

The

inspectors routinely monitored the temperature of the auxiliary

feedwater pump discharge piping to ensure steam binding was

prevented.

c.

Biweekly Inspections

The inspectors conducted biweekly inspections in the following areas:

verification review and walkdown of safety-related tagouts in effect;

review of sampling program (e.g., primary and secondary coolant

samples, boric acid tank samples, plant liquid and gaseous samples);

observation of control room shift turnover; review of implementation

of the plant- problem identification system; verification of selected

portions of containment isolation lineups; and verification that

notices to workers are posted as required by 10 CFR 19.

d.

Areas Inspected

Inspections included areas in the Units 1 and 2 cable vaults, vital

battery rooms, steam safeguards areas, emergency switchgear rooms,

diesel generator rooms, control room, auxiliary building, Unit 1

containment, cable penetration areas, independent spent fuel storage

facility, low level intake structure, and the safeguards valve pit

and pump pit areas. Reactor coolant system leak rates were reviewed

to ensure that detected or suspected leakage from the system was

recorded, investigated, and evaluated; and that appropriate actions

were taken, if required.

The inspectors routinely independently

calculated RCS leak rates using the NRC Independent Measurements Leak

Rate Program (RCSLK9).

On a regular basis, RWPs were reviewed and

specific work activities were monitored to assure they were being

conducted per the RWPs.

Selected radiation protection instruments

were periodically checked, and equipment c*perability and calibration

frequency were verified.

e.

Physical Security Program Inspections

In the course of monthly activities, the inspectors included a review

of the licensee's physical security program.

The performance - of

various shifts of the security force was observed in the conduct of

',

f .

3

daily activities to include: protected and vital areas access

controls; searching of personnel, packages, and vehicles; badge

issuance and retrieval; escorting of visitors; and patrols and

compensatory posts.

Licensee 10 CFR 50.72 Reports

. *(1)

On April 6, 1989, the licensee made a report in accor~ance with

10 CFR 50.72 with regards to loss of the normal power supply to

the

11 F11 bus.

The power loss was caused by a failure in the

switchyard of the 500 KV stepdown transformer -which normally

feeds the

11 F11 bus.

The

11 F

11 bus was supplying normal power to

the Unit 1

11H11 bus and the Unit 2

11J

11 bus ( 4160 volt vi ta 1

buses). Loss of power to the Unit 1 11H11 bus resulted in loss of

power to the running (A) RHR pump for Unit 1. Operators started

the Unit 1

118

11 RHR pump within one minute of the loss of the

11A

11

pump.

RCS temperature did not increase during the time that RHR

cooling was lost.

The No. 1 EOG intentionally was not aligned

to automatically start due to potential vibration problems that

had been identified earlier.

However, after discussion with

station management, the diesel was started and the Unit 1

11H

11

bus was loaded onto the EDG.

Loss of power to the Unit 2

11J

11

bus resulted in an automatic start and load of the No. 3 EOG

onto th*e

11J

11 bus.

RHR was not lost on Unit 2 due to the

operating pump being powered from the Unit 2 11H

11 bus.

During the event, the Unit 1 reactor vessel level, as indicated

by standpipe, was 18.6 feet (approximately 2 to 4 inches above

the reactor ve s se 1 flange).

The Un it was. not in a reduced

inventory condition (3 feet below the vessel flange) as defined

by GL 88-17.

Loss of power to the 11 F

11 bus resulted in loss of

control room indicated standpipe level for the unit. Immediate

operator action was to dispatch an operator into the Unit 1

containment and locally monitor the standpipe level.

No loss of

RCS inventory was experienced during the event.

The licensee

took actions during the next four hours to restore offsite power

to the "F" bus and to transfer emergency busses back to the

11 F11

bus.

In view of the licensee's response to the event, the

inspectors believe that the operators are properly sensitized

to a loss of RHR condition.

(2)

On April 7, 1989, the licensee made a report in accordance with

10 CFR 50.72 as a result of an evaluation of main control room

habitability fo 11 owing a DBA.

The eva 1 uat ion stated that the

accident analysis assumed that the main control room air bottle

system would dump at the same time the OBA occurred. However,

the air bottle system is presently designed to be manually

initiated by the operators.

Using an allowance of ten minutes

for operator action, the licensee determined that a potential

4.

( 3)

4

exists for excessive cumulative radiation exposure to operators

during the 30 days following the accident.

Corrective actions

will include redesign of the actuation system *to allow for

automatic initiation.

