ML18152A032

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Initial SALP Repts 50-280/92-10 & 50-281/92-10 for Stated Period Ending 920404.Major Areas Evaluated:Plant Operations, Radiological Controls,Emergency Preparedness,Maint/ Surveillance,Security & Engineering/Technical Support
ML18152A032
Person / Time
Site: Surry  Dominion icon.png
Issue date: 06/09/1992
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A033 List:
References
50-280-92-10, 50-281-92-10, NUDOCS 9207020238
Download: ML18152A032 (30)


See also: IR 05000280/1992010

Text

"

--*----(-~- -**

. - __ * ..... -_ .... -****- '--'-----,-*.

ENCLOSURE

INITIAL SALP REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION II.

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT NUMBER

50-280,281/92-10

VIRGINIA ELECTRIC AND POWER COMPANY

SURRY UNITS 1 AND 2

FROM MARCH 31, 1991 THROUGH APRIL 4, 1992

9207020238 920609

PDR

ADOCK 05000280

G

PDR

  • \\

I.

II.

III.

IV.

v.

TABLE OF CONTENTS

INTRODUCTION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

SUMMARY OF RESULTS

Overview

.......

. . . . . . . .

1

3

CRITERIA. .................*.*....... *-.................... . 3

PERFORMANCE ANALYSIS ........ .

A.

Plant Operations ****.*...******

B.

Radiological Controls

. . . . . . . . . . . .

C.

Maintenance/Surveillance ************

D.

Emergency Preparedness *..***.

E.

Security ............................ .

F.

Engineering/Technical Support ***.

G.

Safety Assessment/Quality,Verification

  • * * * 4
  • * * * 4

7

  • * * * * * * * * * * * * 9

. ....*...**... 14

. ........ . 16

  • *** 17
      • 21

SUPPORTING DATA AND SUMMARIES ***..***.**..***********..** 2 5

A.

Major Licensee Activities **.***.**.*.*********. 25

B.

Major Direct Inspection and Review Activities ****** 26

c.

Escalated Enforcement Action.................

.26

D.

Licensee Conferences Held During Appraisal Period ** 26

E.

Confirmation of Action Letters..

  • *** 27

F.

Review of Licensee Event Reports

    • .*

.27

G.

Licensing Activities......

. **..*************.* 28

H.

Enforcement Activity

  • .
    • ...*.
  • ****** 28

I.

Reactor Trips * * * . * * .

. . * * *

  • *
  • * * *
  • *.* 28

,; '

-.\\

I.

-~ ** *--,-"'* -*-- *** -'---~-*-*~- --**-----'-~- ~._._.- ~-- --

-~.~-*-* *----**-U ~* . -*

lNTRODUCTION

The Systematic Assessment of Licensee Performance (SALP)

program is an integrated* Nuclear* Regulatory Commission (NRC) *

staff effort to collect available observations and data on a

- periodic basis and to evaluate licensee performance on the

basis of this information~

The SALP program is supplemental

to normal regulatory processes used to ensure compliance.*

with NRC rules and regulations. It*is intended*to.be

sufficiently diagnostic to provide a rational basis for

allocation of NRC resources and to provide meaningful

feedback to the licensee's management regarding the NRC

assessment of their facility's .performance in each

functional area. *

An NRC SALP Board, composed of the staff members listed

below, met on May 5, 1992, to review the observations and

data on performance and to assess licensee performance in

accordance with Chapter NRC-0516, "Systematic Assessment of

L;i.censee Performance."

,

This report is the NRC's assessment of the licensee's safety

performance at Surry for the period March 31, 1991 through

April 4, 1992.

The SALP Board for Surry Units 1 an~ 2 was composed of:

L.A. Reyes, Director, Division of Reactor Projects

(DRP), Region II (RII)

E.W. Merschoff, Deputy Director, Division of Reactor

Safety, RII

B. s. Mailett, Deputy Director, Division of Radiation

Safety and Safeguards, RII

M. V. Sinkule, Chief, DRP Branch 2, RII

M. w. Branch, Senior Resident Inspector, Surry, DRP,

RII

H. N. Berkow, Project Director, Directorate,. II-2,

Office of Nuclear Reactor Regulation (NRR)

B. c .. Buckley, Senior Project Manager, Surry, NRR

Attendees at SALP Board Meeting

P. E. Fredrickson, Chief, DRP Section 2A, RII

A. B. Ruff, Project Engineer, DRP Section 2A, RII

Regional based inspectors and supervisors attended

discussion for the applicable functio~al area.

II.

SUMMARY OF RESULTS

Surry was operated in a safe manner during the assessment

period.

The Plant Operations functional area improved to a

superior level of performance and the Radiological Controls,

2

Emergency Preparedness and Security areas continued to

perform at the superior level.

The improving performance

trend in the Safety Assessment/Quality Verificat.ion area

which was evident during the last assessment period did not

continue during this period.

Both the Engineering/Technical

Support and the Maintenance/Surveillance functional areas

remained at a good performance level~

Several activities

affected more than one functional area.

Material condition

directly impacted the Maintenance/Surveillance functional**

area and indirectly affected other areas such as Plant

Operations.

The upgraded procedures are a definite

improvement.

Some procedure upgrade efforts still lag

others as noted in the Plant Operations and

Maintenance/surveillance areas.

Performance in the Plant Operations area improved to a

superior level, primarily due to the management commitment

to safe operations and to the operators' excellent

performance and their low threshold in identifying problems.

Other contributors were improved plant housekeeping, the

continued innovative use of computer systems and the overall

improvement in operations procedures.

Performance in the Radiological Controls area remained at a

superior level as a result of several contributors.

Management provided strong support to the radiation

protection (RP) program.

Both health physics (HP) and

station personnel worked in concert to reduce the number of

personnel contaminations.

Job planning and w_orker /HP

involvement also continued to reduce the collective dose.

In addition, the new radwaste building contributed to the

high level of performance by significantly reducing the

amount of effluent released from the site.

Improvements in the Maintenance/Surveillance area

performance were noted.

However, when contrasted with

needed material improvements, the overall performance

remained constant.

Although the maintenance backlog

improved from the last period, as did the performance of the

outage and Planning Department, several problems continued

from the last period and contributed to reduced performance.

Specific continuing problems were the prioritization_of

procedures needing upgrading and the slow improvement of the

station's material condition.

Direct management involvement contributed to the continued

superior performance in the Emergency Preparedness

functional area.

This was demonstrated by the ability to

maintain both personnel and facilities ready for any station

emergency.

Performance in the Security area was also maintained at a

superior level.

The professionalism and dedication of the

3

security personnel contributed significantly to this effort.

Prompt response-to identified security problems also

contributed to the high performance level.

Engineering/Technical support performance varied.

Notable

strengths were the motor operated valve (MOV) program,

engineering outage support, and the overall good

communication between Engineering arid other departments.

Areas where improvement was needed included setpoint control

and sensitivity to the potentially serious effects of

station internal flooding.

