ML18152A061

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Insp Repts 50-280/96-02 & 50-281/96-02 on 960211-0323. Violation & Deviation Noted.Major Areas Inspected:Plant Operations Which Included Plant Status,Unit 2 Reactor Shutdown Due to Loss of Containment Integrity
ML18152A061
Person / Time
Site: Surry  
Issue date: 04/19/1996
From: Belisle G, Branch M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A062 List:
References
50-280-96-02, 50-280-96-2, 50-281-96-02, 50-281-96-2, NUDOCS 9605130401
Download: ML18152A061 (27)


See also: IR 05000280/1996002

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Report Nos. :

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/96-02 and 50-281/96-02

Licensee:

Virginia Electric and Power Company

Innsbrook Technical Center

5000 Dominion Boulevard

Glen Allen, VA

23060

Docket Nos.:

50-280 and S0-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

February 11 through March 23, 1996

Inspectors:

Approved by:

Scope:

D. M. Kern, Resident Inspector

W. K. Poertner, Resident Inspector

G.~e~ef

Reactor Projects Branch 5

Division of Reactor Projects

SUMMARY

¥-/1-~~

Date Signe

This routine resident inspection was conducted on site in the areas of nlant

operations which included plant status, Unit 2 re~ctor shutdown due to loss of

containment integrity, Unit 2 startup, quadrant power tilt requirements,

operation with a shut power operated relief valve block valve, Unit 2 letdown

line leak, and Root Cause Evaluation 96-0104 (Loss of Missile Shield

_

Prot~ction for 1-SW-P-lA); maintenance which included Unit 2 residual heat

removal containment penetration leak discovery and repairs, circulating water

expansion joint preventive maintenance program, Unit 2 main steam non-return

valve repair, inoperable Unit 1 pressurizer power operated relief valves,

elevated normal switchgear room temperatures, Unit 2 reactor coolant pump

motor oil leak, recirculation mode transfer relay replacement, service water

valve 2-SW-331 replacement, and station battery 2A test; engineering which

included Unit 2 pressurizer heater capacity evaluation; and plant support

960513040{ 960419

PDR

ADOCK 05000280

G

PDR

ENCLOSURE 3

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which included nuclear oversight corrective action process.

A review of

Updated Final Safety Analysis Report commitments was also conducted.

Results:

Plant Operations

    • .'**

The requirements of Technical Specification 3.8.A and 10 CFR 50.72 were met

during the Unit 2 shutdown to repair a leaking containment penetration

(paragraph 2.2).

The February 26 Unit 2 startup was conducted adequately and operators

implemented appropriate procedures and maintained adequate communication

throughout the unit startup.

Problems encountered were properly resolved with

guidance from senior operations management (paragraph 2.3).

A non-cited violation was identified for not incorporating quadrant power tilt

requirements into unit startup and operating procedures (paragraph 2.4).

One of the Unit 2 power operated i~lief valve block valves was shut due to

power operated relief valve seat leakage.

The Technical Specification

requirements for continued operation were met (paragraph 2.5).

A weld leak inside containment on the Unit 2 letdown line resulted in

isolation of the letdown line and operation with excess letdown in service

until the failed weld could be replaced.

This same weld joint had failed in

December 1995 (paragraph 2.6).

Root Cause Evaluation 96-0104, Loss of Missile Shield Protection for

1-SW-P-lA, was thorough and the recommended corrective actions should prevent

recurrence (paragraph 2.7).

Maintenance

A Violation was identified associated with failure to follow procedure

requirements which resulted in Unit 2 operation for approximately five weeks

with a degraded containment penetration.

Failures involved, 1) not notifying

the Shift Supervisor of water leaks inside the radiological control area, 2)

failure to initiate a Deviation Report on degraded equipment as required, and

3) attempted use of the minor maintenance program to identify a defective weld

(paragraph 3.1).

Deviations from commitments, contained in the June 21, 1993, letter to the

NRC, to reduce core damage probability from flooding, were identified.

Specifically, vendor recommendations for internal inspections of circulating

water rubber expansion joints were not incorporated in the preventive

maintenance program and changes to the inspection and service life replacement

program were not reviewed by the Station Nuclear Safety and Operating

Committee as committed (paragraph 3.2) .

An Unresolved Item was identified associated with preventive maintenance

program deferral weaknesses.

Over half of the circulating water rubber

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expansion joint preventive maintenance tasks have been routinely deferred.

Technical justification to defer Unit 1 rubber expansion joints replacements

during the 1995 refueling outage was weak.

Several preventive maintenance

task deferrals were rescheduled to inappropriate dates (paragraph 3.2).

Electricians effectively replaced and retested the main steam non-return valve

2-MS-NRV-201A supply breaker.

Communications between the electricians and

control room operators during post maintenance testing were good.

Appropriate

actions were implemented to address an inspector identifi~d weakness in the

procedure change approval process (paragraph 3.3).

Repairs to the Unit 1 power operated relief valve air system were well planned

and were completed in a timely manner.

Maintenance personnel demonstrated

good foresight to preplan the relief valve replacement as a contingency

(paragraph 3 A).

Temporary spot coolers have continued to provide adequate cooling to control

rod drive cabinets while the normal switchgear rooms have experienced elevated

temperatures.

Plans .,are on schedule to complete air conditioning upgrades by

mid May 1996.

Compensatory measures are adequate to cool the control rod

drive cabinets through that period (paragraph 3.5).

The issue team performed effectively to evaluate.a Unit 2 reactor coolant pump

oil leak and implemented appropriate corrective action.

The management

decision to reduce .power during the leak investigation demonstrated sound

consideration for personnel radiation exposure (paragraph 3.6).

The recirculation mode transfer relay repl~cement work activity w~s

accomplished in accordance with the work order instructions and the 10 CFR

50.59 safety evaluation adequately justified placing the recirculation mode

transfer mode switch in Refuel (paragraph 3.7).

The service water valve 2-SW-331 work activity was well coordinated and was

expeditiously completed to return the service water system to ser~ice

(paragraph 3.8).

The semi-annual station battery 2A test was accomplished in accordance with

the procedure and the data was recorded and reviewed by the system engineer as

required by the procedure (paragraph 3.9)~

Engineering

The safety evaluation for operation with reduced Unit 2 pressurizer heater

capacity was technically sound (paragraph 4.1).

Two examples were found in which the Updated Final Safety Analysis Report

descriptions were inconsistent with actual plant configurations. Section

9.13.3.6, Control Room and Relay Room Ventilation, did not describe the system

as presently configured.

Tables 5.2.1.a and 5.2.1.b identified 1&2-RH-MOV-

100&200 as motor operated gate valves.

These valves are no l_onger motor

operated (paragraph 6) .

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Plant Support

Procedures being developed to-define*nuclear oversight activities, including

corrective action processing, were appropriate.

Management's decision to

independently assess nuclear oversight effectiveness prior to implementing

further organizational transition demonstrated an appropriate sensitivity to

change management (paragraph 5.1) .

REPORT DETAILS

  • Acronyms used in this report are defined in paragraph 9.

1.0

PERSONS CONTACTED

Licensee Employees

Benthall, W., Supervisor, Procedures

  • Blount, R., Superintendent of Maintenance

Christian, D., Station Manager

Crist, M., Superintendent of Operations

Erickson, D., Superintendent of Radiation Protection

  • Garber, B., Licensing
  • Hanson, S., Supervisor, Maintenance
  • Hayes~ D., Supervisor of Administrative Services

Lovett, C., Supervisor, Licensing

Luffman, C., Superintendent of Security

  • McCarthy, J., Assistant Station Manager, Operations & Maintenance
  • McConnell, F., Materials
  • Miller, G., Corporate, Licensing
  • Patrick, J., Supervisor, Training
  • Saunders, R., Vice President, Nuclear Operations
  • Shriver, B., Assistant Station Manager, Nuclear Safety & Licensing
  • Sloane, K., Superintendent of Outage and Planning
  • Sowers, T., Superintendent of Engineering
  • Stanley, B., Nuclear Oversight
  • Swientonieski, J., Nuclear Safety and Licensing

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics, security

force members, and office personnel.