On April 13, 1989, the licensee made a report in accordance with

10 CFR 50. 72 with regards to loss of the power supply to the

11 F

11

bus. The power loss was caused by a failure to properly conduct

a test by licensee personnel in the switchyard. The

11 F

11 bus was

supplying normal power to the Unit 1

11H

11 bus and the Unit 2 11J

11

bus (4160 volt vital buses). The No. 1 EOG gene~ator was tagged

out for repairs and was not available to provide emergency power

to the Unit 1 "H" bus.

Loss of power to the Unit 2 "J" bus

resulted in an automatic start and load of the No. 3 EOG on the

11J 11 bus.

RHR flow to both units was maintained throughout the

event with no increase in RCS temperature.

Ouri ng the event, the Unit 1 vessel level was 18. 3 feet

(approximately equal

to the reactor vessel flange), and

therefore the unit was not in a reduced RCS inventory.

Loss of

power to the 11 F11 bus resulted in loss of control room indicated

standpipe level for the unit.

Immediate operator action was to

dispatGh an operator into the Unit 1 containment and locally

monitor the standpipe level.

No loss of RCS inventory was

experienced during the event. The licensee took actions during

the next two hours to restore off site power to the II F" bus and

to transfer emergency busses back to the

11 F11 bus.

( 4)

On April 17, 1989, the 1 i censee made a report to the NRC in

accordance with 10 CFR 50.72 with regards to an ESF actuation of

the main control room ventilation dampers.

The dampers went

closed due to a spurious high spike on the chlorine monitor.

The chlorine monitors are no longer required to be installed at

the station and a design change to remove them is in progress.

The high alarm condition on the monitors was reset, the monitors

were removed from service, and the ventilation dampers were

realigned to their normal position.

Within the areas inspected, no violations were identified.

Operational Readiness Program Review (71710)

The inspectors continued to review the licensee's operational readiness

program as discussed in NRC Inspection Reports 280,281/88-51, 89-06, and

89-08.

This effort is being performed in accordance with EWR 88-584,

System Review For Startup, and includes both field walkdowns and a review

of outstanding issues by the system engineers.

The inspectors are

routinely monitoring all aspects of this readiness program.

The following

details some specific inspection areas and findings from this review .

'.

a.

5

Plant Configuration Confirmation

This portion of the program,

performed in

accordance with

Attachment II to the above EWR,

consisted of the station system

engineers conducting field walkdowns of the systems and noting

discrepancies for resolution. These discrepancies were evaluated to

determine if they should be corrected before unit startup and a

justification was written if deferral was recommended.

The inspector reviewed field change

11T11 to EWR 88-584, dated March 2,

1989, that identified and dispositioned discrepancies-as a result of

system walkdowns against 46 station drawings. This walkdown resulted

in the identification of 35 startup issues that were subsequently

added to the official startup list.

The inspector independently

verified that a 11 startup i terns are being tracked on the master

startup list.

In addition to an overall review of this extensive field change, the

inspector selected the following drawings for a more in-depth audit:

Drawing 11448-FB-46C, Sheet 1 of 2, Emergency Diesel Generator

Air Start System.

Drawing 11448-CBM-728, Sheet 2 of 3, Component Coo 1 i ng Water

System.

Drawing 11448-FM-87A, Sheet 1 of 2, Residual Heat Removal

System.

The inspector continued a review of the walkdowns documented via

field change

11U11 to EWR 88-584, dated April 13, 1989, to verify

adequate identification and disposition of discrepancies.

This

general review included the following:

Drawing 11448-FM-084A, Sheet 2 of 3, Containment Spray System

Drawing 11448-FB-0418, Sheet 1 of 1, Main Control Room Bottled

Air System

Drawing 11448-CBM-0848, Sheet 2 of 2, Outside Recirculation

Spray System

Drawing 11448-CBM-084, Sheet 1 of 2, Inside Recirculation Spray

System

Drawing 11448-CBM-0868, Sheet 2 of 3, Reactor Coolant System

The i11spector verified that each discrepancy identified was prop-erly

dispositioned and an appropriate mechanism was in place to require

adequate corrective actions.

For example, if a problem with the

b.

6

drawing was identified, the inspector verified that the drawing

discrepancies were formally submitted and tracked by the station

drawing update group.

No outstanding concerns were identified during

this inspection effort.

Assessment of Outstanding Issues

This item is covered in Attachment IV to EWR 88-084 and includes a

review of outstanding temporary modifications and/or jumpers, station

deviations, commitment items, outstanding safety-related work orders,

outstanding EWRs and open Type 1, 2, and 3 engineering evaluations.

