ML18152A080

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Insp Repts 50-280/97-10 & 50-281/97-10 on 971005-1115. Violations Noted.Major Areas Inspected:Operation,Maint, Engineering & Plant Support
ML18152A080
Person / Time
Site: Surry  Dominion icon.png
Issue date: 12/15/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A081 List:
References
50-280-97-10, 50-281-97-10, NUDOCS 9712300182
Download: ML18152A080 (33)


See also: IR 05000280/1997010

Text

Docket Nos:

License Nos:

Report Nos:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

9712300182 971215.

PDR

ADOCK 05000280

G

PDR

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

50-280. 50-281

DPR-32. DPR-37

50-280/97-10. 50-281/97-10

Virginia Electric and Power Company (VEPCO)

Surry Power Station. Units 1 & 2

5850 Hog Island Road

Surry, VA 23883

.October 5 - November-15. 1997

R. Musser. Senior Resident Inspector

K. Poertner. Resident Inspector

P. Byron. Resident Inspector

_

J. Blake. Reactor Inspector (Sections Ml.1.

Ml.2. and Ml.3)

P. Hopkins. Project Engineer (Sections 01.7.

Ml.5 and Ml.6)

D. Jones. Reactor Inspector (Sections Rl.1 and R8.1)

W. Stansberry, Security Inspector (Sections

Sl.2. S2.1. S2.2. S2.3. S3.1. and S3.2)

R. Haag, Chief. Reactor Projects Branch 5

Division of Reactor Projects

ENCLOSURE 2

.

EXECUTIVE SUMMARY

Surry Power Station. Units 1 & 2

NRC Inspection Report Nos. 50-280/97-10 and 50-281/97-10

This integrated inspection included aspects of licensee operations. engineer-

ing. maintenance. and plant support.

The report covers a six-week period of

resident inspection; in addition. it includes the results of announced inspec-

tions by four regional inspectors.

Operations

Operators performed their assigned duties in an excellent manner during

the Unit 2 shutdown for a scheduled refueling outage.

The Senior

Reactor Operator maintained excellent command and control during the

evolution (Section 01.2).

The licensee's actions to identify an intake canal level probe common

mode failure scenario demonstrated a good safety perspective and were

conducted in a conservative and professional manner.

An Inspection

Followup Item was identified to review the licensee's root cause

evaluation and proposed corrective actions to prevent recurrence

(Section 01.3).

Increased Unit 1 reactor coolant activity indicated that a* fuel cladding

defect had occurred.

The licensee was monitoring and trending coolant

activity on a routine basis.

The activity was well below Technical

Specification allowable values (Section 01.4).

Licensee actions to identify and report the Anticipated Transient

Without A Scram Mitigating System Actuation Circuitry enable setpoint

problem exhibited a good questioning attitude and conservative approach

to operations.

An Inspection Followup Item was identified to review

licensee actions to resolve the issue (Section 01.5).

A Non-cited Violation was identified concerning the failure to perform a

Technical Specification required surveillance on the diesel driven fire

pump within the required frequency (Section 01.6).

Control room charts were observed to be operating correctly and control

room logs were routinely reviewed by operations personnel.

Plant

startup evolutions were conducted in accordance with approved procedures

(Section 01'.7).

No problems were identified during a review of Unit 2 containment

integrity during fuel movement (Section 01.8).

The licensee's preparation of the Unit 2 containment prior to restart

from the refueling outage was adequate.

Minor deficiencies were

identified and corrected prior to containment closeout (Section 01.9) .

Observations by the inspectors during the defueling of the Unit 2

reactor indicated a well controlled process being carried out in

accordance with Technical Specifications (Section 01.10).

2

Maintenance

The licensee's inservice inspection results were well documented. and

the bases for conclusions were conservative (Section Ml.l).

The decision to repair a leaking spare reactor head penetration seal

weld using a mechanical fixture was fully supported-by engineering

analysis (Section Ml.l).

Radiographs of replacement piping welds were in .accordance with required

codes and standards (Section Ml.1).

Consistent evaluations of eddy current inspection results and

conservative tube plugging decisions were strengths in the licensee's

steam generator inspection program (Section Ml.2).

The licensee's flow accelerated corrosion monitoring program continued

to be a well-engineered and conservative program (Section Ml.3).

Surveillance activities associated with s~fety injection accumulator

check valve testing and Number 3 EOG testing were conducted in

accordance with approved procedures and met acceptance criteria

(Section Ml.4).

Maintenance activities on protective relays and the condenser water box

were performed satisfactorily.

Work procedures were adequate and were

being followed (Section Ml.5).

Thirteen observed surveillance tests were performed satisfactorily

(Section Ml.6).

An unresolved item was opened to track resolution of an interpretation

of Technical Specification surveillance frequency requirements

(Section Ml.7).

A violation was identified for inadequate work instructions resulting in

the failure to implement the prerequisite requirements of a safety

evaluation during the replacement of a Consequence Limiting Safeguards

relay (Section Ml.8).

The licensee rebuilt the pressurizer Power Operated Relief Valves during

the Unit 2 Refueling Outage.

Following return of the unit to service.

no indication of seat leakage was observed (Section Ml.9).

The licensee successfully replaced the "C" Reactor Coolant Pump flange

seal.

Installation of pump flange seal bolt number 16 as a "no load"

bolt was determined to be a viable option (Section Ml.10).

Testing on the Unit 2 pressurizer power operated relief valves was

conducted in a cautious and controlled manner and as specified by the

procedure.

The Senior Reactor Operator supervising the test

3

demonstrated superior command and*controi over the evolution

(Section Ml.11).

Engineering

Letdown line modifications were performed during the Unit 2 refueling

outage to correct previous problems with weld leakage (Section El.1).

The inspectors verified that the Unit 2 vital bus Appendix R

modifications had been implemented during the refueling outage

(Section El.2).

Plant Support

During the Unit 2 Refueling Outage, the licensee was properly monitoring

and controlling personnel radiation exposure and posting area

radiological conditions in accordance with 10 CFR Part 20

(Section Rl.l).

Personnel entering the Radiological Controlled Area (RCA) were

adequately briefed on radiological hazards and protective measures

(Section Rl.1).

Housekeeping in the RCA was very good during the Unit 2 Refueling Outage

C Section Rl. 1) .

A significant amount of activity was removed from the Reactor Coolant

System by shutdown chemistry controls in order to reduce exposure to

workers during the Unit 2 Refueling Outage (Section Rl.1).

Health physics practices were observed to be proper (Section Rl.2).

Security and material condition of the protected area perimeter barrier

were acceptable (Section Sl.1).

Compensatory measures were used for vital area access breaches

(Section Sl. 2).

The evaluation of the licensee's program for protected area access

controls for packages. personnel and vehicles revealed that the criteria

of the Physical Security Plan were being followed (Section S2.1).

Criteria in Chapters 1. 4. and 6 of the Physical Security Plan and

Security Plan Implementing Procedures were complied with for alarm

stations and communications (Section S2.2).

Intrusion detection systems and assessment aids were functional. well

maintained. effective for both covert and overt penetration attempts.

and met licensee commitments (Section S2.3) .

4

The review and verification of commitments of selected security and

administrative procedures did not identify any inconsistencies or

ndncompliance (Section S3.1).

The review of three quarterly Security Event Logs verified that the

licensee was appropriately analyzing. tracking, resolving. and

documenting safeguard~ events (Section S3.2).

Report Details

Summary*of Plant Status

Unfr 1 operated at power the entire reporting period.

Unit 2 shutdown for a scheduled refueling outage which began on October 6.

The unit was returned to service on October 31 after the completion of a 25

day refueling outage.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707 40500).

1. 2

a.

The inspectors conducted frequent control room tours to verify proper

staffing. operator attentiveness. and adherence to approved procedures.

The inspectors attended dai.ly plant status meetings to maintain

awareness of overall facility operations and reviewed operator logs to

verify operational safety and compliance with Technical Specifications

(TSs).