2.0

PLANT OPERATIONS (40500, 71707)

2.1

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indications to assess operability.

Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

Plant Status

Unit 1 operated at 100 percent reactor power the entire reporting

period.

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2.2

2.3

2.4

2

Unit 2 operated at 100 percent reactor power until February 22 when the

unit was shutdown to repair a leaking containment penetration (paragraph

--- 2.2) .-

The unit was returned to power operation on February 26.

On

March 13 power was reduced to 30 percent to investigate a RCP oil leak

(paragraph 3.6). The unit operated at 100 percent power for the

remainder of the inspection period.

Unit 2 Reactor Shutdown due to Loss of Containment Integrity

On February 22, at 7:04 p.m., a reactor shutdown of Unit 2 was

commenced.

The shutdown was directed by TS 3.8.A, Containment

Integrity, due to the discovery that containment penetration No. 24 1;1:i.s

leaking and that containment integrity no longer existed for the RHR

containment penetration.

The inspectors were notified by station

management of the leaking containment penetration and that a unit

shutdown had commenced.

The inspectors re~ponded to the site and observed the Unit 2 shutdown.

The inspectors verified that the NRC notification pursuant to 10 CFR

50.72 requirements was made within the required time limits. The

licensee initially ramped the unit from 100 percent to approximately

25 percent reactor power and at 10:44 p.m., the power ramp was stopped

to determine the results of repair activities. The repair attempts

failed and the RO, at 11:47 p.m., recommenced the power ramp to hot

shutdown conditions.

The unit was in hot shutdown conditions at

12:47 a.m., on February 23, meeting the TS requirements.

The unit was

subsequently cooled down to the cold shutdown condition to allow repairs

to the containment penetration. This item is discussed further in

paragraph 3.1.

Unit 2 Startup

On February 26, a Unit 2 reactor startup was initiated following repairs

to the RHR containment penetration.

The inspectors monitored control

room activities throughout the startup and continuously monitored

control room activities from 2 percent power to 30 percent power.

During power escalation to 30 percent power, several problems occurred.

The main turbine did not latch as rapidly as expected due to the manual trip lever hanging up.

During main turbine front end checks, the

turbine tripped when the test lever was partially released by the

operator while a turbine trip condition existed on the trip block.

The

licensee initiated DRs on each of the items identified to document and

correct the problems during future startups.

The inspectors determined

that the startup was conducted adequately and that operators implemented

appropriate procedures and maintained adequate communication throughout

the unit startup.

The inspectors also noted that senior operations

management was present in the control room throughout the unit startup.

Quadrant Power Tilt Requirements

The inspectors reviewed the licensee's implementation of TS 3.12.B.5,

Quadrant Power Tilt.

TS 3.12.B.5 states that the allowable QPT is

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2 percent.

The inspectors determined that the licensee did not monitor

QPT below 50 percent p~wer and that the control room alarms indicating

that a QPT may be present are automatically blocked below SO percent

power.

The inspectors questioned the licensee about the applicability

of the TS requirement.

The licensee initially stated that QPT limits

only applied above 50 percent power.

Standard TSs only require QPT

limits above 50 percent power and the licensee stated that the TS was

interpreted to only apply above 50 percent power consistent with the

standard Westinghouse design philosophy and the accident analysis. This

item was discussed with NRC staff and, although not a safety issue, the

determination was made that the TS as written applies during power

operation (greater than 2 percent power).

This item was discussed with

the licensee and the licensee agreed to implement the TS at all times.

The licensee plans to submit a TS change request to recognize that the

QPT limit only applies above 50 percent power.

The licensee also plans

to revise the operating procedures to require that QPT limits be

monitored at all power levels until the TS change is approved.

The inspectors were unable to determine if QPT limits had been exceeded

during previous power operations below 50 percent power.

The inspectors

did identify that 2-GOP-1.5, Unit Startup, 2% Reactor Power to Maximum

Allowable Power, revision 11, was inadequate because TS 3.12.B.5 QPT

requirements were not incorporated. Specifically, the procedure did not

require continuous monitoring of QPT values while at power.

However,

the GOP as written, did incorporate the TS requirements as the licensee

had interpreted them, in that, step 5.5.10 verified that the installed

equipment to monitor QPT above 50 percent power was enabled after power

level passed through the 50 percent value.

The inspectors identified several instances where power was increased

above 60 percent prior to identifying that a QPT existed.

In the

instances identified, the upper and lower ion chamber deviation alarms,

which indicate a potential QPT, did not clear when power exceeded 50

percent.

The alarms remained illuminated during the power increases

above 50 percent, the point at which the deviation alarm is

automatically unblocked.

When a manual QPT calculation was performed by

the operators, the QPT was greater than 2 percent.

The inspectors were

unable to determine when QPT exceeded 2 percent.

However, the

inspectors could determine that from the time the operators became aware

of the condition, due to the deviation alarms, the time allowed in the

TS action statement was not exceeded.

The inspectors determined that the operations staff did not understand

the QPT requirements during previous unit startups.

The inspectors will

monitor implementation of the QPT TS requirements during future power

reductions and startups.

TS 6.4 requires that detailed procedures be provided and followed for

normal startup, operation, and shutdown of a unit.

Procedure 2-GOP-1.5,

as well as, the Unit 1 GOP did not contain instructions for monitoring

QPT below 50 percent reactor power as required by TS 3.12.B.5 and was

thereby inadequate. This failure constitutes a violation of minor

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significance and is being treated as a Non-cited Violation, consistent

with Section IV of the NRC Enforcement Policy.

This item is identified

  • - as NCV 50-280, 281/96-02-01, Inadequate Unit Startup and Operating

Procedures.

2.5

Operation with a Shut PORV Block Valve

On February 27, the block valve for PORV 2-RC-PCV-2455C was shut to

determine if PORV 2-RC-PCV-2455C seat leakage was the source of elevated

PORV tailpipe temperatures following a Unit 2 restart. Prior to the

Unit shutdown, tailpipe temperature had been reading approximately 136

degrees F and following the return to 100 percent power, tailpipe

temperature had increased to approximately 195 degrees F.

Subsequent to

shutting the block valve, tailpipe temperature began to decrease and

gradually returned to approximately 136 degrees F over several shifts.

Based on this indication the licensee decided to operate with the PORV

inoperable and the associated block valve closed with *power available to

the block valve as allowed by TS 3.1.A.6.

The inspectors reviewed the

licensee's actions and verified that the requirements of TS 3.1.A.6 were

met.

The licensee initiated a WR to repair the PORV seat leakage at the next

refueling outage scheduled to commence in May 1996.

On March 22, the

PORV block valve was reopened to determine if valve seat leakage was

still present. Tailpipe temperature initially remained constant and

then slowly increased to 185 degrees F.

The PORV block valve was

reclosed on March 23.

2.6

Unit 2 Letdown Line Leak

At 2:05 a.m. on March 17, the operators identified that total RCS

leakage, un-identified leakage, and containment sump inleakage had

increased from previous values.

Based on this information the operators

increased monitoring of RCS leakage and requested that containment sump

and containment atmosphere samples be obtained.

Results of the backup

leakage calculations and the samples obtained indicated an RCS leak

inside containment. A containment entry, made at 6:17 a.m., identified

that the RCS leak was located on the normal letdown line at a weld

downstream of valve 2-CH-HCV-2200B.

Normal letdown was secured and

excess letdown was placed in service to isolate the normal letdown line.

The letdown line was manually isolated and the line was drained to allow

inspection and repair of the failed weld.

Leakage never exceeded TS

allowed values.

The inspection of the failed weld identified a 1/2-inch weld crack at a

tee connection downstream of the letdown orifice isolation valves.