The system engineers have been tasked with reviewing the above items

pertaining to their system and evaluating if closure of the item

should be performed prior to unit startup. For those items that will

not be closed prior to startup, a justification for not completing

the i tern must be written and approved by the Superintendent of

Technical Services.

(1) The inspector reviewed field change

11S11 to EWR 88-584, dated

March l, 1989, that addressed closed Type 1, 2, and 3

engineering reports.

No startup items were identified by the

licensee during their evaluation of the above field change. The

inspect.or reviewed each item of this field change with the

accompanying supporting documentation and justification and

concurred with the licensee's evaluations.

No

inspector

discrepancies were identified.

(2) The inspector reviewed parts of field changes J, K, P, W, and AA

made to EWR 88-584, that addressed commitments on which action

did not have to be taken before startup of the units.

Field

changes O and Z to EWR 88-584 were reviewed for commitments on

which action was necessary before startup. The following is a

list of 14 commitments that were reviewed on these seven field

changes.

Nine commitments were evaluated as not requiring

resolution before startup, and include:

Commitment No.

89-2089-001

85-5026-020

88-2168-001

Description

Inspect wiring on hydrogen analyzer

quarterly.

IE Bulletin 85-03, MOV Common Mode

Failure--Operators have been trained but

training documents have not been changed.

Batteries for security diesel to be placed

on preventive maintenanc~ program .

Commitment No.

(cont

1d)

88-2355-00i

88-1615-002

88-1377-001

87-0913-001

88-0811-001

.

88-0020-002

7

Description

Procedure deviation for permanent change

to operation procedure 1-0P-33A.

Deviation

is available to be used when this procedure

is required.

Independent verification (with regards to

station

tagging

program)

revision

to

administrative procedure.

-

Technical Specification change request

No. 204, procedure changes for future core

upgrade.

Future Predictive Analysis Group vibration

program

for

monitorjng

safety-related

equipment.

Westinghouse letter that deals with

outage related maintenance .

Pressurizer safety relief setpoint drift

( LER 88-016).

The following five commitments were evaluated by the licensee

as not requiring resolution prior to unit startup:

Commitment No.

88-1374-001

88-0040-003

84-0201-005

84-1152-004

88-0103-004

Description

Technical Specification Change No. 194(8),

heat up and cooldown curves necessary for

startup.

Commitment to NRC to perform full flow

test on inside recirculation spray pumps

during this outage.

Supplementary response to IEB 84-02 which

identifies additional AC energized relays

~hat must be replaced.

Design changes to feed data into the plant

status computer program for containment

spray fl ow, pressurizer heater status, and

pressure transmitters for the accumulators.

Containment spray system walkdown by NRC

resulting in two work requests and two

drawing changes.

~-j

. .

c.

8

A discussion with the liceosee on commitment 88-0020-002

concerning pressurizer safety relief setpoint drift revealed

that a TS change would have to be made. The acceptance band was

+/-1 percent of the pressure range, but the setpoi nt drifted

beyond this range. Calculations appear to show that +/-3 percent

is acceptable and the setpoint could be maintained within this

range.

The inspector's discussion with the licensee questioned

whether this should be a startup item. The licensee's decision

and action in this area will be evaluated prior to restart and

tracked as IFI 280,281/89-13-01, resolution of pressurizer

safety relief setpoint drift.

Inspection and Review Status

The overall status of the engineering work that pertains to Unit 1

(as of April 24, 1989) was as follows:

Wal kdowns

Total Items:

3341

Items Reviewed:

3341

Startup Items:

287

Commitments

Total Items:

1018

Items Reviewed:

770

Startup Items:

143

Closed Type 1

Total Items:

655

Items Reviewed:

556

Startup Items:

16

EWRs

Total Items:

786

Items Reviewed:

370

Startup Items:

85

Open Type 1,2 & 3

Total Items:

261

Items Reviewed:

251

Startup Items:

56

Temp. Mods.

Total Items:

16

Items Reviewed:

16

Startup Items:

5

Within the areas inspected, no violations or deviations were identified.

5.

Maintenance Inspections (62703)

During the reporting period, the inspectors reviewed maintenance

activities to assure compliance with

the appropriate procedures.

Inspection areas included the following:

a.

9

Evaluation of Maintenance/Modification On

The

Low Head Safety

Injection Pump (1-SI-P-lA)

The inspector continued the review of the maintenance activities

associated with replacement of replica parts in the LHSI pump

manufactured by Byron Jackson.