Instrumentation and safety system lineups were periodically

reviewed from control room indications to assess operability. Frequent

plant tours were conducted to observe equipment status and housekeeping .

Deviation Reports CDRs) were reviewed to assure that potential safety

concerns were properly reported and resolved.

The inspectors found that

daily operations were generally conducted in accordance with regulatory

requirements and plant procedures.

Unit 2 Shutdown for Refueling Outage (RFD)

Inspection Scope (71707)

On October 5. the inspectors observed the licensee remove Unit 2 from

service and shutdown the reactor in preparation for RFO 14.

b.

Observations and Findings

On October 5. the licensee commenced shutting down the Unit 2 reactor in

preparation for RFO 14.

The inspectors noted that the Senior Reactor

Operator (SRO) maintained excellent command and control. Briefings were

thorough and detailed.

The SRO gave frequent briefings before each

significant evolution.

The operators did an excellent job maintaining

steam generator level and feedwater flow.

Procedures were at the

stations and were utilized: The generator output circuit breaker was

opened at 12:37 a.m. on October 6 and the reactor was tripped 20 minutes

later. All systems functioned as designed .

C.

2

Conclusions

Operators performed their assigned duties in an excellent manner during

the Unit 2 shutdown for a scheduled refueling outage.

The SRO

maintained excellent command and control during the evolution.

01.3 Inoperable Intake Canal Level Probes

a.

Inspection Scope (71707)

b.

C.

The inspectors reviewed licensee activities associated with inoperable

intake canal level probes due to marine growth.

Observations and Findings

On October 14. with Unit 2 shutdown for a scheduled refueling outage,

intake canal level probe 2-CW-LE-202 was removed from service to perform

response time testing. The as-found response time did not meet the

required minimum response time.

The level probe was cleaned. retested.

and returned to service.

Canal level probe 2-CW-LE-203 was then removed

from service for testing. The as-found response time for level probe

2-CW-LE-203 also did not meet the a~ceptance criteria. The probe was

cleaned. retested. and returned to service.

Based on the conclusion

that both Unit 2 canal level probes had been inoperable due to a common

mode failure mechanism (marine growth) the licensee declared both Unit 1

canal level probes inoperable and entered a six-hour action statement at

5:26 p.m. to place Unit 1 in hot shutdown in accordance with TS 3.0.1.

The Unit 1 level probes were tested. cleaned. and returned to service.

The as-found values for the Unit 1 canal level probes did not meet the

response time acceptance criteria. The six-hour action statement was

exited at 8:10 p.m. following the return to service of the Unit 1 level

probes.

The inspectors monitored testing activities in progress. reviewed the

applicable TS and verified that the NRC was notified as required by

10 CFR 50.72.

The licensee initiated a Category 1 root cause evaluation

to determine the cause of the event and corrective actions to prevent

recurrence.

The root cause evaluation was still in progress at the end

of the inspection period.

Review of the licensee's root cause

evaluation and proposed corrective actions is identified as Inspection

Followup Item (IFI) 50-280. 281/97010-01.

Conclusions

The licensee's actions to identify an intake canal level probe common

mode failure scenario demonstrated a good safety perspective and were

conducted in a conservative and professional manner.

An IFI was

identified to review the licensee's root cause evaluation and proposed

corrective actions to prevent recurrence .

3

01.4 Unit 1 Failed Fuel

a.

Inspection Scope (71707)

The inspectors reviewed licensee actions with respect to increased

Unit 1 coolant activity.

b.

Observations and Findings

On October 7. an increase in Unit 1 containment gaseous activity was

observed. Subsequent sampling of the Reactor Coolant System (RCS)

identified that the xenon and Iodine 131 concentrations had increased

from previous samples.

On October 15, power was reduced to perform

maintenance activities. Subsequent to the power reduction an iodine

spike was observed.

When the unit was returned to 100 percent power.

iodine levels subsequently returneo to the previous steady state values.

The increased activity and subsequent iodine spike following a power

reduction indicated that a fuel cladding defect had occurred.

Discussions with reactor engineering determined that the fuel failure

was most likely located in a low power positfon on or near the periphery

of the core and was limited to one fuel pin.

The inspectors routinely

reviewed reactor coolant sample results and activity levels were well

within TS allowable values.

The licensee plans to monitor and trend RCS

activity on a normal frequency unless a significant increase in RCS

activity occurs.

c.

Conclusions

Increased Unit 1 RCS activity indicate that a fuel cladding defect had

occurred.

The licensee was monitoring and trending RCS activity on a

routine basis.

RCS activity was well below TS allowable values.

01.5 Anticipated Transient Without A Scram Mitigating.System Actuation

Circuitry (AMSAC)

a.

Irispecti on Scope (71707)

The inspectors reviewed a one hour non-emergency event report associated

with arming of the AMSAC circuitry.

b.

Observations and Findings

On November 12. the licensee made a one hour non-emergency report to the

NRC concerning the interlock setpoint for AMSAC.

The circuitry

automatically enables at 37 percent power as indicated by turbine first

stage impulse pressure.

The design basis of the system assumes that the

system is enabled at 40 percent reactor thermal power.

On November 2.

during the Unit 2 power ascension following a refueling outage the

AMSAC ci r,cui try enabled at 37 percent turbine first stage pressure but

reactor thermal power indicated greater than 40 percent (41~42 percent).

A DR was initiated to document the apparent discrepancy between the

actual thermal power level that the circuitry was enabled at and the

4

power referenced in the Updated Final Safety Analysis Report.

Subsequent review of the DR determined that the system was outside its

design basis.

Requirements for AMSAC are not contained in the TS.

The licensee

administratively controls AMSAC operability in accordance with Virginia

Power Administrative Procedure (VPAP) 2802. "Notifications and Reports."

Revision 7.

The VPAP requires that if AMSAC is inoperable for 30 days.

a special report shall be submitted to the NRC within the next 30 days.

The licensee is still reviewing the issue to determine corrective

actions to ensure that AMSAC enables within the design basis of the

system.

Further review of licensee actions to resolve the issue is

identified as IFI 50-280. 281/97010-02.

c.

Conclusions

Licensee actions to identify and report the AMSAC enable setpoint

problem exhibited a good questioning attitude and conservative approach

to operations.

An IFI was identified to review licensee actions to

resolve the issue.

01.6 Missed Surveillance Requirement

a.

Inspection Scope (71707)

The inspectors reviewed the circumstances surrounding the failure to

perform a TS required .surveillance within the required time period.

b.

Observations and Findings

On October 28. the licensee determined that a TS required Periodic Test

(PT) on the diesel driven fire pump had not been performed within the TS

required frequency.

The pump was declared inoperable and the missed *

surveillance was performed satisfactorily that same day.

TS requires

that the PT be performed every 31 days.

With the TS allowed grace

period included. the surveillance frequency was exceeded by nine days.

The PT was scheduled to be performed within the required frequency by

the Operations Department. however. the PT was incorrectly initialed as

being completed by the operating shift on the PT work schedule due to a

personnel error. Subsequently, engineering notified operations that the

PT had not been received for final review and processing.* Review by

operations determined that the PT had not been performed and the TS

required frequency had been exceeded without declaring the diesel driven

pump inoperable.

The inspectors discussed this event with licensee personnel and reviewed

the corrective actions identified to prevent recurrence. Discussed

corrective actions for this matter included: satisfactorily completing *

the surveillance. initiating a DR (S-97-3132). counseling the involved

individual and adding an administrative enhancement to require

comparison of completed surveillance procedures with the surveillance

C.

5

work schedule. This non-repetitive. licensee identified and corrected

violation is being treated as a Non-cited Violation (NCV) consistent

with Section VII.B.1 of the NRC Enforcement Policy. This matter is

identified as NCV 50-280. 281/97010-03.

Conclusions

An NCV was i denti fi ed concer_ni ng the failure to perform a TS required

surveillance on the diesel fire pump within the required frequency.