Tr.1s

weld connection had previously failed on December 13, 1995 {See NRC

Inspection Reports Nos. 50-280/95-23 and 50-281/95-23).

The December

1995 failure was attributed to lack of fusion between the weld passes.

A weld repair was made and the letdown line was returned to service .

The licensee determined that the probable cause of the second failure

was improper setback in the tc2 connection resulting in high residual

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stresses in the socket weld joint. The licensee ground otit the entire

weld and separated the connection approximately 1/8-inch to ensure

proper setback and then rewelded the connection. -During the NOE

inspections following the welding activities further indications were

identified on the piping adjacent to the original weld area.

The

license~ decided to cut out approximately 1.5 feet of piping and replace

it with new pipe.

The removed piping was saved to allow further

inspection and to determine the failure mechanism.

The licensee was

still evaluating this item at the end of the inspection period.

The

letdown piping was replaced, tested, and the letdown line was returned

to service at 10:03 p.m. on March 20.

The unit remained at 100 percent

power throughout the repair activity.

RCE 96-0104, Loss of Missile Shield Protection for 1-SW-P-lA

The inspectors reviewed RCE 96-0104, Loss of Missile Shield Protection

for 1-SW-P-lA.

This event is discussed in NRC Inspection Reports

50-280/96-01 and 50-281/96-01.

The licensee determined that the primary

cause of the loss of missile protection was personnel error associated

with the field change process and that a contributing factor was a lack

of barriers in the procedures controlling excavations.

The inspectors

reviewed the RCE and the recommendations that resulted from the

evaluation.

The inspectors also verified that the recommendations had

been incorporated into the licensee's commitment tracking system.

RCE

96-0104 was thorough and the recommended corrective actions should

prevent recurrence.

One NCV was identified.

3.0

MAINTENANCE (61726, 62703)

During the reporting period, the inspectors reviewed the following

maintenance and surveillance activities to assure compliance with the

appropriate procedures and TS requirements.

3.1

Unit 2 RHR Containment Penetration Leak Discovery and Repairs

3.1.1 Discovery of Defect

On February 22, during a review of maintenance work by the Nuclear

Oversight Department, a Deficiency Card identifying a crack in the

Unit 2 RHR piping, 6

11 -RH-120-152, -was identified.

Local visual

inspection of the outside surface of the piping by station engineers

found a through-wall leak in the outside isolation barrier of

containment piping penetration No. 24 (RHR to RWST).

The leakage was

estimated at one drop every ten minutes.

The SS was notified and DR

S96-0369 was submitted.

Engineering initiated a series of activities to assess the safety

significance of the event.

The guidance contained within GL 91-18,

Resolution of Degraded and Nonconforming Conditions and on Operability,

was followed.

The significance of the flaw was unknown and could not be

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determined without a flaw evaluation and structural assessment.

Therefore, this ASME,Section XI, Class 2 piping was declared fnoperable

in accordance with the guidance provided in GL 91-18.

At 5:55 p.m. on February 22, the SRO declared that containment integrity

as d~fined in TS 3.8.A and TS section 1 was being violated on Unit 2.

This declaration was based on the SS's review of DR S-96-0369 which

documented the discovery of the weld leak on containment penetration

No. 24.

TS 3.8.A.1 required that containment integrity be

re-established within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> or the unit shutdown to hot shutdown

conditions within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Additionally, the TS required that

after unit shutdown a cool down to cold sh~tdown be completed within 30 _

hours.

3.1.2 Attempted Repairs

After declaring containment penetration No. 24 inoperable, the licensee

initiated repairs to the penetration piping in an attempt to restore

containment integrity. The leak had been observed at a structural, (non~

pressure barrier) saddle weld for piping support H-31.

Valve isolation

was verified and the pip{ng was drained.

The visual crack was ground

out and NOE was performed to ensure defect removal.

Weld repairs were

attempted followed by the required NOE.

After two unsuccessful attempts

to repair the cracked weld, the licensee abandoned their initial efforts

and continued with plant shutdown and cooldown .

3.1.3 Piping Penetration Repairs and Testing

After Unit 2 was in cold shutdown, Code repairs were made to correct the

cracked piping and weld defect.

The inspectors reviewed the work

associated with the repairs to containment penetration No. 24.

Approximat~ly 4 feet of the leaking penetration piping (schedule _10 SS)

was replaced with thicker wall piping. After the licensee determined

that all NOE was completed satisfactorily, the piping welds were tested

at system operating pressure to verify no leakage. A hydrostatic test

of the piping and welds was not conducted because the licensee applied

ASME Code Case N-416-1 which allowed a system pressure test in-lieu of a

hydrostatic test. Additionally, a 46 psig air test was conducted on the

piping to satisfy 10 CFR Part 50 Appendix J containment leak check

requirements.

The inspectors reviewed the applicability of ASME Code

Case N-416-1 to this repair.

The NRC approved the use of this Code Case

at Surry in a letter dated October 14, 1994.

The inspectors also

witnessed the 46 psig air test of the penetration and verified that

acceptance criteria for an acceptable test were met.

The inspectors

also reviewed the radiological controls of the area during radiographic

testing of the new weld joints.

3.1.4 Safety Significance of Event

Engineering calculations performed on February 22 quantified .the

through-wall leakage to have an estimated 10 CFR 50, Appendix J, Type C

leakage rate of .0036 SCFH.

This value when added to previously known

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penetration leakage was well within leakage limits for the containment

penetrations as allowed by 10 CFR 50, Appendix J, Type C leakage

criteria. However, the guidance provided in GL 91-18 required that

ASME,Section XI, Class 2 components be declared inoperable if they are

observed to have through-wall leakage.

The containment penetration

piping through-wall leak was considered a loss of containment integrity.

The affected portion of the RHR piping is normally isolated and not used

during power operation, shutdown, or accident conditions when

containment integrity is required.

The piping constitutes a portion of

the containment isolation system.

Subatmospheric containment conditions

were maintained and containment penetration No. 24 remained isolated

throughout the event with no abnormal indications of containment

leakage.

UFSAR Section 5.2, Table 5.2.1.b, describes containment penetration

No. 24 containment isolation barriers.

The table lists 2~RH-29 as the

inside manual gate valve and indicates that it is not 10 CFR 50 Appendix J leak.tested.

The outside containment isolation valve,

2-RH-MOV-200, is listed as requiring a leak test and is described as a

motor operated gate valve.

The motor has been electrically disconnected

and this valve is now essentially a manually operated gate valve. This

UFSAR inconsistency also exists in Table 5.2.1.a for the Unit 1

application.

The licensee was notified of this UFSAR discrepancy.

With

the inside barrier providing containment isolation, containment

penetration No. 24 remained isolated throughout this event.

Upon

completion of a full evaluation and structural assessment, the licensee

determined that the integrity of containment penetration No. 24 had been

maintained and the containment penetration would have performed its

intended safety function if a postulated accident had occurred.

3.1.6 Regulatory Issues

After successfully repa1r1ng and .testing the containment penetration,

the licensee prepared a JCO in accordance with 10 CFR 50.59.

The

purpose of the JCO was to ensure that structural integrity of the piping

that was not replaced was acceptable pending the results of the ongoing

failure analysis.

Field UT examinations confirmed that the existing

piping wall thickness was greater than the minimum requirements and

assured structural integrity. The inspectors closely monitored the

licensee's activities in this area.

On March 4, additional UT examinations and visual inspections were

performed on piping associated with the similar penetration located in

Unit 1.

No external leakage and no unacceptable wall thinning were

identified.

The Unit 1 piping penetration is fabricated from seamless

pipe and does not have any welded supports within the outside

containment isolation boundary.

Based on these examinations and

observations, the licensee's engineering department concluded that

Unit 1 was not subject to the failure mechanisms contributing to the

Unit 2 leak.

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A preliminary laboratory report based on inhouse electron microscope

scanning of the removed piping samples identified localized indications

of general intergranular attack on the inside surface of the piping.