Initial maintenance activities were

discussed in NRC Inspection Report 280,281/89-08.

The licensee is currently working on the Unit 1 low head SI pump

(1-SP-P-lA) in order to replace the replica parts (non-original

equipment manufacturer parts) previously placed in 1'he pumps.

The

inspector reviewed procedure MMP-P-C-SI-090, Removal, Disassembly,

Inspection, Repair, Reassembly, and Reinstallation of Low Head Safety

Injection Pump "Safety Related" dated August 20, 1987. Completed and

signed off portions of this procedure were reviewed.

All of the parts have been removed from the pump well and wiped to

minimize any contamination.

The Byron Jackson -parts have a number

stenci 1 ed on them and if a number is not present it cannot be

verified as a vendor supplied item. The licensee is replacing all of

the carbon steel bearings, because carbon steel rusts and the

identifying number cannot be maintained.

One coupling out of five

did not have an identifying number and will be replaced.

A new

throttle bushing issued by the licensee's warehouse as a category 1

part for this pump was found to be a replicated part. (Station

deviation No. Sl-89-869).

The maintenance group, engineering, and the vendor are having

discussions concerning the difficulty of pressing the bearings back

onto the shafts.

The

bearings require a nine thousandths

interference fit and this causes an installation problem. The

inspectors will continue to monitor this maintenance activity.

b.

Regulator Replacement in Response to NRC IN 88-24

On April 7, the inspector witnessed replacement of the air supply

regulator on containment isolation valve 1-CC-TV-llOC in accordance

with EWR 89-003, Regulator Replacements In Response To NRC IN 88-24.

The subject NRC IN identifies a potential for overpressurization

failures of solenoid valves caused by an air system pressure greater

than the solenoid design maximum operating pressure differential. A

typical AC powered ASCO solenoid valve used at .;urry has an air

maximum operating pressure differential of 45 psi.

However, the

regulators that are used to reduce the instrument air supply down

from approximately 100 psi are not safety-related and their settings

are not controlled in the station setpoint document.

The licensee could not produce documentation that the maximum

supplied air pressure through the regulators is less than the maximum

operating differential operating pressure of the SOV, and therefore

10

stated that the qualification status of the S0Vs is indeterminate.

The corrective actions specified in the above EWR require replacement

of the upstream regulators with new regulators that are designated

safety-related with their setpoint officially controlled in the

station setpoint document.

This changeout is required on 51

containment isolation valves.

The inspector verified that the work

performed in the fie 1 d was being conducted and documented in

accorda~ce with the licensee's approved procedures.

No discrepancies

were identified.

c.

Emergency Diesel Generator No. 1

The inspectors followed the work being performed on the EOG No. 1 to

correct an excessive vibration problem and inspect for damage as a

result of lube oil contamination. Station deviation Sl-89-818, dated

April 6, 1989, identified excessive vibrations during performance of

the EOG monthly surveillance test.

The observed vibrations were

severe enough to cause the operators to perform an emergency shutdown

of the engine. Work Order No. 3800078912 authorized the removal and

retorquing of the EOG foundation anchor bolts.

The

inspector

witnessed portions of the removal and reinstallation of the anchor

nuts and discussed with the maintenance personnel their observation

that the as-found nuts were not tight.

Maintenance Engineering

inspected the as-found condition and recommended installation of jam

nuts.

In addition, plans were being made to inspect and retorque the

foundation bolts on the remaining two EOGs.

The problem of lube oil contamination was addressed in Work Order

No. 3800079985 and involved high zinc concentrations found in the

lube oil during normal sampling and analysis.

The EOG manufacturer

states that a zinc concentration in excess of 10 ppm in the lube oil

could damage the silver coating on the piston wrist pin bearings.

The samples of lube oil from the No.l EOG were determined to contain

15 to 17 ppm zinc. The samples from the remaining two EDGs were well

within specifications.

The inspector witnessed the removal and

inspection of four power assemblies from the EOG No.1 and concur with

both the licensee engineer and vendor representative that no damage

to the bearing surface had occurred.

The licensee was continuing to

search for the source of the zinc with speculation that the thread

lubricant may have been a contributor.

No discrepancies were

i dent ifi ed.

Within the areas inspected, no violations or deviations were identified.

6.

Surveillance Inspections (61726 & 42700)

During the reporting period, the inspectors reviewed various surveillance

activities to assure compliance with the appropriate procedures as

follows:

Test prerequisites were met.