01.7 Review of Shift Activities During Unit 2 Startup

a.

Inspection Scope (71707)

The inspectors reviewed shift logs and control room chart recorders and

observed shift activities during the Unit 2 startup from refueling.

b .. Observations and Findings

During October 27-31. the inspectors reviewed operation of the

control room chart recorders for both units to assure that pens were

marking properly and the recorders were timing correctly. The

inspectors verified that each chart had been checked by a licensed

operator each shift. Recorders not in use were cl early ma_rked as being

out-of-service.

The inspectors observed that shift logs were frequently reviewed by

control room operators. Additionally, operators maintained positive

control of the plant during pre-job briefings and during the performance

of periodic test procedures.

Preparations for reactor startup and plant operations while

transitioning from the refueling outage to power operations were

conducted safely with good control and communications.

Plant operators

demonstrated good knowledge and awareness of changing plant conditions.

The actions of the plant operators while taking the reactor critical

were conducted in accordance with approved procedures.

c.

Cone l us i ans

Control room charts were observed to be operating correctly and control

room logs were routinely reviewed by operators. Plant startup

evolutions were conducted in accordance with approved procedures.

01.8 Refueling Containment Integrity

a.

Inspection Scope (71707)

The inspectors reviewed containment integrity requirements during Unit 2

refueling activities.

6

b.

Observations and Findings

The inspectors verified that containment integrity was in place prior to

the off-load of fuel assemblies during the Unit 2 RFD.

The inspectors

reviewed applicable procedures and independently verified selected

portions of the containment isolation boundary.

c.

Conclusions

No problems were identified during a review of Unit 2 containment

integrity during fuel movement.

01.9 Unit 2 Containment Closeout Walkdown

a.

Inspection Scope (71707)

On October 27. the inspectors performed a containment closeout walkdown

to review containment conditions prior to unit restart.

b. * Observations and Findings

C.

The inspectors performed a walkdown of the Unit 2 containment prior to

the restart.

The station manager accompanied the inspectors on the

walkdown.

The walkdown encompassed all levels and rooms within the

containment.

Prior to the walkdown. the licensee stated that with the

exception of a few specific areas and items still staged for specific

tasks and tests. the containment was ready to support the return to

service of the unit.

In general. the overall condition of the

containment was adequate for the restart of the unit.

However. a number

of items were discovered during the containment inspection which

indicated that a more thorough walkdown should have been performed.

These items included the following:

Tywrap in the containment sump

Tape on the containment walls and on various pipes

A failed component cooling water pressure gauge on the "B" RCP

A refueling tool wrapped in a plastic sleeve

Numerous small hand tools. wire. nuts. bolts. and threaded 1/4"

stock

Upon exiting the containment. responsibl~ licensee personnel were

informed of the walkdown findings. A list of these deficiencies was

promptly drafted.

The items were corrected prior to the containment

closeout.

Conclusions

The licensee's preparation of the Unit 2 containment prior to restart

from the refueling outage was adequate.

Minor deficiencies were

identified and corrected prior to containment closeout.

7

01.10 Unit 2 Refueling Observations

a.

Inspection Scope (71707)

The inspectors observed the defueling of the Unit 2 Reactor.

b. Observations and Findings

Fuel handling evolutions were observed both in the containment and fuel

building. All observations indicated that the process was well

controlled and was adequately supervised. Technical Specification

requirements for refueling were being met. A monitor was posted at the

access to the refueling cavity to ensure all personnel entering the area

were trained in foreign material exclusion practices and were not taking

unnecessary items into the area.

The refueling evolution for the Unit 2

reactor was completed in accordance with specified requirements.

c.

Conclusions

Observations by the inspectors during the defueling of the Unit 2

reactor indicated a well controlled process being carried out in

accordance with Technical Specifications.

II.

MAINTENANCE

Ml

Conduct of Maintenance

Ml.1

Inservice Inspection (ISI)

a.

Inspection Scope (73753)

The inspectors reviewed ISI activities for the Unit 2 refueling outage.

The ISI review included fabrication and pre-service inspections for

piping welds made as the result of repairs. replacements. and

modifications.

b.

Observations and Findings

This was the first refueling outage in the second. 40-month period of

the third. 10-year. ISI interval. The third. 10-year interval started

May 10. 1994. and the ISI Code of record is ASME Section XI. 1989

Edition with no addenda.

The records for five VT3 component support inspections. eleven VTl

component inspections. sixteen piping component ultrasonic examinations.

twenty-eight piping component surface examinations. three reactor

coolant pump flywheel examinations. and seven reactor coolant isolation

valve stud examinations were reviewed by the inspectors. The licensee

was using computer software for the recording of ISI examination data

and examiner conclusions. and to generate required reports.

As a result

of using the computer. all reports were concise. complete. and legible.

8

During in situ ultrasonic examination (UT) of the 22.5-inch long, by

2.75-inch diameter studs in the "C" cold-leg, loop stop-valve, MOV2595,

several studs showed a reflector that appeared just beyond the back

reflection from the end of the stud. This reflector was of concern to

the UT examiners because it was similar to one of the reflectors

received from one of the notches in the calibration block.

The inspectors reviewed the _final disposition of the UT indications in

Stud No. 11, (the one with the largest signal) which was removed from

the valve and replaced.

The suspect Stud No. 11 was subjected to

visual, fluorescent liquid penetrant. and additional ultrasonic

examinations. The original ultrasonic signal was still present after

removal, but 1there were no indications found by the visual and surface

examinations.

Based on these additional examinations. the licensee

concluded that the signals were geometric or beam redirection signals.

and therefore the remaining studs were acceptable for continued service.

The inspectors agreed with the conclusions reached by the licensee.

The licensee's visual inspections of the reactor vessel head revealed

boron residue on the stalk of Spare Head Penetration Number 19.

The

residue emanated from the area of the welded seal canopy at the threaded

connection to the stalk. After reviewing available options for the

repair of the leaking seal canopy, the licensee elected to use a

mechanical fixture manufactured by ABB-Combustion Engineering (ABB-CE).

The inspectors monitored the licensee's decision process. and reviewed

the completed 10 CFR 50.59 analysis for this application of a mechanical

fixture to repair a reactor coolant pressure boundary leak.

By

definition. the welded seal canopy only provides a leak barrier for the

acme-threaded connection which is the reactor coolant boundary;

therefore. the inspectors agreed that the use of a mechanical fixture

would not require NRC approval.

The inspectors reviewed the radiographs associated with the replacement

of piping components in reactor coolant and secondary systems.

Particular attention was given to radiographs of welds involved with the

replacement of components in the reactor coolant letdown system and

steam generator feedwater piping inside containment.

The radiographs

reviewed were of acceptable quality.

The inspectors agreed with the

licensee's interpretation of weld quality.

c. * Conclusions

The licensee's inservice inspection results were well documented; and

the bases for conclusions were conservative. The decision to repair a

leaking spare reactor head penetration seal weld using a mechanical

fixture was fully supported by engineering analysis.

Radiographs of

replacement piping welds were in accordance with required codes and

standards .

9

Ml.2 Steam Generator Inspection

a.

Inspection Scope (50002) .

The inspectors reviewed procedures and documentation associated with the

eddy current examination of the Unit 2 "B" Steam Generator (SG).

b.

Observations and Findings

The Unit 2. Model 51 SGs were replaced with Model 51F SGs in 1980.

The

Model 51F SGs contain thermally treated Alloy 600 Inconel tubing with

stainless steel quatrefoil support plates. The tube ends were

hydraulically expanded for the full depth of_the tube sheet.

Since 1993. the licensee's SG inspection program required that one SG be

comprehensively inspected per outage.

The SG inspected during the

current outage was the "B" SG.

The inspection consisted of a bobbin

inspection of 100% of the tubes; a Motorized Rotating Pancake Coil

(MRPC) inspection of 20% of the tubes at the top of the tubesheet; and

an MRPC inspection of 20% of the Row 1. Li-Bends.