This general attack was greater at the point of failure.

Evidence of

arc strikes and cold lap were also identified in the failure area.

The

resultant stiffness of the fixed, welded, saddle support concentrated

piping stresses in the overlapping welds resulting in a localized

through-wall leak after approximately 23 years of service.

Additionally, piping samples were sent to an off-site vendor for

independently analysis which will include chemical analysis,

characterization of mechanical properties, and microstructure and

surface analyses.

The inspectors reviewed the issues associated with identification and

resolution of this condition adverse to quality.

The leaking

penetration was initially identified by*a decontamination technician

performing routine duties on January 16, 1996.

A DC was submitted on

the same day to document the leak.

VPAP 2002, Work Request and Work

Order Tasks, revision 5-PSI including PAR 5-PS-2, specified the~ethod

to be used when a maintenance deficiency was identified.

Paragraph

6.2.b specified that any leakage identified in the RCA be reported to

the SS.

Additionally, paragraphs 6.2 and 6.9 defined what methods are

to be used to document maintenance deficiencies.

Two methods were

described, a WR and a DC.

Paragraph 6.9.1 described corrective

maintenance activities that can be covered by a DC as minor maintenance .

Attachment 11 of VPAP 2002 listed examples of minor maintenance

activities that can be controlled by the DC system.

Repairs of a

cracked and leaking piping weld are not included as minor maintenance.

Neither a DC or a WR are used as vehicles to promptly notify the control

room or SS of deficient conditions that may impact equipment or system *

operability.

The licensee contended that the DR system, described in

VPAP 1501, Deviation Reports, revision 4-PSl, is the vehicle used to

alert the control room and SS of deficiencies that may impact

operability.

When the leak was identified on January 16, 1996, a DC was

improperly used to document the deficiency, the control room was not

notified as required, and a DR was not submitted.

The inspectors

discussed the problems associated with the identification and correction

of the described condition adverse to quality with the Superintendent of

Operations and both ASMs.

Subsequent to the inspectors' discussions,

DR S96-0413 was submitted on February 28, to address the delay in

correcting a condition adverse to quality. A subsequent review of all

open DCs by the licensee verified that there were no other conditions

that compromised compliance with TSs.

Corrective actions in response to

DR S96-0413 should assure that plant conditions having the potential to

affect compliance with TSs are promptly identified in accordance with

station administrative procedures.

TS 6.4 requires that detailed written procedures be provided and

followed for preventive or corrective maintenance operations which would

have an effect on safety of the reactor.

VPAP 2002, Work Request and

Work Order Tasks, revision 5-PSI including PAR 5-PS-2 specifies the

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method to be used when a maintenance deficiency is identified.

Paragraph 6.2.b specifies that any leakage identified int.he RCA be.

reported to the SS.

Additionally, -paragraphs 6.2 and 6.9 defines what

method is to be used to document maintenance deficiencies.

VPAP 1501,

Deviation Reports, revision 4-PSl requires that deviations be reported

on a DR.

When the leak was identified on January 16, 1996, a DC in-lieu

of a WR was improperly used to document the deficiency, the control room

was not notified as required, and a DR was not submitted.

These

failures to follow procedures are identified as VIO 50-281/96-02-02,

Failure to Follow Procedures Resulting in Degraded Containment

Penetration.

Circulation Water Expansion Joint PM Program

The Surry response to NRC GL 88-20, IPE for Severe Accident

Vulnerabilities, identified a l.lE-3 per year CDF associated with

internal flooding*.

Several compensatory actions and plant modifications

were promptly implemented to reduce the likelihood and mitigate the

consequences of internal flooding.

NRC Inspection Report Nos.

50-280/91-31, 50-281/91-31, 50-280/91-33, and 50-281/91-33 documented

initial actions taken to address internal flooding.

VEPCO letter

92-299A dated October 30, 1992, reevaluated the CDF for internal

flooding at 2.3E-5 per year based upon completing planned modifications.

The turbine building SW and CW REJ inspection and replacement PM program

was a significant factor in reducing the CDF.

The inspectors reviewed

this program to determine whether appropriate actions were implemented

to maintain the reduced CDF associated with internal flooding.

3.2.1 PM Program Scope

The SW and CW REJ PM program included periodic inspections and

replacement PMs for 52 REJs located in the turbine building ..

The

inspectors reviewed system drawings, the PM scheduling data base,

procedure O-MCM-1003-01, Expansion Joint Removal, Inspection, and

Installation, revision 6, and recent WOs for completed REJ inspections.

The inspectors. concluded that O-MCM-1003-01 was well written and fully

incorporated vendor recommendations for external REJ inspections.

Recent exterior inspection results were documented in good detail and

the PM program scope incorporated all REJs which could be significant

contributors to turbine building flooding.

The inspectors observed that the PM program did not incorporate internal

REJ inspections which were recommended in the vendor manuals as a means

to detect symptoms of premature failure. A recent (December 1995)

catastrophic REJ failure at a similar nuclear power plant resulted from

internal erosion.

External inspections performed shortly before the REJ

failure had not identified symptoms of REJ degradation.

Internal

failure prior to external degradation was not previously considered as a

viable REJ failure mechanism in the Surry SW and CW REJ PM program.

The inspectors questioned whether external inspections alone were

adequate to properly evaluate REJ condition.

System engineers informed

,:

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10

the inspectors that internal inspections had been previously

recommended, but were not formally added to the PM program.

Informal

internal CW REJ inspections were performed during the last three

refueling outages with satisfactory results.

The inspectors reviewed

the last two Engineering Outage Summary Reports and confirmed that 13 of

the 24 CW REJs were internally inspected with no indication of

degradation.

The Maintenance Superintendent informed the inspectors

that PMs for internal REJ inspection were being developed and would be

added to the PM program based on the recent industry operating

experience review.

3.2.2 Current REJ Age/Condition

The twentyfour 96-inch CW REJs associated with the main condensers were

the largest in the PM program.

The inspectors reviewed completed work

documents and confirmed that 16 of these REJs (1-REJ-CW-lOOA/8/C/D,

1-REJ-CW-106A/B/C/D, 2-REJ-CW-200A/B/C/D, and 2-REJ-CW-206A/B/C/D) were

replaced during 1988-1989.

Purchase documents and engineering

evaluations specified an eight year service life for these REJs.

Based

on observed degradation, the remaining eight CW REJs (1-REJ-CW-

lOlA/B/C/D and 2-REJ-CW-201A/B/C/D) were replaced in 1992.

Purchase

documents specified a 10 year service life for these REJs.

The

procurement specifications precisely identified CW system configuration,

pressures, and CW water chemistry to which the REJs would be exposed.

Although the CW system is non-safety related, the CW REJs were procured

as safety related components to assure high quality standards were

maintained.

The inspectors concluded that good quality controls were

applied through the procurement and installation process. All 24 CW

REJs were within their vendor recommended service life period at the

close of this report period.

3.2.3 REJ Inspection/Replacement Status and Deferrals

The CW -REJ PM program was initially established in 1992 ~1th REJ

inspection required every RFO and REJ replacement required every five

RFOs.

The inspectors reviewed maintenance records and noted that over

60 percent of scheduled CW inspection PMs were deferred.

SW inspection

and replacement PMs were current.

Five of the oldest 16 CW REJs have

not been inspected since installation in the 1988-1989 timeframe.

Three

or the five CW REJs not inspected (1-REJ-CW-106A/B/C) will exceed their

specified service life prior to the next scheduled Unit 1 RFO.

The-inspectors expressed concern that an inordinate number of CW REJ PMs

were being deferred and that planning and evaluation for CW REJ

replacement prior to the end of specified service life appeared to be

slow.

Maintenance management informed the inspecto~s that the initially

established frequency for REJ inspection was too aggressive.

In

addition, each inspection required REJ flood shield removal which in

turn introduced some minor risk of flooding.