11

Tests were performed in accordance with approved procedures.

Test procedures appeared to perform their intended function.

Adequate coordination existed among personnel involved in the test.

Test data were properly collected and recorded.

Inspection areas included the following:

a.

Emergency Diesel Generator Fuel Oil Supply

On March 4, the inspector witnessed testing of the emergency fuel oil

pump 1-EE-P-lA in accordance with test procedure PT-22.2, Emergency

Fuel Supplies. This pump supplies makeup fuel from the inground fuel

oil tank to the wall tanks in each EOG room.

The test verified that

the pump automatically starts and stops on specific levels in the

wan tank. The inspector discussed the test with station personnel

i nvo 1 ved and noted that severa 1 prob 1 ems were *; dent i fi ed with the

level indication in the wall tanks. The licensee agreed that further

testing of the diesel pumps that transfer fuel from the wall tank to

the skid tank is warranted and stated that a test procedure is being

prepared.

N9 discrepancies were noted.

b.

Functional Test of the Low Head Safety Injection System

The inspector reviewed the recently developed surveillance test,

1-PT-18.3E, Refueling Test Of LHSI Lines To Charging Pumps, which

ensures that an operable flowpath exists from the LHSI pumps to the

charging pumps via the recirculation mode transfer piping.

The

licensee discovered during

an

investigation of a previously

identified valve labeling and power supply problem (ref. IR 280,281/

88-45) that they had never functionally tested the flowpath from the

LHSI

pumps to the charging pumps.

The inspector verified the

fl owpath specified in the test procedure and discussed the test

method with the appropriate system engineer.

No discrepancies were

i dent ifi ed.

c.

Emergency Diesel Generator No. 3

The inspector reviewed periodic test 2-PT-22.3C, Diesel Generator No.

3 Test, dated February 22, 1988.

This survei 11 ance procedure

implements the requirements of TS 4.6.A.1.a that each emergency

diesel generator has a manually initiated start followed by

synchronization with other power sources and assumption of load by

the diesel generator up to 2750 kw.

This is a monthly test and

requires a minimum duration of 30 minutes.

On April 7, the __inspectors attended the pre-briefing with the SROs

and ROs to discuss the running of the No. 3 EOG.

On this date-,

observations were made of the RO taking oil samples, running the air

d.

12

compressor diesel, making valve alignments, recor.ding proper level of

cooling water, etc.

In the main control room, the inspectors

observed the starting and manual synchronization of the diesel with

other power sources. The periodic test instructions suggest running

the diesel for approximately two hours; however, the test was

terminated after approximately 35 minutes because rainwater was

entering the air louvers in the close vicinity of the electronic

control cabinets, with some water hitting the cabinets. The licensee

terminated the test to evaluate any adverse effects the rain might

have on the electronic controls. This condition was identified as a

deviation report in the licensee's corrective actiol't program.

No

discrepancies were observed during the performance of the periodic

test.

Functional Testing of Unit 1 IRS Pumps.

The inspector reviewed the test procedure which was used to conduct

operability testing of the Unit 1 IRS pumps 1-RS-P-lA and 1-RS-P-18.

Test procedure 1-ST-214, Operability of IRS Pumps for Unit 1 was

conducted on 1-RS-P-lA on April 3, 1989, and on 1-RS-P-18 on April 4,

1989.

The

inspector verified that the procedure adequately

documented the conduct and results of the testing.

The procedure

copy that was reviewed had three procedure deviations which were

incorporated* prior to or during testing.

The deviations received

required reviews for 10 CFR 50.59 compliance and were approved by the

station safety committee as required by TS.

No discrepancies were

identified.

Within the areas inspected, no violations or deviations were identified.

7.

Licensee Event Report Review (92700)

The inspectors reviewed the LERs listed below to ascertain whether NRC

reporting requirements were being met and to determine appropriateness of

the corrective actions. The inspector's review also included followup on

implementation of corrective action and review of licensee documentation

that all required corrective actions were complete.

LERs that identify violations of regulations and that meet the criteria of

10 CFR, Part 2, Appendix C,Section V are identified as LIVs in the

following closeout paragraphs.

LIVs are considered first-time occurrence

violations which meet the NRC Enforcement Policy for exemption from

issuance of a Notice of Violation.

These items are identified to allow

for proper evaluations of corrective actions in the event that similar

events occur in the future.

(Closed) LER 280/87-14, Inadequate Review of AFW Supply Following

Safeguards.