The licensee also

conducted a comparative study of eleven indications. found with their

standard 0.115-coil MRPC probe. using Plus Point eddy current ultrasonic

examinations.

As a result of the eddy current examinations. the licensee*elected to

plug five tubes. Three of the tubes. R37-C59. R36-C69. and R40-C70.

were plugged due to measured AntiVibration Bar (AVB) wear.

The measured

AVB wear was only approximately 20% through-wall. but conservative

growth rate calculations postulated growth to near 40% through-wall by

the end of three operating cycles. when SG "B" is due for its next

inspection.

The other two tubes. Rl-C34 and Rl-C35. contained

indentation restrictions at the top of the tubesheet.

The licensee

postulated that the tubes had been "dinged" during a past pressure

pulse/chemical cleaning operation in June 1994. and elected to plug the

tubes as a precautionary measure.

The inspection plan and results were discussed during a conference call

between NRC and the licensee on October 22. 1997.

c.

Conclusions

Consistent evaluations of eddy current inspection results and

conservative tube plugging decisions were strengths in the licensee's

steam*generator inspection program.

Ml.3

Flow Accelerated Corrosion (FAC) Program

a . Inspection Scope (49001)

The inspectors reviewed procedures. records. and documents related to

the monitoring of FAC in secondary piping and components.

10

b.

Observations and Findings

The inspectors reviewed the records associated with the inspection and

replacement of piping components in the steam and feedwater systems.

The records showed that the FAC program is a mature program. in that

predictions for the amount of wall loss in the piping systems were

generally accurate.

In the majority of cases with unacceptable wall

thicknesses. the program had predicted these results. and replacement

piping components were on hand.

The inspectors did note an exception to the FAC program predictions

occurred in a straight run of piping immediately downstream of a flow

control valve. This area of corrosion was not predicted by the computer

program. but was included for inspection because of the licensee's FAC

engineering personnel monitoring experiences at other plants. where FAC

in piping downstream of flow control valves had been observed.

Without

available replacement piping, the licensee was able to justify using a

weld buildup to restore the required wall thickness until the next

refueling outage.

c.

Conclusions

The licensee's flow accelerated corrosion monitoring program continued

to be a well-engineered and conservative program.

Ml.4 Emergency Diesel Generator (EOG) and Safety Injection (SI) Accumulator

Check Valve Testing

a.

Inspection Scope (61726)

The inspectors observed portions of surveillance tests performed on the

Number 3 EOG and Safety Injection Accumulator check valves.

b.

Observations and Findings

On October 5. the inspectors observed portions of Operations Periodic

Test (OPT) O-OPT-EG-001. "Number 3 Emergency Diesel Generator Monthly

Start Exercise." Revision 10-Pl. The inspectors considered that the

pre-job brief was thorough and the precautions were adequately

discussed.

The operators had the procedure at the job site and

constantly used it. The inspectors observed independent verification of

procedural steps. The operators were cautious and thorough.

The

results of the OPT were satisfactory.

On October 15. the inspectors observed portions of 2-0PT-SI-022. "SI

Accumulator Discharge Check Valve Test With Reactor Head Removed."

Revision 1-Pl. The test was modified to allow for performing the

surveillance with the Reactor Vessel Upper Internals not installed. The

core specimen access plugs were removed to prevent them from becoming

dislodged and falling to the bottom of the reactor vessel.

The upper

internals are normally placed in the reactor vessel for the performance

of this test and they rest on the access plugs which prevents them from

11

becoming dislodged.

The surveillance verifies by acoustic monitoring or

accumulator discharge flow that the check valves stroke full open.

The

check valves in each accumulator line are tested by acoustic monitoring

every third refueling cycle. Accumulator line "A" check valves, 2-SI-

107 and 2-SI-109, were acoustically monitored during RFO 14.

The

inspectors reviewed Safety Evaluation 96-045, Revision 3, which

evaluated the performance of the test with the upper internals removed.

The inspectors also reviewed completed Procedure 2-0PT-SI-022, Revision

1-Pl. All six SI check valv~s met the acceptance criteria as specified

in 2-0PT-SI-022.

c.

Conclusions

Surveillance activities associated with SI accumulator check valve

testing and Number 3 EOG testing were conducted in accordance with

approved procedures and met acceptance criteria.

Ml.5 Maintenance Activities

a.

Inspection Scope (62707)

The inspectors observed and reviewed maintenance activities to verify

that activities were conducted in accordance with TS, procedures,

regulatory guides, and industry codes or standards.

b.

Observations and Findings

The inspectors observed all or portions of the following Work Order (WO)

activities:

W0-368064 Perform protective relay maintenance and testing

W0-374842-01 Scrape, clean tubes and return "B" condenser water

box to service

The inspectors found that the maintenance activities were performed with

the proper tools on the correct equipment with the procedures and work

packages present and in use.

Pre-job briefings were accomplished with

appropriate personnel. Supervisory personnel were present to ensure

procedural adherence.

c.

Conclusions

The observed maintenance activities were performed satisfactorily.

Work

procedures were adequate and were being followed.

Ml.6 Surveillance Observations

a.

Inspection Scope (61726)

The inspectors observed and reviewed surveillance testing acti vi ti es to

verify that testing was performed in accordance with procedures, test

12

instrumentation was calibrated. Limiting Condition for Operations (LCOs)

were met. and any deficiencies identified were properly reviewed and

resolved.

b. Observations and Findings

The inspectors observed all or portions of the following surveillance

tests:

2-NSP-RX-014 "Control Rod Exercises." Revision 4

2-IPT-RP-AFW-001 "Under Voltage and Low-Low Steam Generator Logic

Start of the Steam Driven Auxiliary Feed Water Pump." Revision 6

2-PT-s:s "Consequence Limiting Safeguards Logic (Hi-Hi Train)

Verify Operability," Revision 9

2-IPT-RP-TM-001 "Turbine Trip Signal Input to Reactor Protection

System Functional Test." Revision 6

2-IPT-CC-MS-484 "Steam Line Flow Protection Loop F-2-484 Channel

Calibratioh," Revision 8

2-IT-CC-RC-412 "Delta T and TAvG Loop T-2-412 Channel Calibration."

Revision 16

2-PT-8.2 "Reactor Protection Logic Operability," Revision 10

2-0PT-FW-001 "Motor Driven Auxiliary Feedwater Pump 2-FW-P3A

Operability Test." Revision 5

2-0PT-FW-002 "Motor Driven Auxiliary Feedwater Pump 2-FW-P3B

Operability Test." Revision 6

2-NPT-RX-014 "Hot Rod Drive By Bank Operability," Revision- 4

2-NSP-RX-005 "RPI Calibration Data Collection." Revision 6

2-0P-RX-006 "Withdrawal Of Control Rods Banks To Critical

Conditions." Revision 6

2-IT-CC-RPI-001 "Analog Rod Position Indication System

Operability," Revision 4

The inspectors found that the work performed under these activities was

conducted* in a very professional manner.

All of the surveillances

observed were performed with the procedures present and in use.

Effective crew briefings were accomplished prior to performance of the

PTs.

-~-~--------------------~~--------------

13

c.

Conclusions

Thirteen observed surveillance tests were performed satisfactorily.

Ml.7 Refueling Surveillance Frequency Requirements

a.

Inspection Scope (61726)

The inspectors reviewed an issue involving surveillance frequency

requirements specified ih Section 4.1 of the TS ..

b.

Observations and Findings

During a routine inspection. questions were raised concerning the TS

surveillance frequency requirements specified in TS Section 4.1.

Specifically, Table 4.1-1, "MINIMUM FREQUENCIES FOR CHECK, CALIBRATIONS.