The improving performance trend noted at the end of the last

assessment_period was not sustained in the Safety

Assessment/Quality Verification functional area during this

period.

Several activities, such as the self-assessment

program and resolution of licensee-perceived safety-

significant issues, remained at a high level of performance.

However, the continued difficulty of resolving recurring

problems detracted from the previous improving trend.

Overview

Performance ratings assigned for the last assessment period

and the current period are shown below.

Functional Area

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency Preparedness

Security

Engineering/Technical

Support

Safety Assessment/

Quality Verification

III. CRITERIA

Rating Last

Period

2 Improving

1

2

1

1

2

2 Improving*

Rating This

Period

1

1

2

1

1

~

2

The evaluation criteria which were used, as applicable, to

assess each functional area, are described in detail-in NRC

Manual Chapter 0516.

This Chapter is in the Public Document

Room files.

Therefore, these criteria are not repeated

here, but will be presented.in detail at the public meeting

to be held with the licensee management.

. I

IV. PERFORMANCE ANALYSIS

A.

Plant Operations

1.

Analysis

4

This functional area addresses the control and performance

of activities directly related to operating the units,

including fire protection.

Unit 1 operated in an excellent manner during the assessment

period. The unit completed a. run of 379 days of continuous

operation.

The unit experienced two turbine runbacks and

one manual reactor trip during the period.

At the end of

the assessment period the unit was in the middle of a

scheduled 64 day refueling outage.

Unit 2 operated inconsistently throughout the assessment

period due to equipment-related problems.

Equipment

problems resulted in: l)delaying plant startup following a

refueling outage, 2)two automatic reactor trips (one with

safety injection), 3)four forced outages, and 4)two turbine

runbacks.

Overall ope~ator performance was good, with few personnel

errors.

Early in the assessment period, the licensee

identified several operator errors that occurred during the

Unit 1 outage which were attributed to a lack of attention

to detail and sensitivity to control of plant configuration.

The errors included- failure to tag out the correct emergency

diesel generator {EDG) fuel transfer pump, failure to sample

service water (SW) to a component cooling water heat

exchanger, and failure to properly control the emergency

ventilation system configuration.

Operation's management

involvement in review of these events and actions

implemented were effective in improving operator perfor-_

mance.

Throughout the remainder of the period operator

errors were minimal.

Good communications and self-checking

techniques were typical among operations personnel, and

communications between operations and other departments were

also good.

Systems that required maintenance were properly

isolated, returned to service and tested.

Operators had a low threshold_for identifying problems.

Station deviations were-written by operators whenever they

perceived plant problems or whenever personnel actions were

questionable.

Operators continued to respond to events in an excellent

manner.

Operators responded to two automatic reactor trips,

one manual reactor trip and four turbine runbacks~promptly

and conservatively.

Although the turbine runbacks were

challenging, the operators were able to safely maintain the

5

unit at power when responding to the runback events.

Also,

operator actions were good during unit startups, shutdowns

and reduced inventory conditions.

Shift licensed staffing levels continued to be a

strength.

Operating shifts were staffed with a minimum

of four senior reactor operators (except that one shift

had three SROs) and five reactor operators which was

well in excess of Technical Specifications (TS) and 10

CFR 50.54 minimum staffing requirements. Operator

turnover was very low. Overtime worked by licensed and

non-li.censed operators was not excessive and was

closely monitored by management.

At the end of the

assessment period operator*working conditions were

improved by consolidation and upgrading Operations

Department work areas.

The emergency operating procedures (EOP) were updated this*

assessment period to rectify inconsistence that were

identified during the previous assessment period.

The

updated EOPs aided to the operators in responding to events.

The fire protection program was well implemented*.

Fire

brigade and control room staffing for alternate safe

shutdown for fire events were considered effective.

Procedures for implementing the fire protection program were

good; however, a weakness in station policy was identified

involving control of boundary doors for areas protected with

a carbon dioxide fire suppression system *. On two occasions

station personnel identified doors that were improperly

blocked open without a fire watch being stationed, as

required by TS. - This was satisfactorily resolved by

installing signs on*the doors warning personnel that the

doors require special controls when opened.

Housekeeping throughout the plant was generally good during

the assessment period.

This area was identified as. a

challenge during the previou~ assessment period.

Management's commitment to improve standards was evident as

the station's painting program progressed into the diesel

generator rooms and charging pump cubicles.

Housekeeping in

the condensate polishing building, boric acid flats,-turbine

building and auxiliary building was improved by repainting

walls and refinishing floors.

The refinishing of floors

occas.ionally _ resulted in poor .. housekeeplng in adjacent

areas.

Increased management attention, however,

subsequently improved housekeeping in these areas as well.

Housekeeping in the _fuel pool area was excellent.

Management demonstrated a strong commitment to safe

operations throughout the assessment period.

This was

clearly evident by the continued support of policies and

programs implemented.in this and previous assessment periods

L

6

in the areas of decision making, minimizing control room

annunciators, configuration management, *upgraded procedures,

and development of computer programs.

These policies and

programs are discussed in the following.paragraphs.

Generally, management made conservative decisions for

plant operations. -On one occasion Unit 2 was

voluntarily shutdown to repair reactor coolant system

leakage prior to approaching the TS reactor coolant

system leakage limit.

On another occasion a Unit 2

outage was extended in order to perform a modification

that improved plant safety and reduced reliance on

operator compensatory actions._ Occasionally, however,

manual operator actions were used to aid in the

operation of components in *1ieu of promptly repairing

the component.

The station policy to maintain a "black board" condition for

control room annunciators was generally effective in

minimizing the number of lit control room indicators.

Plant component labeling problems were identified in

previous assessment periods.* The Configuration Management

Program to identify and relabel safety related and nonsafety

related plant equipment, initiated during the previous

assessment period, was on schedule.

The majority of the

verification walkdowns were complete and the actua,l labeling

_of plant equipment has commenced with the initial

concentration on the new radwaste facility and then on the

Unit 1 containment.

The program's overall completion date

is scheduled for March 1993.

Also, no problems were noted*

with the use of control room critical drawings during the

~ssessment period.

Operations Department procedures were generally good.

At

the end of the assessment period, the operations portion of

the Technical Procedure Upgrade Program (TPUP) was

approximately one-third complete, which exceeded program

goals.

This program was closely monitored by management.

Reports were routinely issued to keep management informed of

program status and station personnel were surveyed quarterly

in order to evaluate program effectiveness.

Plant startup

and reduced inventory procedures were examples of quality

procedures.

However, procedures that had not been upgraded

were identified as-being --inadequate and contributed to

problems in the areas of high oxygen concentration in the

waste gas decay tanks (WGDT), use of the turbine load

limiter as described in the Updated Final Safety Analysis

Report (UFSAR), and establishment of containment integrity

during refueling operations.

These issues are also

discussed in the Safety Assessment/Quality Verification

area.