The issue involved a scenario in which AFW could be

an operating unit due to a HELB in the main steam valve house.

single active failure of the opposite unit's available AFW pump

HELB in

lost to

With a

a total

13

loss of AFW to the affected unit would result. Corrective action included

immediate administrative control to ensure that when a unit is above 350

degrees/450 psig, two AFW pumps are available from the other unit.

The

licensee also submitted a TS change to require this action. The inspector

reviewed the corrective action and verified that the TS change was

submitted.

This LER is closed.

(Closed) LER 280/87-38, Increased Off-Site Thyroid Dose Calculations from

Steam Generator Tube Rupture due to Post Trip Steam Generator Tube

Uncovery.

The issue involved determination of a condition in which a

potential exists for uncovering of a tube break after a ~team generator

tube rupture event. This issue was identified after the North Anna steam

generator tube rupture event which occurred on July 15, 1987.

The

licensee's initial evaluation concluded that the additional thyroid dose

would be below regulatory limits.

However, the issue has been assigned

for additional generic review by a Westinghouse program.

The program was

proposed to the WOG and is expected to be completed in 1989.

The

inspector reviewed the LER and also determined that the issue resolutions

will be reviewed by other technical NRC groups.

This LER is closed.

8.

Action on Previous Inspection Findings (92701, TI 2515/100 & 101)

a.

(Closed) !Fi 280,281/87-13-02, Followup on Licensee Performance for

Decay Heat Removal Evolutions during Low Reactor Coolant Level

Operation.

The issue involved the licensee's evaluation and

implementation of lessons learned from NRC IN 87-23, Loss of Decay

Heat Remova 1 During Low Reactor Coo 1 ant Leve 1 Operation.

After

issuance of the IN, the licensee took actions to implement design

changes to both units for the installation of permanent level

instrumentation to monitor

RCS

level during reduced inventory

operation. This level instrumentation was installed for both units

during their respective refueling outages in 1988.

On October 17, 1988, the NRC issued GL 88-17, Loss of Decay Heat

Removal.

The GL requested that each 1 i censee respond to act i ans

taken with regard to implementation of eight recommended expeditious

actions which are discussed below, and to respond to actions taken

with regard to six programmed enhancement recommendations discussed

in the attachment to the GL.

The licensee submitted their response

to the GL expeditious actions request by letter dated January 6,

1989, and responded to the GL programmed enhancement recommendations

request by letter dated February 3, 1989.

The inspectors reviewed the licensee I s responses to GL 88-17 and

conducted specific reviews of the eight recommended expeditious

actions as outlined in the licensee's January 6, 1989 reply.

The

following is a brief description of the recommended actions of the

licensee's response and the inspectors' fi~dings.

14

TRAINING - Discuss the Diablo Canyon event, related

lessons learned, and implications with appropriate

personnel.

Provide training shortly before entering

inventory condition.

events,

plant

reduced

The licensee's response stated that the event had been discussed

with operations personnel including specific evolutions involved

in

cooldown/draindown operation.

The

inspectors verified

through discussions with operators that they had received

training on specific evolutions involved in cooldown/draindown

operations and that they were sensitized to pot'ential loss of

OHR.

The inspector also determined that the training included

reviews of all procedural and administrative changes implemented

as a result of the licensee's response to GL 88-17.

CONTAINMENT CLOSURE -

Implement procedures and admi ni strati ve

controls that reasonably assure that containment closure will be

achieved prior to the time at which core uncovery could result

from a loss of OHR coupled with the inability to initiate

alternate cooling or addition of water to the RCS inventory.

The licensee's response stated that procedures require that the

status of the containment configuration be established and

verifiea prior to entering a reduced inventory condition (water

level lower than 3 feet below the vessel flange).

In addition,

the AP for loss of RHR capability directs containment closure

action to be initiated and continued until the RHR system is

returned to service and core conditions are verified normal.

The

inspectors verified that the licensee has

prepared

procedures and administrative controls to reasonably assure that

containment closure will be achieved prior to the time at which

core uncovery could occur.

This was done by reviewing OP-lG,

Refueling Containment Integrity and RCS Mid-Loop Containment

Closure Checklist; Standing Order No. 7, Operation When the RCS

Is Partially Drained; and AP 27.00, Loss of Decay Heat Removal

Capability.

RCS TEMPERATURE - Provide at least two independent, continuous

temperature indications that are representative of the core exit

conditions whenever the RCS is in a mid-loop condition.