AND TEST OF INSTRUMENTATION CHANNELS," defines frequency "R" as "Each

Refueling Shutdown," while Table 4.1-2. "ACCIDENT MONITORING

INSTRUMENTATION SURVEILLANCE REQUIREMENTS," defines frequency "R" as

"Refueling." Table 4.l-2A. "MINIMUM FREQUENCY FOR EQUIPMENT TESTS,"

specifies a frequency of "Each refueling shutdown"* for line items 3, 6,

8, 14a and b. 15. 16. 17, and 18.

The licensee has interpreted the

frequency of terms "Each Refueling Shutdown" and "Refueling" to be any

time during the 18-month operating cycle.

If a surveillance test with a

specified frequency of "Each Refueling Shutdown" or "Refueling" can only

be accomplished during a unit shutdown. the licensee performs it at that

time.

However. if the licensee has determined that a test with these

specified frequencies can be performed with the unit on-line. they view

that the test can be performed at any time within the 18-month operating

cycle.

The licensee has an informal practice of accomplishing these on-

line tests 30 days or less prior to a unit refueling outage.

The validity of the licensee* s TS interpretation .is being reviewed by

the NRC.

Until this matter is resolved. this matter will be tracked as

Unresolved Item 50-280. 281/97010-04.

c. Conclusions

An unresolved item was opened to track resolution of an interpretation

of TS Surveillance frequency requirements.

Ml.8 Safety Evaluation of Relay Replacement/Engineered Safety Feature (ESF)

Actuation

a.

Inspection Scope (62707)

The inspectors reviewed the circumstances surrounding an ESF Actuation

during the replacement of a Consequence Limiting Safeguards (CLS) Relay .

14

b.

Observations and Findings

C.

On*October 11. at approximately 2:22 p.m .. during the replacement of

Relay 1812 in the "B" train of the Unit 2 Hi-CLS circuitry, an

inadvertent short circuit occurred while landing a lead which actuated

the "B" train of Hi-CLS.

At the time of the event. Unit 2 was in

refueling shutdown with the Residual Heat Removal System in service.

The actuation of the "B" train of Hi-CLS caused the actuation of the "B"

train of Safety Injection (SI).

All equipment expected to actuate on

the Hi-CLS and SI responded as designed (with the exception of equipment

removed from service). The Number 3 Emergency Diesel Generator auto

started but did not synchronize to its bus as power was never lost from

its associated bus.

At no time during the event was the residual heat

removal capability lost. Following verification that a valid Hi-CLS

signal was not present. the operators returned equipment to the normal

standby condition. This matter was reported to the NRC in accordance

with 10 CFR 50.72 and 50.73.

In preparation for the relay replacement. the licensee drafted Temporary

Modification S2-97-8 which provided instructions to install a jumper to

allow the replacement of Relay 1812. This Temporary Modification was

supported by Safety Evaluation 97-138 which stated that train "B" of

Safety Injection would be defeated during the evolution. The safety

evaluation further stated that a formal tracking mechanism would be used

to ensure that this condition was met.

Contrary to these specified

requirements. the Safety Injection signal was not defeated nor was a

formal tracking method used to ensure the condition was met due to

inadequate implementing instructions in the controlling work documents.

Specifically, Work Order (WO 00375660-02) and Procedure O-ECM-1801-01.

"Westinghouse Type BF or BFD Relay Replacement." Revision 10. the

procedures controlling the relay replacement activity, did not contain

specific instructions to ensure that the requirements specified in

Safety Evaluation 97-138 were implemented.

This failure represents a

breakdown in controlling plant configuration for a maintenance activity.

This is a violation of Technical Specification 6.4.A.7 and will be

tracked as Violation 50-281/97010-05.

Conclusions

A violation was identified for inadequate work instructions resulting in

the failure to implement the prerequisite requirements of a safety

evaluation during the replacement of a CLS relay. *

Ml.9 Unit 2 Pressurizer Power Operated Reli~f Valve (PORV) Maintenance

a.

Inspection Scope (62707)

The inspectors reviewed licensee activities involving corrective

maintenance of the Unit 2 pressurizer PORVs .

15

b.

Observations and Findings

Prior to the Unit 2 RFD, PORV 2-RC-PCV-2456 was inoperable with its

associated block valve closed due to valve seat leakage.

Pressurizer

PORV seat leakage has been an ongoing problem and was not successfully

addressed for the Unit 1 pressurizer PORVs during the previous Unit 1

RFD.

During the October. 1997, Unit 2 RFD. the licensee rebuilt both

pressurizer PORVs in accordance with procedure O-MCM-0419-01. "Copes-

Vulcan 2 Inch 1500 LB Reverse Acting Valve Overhaul." Revision 8.

During the overhaul of the valves .. direct oversight of the Virginia

Power Maintenance personnel was provided by a Copes-Vulcan vendor

representative. This maintenance overhaul included the replacement of

numerous valve parts (valve plug, cage, packing, stem and various

gaskets). The inspectors reviewed the associated documentation for the

pressurizer PORV overhaul and found no discrepancies.

Following the return of Unit 2 to service on October 31 and for the

remainder of the inspection period, no abnormal pressurizer PORV

tailpipe temperatures have been noted.

Monitoring tailpipe temperatures

for the remainder of the operating cycle will ultimately determine the

success of the pressurizer PORV repair.

c. {onclusions

The licensee rebuilt the pressurizer PORVs during the Unit 2 RFD.

Following return of the unit to service, no indication of seat leakage

was observed.*

Ml.10 Unit 2 C Reactor Coolant Pump (RCP) Flange Seal Replacement

a.

Inspection Scope (62707)

The inspectors observed and reviewed the licensee's actions to replace

the Unit 2 "C" RCP flange seal during the RFD.

b.

Observations and Findings

Prior to the Unit 2 RFD. the licensee determined that the "C" RCP flange

seal would be replaced due to observed flange leakage.

To gain access

to the seal, this evolution required removal of the RCP motor and lower

rotating unit including the 24 flange bolts.

While in the process of removing the 24 flange bolts. the licensee

experienced difficulty in the removal of bolt number 16.

Following the

removal of bolt number 16, inspection of the bolt hole revealed that the

majority of the threads were no longer intact (having been stripped

during bolt removal) .

The licensee determined that in lieu of repairing the damaged threads

during the present refueling outage, they would replace the RCP with

bolt number 16 as a "no load" bolt.

To support this decision, the

16

licensee obtained a detailed analysis from Westinghouse demonstrating

the acceptability of this option. This option recommended that during

the operating cycle. if the unit was to go to cold shutdown twice. the

pre-load on the remaining 23 bolts should be verified as acceptable

prior to restarting the unit.

The licensee also had two machining

vendors inspect the damaged bolt hole to provide permanent repair

options during a future refueling outage.

The inspectors followed this*issue in detail. A review of the

information provided by Westinghouse indicated that the "no load" bolt

option was viable. The inspectors wa~kdown of containment with RCS

pressure at 300 psig indicated no flange leakage. A licensee walkdown

with the unit at normal operating temperature and pressure also

indicated no pump flange leakage.

RCS leakage following the return of

Unit 2 to service was low and continued in this manner for the remainder

of the inspection period.

c.

Conclusions

The licensee successfully replaced the "C" Reactor Coolant Pump flange

seal. Installation of pump flange seal bolt number 16 as a "no load"

bolt was determined to be a viable option.

Ml.11 Unit 2 Pressurizer PORV Testing

a.

Inspection Scope (61726)

The inspector observed a portion of the setup and testing of the

pressurizer PORVs prior to the return to service of Unit 2.

b.

Observations and Findings

On October 24. the inspectors observed portions of the performance of

Procedure 2-0PT-RC-001. "PRZR PORV Refueling Test.* Revision 4.

This

test provides instructio.ns to perform a complete checkout of the Unit 2

pressurizer PORVs and their associated equipment. Testing was conducted

in a cautious and controlled manner and as specified by the procedure.

The Senior Reactor Operator supervising the test demonstrated superior

command and control over the evolution.

When problems were encountered.

the test was stopped and a well thought out course of action was taken.