.,

_.,__ ' .. *-*-** .... *: ...... .. -.. * .. ________ .._ ------~-~-'----.... *---- *--*~---***-*----***-* *-

.,

7

The licensee continued to be innovative in using computer

systems to improve the effectiveness of-plant operation.

A

new computer program was implemented during the assessment

period to record and trend hours spent in TS action

statements. This new computer program enhanced the ability

to focus on problem areas. The ability* to*retrieve and

display parameters easily continued to be a-strength;

primarily through the extensive use of hand-held computer~-

for taking logs throughout the plant.

The licensee

continued the development of additional computer programs

including one for annunciator response procedures and for TS

in.formation.

One violation was issued during the assessment period.

2.-

Performance Rating

Category:

1

3.

Board Recommendations

None

B.

Radiological Controls

1.

Analysis

This functional area addresses those activities related to

radiation safety and primary/secondary chemistry control.

The licensee's RP department had*a highly qualified staff

and station management continued to be actively involved and

supportive of the RP Program.

Management oversight of the

program was, in part, maintained through a corrective action

program that promptly and consistently recognized and

.address_ed non-reportable radiological problems.

The

licensee has several programs for self-assessment and

audits.

For example, quality assurance (QA) performed

radiological audits and comprehensive (two-three month)

assessments, corporate RP performed radiological assessments

and station RP monitored radiological compliance through

radiation problem reports and daily assessments by HP

technicians.

The licensee's program to provide specialized training

exceeded the requirements of the regulations and continued

to make positive contributions to the RP program.

For

example: 1) the licensee sent 36 HP technicians (in training

shifts of six people each) to other utilities for one-week

familiarizations; 2) prior to the recent outage, all site

services personnel received a day of training in dose

reduction; and 3) in preparation for resistance temperature

detector (RTD) bypass manifold removal, tpe licensee

8*

constructed a realist.ic full-size mockup and ensured that

all personnel that would be working on in-plant RTDs were

fully trained.

In addition, the licensee added a group

training mockup (GTM) to its Advanced Radiation Worker (ARW)

Program.

The GTM represents a plant system comprised of

valves, demineralizers, pumps, and electrical cabinets that

are representative of those in-plant.

The licensee

completed the training of 88 percent of mechanical

maintenance personnel as ARW-qualified and continued to

achieve 100 percent attendance at continuing training during

outage periods.

Participation by station personnel from all departments was

effective in controlling contamination.

The

number of

personnel contaminations in this assessment period was 164,

as opposed to 187 in the previous assessment period.

Although progress was slow during the beginning of the

assessment period, the licensee's reclamation project

received increased attention to reduce the amount of

contaminated area from 11,500 ft 2 at the end of the last

  • assessment period to 9,645 ft 2 at the end of this period.

The licensee continued to reduce the collective dose at the

station, with the 1991 value significantly.less than the

1990 value.

A primary factor in the station's dose

reduction was the active ALARA staff and worker involvement

in dose reduction.

A result of this effort was that the

dose to individuals working on the ROT bypass manifold

removal project was s*ignificantly less than* projected.

Another factor was the station's efforts to reduce the out-

of-core source term, such as, hot spot flushes, elevated pH,

zircoloy fuel grid spacers, early shutdown boration,

peroxide injection, and removal of the Unit 1 RTD bypass

lines.

A third factor was the HP Engineering personnel and

Station Systems/Design Engineering working together.to

install lead shielding both temporarily and permanently, at

key locations in operating systems both inside and outside

containment.

Some dose rate reductions of 10-fold were

realized.

The licensee used innovative methods of dose and

source term reduction, such as green flashing lights to

denote low dose waiting areas in containment; telemetric

dosimetry to allow HP to monitor workers dose remotely; and

a video disc system for viewing plant systems for planning

and briefing purposes.

The licensee took significant steps to control the amounts

of radioactive effluents released from the site.

For

example, the new radwaste facility, which was brought on

line late in the assessment period,. significantly reduced

the release of radioactivity in liquids from the site.

Since the new radwaste facility was *brought on line during

the latter part of the assessment period, the licensee's

records indicated essentially no curies released.* The tota.l

L

. 9

body and organ doses for these effluents for 1991 were less

than 2 percent of the 40 CFR 190 limits.-

_There were no

unplanned releases that required reporting to the NRC and

there were no significant changes in th~ amounts of

effluents released from the site during the assessment

period.

During the last assessment period, the licensee had

.

continuing problems with radiation monitors.

This was not

observed during this period and the licensee's Radiation

Monitoring System was effeqtively maintained.* The testing

anp calibration of monitors was performed as required.

Only

one monitor was inoperable for a period of greater than 30

days. Alternate sampling and analysis were performed as

required.

The monitor was *replaced and satisfactorily

operated during the remainder of the assessment period *.

The licensee's program for monitoring and controlling

primary chemistry parameters was effective. TS primary

chemistry parameters were maintained within limits.

Other*

primary chemistry parameters were generally maintained

within administrative limits, and when outside these limits,

were r*eturned in a timely manner.

In addition, the licensee

was in agreement with the radioisotopes analyzed as part of

the NRC's Confirmatory Measurements Program.

The licensee's program for radioactive waste shipments was

good in that technicians were adequately trained and

performed their duties competently.

However, there was one

problem where the licensee failed to properly identify the

physical form of radioactive material prior to it being

released for transportation on a public.highway.

'

.

.

One violation was issued during the assessment period.

2.

Performance Rating

Category:

1

3. *

Board Recol'limendations

None

C.

Maintenance/Surveillance

1.

Analysis

This functional area addresses those activities related to

equipment condition, maintenance, surveillance performance,

and equipment testing.

overall.plant material condition was considered to be

satisfactory. * Significant improvements involved

,.

10

installation of auxiliary feedwater (AFW) full flow

recirculation test piping, fuel transfer cart modification,

main feedwater flow element replacement, installation of new

letdown valves, installation of new Ame~ican Society of

Mechcinical Engineers (ASME)Section XI instrumentation,

coating of the SW piping, and ~ecovery of the gas stripper.,

which greatly reduced the gaseous releases to the

atmosphere.

Areas that have been recognized by the licen~ee

as needing additional management attention were control rod

drive (CRD) failures, RTD manifold leaks, containment

personnel airlock malfunctions, sticking SW temperature

control valves for the high head safety injection (HHS!)

pumps, and rain and ground water leaks.

since 1990, failed

or degraded CRDs have resulted in unit runbacks and forced

outages.

Several RTD bypass manifold leaks resulted in

forced outages.

At the end of the assessment period these

manifolds were being removed on Unit 1 and are scheduled to

be removed during the February 1993 Unit 2 refueling outage.

Containment personnel airlock malfunctions resulted in

.

personnel being trapped in the airlock and delayed refueling

activities.

Rain water and ground water leaks onto safety

related equipment continued to be a problem.