PM task evaluations were

processed in January 1996 to revise the inspection frequency to every

other RFO.

The -inspectors determined that the justification to revise

CW inspection frequency was adequate.

However, the inspectors noted

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that the PM task evaluation was approved without SNSOC concurrence.

VEPCO letter 93-163A, dated June 21, 1993, stated that future chang~s to

  • inspection and replacement activities will be made based on engineering

evaluation and be reviewed by the SNSOC as appropriate. This issue is

discussed further in the paragraph 3.2.5 below.

Replacement PMs for seven CW REJs and thre~ safety related SW REJs were

deferred in July 1995 using PM deferral 95-088.

Three of the CW REJs

will exceed their service life prior to the next Unit 1 RFO.

One

additional CW REJ (l-CW-REJ-1068) will exceed its service life prior to

the next Unit 1 RFO, but has not been deferred.

The inspectors reviewed

PM deferral 95-088 and noted that several deferred REJs had never been

inspected.

No Unit 1 CW REJ internal inspections had been documented at

the time the deferral was approved.

The inspectors concluded that the

PM deferral justification was weak.

The inspectors reviewed the PM database and observed that deferral 95-088 rescheduled the seven CW and three SW REJ replacements from 1995

to 2003 (RFO 19). Therefore the replacement PM for these REJs would not

come due for evaluation or performance for an additional eight years.

Additionally, l-SW-REJ-1028 which was not included in this deferral had

also been rescheduled for RFO 19.

The inspectors also noted that a

recent 1-CW-REJ-lOOA inspection PM had been closed to a replacement PM

(308591-01) which was deferred and therefore the inspection was not

performed.

Upon further follow-up the inspectors identified weaknesses

in PM deferral process.

The res pons i bil ity and method to specify the

next scheduled PM performance date was not clearly described in

VPAP-0803, Preventive Maintenance Program, revision 4, or consistently

understood within the Maintenance Department.

The inspectors reviewed

several more recent PM deferrals, and noted that maintenance engineers

had added a data field to their deferral justification which more

clearly specified the next scheduled date.

The new field clearly

identified the new performance date, but had not been incorporated into

VPAP-0803.

The inspectors discussed these observations with the

Maintenance Superintendent.

He informed the inspectors that the

inspectors' identified scheduling discrepancies had been corrected.

The

inspectors questioned whether additional PMs were improperly scheduled

in the PM data base.

The Maintenance Superintendent stated he would

consider reviewing this question.

The Unit 2 RFO is currently scheduled for May 1996.

Eight CW REJs were

due for replacement per the PM schedule.

Although the outage scope was

not finalized., the inspectors noted that no work orders had been written

or materials ordered for these jobs by mid-February.

The Maintenance

Support Supervisor informed the inspectors that the replacement PMs were

being reviewed for possible deferrals.

The inspectors questioned

whether there was sufficient lead time to procure replacement REJs and

plan the WOs in the event the deferrals were not justified. The REJ

replacement PMs represented a significant cost and work scope impact on

the RFO schedule.

Station management directed that the eight

replacement PM WOs be added to the Unit 2 RFO work scope.

The

Maintenance Superintendent informed the inspectors that these PMs would

12

be performed during the upcoming Unit 2 RFO unless an acceptable

technical basis for deferral was developed.

The inspectors determined

--that planning for the CW REJ replacements was-slow to develop.

Maintenance management appeared to be planning the RFO work scope to

exclude the CW REJ replacements prior to initiating the PM deferral

process.

Management resolution to add the PMs to the RFO work scope

pending deferral justification and approval was appropriate.

3.2.4 Level 1 Management SW And CW REJ PM Program Review

Engineering perso~nel had previously raised concerns regarding ihe

apparent large number of SW and CW REJ PM program deferrals.

Management

Level 1 review No. 1164 was performed to evaluate the SW and CW REJ

inspection/replacement PM program.

The inspectors discussed the Level 1

report with the Maintenance Support Department manager.

Recommendations

included (1) replace the eight scheduled CW REJs during the May 1996

RFO, (2) establish a formal PM for. CW REJ internal inspections, and (3)

contract the vendor to perform hydrostatic and destructive testing on

two removed CW REJs to provide additional data to support possible

service life extension.: The Level I report was scheduled for SNSOC.

review at the close of the inspection period.

In addition, maintenance

engineers initiated an operating experience review to assess

applicability from the December 1995 reported industry REJ failure

event.

During this inspection period station management also directed

station engineering to perform an independent SW and CW REJ PM program

review.

3.2.5 Conclusion

A Deviation from two commitments, contained in the June 21, 1993, letter

to the NRC, to reduce core damage probability from flooding, was

identified.

First, the licensee's letter stated that their REJ

inspection process would include manufacturer's recommendations.

Manufacturer's technical information recommended that an internal

inspection be included as an important element of an inspection pr6gram.

However, the formal preventive maintenance inspection program did not

include provisions for internal inspections of CW REJ.

The second

deviation involved SNSOC not reviewing changes to the inspection and

service life replacement program as committed.

Specifically, PM task

evaluations were processed in January 1996 to revise the inspection

frequency of the REJ to every other RFO and this PM task evaluation was

not reviewed by SNSOC as required.

This item is identified as

DEV 50-280, 281/96-02-03, Deviation from Commitments Involving Internal

Flooding.

The inspectors noted several conditions that warrant management's

attention.

Over half of CW REJ PMs have been routinely deferred.

Planning and evaluation for CW REJ replacements prior to the end of

their specified service life were slow.

Technical justification to

defer Unit 1 CW REJ replacements during the 1995 RFO was weak.

Several

PM deferrals were rescheduled to inappropriate dates. These conditions

in the PM deferral process may indicate inadequate controls for

3.3

13

scheduling PMs.

This issue is identified as URI 50-280, 281/96-02-04,

Review Preventive Maintenance Program Deferral Process.

Unit 2 Main Steam Non-Return Valve Repair

Each main steam header contains a NRV which functions as a check valve

to prevent reverse flow from the other SGs when a steam line break

occurs upstream of the NRV.

A motor operator provides backup capability

to shut the NRV from the control room in the event that the check valve

does not fully seat upon reverse flow.

The inspectors verified that the

NRVs were installed and functioned as described in the UFSAR.

On

February 26, during unit startup verifications, the supply breaker for.

NRV 2-MS-NRV-201A tripped while attempting to close the valve.

The SS

initiated a priority I WR to repair and retest 2-MS-NRV-201A.

This work

activity was a critical path item for unit startup.

The inspectors

interviewed personnel, reviewed work documents, and observed work

activities to evaluate the breaker repair.

El ect.ri ci ans meggered the valve motor with satisfactory results and

reset the NRV breaker.

The breaker tripped again when operators

attempted to shut the valve a second time.

Electricians observed that

motor current had remained within the breaker rating and determined that

the breaker should be replaced. A replacement breaker was tested and

installed using WO 337079 and procedure O-ECM-0306-02, Motof Control

Center Maintenance, revision 12.

The inspectors reviewed the WO,

discussed the job with the work crew, and observed breaker replacement

and retest activities. The WO contained appropriately detailed

instruction for the breaker repair. The electricians clearly understood

their work activities and performed the breaker replacement and PMT in

an acceptable manner.

Communications between the electricians and

control room operators during the PMT were good.

Procedure O-ECM-0306-02 is a general procedure which can be used to

perform maintenance on a variety of 480 volt MCC cubicals, breakers, and

thermal overload devices.

The work crew initiated a PAR to modify the

overload trip device test duration and manual valve positioning

requirements specified in O-ECM-0306-02.

The PAR process may be used to

implement procedure changes in a shorter time period than is needed by

the formal procedure revision process.

Both procedure changes and

procedure revisions are discussed in VPAP-0502, Procedure Process

Control, revision 7.

The proposed changes were intended to shorten the

work activity duration by several hours.