The licensee's response stated that procedures for draining the

RCS will be revised to ensure at least two incore temperature

indicators are operable prior to draining the RCS to a reduced

inventory condition.

The incore temperature will continuously

indicate in the control room and will be periodically monitored

by the operators.

The temperature readings are periodically

recorded on the control room shutdown logs by the control room

operators.

The inspectors verified that controlling procedures

.,

15

for draining the RCS were revised to ensure at least two incore

temperature indicators are operable prior to draining the RCS to

a reduced inventory condition. The inspector also verified that

the

contra l

room

operators peri odi ca lly recorded these

temperature readings in their logs. Also, it was verified that

RCS temperature curves were incorporated into AP 27.00, Loss of

Dec~y Heat Removal Capability.

RCS WATER LEVEL - Provide at least two independent, continuous

RCS water level indications whenever the RCS is in a reduced

inventory condition.

The licensee's response stated that one continuous means of

level

indication has

been

installed which

provides for

continuous readout in the control room.

This system also

provides for an alarm for loss of shutdown cooling at a level of

12 feet, 4 inches.

The second means of level indication is

still under review.

The inspectors verified that the licensee

has a permanently installed water level

instrument with

continuous readout in the control room whenever the RCS is in a

reduced inventory condition. This instrument alarms when water

level decreases to 12 feet, 4 inches (approximately 7 inches

above mid-nozzle).

This system is currently operable on both

units.* The licensee has committed to installing a second

independent channel during the next respective unit refueling

outages.

RCS

PERTURBATION -

Implement procedures and administrative

controls that generally avoid operations that deliberately or

knowingly lead to perturbations to the RCS and/or to systems

that are necessary to maintain the RCS in a stable and

controlled condition while the RCS is in a reduced inventory

condition.

The licensee's response stated that an operations procedure for

assessing maintenance activities that could potentially cause a

loss of RCS inventory, is being developed.

The inspectors

verified that the licensee had prepared a procedure, OC-28,

Assessment of Maintenance Activities for Potential Loss of

Reactor Coolant Inventory, which allowed for assessment of work

on systems for potential loss of reactor cool ant inventory

during reduced RCS inventory conditions. This procedure allows

for operator evaluation of work to be performed based on

guidelines for the assessment.

The procedure also established

additional controls to assure that maintenance activity will not

adversely affect RCS inventory.

RCS INVENTORY ADDITION -

Provide at least two availdble or

operable means of adding inventory to the RCS

that are in

addition to pumps that are part of the OHR systems.

These

should include at least one high pressure injection pump.

J

16

The licensee's response stated that procedures will be revised

to require that one high head and one low head safety injection

pump with appropriate flowpaths be provided prior to RCS

dra i ndown into a reduced inventory condition.

The inspectors

verified that the 1 i censee has a procedure which requires at

least two available or operable means of adding inventory to the

RCS in addition to the RHR system.

This requirement is

accomplished by OC-6, Boric Acid Flow Paths and Tech Spec Heat

Trace Circuit Verification.

The procedure requires that in a

reduced inventory condition, one CHG/SI pump and one LHSI pump

must be available with appropriate flowpaths to the core.

NOZZLE DAMS - Implement procedures and administrative controls

that reasonably assure that all hot legs are not blocked

simultaneously by nozzle dams unless a vent path is provided

that is large enough to prevent pressurization of the upper

plenum of the reactor vessel.

The licensee's response stated that RCS* 1oop isolation is

obtained by the use of loop isolation valves. Therefore, nozzle

dams are not used.

The inspectors verified that the licensee

does not presently use steam generator nozzle dams.

LOOP STOP

VALVES -

Implement procedures and administrative

controls that reasonably assure that all hot legs are not

blocked simultaneously by closed loop stop valves unless a vent

path is provided that is large enough to prevent pressurization

of the reactor vessel

upper plenum or unless the

RCS

configuration prevents vessel water loss if reactor vessel

pressurization should occur.

The licensee's response stated that this condition will be

contro 11 ed by procedures to assure that one 1 oop remains

unisolated with the respective loop bypass valve open.

The

inspectors verified that the licensee has implemented procedure

and administrative controls that reasonably assure that at least

one 1 oop remains uni so 1 ated with the respective 1 cop bypass

valve open.

This is accomplished by Standing Order No. 7,

Operation When the RCS Is Partially Drained.

The

inspectors consider that the licensee has satisfactorily

implemented the eight recommended expeditious actions responses to GL 88-17 as outlined in their January 6, 1989 reply.