Late in the

assessment periog, the licensee completed an evaluation of

the condition of the roofs and the necessary paving and

grading to correct the rain and ground water intrusion

problem.

A five year plan was developed.

A contract for

auxiliary building roof repair was issued and work was

started.

The staffing level in the Maintenance Department, except for

maintenance engineering, was adequate, similar to the

previous assessment period.

The maintenance engineers are

responsible for the Cause Determination Evaluation (COE)

Program.

The backlog of CDEs (formerly named Component

Failure Evaluation Program) was noted as needing improvement

during the previous assessment period and, although some

improvements were made, the backlog increased about.ten

percent during this period.

This growth was caused

primarily by an increase in the number of requests.

At the

end of the assessment period, the licensee was preparing to

increase the maintenance engineering staff to decrease the

backlog and to accommodate the increase in the number of

evaluation requests.

Although staffing in this area was

low, the quality of work remained good.

An example of a

thoroughcomponent-failure.analysis involved problems

identified on two of the EDGs when they failed to achieve

rated speed during automatic starts.

Also, the addition of

a new metallurgical laboratory greatly .increased the

technical capabilities for failure investigation of

components.

Maintenance foreman and craft personnel generally

demonstrated good job skills during the assessment period.

L

11

Strengths in this area were identified in the coordination

of numerous maintenance activities associated with

switchyard transformer replacement, trouble shooting

activities on a reactor trip breaker, apd the replacement of

a main steam pressure transmitter.

Problems were identified

with foreign material exclusion in the SW system and

improper control of trouble shooting activities associated

with the CRD system. *

The maintenance training and qualification program was good

and contributed to a thorough understanding of the work.

The presence of equipment, mockup, and dedicated training

specialists at the training facilities allowed the licensee

to train all levels of craft and the maintenance teams.

A high maintenance backlog existed during several of the

previous assessment periods.

A significant amount of

management attention, including improved planning,

availability of parts, and high-level reporting, was applied

to this area and effective results were achieved.

The*

number of non-outage corrective maintenance work orders

decreased by approximately one-half during this assessment

period.

The average age of these work orders also decreased

by almost two-thirds.

Unavailability of parts was a contributor to the maintenance

backlog during the previous assessment period.

The licensee

estaplished a goal of less than ten percent of the work

orders on hold for material unavailability in 1991.

This

goal was met by a large margin, with less than two percent

of the work orders on hold for lack of materials or the

unavailability of parts at the end of the assessment period.

The outage and Planing Department's performance improved

during this assessment period particularly in the area of

planning and scheduling.

Improved planning contributed to a

decrease in work order backlog.

The planning weakn~sses

identified in the previous aspessment period were adequately

addressed and improvements in planning/operation

communication were noted.

This effort contributed to the

decrease in the non-outage corrective maintenance backlog

and the decrease in the average age of the work orders.

The

planning process was made more effective by assigning an

individual planner to a particular maintenance crew.

During

the outages, a.train availability window method for working

on systems helped to better organize the related outage

work.

Maintenance performance of outage related activities during

the Unit 2 outage early in the assessment period was good.

Maintenance engineering support in the resolution of craft

problems was noteworthy.

Individual maintenance crews were

assigned either specific components and/or specific areas of

12

responsibility.

This technique promoted accountability and

ownership.

Good job skills were demonstrated by craft

personnel and foremen.

The efficiency and knowledge that

.was demonstrated during the trouble shopting of a reactor

trip breaker was also a strength in this area.

Two

personnel errors resulted in significant plant problems.

The first involved an event that necessitated a manual trip.

of the reactor when the removal of a fuse caused the

dropping of a second control rod.

The second issue involved

a-partial blockage of SW.flow to the recirculation spray-

heat exchanger (RSHX) when the foreign material exclusion

pr.ogram was not followed and a rain suit was left in the SW

line.

The TPUP progressed better than planned during this period.

This program involves approximately 3100 maintenance

procedures and was approximately 22 percent complete.

The

quality of the new procedures was good. Procedural

adherence, which was identified as a problem during the

previous assessment period, was much improved during this

period.

However, the upgrade of instrumentation and control

(I&C) procedures was approximately 50% behind schedule.

The

schedule problems with the I&C procedures was also noted in

the previous assessment period.

The* lack of detail in older

generic maintenance procedures contributed to equipment

problems.

A specific problem with air operator procedures

involved a containment isolation valve that failed to close

because too many springs had been installed in the valve

seat and a pressurizer spray valve that malfunctioned

because of improper assembly.

At the end of the assessment

period all of* the air operated valve maintenance procedures

were being revised.

The Preventive Maintenance. (PM) Program was effectively

implemented.

-The deferral rate for PMs was very low.

An

isolated weakness was identified in the program when the

licensee discovered that several pressure switches installed

on systems important to safety were not in a periodic

calibration program.

Reliability centered maintenance

studies were initiated and completed for several safety-

related systems.

The maintenance trending program data base

was derived from the*work plan tracking system and station

deviation reports.

This program functioned well and was

noted as an improvement from the previous assessment period.

The MOV program continued to be a strength during this

assessment period.

The licensee displayed in-depth

knowledge and a clear understanding of MOV issues which were

enhanced by participation in several MOV user groups.

Several concerns in the program were identified which

involved engineering assumptions and electrical

calculations.

These program corrections were made in time

r

' '

13

for implementation during the Unit 1 Spring 1992 refueling

outage.

During the previous assessment period, a new Post-

.Maintenance Test Program (PMT) was implemented.

The program

uses a series of matrixes of required tests for each of the

program's safety-related components.

Even though several

problems occurred during the assessment period, the overa~l

program was effective in developing good tests .. one of the

problems occurred during a trip of Unit 2 in August 1991

when the #3 EDG automatically started but did not achieve

its nominal speed and was declared inoperable *.

The root

cause was lack of management oversight and control of

functions related to maintenance activities.

The site

safety committee had approved instructions for governor

adjustment using a fast start of the EDG, which would have.

detected the problem of low speed and inoperability, but the

PMT followers in the work package only required a slow

start.

Implementation of the surveillance program was generally

good during the assessment period.

With the installation of

the new AFW full-flow recirculation flow path, surveillance

for both units' AFW pumps was enhanced.

Performance of

these surveillances was closely tracked because of proplems

identified during past assessment periods.

Post-criticality

testing for Unit 2 startup was adequate.

The accurate

prediction of the reactor power distribution with a fully

inserted rod demonstrated the licensee~s*strength in core

analysis.

However, there were two missed surveillances that

occurred during the previous assessment period but were

discovered in this period.

In one instance the interval

between surveillances on Unit 2 hot channel factors exceeded

the TS requirements and in the other, a containment spray

surveillance exceeded its grace period.

The licensee's

corrective actions .appeared to be effective since instances

of missed survei.llances did not occur during this assessment

period.

However, several surveillances were considered to

be ineffectively implemented in that the procedures were

inadequate.