The inspectors determined that

the PAR was technically justified for the 2-MS-NRV-201A repair activity.

The work crew demonstrated good initiative to develop the PAR and

processed the procedure change in accordance with VPAP-0502.

The category B procedure change was authorized by the Maintenance

Superintendent.

The inspectors questioned who else was authorized to

approve this Category B (change of intent) procedure change.

The

electrical supervisor informed the inspectors that either the

Maintenance Superintendent, the designated MMOC in the absence of the

Maintenance Superintendent, or SNSOC could approve the change.

The

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3.4

3.5

14

MMOCs, who was identified by the crew as an acceptable approval

authority was.not on the SNSOC approved manager list to approve Category

-B PARs.

The Maintenance Superintendent st~ted that he would reemphasize

his PAR approval expectations with all department personnel.

SNSOC also

revised the approved manager list to permit MMOCs who are qualified as

Maintenance Department SNSOC alternates to approve Category B PARS/ The

inspectors concluded that these actions were adequate to ensure proper

procedure revision approval.

Maintenance engineers determined that the 2-MS-NRV-201A breaker thermal

trip element had degraded due to age.

This breaker was original plant

equipment.

PM schedulers informed the inspectors that non-safety

related molded case circuit breakers, such as 2-MS-NRV-201A, are not

included in the PM program.

The Maintenance Superintendent informed the

inspectors that this item would be evaluated as part of an ongoing

breaker PM scope review.

The inspectors determined that this action was

appropriate.

Inoperable Unit 1 PZR PORVs

At 6:42 a.m. on February )o, the PZR PORV low air pressure alarm was

received in the Unit I control room.

Operators declared both PORVs

inoperable and shut the PORV block valves as required by TS 3.1.A.6.b.

Technicians promptly entered containment and determined that the

pressure regulator from the backup air supply bottles to PZR PORV

I-RC-PCV-1456 had failed.

The unaffected PORV was promptly restored.

The regulator failure caused the air line relief valve to lift and

depressurize the air bottles.

WO 336760 was initiated to replace

I-IA-PCV-102 and return the backup bottle air supply system to service.

The inspectors observed work activities to evaluate repair timeliness

and effectiveness.

The inspectors reviewed WO 336760 and attended the work prebriefings~

Briefings were detailed and radiological considerations were clearly

understood by the work crew.

Technicians also prepared contingency

materials to replace the downstream relief valve, l-IA-RV-127, in the

event it failed to properly reseat. After replacing l-IA-PCV-102

technicians pressurized the air line and determined that the relief

valve had not fully reseated.

The relief valve was promptly replaced,

l-IA-PCV-102 was adjusted, and l-RC-PCV-1456 was restored to service.

Coordination between maintenance and operations personnel was good.

The

inspectors concluded that repairs to the PORV backup air system were

well planned and completed in a timely manner.

Maintenance personnel

demonstrated good foresight to preplan the relief valve replacement as a

contingency.

Elevated Normal Switchgear Room Temperatures

Four DRs initiated during this report period identified elevated

temperatures in the Unit 1 normal switchgear room.

Room temperature

reached a high of 94 degrees on March 5.

Room temperatures exceeded 90

degrees F again on March 14 when the Unit I normal switchgear room air

15

conditioning unit became inoperable.

Prolonged exposure to elevated

temperatures had previously degraded CRD circuit cards which

- necessitated two manual reactor trips in 1995.

Corrective actions

included CRD circuit card replacements, circuit card testing, and

planned ventilation modifications. Spot coolers were installed in May

1995 as a temporary modification to supplement normal room cooling to

the CRD power cabinets.

The inspectors verified that the spot coolers

continued to operate throughout this report period.

The inspectors

reviewed the scheduling status for the planned permanent air

conditioning upgrade to determine whether appropriate actions were being

taken prior to the onset of the hot weather period.

DCP 95-19 was written to upgrade the Unit 1 and Unit 2 normal switchgear

room air conditioning capacity to 80 tons per room.

WOs 333007 and

333008 were written to implement the air co~ditioning upgrade.

The

inspectors walked down the intended modification in the field and

discussed WO status with work planners and schedulers.

Materials for

DCP 95-19 were scheduled to arrive on-site on March 16 and work was

scheduled to begin the following week.

Planners estim~ted that the work

would take eight weeks to complete, with projected completion in mid May

1996.

The inspectors concluded that the schedule to complete the air

conditioning upgrade by mid May was adequate.

Although warm

temperatures may be experienced earlier, the temporary spot coolers and

existing temperature monitoring during operator tours is adequate for

that period.

Planners were knowledgeab1e regarding ventilation system

design.

3.6

Unit 2 Reactor Coolant Pump Motor Oil Leak

On March 5, electricians entered containment to investigate a RCP IA oil

reservoir hi-low level alarm.

RCP upper thrust bearing temperature

remained normal.

Technicians observed that oil level was low and added

21 gallons of oil to restore the reservoir to the normal indicated

level.

The same RCP motor experienced oil loss and elevated upper

thrust bearing temperatures in December 1995 as documented in NRC

Inspection Report Nos. 50-280/95-23 and 50-281/95-23.

The inspectors

monitored licensee actions to evaluate and address the RCP oil loss.

After reviewing related maintenance history and discussions with the

vendor, the ongoing RCE team determined that an active RCP IA oil leak

existed.

Further, the RCP IA oil level indicator and low level alarm

were unreliable due to suspected partial blockage in a level standpipe

drain hole.

While each continued to provide some information, accuracy

was questionable and results were not always repeatable.

The inspectors

noted that the RCP oil leak rate appeared to have increased following

the RCP IA start on February 25 during the preparations for unit

startup.

The RCE team postulated that the most likely locations for a

leak were associated with the RCP bearing lift pump supply line from the

upper RCP oil reservoir or the oil cooler.

Subsequent observations and

oil additions confirmed that the leak rate had changed from 0.3 gpd to

about 2.5 gpd.

3.7

16

A separate RCP oil leak issue team was established and SE 96-021 was

written to evaluate continued reactor operation with the existing RCP IA

- oil leak.

The evaluation considered the leak -rate, compensatory

measures including increased RCP bearing temperature monitoring,

remaining volume available in the RCP oil collection tank, and ability

to add oil to the RCP upper oil reservoir. Management concluded that an

unreviewed safety question did not exist.

The inspectors determined

that SE 96-021 was technically sound.

The issue team determined that based on the existing leak rate, the oil

collection tank did not have sufficient volume to support continued RCP

operation beyond mid-March.

The team established a plan of action to

install a TM to drain the oil collect tank, perform inspections to

verify the leak location, and add oil to maintain sufficient bearing

cooling.

The inspectors observed team activities and discussed the leak

identification plan with the team.

The team maintained a good focus on

both equipment and personnel safety.

RWP 96-2-1129 was established to support RCP oil leak investigation and

associated maintenance activities.

Eleven containment entries wire made

from March 4 through March 13.

Reactor power was temporarily reduced to

30 percent to reduce personnel exposure during a series of five entries

on March 13.

Radiation levels in the vicinity of the oil collection

tank were reduced by a factor of 3. Total personnel exposure for this

job during the March 4-13 period was 3.247 REM.

The inspectors reviewed

the RWP, discussed radiological precautions with workers, and concluded

that the work activities were well planned with appropriate

considerations for personnel exposure.

On March 13, electricians identified a packing leak from a drain valve

on the oil supply line from the RCP upper oil reservoir to the lube oil

cooler.

The packing was tightened which reduced the oil leakrate. Oil

was drained from the collection tank and eight gallons of oil was added

to restore normal upper reservoir level. Operators plan to continue

enhanced bearing temperature monitoring and the team plans to continue

oil leak evaluation. Outage plans were modified to schedule the RCP IA

motor for replacement during the upcoming Unit 2 refueling outage.

The

inspectors concluded that the RCP oil leak issue team performed

effectively to evaluate the oil leak and initiated appropriate

corrective action.