This item is

closed.

b.

(Closed)

IFI

280,281/88-33-0l,

Followup

on

Sequence of Data

Collection for Testing AFW Pumps. This issue involved the adjustment

of the turbine-driven AFW pump speed prior to collection of data*for

the monthly surveillance. The licensee agreed that clarification of

the test procedure was warranted and issued a revision to periodic

..

17

test 1 and 2-PT-15.lC dated March 23, 1989.

The inspector reviewed

the revised test procedure and noted that an engineering evaluation

is now required before proceeding if the as found pump speed is

outside an allowable range.

This item is closed.

c.

EDG Fuel Oil Handling and Storage (TI 2515/100)

On January 16, 1987, the NRC issued IE Information Notice 87-04

alerting lice~sees of potentially significant problems pertaining to*

long-term storage of EDG fuel oil.

The inspector reviewed the

licensee 1s program for storage and handling of EDG .fuel oil as a

result of information provided in the Notice.

Discussions with the

licensee revealed the following:

New procedures are being put into place for sampling the fuel

oil in the tanks for oxidation and biological contamination.

Additional fuel sampling ports are being added to some of the

tanks.

Fuel oil filters and strainers are in the preventive maintenance

program.

No violations or deviations were identified.

9.

Exit Interview

The inspection scope and findings were summarized on May 2, 1989, with

those individuals identified by an asterisk in paragraph 1. The following

new items were identified by the inspectors during this exit:

One IF! (paragraph 4.b) was identi°fied for followup on resolution of

pressurizer safety relief setpoint drift (280, 281/89-13-01).

The licensee acknowledged the inspection findings with no dissenting

comments.

The licensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

10.

Index of Acronyms and Initialisms

AFW

AP

cc

ccw

CFR

CHG

OBA

DHR

AUXILIARY FEEDWATER

ABNORMAL OPERATING PROCEDURE

COMPONENT COOLING

COMPONENT COOLING WATER

CODE OF FEDERAL REGULATIONS

CHARGING

DESIGN BASIS ACCIDENT

DECAY HEAT REMOVAL

~ ,


DPI

DR

EOG

EMP

ESF

ESW

EWR

GL

GPM

HELB

HPSI

IE

IFI

IN

IR

IRS

ISI

LER

LHSI

LIV

LOCA

MOV

NRC

NRR

OP

PM

PPM

PSI

PSIG

PT

QA

QC

RCS

RHR

RG

RO

RSS

RWP

RWST

SI

sov

SRO

SW

TS

UFSAR

URI

WOG

18

DELTA PRESSURE INDICATORS

DEVIATION REPORT

EMERGENCY DIESEL GENERATOR

ELECTRICAL MAINTENANCE PROCEDURE

ENGINEERED SAFETY FEATURE

EMERGENCY SERVICE WATER

ENGINEERING WORK REQUEST

GENERIC LETTER

GALLONS PER MINUTE

HIGH ENERGY LINE BREAK

HIGH PRESSURE SAFETY INJECTION

INSPECTION AND ENFORCEMENT

INSPECTOR FOLLOWUP ITEM

INFORMATION NOTICE

INSPECTION REPORT

INSIDE RECIRCULATION SPRAY

INSERVICE INSPECTION

LICENSEE EVENT REPORT

LOW HEAD SAFETY INJECTION

LICENSEE IDENTIFIED VIOLATIONS

LOSS OF-COOLANT ACCIDENT

MOTOR OPERATED VALVE

NUeLEAR REGULATORY COMMISSION

NUCLEAR REACTOR REGULATION

OPERATING PROCEDURE

PREVENTATIVE MAINTENANCE

PARTS PER MILLION

POUNDS PER SQUARE INCH

POUNDS PER SQUARE INCH GAUGE

PERIODIC TEST

QUALITY ASSURANCE

QUALITY CONTROL

REACTOR COOLANT SYSTEM

RESIDUAL HEAT REMOVAL

REGULATORY GUIDES

REACTOR OPERATOR

RECIRCULATION SPRAY SYSTEM

RADIATION WORK PERMIT

REFUELING WATER STORAGE TANK

SAFETY INJECTION

SOLENOID OPERATED VALVE

SENIOR REACTOR OPERATOR

SERVICE WATER

TECHNICAL SPECIFICATIONS

UPDATED FINAL SAFETY ANALYSIS REPORT

UNRESOLVED ITEM

WESTINGHOUSE OWNER 1S GROUP