These examples involved the motor driven AFW

pump undervoltage start relays having improper set-points

designated in the procedure and a relay in the safety

injection system logic sequence not being tested as an

active component.

These surveillances were repeated to

ensure operability.

Three violations were issued during the assessment period.

2.

Performance Rating

Category:

2

V

I

1

14.

3.

Board Recommendations

As in the last assessment period, material condition

. deficiencies continued to contribute to:operations and

maintenance problems *. Although the Board recognizes that

there has been improvement.in this area, continued

management attention is needed.

D.

Emergency Preparedness

1.

Analysis

  • This functional area addresses * activities reiated to the

Emergency Plan, support for and training of emergency

response organizations both onsite and offsite, and licensee

performance* during emergency exercises and actual events.*

The licensee continued to maintain an excellent. emergency

preparedness program.

Management support was evident

throughout the period as the licensee continued to maintain

in a state of readiness the basic emergency preparedness

elements needed to implement the Emergency Plan and its

procedures in response to emergency events.

Program

strengths included.a strong.management commitment to

emergency preparedness staffing resulting in an effective

base of* expertise at bo_th corporate and site levels.

The

licensee also effectively addressed routine and exercise

inspection findings through the use of a thorough corrective

action program as well as a comprehensive open issues

tracking system.

Other program strengths identified

included an effective emergency response organization

training program and a comprehensive independent audit

function. *

The licensee continued to build on a strong emergency

response capability through numerous self-initiated program.

enhancements.

The licensee conducted several full-facility

activation exercises in order to maintain a heightened state

of overall response readiness.

In addition, the licensee

conducted several specialty drills such as offsite

notification.

Other licensee initiatives during the

assessment period included enhancements in the public

information program, installation of electronic sirens in

tbe early warning system in order to improve the system's

reliability,--use-of new pagers for improving the ability to

notify key emergency response organization personnel, and

implementation of an Emergency Response Data System before

the required time.

During the November 1991 full participation exercise, the

licensee demonstrated the ability to staff the emergency

organization in a timely manner and the staff demonstrated

the ability to effectively implement the Emergency Plan.

I

L

15

The overall emergency response was effective and

demonstrated a high level of proficiency.

During the

exercise, alternates replaced key emergency response

personnel who were called to attend to ~n actual

transportation accident which involved the licensee's

radioactive material.

The alternates performed well,

indicating good emergency organization training, and good

emergency response depth.

Furthermore, the licensee

demonstrated an effective overall incident response

capability in responding to the radioactive material

accident, as discussed in the Radiological Controls area.

The licensee provided extensive resources at the accident

scene in a prompt and overall effective manner which was

integrated with state and local response organizations.

This effort minimized the adverse effects of the accident.

Throughout the exercise, the licensee demonstrated the

ability to perform effective dose projections, and

radiological monitoring, a.nd to make proper protective

action recommendations.

Other observed strengths during the

exercise included:

good emergency response command and

control; prompt activation of the emergency response

facilities; timely event classifications and declarations;

effective communications with state and local authorities;

good assessment and mitigation of plant damage; and a lead

controller communications network that provided effective

exercise control.

Although there were no exercise

-

weaknesses, one issue was identified regarding delays in

access for emergency control teams entering the radiation

control area during emergency conditions.

The licensee

completed corrective action in this area.

overall, the

licensee's performance during the exercise was good, with

the licensee meeting their exercise objectives and

demonstrating a capability to protect the public health and

safety in the event of a radiological emergency.

During the assessment period, the licensee's Emergency Plan

was implemented three times in response to actual events,

each involving the declaration of an Unusual Event. In each

case, the event classification was prompt and correct,

onsite response actions were appropriate, and offsite

authorities were notified in accordance with applicable

requirements.

No violations or exercise weaknesses were identified during

the assessment period.

2.

Performance Rating

category: 1

'

3.

Board Recommendations

None

E.

Security

1.

Analysis

16

.This functional area addresses those security activities

related to protection of vital plant systems and equipment,

and the Fitness for Duty Program.

The Security Program was effectively -implemented during the

assessment period.

Security personnel continued to

demonstrate professionalism and ~edicated performance in the

accomplishment of assigned duties.

Continued strong support

by corporate and station management was evident by the

renovation of the primary personnel access portal to enhance

security control for site access.

This new facility was

equipped with new.and improved x-ray, metal and explosive

detection equipment, and provided larger and state-of-the-

art work areas for security management and administrative

staff.

Also, the delay capability of the perimeter barrier

was enhanced by installation of razor ribbon to increase

penetration time for intruders or potential adversaries.

In response to tactical issues identified during an

Operational Safeguards Response Evaluation, the licensee

promptly upgraded facilities by installing a metal

reenforced barrier over plate glass windows in the access

portal.

In addition, two areas within the new personnel

access portal, exterior to the protected area, were

identified by the NRC as potential penetration paths into

the protected area.

The licensee immediately installed

intrusion detection equipment in both locations to further

enhance detection capability.

Problems with the in-plant security computer occasionally

caused delays in licensee staff being able to access areas

in the plant.

Operations personnel have keys to gain access

to these areas, but do not routinely carry these keys.

Security management recognized this problem and installed a

vital area override system as an interim measure until the

forthcoming in-plant security system upgrades are completed.

Security management-was effective, shift staffing was good

and the quality of training provided the security force was

excellent.

During the Operational Safeguards Response

Evaluation drill runs, the licensee demonstrated strengths

in security management, perimeter barriers, response team

performance, detection, assessments, training, weapons, and

command, control and communications;

Operations personnel

participation in these security response activities was also

a strength.

.

17

The coordination and management of security plan revisions

continued to be excellent.

During the assessment period,

the licensee submitted.a comprehensive re-formatted physical

security plan that clarified requiremen~s and commitments.

The security plan was undergoing an additional revision at

the end of the assessment period.

Implementation of this

revision will enhance the physical*security protection of

safety-related equipment and is scheduled to be completed.in

1997.

The licensee's Fitness For Duty Program was effective and

continued to meet the drug-free work place objective.

This

program was administered by a trained professional staff and

had an aggressive audit and management oversight.

The

Program also continued to test for a broader spectrum of

drugs than required by the NRC.

No violations were issued during the assessment period.

2.

Performance Rating

Category: 1

3.

Board Recommendations

None

F.

Engineering/Technical Support

1. Analysis

This. functional area addresses activities associated with

engineering and technical support, including activities

associated with design of plant modifications, engineering,

and technical support for .operations and operator training.

overall engineering and technical support was effeqtive

during the assessment period~ Notable performance included

the design and installation of a barrier for the condenser

inlet water box that was used during a service

water/circulating.water expansion joint replacement.

This

barrier allowed the required safety trains of the

recirculation spray system to remain in service during the

modification.

Another example was the design and

construction of. the radwaste facility which was placed in

service in 1991. It minimized personnel exposure and was

designed for efficient operation and maintenance.

At the

end of the*assessment period the new Administration Building

was completed.