Recirculation Mode Transfer Relay Replacement

On March 9, during the performance of procedure l-PT-8.6, RMT Logic,

revision 7, several unanticipated annunciators were received and relay

actuation were heard when the test switch was being manipulated to test

the-channel 1 and 3 matrix.

Testing was stopped to evaluate the

discrepancy.

The licensee determined that the channel 1 RWST level

relay R-CS-100A2 was not functioning properly.

The channel was declared

inoperable and the channel was placed in bypass per TS Table 3.7-2

Action 7.a .

3.8

3.9

17

Relay R-CS-100A2 was replaced on March 12 per WO 00337953.

The

inspectors reviewed the WO, the associated 50.59 evaluation to place the

~ssociated RMT mode switch in Refuel during the relay replacement, ~nd

observed work activities in progress.

The inspectors also verified that

the associated TS requirements and post maintenance testing activities

were met.

The work activity was accomplished in accordance with the WO

instructions and the 50.59 evaluation adequately justified placing the

RMT mode switch in Refuel.

Service Water Valve 2-SW-331 Replacement

On March 12, the licensee replaced valve 2-SW-331 due to seat leakage.

Valve replacement required that one of two service water flow paths to

the charging pump service water subsystem and the main control and

emergency switchgear room air conditioning condensers be removed from

service.

The maintenance activity placed both units in a 24-hour LCO

action statement per TS 3.14, Circulating and Service Water Systems.

The LCO action statement was entered at 4:58 a.m. on March 12.

Valve

2-SW-331 was replaced and the service water system was returned to

service at 1:05 p.m. on March 12.

The inspectors monitored the valve

replacement activities, verified that the TS requirements were met and

verified that the system isolation was adequate.

The work activity was

well coordinated and was expeditiously completed to return the service

water system to service .

The inspectors reviewed UFSAR section 9.13.3.6, Control Room and Relay

Room Ventilation.

During the review the inspectors determined that the

UFSAR did not describe the system as presently configured.

The UFSAR

stated that three refrigeration chillers serve the ventilation system

and that all three chillers are located in MER-3.

The actual

configuration of the refrigeration chillers had been modified by a

design change to add two additional chillers located in a ~eparate MER

called MER-5.

This design change added redundancy and separation to the

refrigeration chiller system.

This item was identified to the licensee

for resolution.

The licensee stated that an UFSAR change was being

pursued to change the UFSAR section but had not been completed prior to

the inspectors review.

The licensee presently plans to submit the UFSAR

change in April 1996.

Station Battery 2A Test

On February 29, the inspectors observed the performance of procedure

O-EPT-0104-01, Semi-Annual Station Battery Test, revision 2, conducted

on station battery* 2A.

This surveillance procedure implements the

requirements of TS 4.6.C.1.d.

TS 4.6.C.1.d requires that twice a year,

during normal operation, the battery charger be turned off for

approximately five minutes and the battery voltage and current be

recorded at the beginning and end of the test. The TS states that the

test shall be considered satisfactory if the new data when compared to

the old data indicates no signs of abuse or deterioration and the

battery performs within acceptable limits as established by the

manufacturer's discharge characteristic curves.

The inspectors verified

18

that the activity was accomplished in accordance with the procedure and

that the data was recorded as required.

The system engineer reviewed

the data 1mmediately following the performance of the procedure and

stated that the values obtained were consistent with previous tests and

that no battery degradation had occurred from the previous performance

of the procedure.

The inspectors reviewed UFSAR Section 8.4.4, 125V Direct Current System,

and Section 8.6, Tests and Inspections.

The inspectors determined that

the UFSAR *adequately described the 125 VDC system with respect to the

semi-annual battery test.

One violation and one deviation was identified.

4.0

ENGINEERING (37551)

4.1

Unit 2 PZR Heater Capacity Evaluation

On February 24, PZR heaters 64, 65, and 66 were determined to be

inoperable due to an electrical ground.

Due to these heater failures,

the heater output available from the J emergency bus was reduced to 150

KW.

This was less than the 200 KW heater design capacity identified in

UFSAR section 4.2.2.2.

SE 96-114 was prepared to assess continued

operation and reactor startup with the three PZR heaters inoperable.

The inspectors attended the SNSOC SE review to determine whether the

evaluation scope and conclusions were appropriate.

TS 3.1.A.5.a requires at least 125 KW of heaters be available from an

emergency bus to assure natural circulation capability during a loss of

off-site power event.

In response to NUREG-0737, Clarification of TMI

Action Plan Requirements, the licensee committed to maintain at least

125 KW PZR heater capacity available on each emergency bus (Hand J

buses).

The SE noted that the remaining PZR heater capacity satisfied

license requirements and sufficient heater capacity would be available

to maintain natural circulation in the event either the J or H emergency

bus became deenergized.

The remaining PZR heaters can be isolated from

the main control room and controlled from the alternate shutdown panel.

Therefore the capability to establish natural circulation and achieve

safe shutdown conditions following a fire was maintained.

The SNSOC

concluded that continued operation with 150 KW heater capacity on the

J emergency bus satisfied license requirements and did not pose an

unreviewed safety question.

The inspectors-determined that SE 96-114

was technically sound and that the SNSOC reviewed the issue in

appropriate detail.

No violations or deviations were identified.

5.0

PLANT SUPPORT (71750)

The inspectors conducted facility tours, work activity observations,

personnel interviews, and documentation reviews to determine whether

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license programs met regulatory requirements in the areas of oversight,

radiological *protection, security and fire protection.

Nuclear Oversight Corrective Action Process

The Surry Station Nuclear Oversight Organization was established

November 1, 1995, as part of the Virginia Power QA reengineering

project.

The station organization consists of the Director, nine

auditors who perform formal audits as directed by the VEPCO audit

coordinator, and four nuclear specialists.

VPAP-1801, Nuclear Oversight

Internal Audit Program, revision 3, provides guidance for QA audit

finding resolution.

However, specialists do not perform audits.

The

inspectors have monitored nuclear oversight specialist activities and

noted that the specific roles, responsibilities, and oversight processes

are not formally defined.

The inspectors observed that nuclear

specialists have actively tracked day to day performance in the field,

but questioned how specialists initiated and tracked corrective actions

to problems which they observed.

The inspectors met with the Director SNOS, to discuss the methods by

which SNOS resolves observed performance problems.

Currently,

specialists track performance observations using the QATTS system and

meet with the Director SNOS weekly to discuss perceived weaknesses or

trends.

The Director SNOS then drafts a list of current oversight

issues and informally discussei them with the Station Director weekly .

Specialists formally use the DR process to initiate corrective actions

for significant problems they identify.

The inspectors noted that DR

corrective action closure does not require SNOS involvement and

questioned how SNOS tracks issue closure.

The Director SNOS said that

as a temporary measure, he and the specialists currently review all DR

closures for issues they initiated. The inspectors determined that

although this practice was not proceduralized, corrective action closure

was adequately tracked.

The Director SNOS stated that oversight roles and processes were in

transition and that procedures would be formalized shortly.

VPAP-1601,

Corrective Action, revision 3, and VPAP-1801 are being revised to

specifically provide an independent process for SNOS specialists to

initiate corrective action to oversight issues and to escalate findings

as needed.

A new SNOS department procedure is being written to define

the oversight mission, specialist responsibilities, and internal

processes to identify and resolve oversight issues and observations.

The inspectors reviewed recent*oversight issues with the Director SNOS

and concluded that the issues being identified indicated a good level of

oversight involvement.

Processes being developed to better define SNOS

activities including methods to independently initiate and track

corrective actions were appropriate.

The revised procedures for Nuclear Oversight are anticipated to be

issued and implemented in early Spring.

MSRC members recently discussed

the QA reorganization with the inspectors and with station management.

The station director indicated that nuclear oversight organization

20

effectiveness would be independently evaluated prior to implementing the

next stages of the Vision 2000 reengineering program at Surry Station.