The test was completed satisfactorily.

c.

Conclusions

Testing on the Unit 2 pressurizer PORVs was conducted in a cautious and

controlled manner and as specified by the procedure.

The Senior Reactor

Operator supervising the test demonstrated superior command and control

over the evolution .

17

III. Engineering

El

Conduct of Engineering

El.1 Unit 2 Letdown Line Orifice and Valve Replacement

a.

Inspection Scope (37551)

The inspectors reviewed the licensee's actions related to replacement of

the Unit 2 letdown line orifices and valves.

b.

Observations and Findings

On September 11. 1996. the licensee experienced the fourth socket weld

failure in the Unit 2 letdown line in 12 months.

The licensee

determined that the flow orifices (2-CH-R0-20RLD1-3). letdown orifice

block valves (2-CH-HCV-2200A-C). and some piping had to be replaced.

Design Change Package (DCP)96-040. "CVCS Letdown Piping Modification."

was issued to accomplish this work.

The licensee determined that the

modification would be accomplished in two phases.

They replaced some of

the piping and supports downstream of the orifices to change the

configuration and replaced, where practical. socket welds with butt

welds.

This work was accomplished during a December 1996 outage. This

effort was documented in more detail in Inspection Report Nos. 50-280 .

281/96-13.

The second phase was to replace the orifices and the orifice block valve

bodies and modify the valve supports during RFD 14.

The replacement

valve bodies required butt welds rather than the original socket welds.

WOs 357847-01 through -04. 357848-01 through -03. and 357850-01 through

-03 were issued to replace the valve bodies (2-CH-HCV-2200A-C).

The

  • remainder of the work was accomplished by WOs 351999-02.-03. -16. and

-17.

The inspectors reviewed DCP 96-040 and the completed WOs and

verified that the work scheduled for RFD 14 had been completed. The

inspectors verified that DCP 96-040 has been completed.

c.

Conclusions

Letdown line modifications were performed during the Unit 2 RFD to

correct previous problems with weld leakage.

El.2 Appendix R Modifications

a.

Inspection Scope (37551)

The inspectors verified that the vital bus Appendix R modifications were

accomplished during the Unit 2 RFD.

b.

Observations and Findings

The inspectors observed portions of the work activities associated with

DCP 94-015. "Appendix R Vital Bus Modifications." and verified that the

18

associated WOs 38332754-01 and -02 had been completed.

The

modifications replaced the incoming feeder breakers in panels 2-I. 2-IA.

2:II. 2-IIA. 2-III. 2-IIIA. 2-IV. and 2-IVA with manual switches and

installed fuse blocks in Uninterruptable Power Supplies 2A-1 and 2A-2.

These modifications were implemented to meet the requirements of

Appendix R.

The licensee plans to implement the modifications on the

Unit 1 vital busses at the next scheduled refueling.outage.

c.

Cone l usi ans

The inspectors verified that the Unit 2 vital bus Appendix R

modifications had been implemented during the refueling outage.

IV. Plant Support

Rl

Radiological Protection and Chemistry (RP&C) Controls

Ri.1 Occupational Radiation Exposure Control Program

a.

Inspection Scope (83750)

b.

The inspectors reviewed implementation of selected elements of the

licensee's radiation protection program during the Unit 2 RFO.

The

review included observation of radiological protection activities

including pre-work briefings. personnel exposure moni tori n*g.

radiological postings, and verification of posted radiation dose rates

and contamination levels within the Radiologically Controlled Area

(RCA).

Those activities were evaluated for consistency with the

programmatic requirements. personnel monitoring requirements.

occupational dose limits. radiological posting requirements. and survey

requirements specified in Subparts B. C. F. G. and J of 10 CFR 20.

Observations and Findings

The inspectors conducted frequent tours of the RCA to observe radiation

protection activities and practices. Personnel preparing for routine

entries into the RCA were observed being briefed on the radiological

conditions in the areas to be entered. The briefings were given by

radiation control personnel before access was granted and covered the

dosimetry, protective clothing, and equipment required by the Radiation

Work Permit (RWP) for the entry.

The administrative limits for the

allowed dose and dose rate for the entry were emphasized during the

briefings. The briefings provided thorough descriptions of the existing

dose rates which could be encountered during the entry.

The inspectors

determined that personnel entering the RCA were adequately briefed on

the radiological hazards which could be encountered while in the RCA and

the radiological protective measures required to be taken during the

entry.

In addition to observing briefings for routine RCA entries. the

inspectors attended a briefing given specifically for work to be

performed under RWP 97-2-4102 in the Unit 2 "C" Reactor Coolant Pump

(RCP) Cubical.

Dose rates in that area were elevated and therefore

additional precautions were implemented. Those precautions included

.*

19

continuous Health Physics coverage, radiation and contamination surveys

of the equipment being worked on. and use of telemetric dosimetry.

In

addition to the radiological conditions and protective measures

addressed during briefings for routine entries-. the scope of work and

detailed discussions of how to accomplish each task were addressed

during this briefing. The inspectors determined that personnel were

adequately briefed on radiological hazards: protective measures and work

to be performed.

The inspectors observed the use of personal radiation exposure

monitoring devices by personnel entering and exiting the RCA.

Thermoluminescent Dosimeters (TLDs) were used as the priTT)ary device for

monitoring personnel radiation exposure.

In addition. Digital Alarming

Dosimeters (DADs) were used for monitoring the accumulated dose and the

encountered dose rates during each RCA entry.

The DADs were set to

alarm at administrative limits established for the specific RWP under

which the RCA entry was being made.

As the individuals exited the RCA.

the accumulated dose and encountered dose rate information was

transferred from the DADs to the Personnel Radiation Exposure Management

System (PERMS) data base in order to track individual exposures.

During

tours of the RCA the inspectors noted that the required dosimetry was

being properly worn by personnel when entering and while in the RCA.

The inspectors also noted that personnel exiting the RCA routinely

surveyed themselves for contamination using Personal Contamination

Monitors CPCMs).

The inspectors reviewed As Low As Reasonably Achievable CALARA) program

details. implementation. and goals for the current Unit 2 RFO.

Based on

the scheduled activities. daily and cumulative exposure projections were

established.

Individual exposures. based on data from DADs and PERMS.

were summarized by RWPs on a daily basis and allocated to the various

organizational departments.

Daily reports of the collective and

departmental exposures. along with their respective projected goals were

issued for monitoring purposes.

Plots of daily and cumulative exposure

vs. their respective projections were also distributed daily.

The

projected cumulative exposure for the planned 30 day Unit 2 RFO was 115

man-rem with a challenge goal of 100 man-rem.

As of day 11 of the RFO

(October 16) the daily and cumulative exposures were well within the

projected and challenge goals for the RFO.

The annual ALARA goal for

the site was established at 358 man-rem for the year 1997.

As of

October 16. the Year-To-Date (YTD) site collective dose was

approximately 52 man-rem above the projected YTD site collective dose.

The projected site collective dose was exceeded due to a 20 day

extension of the Unit 1 RFO. several unplanned outages. and other

emergent work.

The ALARA goal for the Unit 1 RFO. which occurred

earlier in the year. was 181 man-rem and the actual exposure was 222

man-rem.

The inspectors noted that the projected goals for the exposure

during the Unit 1 RFO and YTD site collective exposure were exceeded but

midway through the current Unit 2 RFO the projected goals for exposure

were being met.

The inspectors also reviewed records for individual

radiation exposures from the licensee's PERMS data base.

Those records

indicated that the YTD maximum individual exposures for Total Effective

C .

20

Dose Equivalent (TEDE). skin. extremity, and lens of the eye were 1.8.

4.2. 4.9. and 1.8 rem respectively.

The inspectors determined that

those exposures were well within the occupational dose limits specified

in 10 CFR 20.1202.

During the inspection the licensee was in the

process of an internal dose assessment for an individual that had

ingested a small amount of radioactive material. Preliminary estimates

indicated that the uptake was approximately 0.06 per.cent of the Annual

Limit on Intake CALI). or a Committed Effective Dose Equivalent (CEDE)

of 3 mrem.