This was a significant improvement in that

work stations for engineering personnel and other

departments were upgraded and consolidated into one area.

.

'

18

station engineering performance during the Unit 2 outage was

good. The quality and technical content.of engineering

design change packages and work requests provided in support

of the outage replacement of feedwater flow elements and the

installation of new letdown isolation valves were good.

The

technical reviews of completed modifications were timely and

fully supported unit startup from the refueling outage.

Station engineering developed a priority evaluation process

to support outages and verify that modifications were

implemented in a timely fashion.

This review and

prioritization of engineering work requests and design

change packages assigned to Nuclear Engineering Services was

implemented at the end of the assessment period and

  • scheduled to be completed in June 1992.

Technical support activities of welding and non-destructive

examination were effective during the assessment period.

However, some ISI drawings and sketches contained errors in

piping and welding configurations, which caused confusion

    • when comparisons were made between the field condition and

the ISI drawings.

System engineer involvement with the verification portion of

the Design Basis Documentation Program was good.

During

this effort, design engineering discovered that the existing

calculations for the intake canal were incomplete and did

not document all design input values and loading conditions.

Conservative actions were taken to assure appropriate

compensatory measures were put in place until the

calculations could be corrected.

The MOV program continued to be a strength during this

_ assessment period.

The licensee displayed in-depth

knowledge and a clear understanding of MOV issues which were

enhanced by participation in several MOV user groups.

The

program was generally consistent with the recommendations of

Generic Letter 89-10.

Strengths were noted in the program

relative to training, recognition of the need to measure

valve torque in testing, and the corrective action program.

several concerns in the MOV program were identified by the

NRC which involved engineering assumptions, and electrical

calculations.

Several of these program corrections were

made in time for implementation during the Unit 1 Spring

1992 refueling outage.

At the beginning of the assessment period, weaknesses were

noted with setpoint control.

Discrepancies existed between

the set-points specified in the setpoint control program

procedures and the I&C implementing procedures.

Other

design problems in instrumentation occurred during the

assessment* period including the failure to ensure that

instrument accuracies assumed in the design change

I

19

calculation were used by the site organization.

This

resulted in a request for relief from ASME Section XI

requirements.

Another problem associated with steam flow

protection setpoints required the TS ba~ed value to be

reduced due to instrument scaling uncertainties.

In both of

these examples, engineering developed conservative interim

positions until the final resolution could be developed.

The control of setpoints was assessed and program changes_to

strengthen this area were under development at the end of

the assessment period with a late 1992 implementation date.

Good communications were observed between engineering,

construction, and operations departments during trouble

shooting and corrective action for a licensee discovered

problem with Unit 2's AFW system piping.

This piping, which

is partly underground, had been incorrectly routed during

initial piant construction.

This configuration error was

discovered during a modification for the AFW pumps'

recirculation flowpaths and was promptly addressed and

rapidly resolved.

One area where the licensee should have been more aggressive

was in reporting and reacting to the results of the

individual plant examination (IPE) efforts.

In early 1991.

the licensee identified a significant core damage frequency

that could result from postulated internal flooding of the

Units 1 and 2 turbine buildings.

The licensee established

an independent team to reaffirm the flooding vulnerability

and reported its findings in a final August 30, 1991. IPE

submittal.

The licensee should have been more proactive in

notifying the NRC when the flooding vulnerability was first

identified and should have defined, committed to and/or

implemented appropriate mitigative actions prior to

submittal of the Ii?E report.

However, following submittal

of the report, the licensee was responsive to the NRC

concerns and implemented inspections, procedural changes,

training, and limited plant modifications.

As a result of

  • NRc involvement, the scope of the original planned

modifications and activities was expanded and the

implementation schedule accelerated.

Station engineering provided good support to operations and

provided operability determination information to the shift

-supervisor as needed.

Equipment failures, for the most

part, _got immediate-attention.

However, an operability

determination issue for the #2 EOG operating at reduced

frequency was delayed for several days because of

engineering workload and no priority support from corporate

design engineering.

The reduced frequency event occurred as

a result of a conflict in the work governing documentation

  • which went undetected by station personnel.

'

20

Corporate engineering effectively continued the support of

the predictive and PM program to monitor erosion-corrosion

wear rates and initiated several changes in plant water

chemistry and processes to aid in this reduction.

Corporate

engineering undertook a comprehensive overview of the

inspection program to optimize the component replacement-

program as a function of safety and efficiency.

Recent station and corporate engineering support of special

testing and response to emerging issues was excellent.

One

example involved the timely technical evaluations provided

for the replacement of a leaking switchyard station service

transformer whose failure could have caused a loss of the

power supply to the emergency buses.

A second example

involved special testing of the SW supply to the RSHXs which

identified problems of flow restriction and radiation

monitor sampling pump design deficiencies.

A third example

involved engineering response to concerns with containment

shroud cooler efficiencies which may have contributed to the

CRD coil failures and dropped rods discussed in the

Maintenance/Surveillance area.

This emerging issue was

addressed with minimal impact on an already demanding

outage.

An effective licensed operator training program was

demonstrated by a 94% pass rate on initial and

requalification examinations administered during the

assessment period.

The Generic Fundamentals Examination*was

administered to fourteen candidates.

A 100% pass rate was

achieved on the examination.

This was an improvement over

the results achieved during the previous assessment period.

The licensee provided quality questions on the written

requalification examination and the Job Performance

Measurements.

The licensee's pre-review of the NRC written

initial examination was of limited effectiveness in that

several post-examination changes were required due to

technical inaccuracies which were not reflected in the

reference materials and not detected in the pre-review. The

simulator scenarios were well written and constructed.

Equipment simulation was sufficient to test the candidate's

knowledge level of plant operation and procedure usage.

Instructors effectively evaluated the candidates

performance.

One.violation was issued during the assessment period.

The

licensee denied this violation and the denial was under NRC

review at the end of the assessment period.

2.

Performance Rating

category': 2

I

It'

21

3.

Board Recommendations

None

G.

Safety Assessment/Quality Verification

1.

Analysis*

This functional area addresses those activities related to

licensee*implementation of safety.policies;. amendments,

exemptions and relief request; response to Generic Letters,

B~lletins, and Information Notices; resolution of safety

issues; reviews pf plant modifications performed under 10

CFR 50.59; safety review committee activities; and the use

of feedback from self-assessment programs and activities.

The senior plant and corporate*management structure

continued to be stable and effective.

The licensee's self-

assessment program continued to identify and refocus

attention and improved overall performance.

The self-

assessment by Corporate Nuclear Safety (CNS) determined that

recommendations from several of the older event reviews had

not been followed up and there was no way to verify that

corrective action was complete.

CNS modified their issue

tracking_ and trending program to strengthen this area and

provide the needed followup reviews.

The continued.use of

the Performance Annunciator Panel Program ena~led management

to focus. on areas that warranted additional attention.