  • This would be done to ensure the oversight organization was ready to

provide appropriate independent assessment during further organizational

transition.

The inspectors concluded that this decision was appropriate

to maintain sound independent oversight capability.

No violations or deviations were identified.

6.0

REVIEW OF UFSAR COMMITMENTS (61726, 71707)

A recent discovery of a licensee operating their facility in a manner

contrary to the UFSAR description highlighted the need for a special*

focused review that compares plant practices, procedures, and/or

parameters to the UFSAR descriptions. During this inspection period

(February 11 through March 23, 1996) the inspectors reviewed the

applicable sections of the UFSAR that related to the inspection areas

discussed in this report to ensure that UFSAR wording was consistent

with the observed plant practices, procedures, and/or parameters. Jhe

following inconsistencies were noted:

UFSAR section 9.13.3.6, Control Room and Relay Room Ventilation,

stated that three refrigeration chillers serve the ventilation

system and that all three chillers are located in MER-3.

The

actual configuration of the refrigeration chillers had been

modified by a design change to add two additional chillers located

in a separate MER called MER-5.

This design change added

redundancy and separation to the refrigeration chiller system.

The licensee stated that an UFSAR change was being pursued to

change the UFSAR section but had not been completed.

The licensee

presently plans to submit the UFSAR change in April 1996.

UFSAR Table 5.2.1.b, describes containment penetration No. 24

containment isolation barriers. The outside containment isolation

valve, 2-RH-MOV-200, is described as~ motor operated gate valve.

The motor has been electrically disconnected and this valve is now

a manually operated gate valve.

This inconsistency also exists in

Table 5.2.1.a for the Unit 1 application.

The licensee was

notified of this minor UFSAR discrepancy for their resolution.

7.0

OTHER NRC PERSONNEL ON SITE

On February 13, the NRC Chairman, Dr. Shirley A. Jackson, visited the

site. Dr. Jackson toured the plant, met with licensee management and

the inspectors to discuss plant status and current issues at the

facility and held a press conference.

There were no local officials in

attendance.

Dr. Jackson was accompanied by members of her staff and the

Region II Regional Administrator, Mr. Stewart Ebneter.

On March 8 and 9, Mr. B. Buckley, Senior Project Manager, NRR, and

E. Imbro, Project Director, NRR, were on site to review the design basis

for spent fuel storage and corp off-load practices.

-. *

8.0

9.0

21

On March 19, Mr. W. Gloersen, a Region II inspector, and a three man

NMSS Team visited the site for the purpose of touring the Independent

-Spent Fuel Storage Installation and to review cast loading and unloading

practices and procedures.

On March 21, Mr. J. Johnson, Deputy Director of Reactor Projects, and

Mr. G. Belisle, Branch Chief, both from Region II, visited the site.

Mr. Johnson and Mr. Belisle toured the plant and met with licensee

management and the inspectors to discuss plant status and current issues

at the facility.

While on site, Mr. Johnson and Mr. Belisle attended

the IPAP exit.

On March 21, Mr. P. Koltay, IPAP Team Leader, visited the site for the

purpose of conducting the IPAP exit.

EXIT

The inspection scope and findings were summarized on March 27, 1996, by

M. W. Branch with those persons indicated by an asterisk in paragraph 1.

The inspectors d~scribed the areas inspected and discussed in detail the

inspection results.

On April 18, 1996, M. W. Branch discussed the NCV

with the Assistant Station Manager for Operations and Maintenance. A

listing of inspection findings is provided.

Proprietary information is

not contained in this report.

Dissenting comments were not received

from the licensee .

~ Item Number

Status

Description and Reference

NCV

50-280, 281/96-02-01

Closed

Inadequate Unit Startup and

Operating Procedures

(paragraph 2.4)

VIO

50-281/96-02-02

Open

Failure to Follow Procedures

Resulting in Degraded

Containment Penetration

(paragraph 3.1.6).

DEV

50-280, 281/96-02-03

Open

.Deviation From Commitment to

Reduce Probability of Cor0

Damage From Flooding

(paragraph 3.2.5).

URI

50-280, 281/96-02-04

Open

Review Preventive Maintenance

Program Deferral Process

(paragraph 3.2.5).

ACRONYMS

ASME

AMERICAN SOCIETY OF MECHANICAL ENGINEERS

ASM

ASSISTANT STATION MANAGER

CFR

CODE OF FEDERAL REGULATIONS

CDF

CORE DAMAGE FREQUENCY

i I

I

I I

I

,I

"

1

f *

22

CRD

CONTROL ROD DRIVE

cw

CIRCULATING WATER

DEV

DEVIATION

DC

DEFICIENCY CARD

DCP

DESIGN CHANGE PROGRAM

DR

DEVIATION REPORT

ECCS

EMERGENCY CORE COOLING SYSTEM

F

FAHRENHEIT

GL

GENERIC LETTER

GOP

GENERAL OPERATING PROCEDURE

GPO

GALLONS PER DAY

!PAP

INTEGRATED PERFORMANCE ASSESSMENT PROCESS

IPE

INDIVIDUAL PLANT EXAMINATION

JCO

JUSTIFICATION FOR CONTINUED OPERATION

KW

KILOWATT

LCO

LIMITING CONDITION FOR OPERATION

MCC

MOTOR CONTROL CENTER

MER

MECHANICAL EQUIPMENT ROOM

MMOC

MAINTENANCE MANAGER ON CALL

MSRC

MANAGEMENT SAFETY'.~EVIEW COMMITTEE

NOE

NONDESTRUCTIVE EXAMINATION

NMSS

NUCLEAR MATERIALS SAFETY & SAFEGUARDS

NRC

NUCLEAR REGULATORY COMMISSION

NRV

NONRETURN VALVE

PAR

PROCEDURE ACTION REQUEST

PDR

PUBLIC DOCUMENT ROOM

PM

PREVENTIVE MAINTENANCE

PMT

POST MAINTENANCE TEST

PORV

POWER OPERATED RELIEF VALVE

Psig

POUNDS PER SQUARE INCH GAGE

PZR

PRESSURIZER

QA

QUALITY ASSURANCE

QPT

QUADRANT POWER TILT

QATTS

QUALITY ASSURANCE TRACKING AND TRENDING SYSTEM

RCA

RADIATION CONTROL AREA

RCE

ROOT CAUSE EVALUATION

RCP

REACTOR COOLANT PUMP

RCS

REACTOR COOLANT SYSTEM

REJ

RUBBER EXPANSION JOINT

REM

ROENTGEN EQUIVALENT MAN

RFD

REFUELING OUTAGE

RHR

RESIDUAL HEAT REMOVAL

RMT

RECIRCULATION MODE TRANSFER

RO

REACTOR OPERATOR

RWP

RADIATION WORK PERMIT

RWST

REFUELING WATER STORAGE TANK

SCFH

STANDARD CUBIC FEET PER HOUR

SE

SAFETY EVALUATION

SG

STEAM GENERATOR

SNOS

STATION NUCLEAR OVERSIGHT

SNSOC

STATION NUCLEAR SAFETY AND OPERATING COMMITTEE

SRO

SENIOR REACTOR OPERATOR

.

. ,....;-,

'1 *

ss

SW

TM

TMI

TS

UFSAR

URI

UT

voe

VEPCO

VIO

VPAP

WO

WR 23

SHIFT SUPERVISOR

SERVICE WATER

TEMPORARY MODIFICATION

THREE MILE ISLAND

TECHNICAL SPECIFICATION

UPDATED FINAL SAFET°Y ANALYSIS REPORT

UNRESOLVED ITEM

ULTRASONIC TEST

VOLT DIRECT CURRENT

VIRGINIA ELECTRIC AND POWER COMPANY

VIOLATION

VIRGINIA POWER ADMINISTRATIVE PROCEDURE

. WORK ORDER

WORK REQUEST