Licensee records* indicated that this event occurred on

October 11. 1997. while the individual was performing a visual

inspection of the fuel transfer equipment in the Unit 2 Fuel Building

transfer canal.

During the time that the individual was performing the

work. the fuel transfer tube was open and the Fuel Building filtered

exhaust fans were started. Air flow from the Unit 2 Containment

Building through the transfer tube apparently swept radioactive

particles into the Fuel Building through the transfer canal where the

individual was working.

Deviation Report S-97-2844 was initiated for

this loss of contamination control event and the Operations Department

was assigned the responsibility for taking corrective actions.

During tours of th~ RCA the inspectors noted that general areas and

individual rooms were properly posted for radiological conditions.

Posted survey maps were used to indicate dose rates and contamination

levels at specific locations within rooms.

At the inspectors' request.

a licensee Health Physics staff member performed dose rate and

contamination surveys in several rooms and locations.

The inspectors

verified that the survey instrument readings were consistent with the

dose rates and contamination levels recorded on the posted survey maps.

The inspectors also noted that housekeeping was very good throughout the

RCA.

The inspectors also discussed with the licensee the primary coolant

chemistry controls used during reactor shutdown for the Unit 2 RFO.

Those controls included injecting additional boric acid into the coolant

during cooldown and injecting hydrogen peroxide after cooldown in order

to cause the release of radioactive material from the internal surfaces

of the Reactor Coolant System (RCS).

The radioactive material could

then be removed from the coolant by the filters and demineralizers in

the Chemical and Volume Control System (CVCS).

The licensee indicated

that approximately 176 curies (Ci) of cobalt-58 and 8.6 Ci of cobalt-60

were removed from the primary coolant. The overall effectiveness of

these shutdown chemistry controls would be evaluated based on the

reduction in the dose rates from specific locations in the plant and

from specific pieces of equipment.

The licensee indicated that the

results of that assessment would be documented in the ALARA report which

is scheduled to be issued 30 days after the RFO.

Conclusions

Based on the above reviews and observations. the inspectors concluded

that the licensee was properly monitoring and controlling personnel

21

radiation exposure and posting area radiological conditions in

accordance with lO*CFR Part 20.

Personnel entering the RCA were ad~quately briefed on radiological

hazards and protective measures.

Housekeeping in the RCA was very good during the Unit 2 RFD.

A significant amount of activity was removed from the RCS by Shutdown

Chemistry Controls in order to reduce exposure to workers during the

Unit 2 RFD.

Rl.2 Radiological Protection and Chemistry Controls (71750)

On numerous occasions during the inspection period. the inspectors

reviewed Radiation Protection (RP) practices including radiation control

area entry and exit. survey results. and radiological area material

conditions.

No discrepancies were noted. and the inspectors determined

that RP practices were proper.

RB

Miscellaneous RP&C Issues (92904)

R8.1

(Closed) Violation 50-280. 281/97002-06: Multiple examples of failure to

foll ow radiation protection procedures.

RWP requ_i rements were not

fo 11 owed when i ndi vi duals failed to exit the RCA when thei'r DADs al armed

and individuals entered the RCA without DADs.

Licensee management

issued memorandums to station personnel stressing management

expectations for procedural compliance and personal accountability. A

Root Cause Evaluation of these events determined that the arrangement of

the area for in-processing to the RCA and the number of tasks required

for RCA entry were distracting to workers.

The flowpath for in-

processing to the RCA was rearranged to focus personnel on entry

requirements and. during periods of frequent entries. an individual was

posted at the RCA entrance to monitor compliance with dosimetry

requirements.

Sl

Conduct of Security and Safeguards Activities

Sl.l General Comments

On numerous occasions during the inspection period. the inspectors

performed walkdowns of the protected area perimeter to assess serurity

and general barrier conditions.

No deficiencies were noted and the

inspectors concluded that security posts were properly manned and that

the perimeter barrier's material condition was properly maintained.

Sl.2 Compensatory Measures

a.

lnspection Scope (81700)

Verified that the licensee employs compensatory measures when security

equipment has failed or performance has been impaired and that the

22

compensatory measures employed do not reduce the effectiveness of the

security system.

b.

Observations and Findings

Three compensatory measures were evaluated and observed_during the

inspection. Security officers were posted as compen$atory measures at

the containment personnel and equipment hatches.

Another security

officer was posted at the vehicle access door for the spent fuel vital

area.

The officers were equipped with appropriate dosimetry and were

aware of the procedural duties of their post. Appropriate security

measures compensated for the vital area access breaches in effect during

the ongoing outage.

None of the compensatory measures were due to

inoperable or malfunctioning equipment.

c.

Conclusions

Through observations. discussions with security force personnel. and

document review. the inspectors concluded that the licensee used

compensatory measures for vital area access breaches.

S2

Status of Security Facilities and Equipment

S2.l Protected Area Access Controls

a.

Inspection Scope (81700)

Evaluated the licensee's access control program for allowing packages.

personnel. and vehicles to enter the protected area to ensure compliance

with criteria in Chapters 2. 3. and 4 of the Physical Security Plan

(PSP).

b.

Observations and Findings

The inspectors reviewed appropriate access control procedures to. ensure

that the licensee provided appropriate access controls for the protected

areas.

Personnel. hand-carried packages or material. delivered packages or

material. and vehicles were searched before being admitted to the

protected area. Security personnel searched for firearms. explosives.

incendiary devices. and other items that could be used for radiological

sabotage.

These searches were either by physical search or by search

equipment.

Vehicle searches included a search of the cab. engine

compartment. undercarriage. and cargo areas.

The inspectors reviewed the following aspects of the personnel access

control program.

A coded and numbered picture badge identification

system was used for personnel who were authorized unescorted access to

the protected and vital areas. The codes corresponded to vital areas to

, which individuals had authorized access. Picture badges issued to

nonlicensee personnel indicated the authorized access areas and showed

23

that no escort was required.

Personnel displayed their badges while

within the protected area. Visitors authorized escorted access to the

protected area were issued a badge that showed an escort was required.

and were escorted by licensee-designated escorts while in the protected

area.

The licensee used biometric hand geometry to ensure

identification of individuals entering the protected area.

Access control program records were available for review and contained

sufficient information for identification of persons authorized access

to the protected area.

The licensee maintained access records of keys,

key cards. key codes. lock combinations. and other related equipment

during a person's employment or for the duration that these items were

used.

The inspectors reviewed the controls for entry and exit of packages and

material to and from the protected area.

Security personnel confirmed

the authorization of. and identified packages and material at access

control portals before allowing them to be delivered.

The licensee used

security force personnel and X-ray equipment to identify and confirm

that prohibited material was not entering the protected area.

The inspectors reviewed vehicle access control.

Individuals who

controlled the admittance control hardware that allowed vehicle access

to*protected areas were protected in a bullet resistant alarm station.

Armed security force personnel controlled the vehicle access search

area. Security force personnel escorted nondesignated vehicles while

within the protected area.

c.

Conclusions

The evaluation of the protected area access controls for packages.

personnel and vehicles revealed that the criteria of the PSP were being

followed.

S2.2 Alarm Stations and Communications

a.

Inspection Scope (81700)

b.

Evaluated the licensee's alarm stations and communication equipment to

ensure that the application of the criteria in Chapters 1. 4. and 6 of

the PSP and Security Plan Implementing Procedure (SPIP)-03.

"Central/Secondary Alarm Station Operation." Revision 3. dated

January 29. 1997, were implemented.

Observations and Findings

The inspectors verified that annunciation of protected and vital area

alarms occurred audibly and visually in the alarm stations. The

licensee equipped both stations with communication equipment and limited

closed circuit television (CCTV) assessment capabilities. Protected

area alarms were assessed by security officers in defensive positions

around the protected area. Alarm systems were tamper-indicating and

24

self-checking, and provided with an uninterruptable power supply. These

alarm stations were continually manned by capable and knowledgeable

security operators.