The

new integrated QA audit process was*effective and all

required audits were performed.

The station continued to

conduct performance*-based observations to augment the

required audits.

The number of assessments performed was

somewhat constrained by resources and prioritization was

necessary.

However, staffing levels were adequate.and

personnel well-experienced to perform the assigned

functions.

A significant portion of the QA assessments were

at the request of the Station Manager and this process

demonstrated that both the plant and QA were striving to

improve performance and overall quality.

Control of

operator overtime, use of operator aids, and implementation

of justification for continued operation commitments were

examples of assessments that complemented plant operations

and appeared to have improved safety.

The licensee' .. s corporate -staffing and committee structure

performed timely and detailed assessment of emerging safety

issues.

The licensee's safety review function is

accomplished through the use of both the onsite [Station

Nuclear and Safety Operating Committee (SNSOC)] and offsite

[Management Safety Review Committee (MSRC)] committees as

well as. the industry experience review group (IERG).

The

details and quality of the safety reviews conducted by the

onsite safety review committee in this assessment period

I

I

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22

were good.

An example of a strength identified in this area

was the thorough and in-depth safety oversight review of the

troubleshooting and repair of a Unit 2 reactor trip manual

pushbutton failure.

In contrast to th~s strength, however,

was a decision to place the recirculation mode transfer key

switches in the refueling position, which defeated the

automatic transfer mode and violated TS requirements.

Discussions in the MSRC meetings were frank and straight-.

forward with the consultants significantly contributing by

providing a broader perspective through alternative view-

points.

The licensee exceeded the TS requirements for

committee staffing and meeting frequency in all areas.

Timely evaluation of the Salem turbine damage and the French

reactor CRD mechanism nozzle cracks were two examples of

IERG involvement.

In the case of the turbine damage issue

turbine overspeed testing was suspended until the licensee

determined that plant procedures were acceptable.

Licensee

management maintained several oversight groups that are in

addition to those required by TS. For example: 1) the plant

manager utilizes a Management Review Board to review items *

of interest and provide feedback, and 2) the Senior Vice

President, Nuclear, receives advice from a Nuclear Oversight

which includes executive managers from other utilities.

Strengths were identified in the timely resolution of safety'

issues *which the licensee *considered as* safety significant.*

Examples included the installation of a second means of

level indication for reduced inventory operations ahead of

the original commitment date and prior to entry into reduced

inventory.

Another involved the correction of a problem

with switchyard breaker logic, that was being compensated

for by requiring operator .actions during an unplanned outage

even though the non-mandatory repairs extended the outage.

The commitment to problem resolution was also evident, by

the established low threshold for deficiency identification.

Several examples such as steam flow setpoint errors,

charging pump switch alignment, and SW radiation sample pump

deficiencies demonstrated the licensee's ability to identify

long-standing problems of incorrect design or calculations

assumptions.

  • However, during this assessment period, the licensee*

continued to have some difficulty in resolving conditions

adverse to quality.

For example, there were several cases

that indicated a willingness to live with recurring problems

such as seal head low level alarms on an outside

recirculation spray pump and a low head safety injection

pump.

Recurring failures of the SW temperature control

valves needed to cool the HHSI pump lubricating oil system

were also not promptly corrected and a failure to identify

and correct the installation of an improperly sized air

tubing for the feedwater regulating valve contributed to

,

I.

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23

valve instability which may have been the initiator of an

operational transient.

The licensee's implementation of safety. evaluation

assumptions into station procedures were, for the most part,

effective.

However, several examples of not incorporating

safety evaluation assumptions into plant procedures were

evident during the assessment period.

First, a TS change to

radioactive gas storage requirements was improperly

implemented through station procedures and resulted in non-

conservative operator actions when the WGDT oxygen and

hydrogen concentration exceeded the TS limit.

Second, UFSAR

described actions associated with control of the tu,rbine

load limiter were not incorporated in station procedures,

contributing to a brief increase in unit power that exceeded

the license power limits.

Finally, a 10 CFR 50.59 safety

analysis commitment for inspecting the control rod guide

tube flexures for Unit 2 during a refueling outage was not-

factored into station procedures.

This oversight allowed

unit operation for two cycles with possible loose parts.

During the previous assessment period, the licensee

identified that the UFSAR was not current as to past

modifications to the facility.

However, the licensee did

not recognize that some of the data from portions of the

original FSAR also needed upgrading.

Several instances of

errors in the UFSAR and plant procedures resulted in

operations and testing that violated the assumptions used in

some of the transient analyses and TS bases.

Management

recognized the need for an accurate UFSAR and modified their

update program to include a quality review.

During the previous assessment period, deficiencies were

identified with the implementation of an effective root

cause evaluation program and also ensuring the appropriate

training for evaluators.

Root cause training continued into

this assessment period and was accomplished for a l~rge

number of personnel from dif(erent organizations throughout

the plant.

During this assessment period, root cause

analyses were effective in identifying needed corrective

actions to improve performance.

For example, the

determination that several of.the CRD failures (discussed in

the Plant Operations and Maintenance/Surveillance areas)

were temperature related resulted in the development and

implementation of -ventilation modifications to improve CRD

cooling during the Unit 1 refueling outage late in the

assessment period.

Commitment tracking.was identified in previous assessments

as not being effective.

Improvements were noted during this

assessment in that IPE commitments_ that were being revised

on a frequent basis were effectively tracked and completed

by the licensee without any missed commitments.

I

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24

Additionally, for the Unit l1mini-outage late in the

assessment period, the licensee's program was effective in

identifying those commitments that were required to be

completed during the first shutdown of ~ufficient duration~

Considerable licensing activity took place during this

assessment period.

For the most part, licensing submittals

were timely and of high quality, demonstrating the

licensee's thorough understanding of technical issues and

regulatory requirements as well as a conservatism in the

approach to safety.

Examples of high quality submittals

we.re amendments relating to: (1) opposite train operability

testing, (2) engineered safety features instrumentation

upgrade, and {J) surveillance frequency for recirculation

spray and containment spray check va.l ves.

The analyses of

the no significant hazards issues were complete and correct.

However, while submittals in most cases were timely, some

responses to requests for additional information were late.

Responses to NRC Bulletins, Generic Letters, and other

regulatory requests were, in most cases, timely, technically

correct, and satisfied staff concerns.

One example of good

technical completeness was the licensee's response to

Bulletin 88-08 relating to thermal stresses in piping

Although no

response was required related to Supplement 3 of the

Bulletin, the licensee did address it.

However, the

licensee's response to Generic Letter 88-14, "Instrument Air

System Problems Affecting Safety-Related Systems" has been

protracted.

There have been three submittals to date, the

latest of which was found deficient.

Moreover, one proposed

modification to the containment air system, which was later.

abandoned, contained a flaw that should have been detected

earlier by the licensee.

The fl*aw would have increased the

radiological gas release during normal plant operation by a

factor of 2 to 10, depending on the specific modification

selected.

The use of the "top 10 11 licensing issues mana,gement tool,

which is updated on a continuous basis and submitted

. quarterly, continued to be an effective method of focusing

on the high priority issues.

The licensee's staff was

effective in anticipating and identifying potential problems

related to TS and regulatory requirements so that resolu-

tions can be obtained on a non-emergency basis.

The licen-

see maintained an adequate and competent staff both at the

plant and at the corporate office to support licensing

activities.

Shutdown risk management greatly improved during the

assessment period.

Sensitivity to loss of equipment needed

to respond to transients or accidents during shutdown

operations increased.

As part of these improvements the

25

licensee developed and implemented a new program,-

Shutdown/Refueling Shutdown Critical Parameters.

This

program provided an additional m~thod of monitoring plant

parameters and systems important to safety during outages.

The program also developed a seven day look-ahead matrix to

evaluate the effect of scheduled maintenance on critical

plant parameters.

Emphasis on shutdown risk resulteq. in the

elimination of two scheduled mid-loop operations during the

Unit 1 refueling outage.

However, at the end of the assessment period a weakness in

the area of shutdown risk management was noted when Unit 1

refueling operations were performed in parallel with

maintenance on main steam valves.

Controls were not in

place to prevent breaches of containment integrity and

resulted in .a violation of-TS which occurred due to the

installation of improperly sealed blanks over containment

openings.

Six violations were issued during the assessment period.

2.

Performance Rating

category:

2

3.

Board Recommendations

The Board is concerned that the improving trend noted at the

end of the last assessment period was not sustained during

this period.

The inability to prevent the recurrence of

several safety problems contributed to the above rating.

Management attention is needed to get these areas back on

track.

V *. SUPPORTING DATA AND SUMMARIES

A.

Major Licensee Activities

Unit 1 began the assessment period at power.

During this

assessment period the unit completed a run of 379 days of

continuous operation.

The unit experienced one manual reactor trip during the period.

At the end of the period,

the unit was in day 36 of a scheduled 64-day refueling

outage.

Unit 2 began the assessment period in a refueling outage.

Equipment-related problems occurred throughout the

assessment period which resulted in a delayed startup from

the refueling outage, two automatic reactor trips {one with

a safety injection), four forced outages, and two turbine

runbacks.

At. the end of the assessment period, the unit wa_s

operating at full power.

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26

One management and/or organization change occurred during

the assessment period.

Near the end of*the assessment

period the Vice Presidents of Nuclear Operations and Nuclear

Services exchanged positions.

B.

Major Direct Inspection and Review Activities

During the assessment period, 35 inspections were conduct~d.

Six of these were special inspections:

(1) evaluation of

the annual emergency exercise; (2) evaluation of the

licensee's activities to reduce the vulnerability.for

internal flooding; (3) an inspection associated with

implementation of the MOV program; (4) administration of the

operator requalification examination; (5) a security

operations safeguards response evaluation; and (6) a

followup to the EOP team inspection.

Eight management

meetings and one enforcement conference were also conducted

during this assessment period.

c.

Escalated Enforcement Action

A Severity Level III Violation with a civil penalty was

issued for the failure of EDG # 3 to perform its safety

function with the loss of off-site power.

A Severity Level III Violation with a civil penalty was

issued for inoperability of the automatic start feature for

the HHS! pumps.

D.

Licensee Conferences Held During Appraisal Period

June 17, 1991 - Meeting at Surry Nuclear Information Center.

to present the SALP Board Assessment.

August 19, 1991 - Meeting at Region II to discuss North Anna.

and Surry emergency preparedness plans and programs.

September 17, 1991 - Enforcement Conference at NRC Region II

office to discuss the failure of the# 3 EDG's safety

function during a loss of off-site power, and inoperability

of the automatic start feature of the HHS! pumps.

October 9, 1991 - Meeting in Rockville, Maryland to discuss

and obtain additional information on the licensee's internal

flooding analysis portion of their IPE.

October 17. 1991 - Meeting in Rockville, Maryland to discuss

status of all active licensing issues.

November 21, 1991 - Meeting in Rockville, Maryland to

discuss the reanalysis of the internal flooding issue as

described in the IPE Report.

'

' .. * * *

27

January 10, 1992 -

Management meeting at NRC Region II

office to discuss the licensee's self-assessment.

February 27. 1992 -

Management meeting in Rockville,

Maryland to discuss status of all active licensing issues.

.

  • ..

March 30, 1992 - Meeting in Rockville, Maryland to discuss

various licensing issues, current plant status, and IPE.

E.

Confirmation of Action Letters

None

F.

Review of Licensee Event Reports {LERs}

During the assessment period, a total of 38 LERs were

analyzed.

The distribution of these events by cause, as

determined by the NRC staff, is as*follows:

Cause

Unit 1 or Both

Unit 2

Totals

Component Failure

4

6

10

Design

3

1

4

Construction, Fabrication

or Installation

1

0

1

Personnel Error

- Operating Activity

6

2

8

- Maintenance Activity

3

2

5

- Test/Calibration

8

'2

10

-

Other

0

0

0

Other

Total

25

13

38

Note 1:

With regard to the area of "personnel error," the

NRC considers the lack of procedures, inadequate procedures,

and erroneous procedures to be classified as personnel

errors.

Note 2:

The "Other" category is comprised of LERs wh.ere

there was a.spurious signal or a totally unknown cause.

Note 3:

The above information was derived from a review of

LERs performed by the NRC staff and may not completely

coincide with the licensee's cause assignments.

  • '*

I(

... ~

. ...s..--

____ _.. _____ -* ***. _..:..~---* -

  • ----~--*-----*----*-*--*----**-***---****~-.

28

G.

Licensing Activities

During the assessment period, 32 license amendments, 4

relief requests and 30 other licensing actions were issued

or processed.

  • *

H.

Enforcement Activity

FUNCTIONAL

AREA

NO. OF VIOLATIONS IN SEVERITY LEVEL

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency Preparedness

Security

Engineering/Technical

Support

Safety Assessment/

Quality Verification

TOTAL.

IV

1

1

2

5

10

III

II I

1

1

2

  • Violation has been denied by the licensee and is being

reviewed by the staff.

I *

Reactor Trips

On January 2, 1992, Unit 1 was manually tripped from 56%

power when control rod H-2 dropped when trouble shooting

control rod E-5.

The CRD movable coil fuse for H-2 was

erroneously removed for trouble shooting E-5.

On August 2, 1991, Unit 2 experienced a safety injection and

a reactor trip from 94% power.

The cause of the event was a

combination of voltage spiking problems tripping the high

steam flow reference comparator and failed instrument

channels causing low steam line pressure.

On December 17, 1991, Unit 2 restarted after repairing a

flange leak, but at 30% power the unit had an automatic reactor trip when SG level control problems caused a high

level in 'B' SG.

The high level set point tripped the main

feed pump.

The turbine subsequently tripped which was

followed by a reactor trip.