The stations were independent yet redundant in

operation.

The central alarm station's interior was not visible from

within or from outside the protected area. and no single act could

remove the capability of calling for assistance or otherwise responding

to an alarm.

The walls. doors. floors. and ceilings.of the alarm

stations were bullet-resistant .

. The licensee provided means for monitoring and observing, by human eye

or CCTV. persons and activities in the isolation zone and exterior areas

within the protected area. These means provided for assessing intrusion

alarms for possible threats occurring in the isolation zone and exterior

areas within the protected area.

The transmission and control lines

used in the CCTV intrusion alarm assessment system had line supervisibn

and tamper indication.

The inspectors evaluated the equipment. operation. and maintenance of

internal and external security communication links. and determined that

they were adequate and appropriate for their intended function.

Each

security force member could communicate with an individual in each of

the continuously manned alarm stations. who could call for assistance

from other security force personnel and from local law enforcement

agencies. The alarm stations had the capability for continuous two-way

voice communication with local law enforcement agencies through radio

  • and the conventional telephone service. The licensee had compensatory

measures for defective or inoperable communication equipment.

Eight randomly selected Security Shift Blotters from October 22. 1994.

to October 20. 1997. were reviewed to verify that security plan and

procedure commitments in this area were being conducted and properly

documented.

c.

Conclusions

Based on this evaluation. the inspectors concluded that the licensee was

complying with the criteria in Chapters 1. 4. and 6 of the Physical

Security Plan and Security Plan Implementing Procedures for alarm

stations and communications.

S2.3 Protected Area Detection and Assessment Aids

a.

Inspection Scope (81700)

Inspected the licensee's protected area intrusion detection systems and

assessment aids to verify that they were functionally effective and met

licensee commitments in Chapters 2 and 4 of the PSP.

b.

Observations and Findings

The licensee had installed intrusion detection systems that could detect

attempted penetrations through the exterior isolation zones. and

C.

25

attempts to gain unauthorized access to the protected area.

The

licensee segmented the intrusion detection systems into enough alarm

zones to provide adequate coverage of the protected area perimeter

barrier and isolation zones.

The detection aids and alarm devices.

intluding transmission lines. were tamper-indicating and self-checking.

Sensors continued to function normally during loss of normal power.

The

licensee had compensatory measures to replace defective nr inoperative

detection aids.

The inspectors found through document review and

observation that the licensee had installed and tested detection and/or

surveillance subsystems for the protected areas.

The systems consisted

of motion. thermal. and volumetric detection equipment to discover and

assess unauthorized activities and conditions. These systems sent alarm

conditions to response force personnel through the alarm stations and

defensive positions allowing for response force personnel to assess and

correct the conditions.

The licensee used defensive positions (towers) to provide the initial

assessment and necessary response to the protected area alarms.

The

inspectors examined the licensee's defensive positions and found them to

be adequately placed.

They provided full fields of view and

unobstructed observation of the protected area barriers and is6lation

zones.

The licensee equipped these defensive positions with special

equipment as defined in the PSP.

Persons inside these defensive

positions were protected within the UL752 criteria .

Eight randomly selected Security Shift Blotters from October 22. 1994.

to October 20. 1997. were reviewed to verify that security plan and

procedure commitments in this area were being conducted and properly

documented.

Conclusions

Based upon the above evaluation. the inspectors concluded that the

licensee's intrusion detection systems and assessment aids were

functional. well maintained. effective for both covert and overt

penetration attempts. and met licensee commitments.

S3

Security and Safeguards Procedures and Documentation

S3.l Security Procedures

a.

Inspection Scope (81700)

b.

Reviewed a sample of implementing procedures to verify that the

procedures are consistent with plan commitments and practices.

Observations and Findings

The inspectors reviewed two Virginia Power Administrative Procedures and

twelve Security Plan Implementing Procedures.

Five procedures were

selected to verify commitments the licensee had made in the procedures.

The procedures selected pertained to all security areas inspected:

C.

26

procedural reviews. annual protected area perimeter and vehicle barrier

system walk downs. annual key core rotations. annual key card inventory,

and the vital area access authorization list.

Conclusions

The review and verification of commitments of selected security and

administrative procedures did not identify any inconsistencies or

noncompliance.

S3.2 Security Event Logs (SELs)

a.

Inspection Scope (81700)

Review a sample of event logs to verify that the licensee appropriately

analyzed. tracked. resolved. and documented safeguards events that the

licensee determined did not require a one hour report to the NRC.

b.

Observations and Findings

The inspectors reviewed quarterly SELs from the fourth Calendar Year

(CY) Quarter (QTR) 1996 to the second CY QTR 1997.

The total number of

events for each QTR was 12 for the fourth QTR 1996. 27 for the first QTR

1997. and 40 for the second QTR 1997.

The increases in the first two

QTRs of 1997 were mostly related to an outage.

The most significant

logged events during these two QTRs were unsecured vital area doors (14)

and lost badges (14).

The Deviation Reports for these events were

reviewed.

These events were licensee identified. human error. nonwilful

events with insignificant safety implications. The inspectors noted

eight computer hardware events logged in the second QTR 1997.

This

issue was discussed in paragraph 2.1 of Inspection Report 50-280.

281/96-06.

The security computer upgrade is still part of the key card

upgrade program that is scheduled for early 1998.

Noteworthy was that*

since January 1. 1996. to October 20. 1997. there have been only 16

security caused events documented in the SELs.

c.

Conclusions

The review of three quarterly SELs verified that the licensee was

appropriately analyzing, tracking, resolving, and documenting safeguards

events.

V. Management Meetings

Xl

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on November 25. 1997.

The

licensee acknowledged the findings presented .



_____ a:--____

_

27

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. _No proprietary information was

identified.

PARTIAL LIST OF PERSONS CONTACTED

Licensee

M. Adams. Superintendent. Engineering

R. Allen. Superintendent. Maintenance

R. Blount. Assistant Station Manager. Nuclear Safety & Licensing

D. Christian. Station Manager

E. Collins. Director. Nuclear Oversight

M. ~rist. Superintendent. Operations

L. Hartz. Engineering Manager

B. Shriver. Assistant Station Manager. Operations & Maintenance

T. Sowers. Superintendent. Training

B. Stanley. Supervisor. Licensing

W. Thorton. Superintendent. Radiological Protection

H. Travis. Engineering NOE Manager

IP 37551:

IP 40500:

IP 49001:

IP 50002:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 73753:

IP 81700:

IP 83750:

IP 92904:

Opened*

INSPECTION PROCEDURES USED

Onsite Engineeri~g

Effectiveness of Licensee Controls in Identifying. Resolving, and

Preventing Problems

Inspection of Erosion/Corrosion Monitoring Programs

Steam Generators

Surveillance Observation

Maintenance Observation

Plant Operations

Plant Support Activities

Inservice Inspection

Physical Security Program for Power Reactors

Occupational Radiation Exposure

Followup - Plant Support

ITEMS OPENED AND CLOSED

50-280. 281/97010-01

IFI

Review canal level probe RCE and corrective

actions (Section 01.3).

50-280. 281/97010-02

50-280, 281/97010-03

IFI

Review licensee actions to resolve AMSAC enable

setpoint issue (Section 01.5).

NCV

Failure to perform a required TS surveillance

(Section 01. 6).

50-280, 281/97010-04

50-281/97010-05

Closed

50-280, 281/97010-03

50-280, 281/97002-06

28

URI

TS surveillance frequency requirement questions

(Section Ml. 7).

VIO

Inadequate work instructions resulted in the

failure to implement the requirements of a

safety evaluation (Section Ml.8).

NCV

Failure to perform a required TS surveillance

(Section 01. 6).

VIO

Multiple examples of failure to follow radiation

protection procedures (Section R8.1) .