ML18106A636

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Insp Repts 50-272/98-03 & 50-311/98-03 on 980316-0503. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML18106A636
Person / Time
Site: Salem  
Issue date: 05/22/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18106A630 List:
References
50-272-98-03, 50-272-98-3, 50-311-98-03, 50-311-98-3, NUDOCS 9806030294
Download: ML18106A636 (29)


See also: IR 05000272/1998003

Text

Docket Nos:

License Nos:

Report No.

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

U.S. NUCLEAR REGULATORY COMMISSION

50-272, 50-311

DPR-70, DPR-75

REGION I

50-272/98-03, 50-311 /98-03

Public Service Electric and Gas Company

Salem Nuclear Generating Station, Units 1 & 2

P.O. Box 236

Hancocks Bridge, New Jersey 08038

March 16, 1998 - May 3, 1998

S. A. Morris, Senior Resident Inspector, Salem

S. M. Pindale, Senior Resident Inspector, Hope Creek

F. J. Laughlin, Resident Inspector, Salem

H. K. Nieh, Resident Inspector, Salem

G. S. Barber, Project Engineer

T. H. Fish, Operations Engineer

N. T. McNamara, Emergency Preparedness Specialist

E. B. King, Physical Security Inspector

R. L. Fuhrmeister, Reactor Engineer

K. Young, Reactor Engineer

James C. Linville, Chief, Projects Branch 3

Division of Reactor Projects

9806030294 980522

PDR

ADOCK 05000272

G

PDR

-1

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EXECUTIVE SUMMARY

Salem Nuclear Generating Station

NRC Inspection* Report 50-272/98-03, 50-311 /98-03

This integrated inspection included aspects of licensee operations, engineering,

maintenance, and plant support. The report covers a seven-week period of resident

inspection; in addition, it includes the results of announced inspections of the emergency

preparedness programs by regional inspectors.

Operations

Overall, Salem plant management and staff controlled the Unit 1 reactor startup and power

ascension test activities well. The operating crews were attentive, used excellent

communication skills, and responded appropriately to planned and emergent events and

issues. Reactor engineering and chemistry department support, a*s well as pre-evolution

briefings, were usually of good quality although some deficiencies were observed during

low power physics testing. Strong management and quality assurance oversight was

indicated by continuous on-site management presence during restart activities and the

willingness to halt further plant evolutions following the identification of emergent issues.

Good self-assessment capability was evident during hold point release discussions with the

NRC Salem Assessment Panel. (Section 01 . 1)

Operators responded promptly and effectively to an unexpected loss of the 21 steam

generator feed pump while a 100% power. All plant equipment functioned as designed

during the-transient. (Section 01.2)

The 1 25 volt DC electrical distribution system was properly aligned for existing plant

conditions at Unit 1 and 2. Material condition and housekeeping were acceptable.

Adequate survejllance test procedures were implemented to verify system operability.

(Section 02.1)

PSE&G's actions to address and correct the cause of missing service water (SW) strainer

filter disks and cracked filter disk retaining rings were appropriate and promptly

implemented. Unit 2 control operators responded promptly to the clogging of two SW

pump discharge strainers in the SW same loop. PSE&G management's decision to take

Salem unit 2 off-line for strainer repairs was appropriate, and corrective actions were

adequate. (Section 02.2)

Maintenance

PSE&G determined that the lack of clear ownership for and coordination of recent

emergency diesel generator (EDG) on-line maintenance outages resulted. in unnecessary

delays in work completion, extending the overall equipment unavailability time. Inadequate

tagging controls during the 28 EDG outage resulted in an electrical breaker blocking tag

being released while personnel were actively working on equipment supplied by that

breaker. (Section M1 .2)

ii

PSE&G implemented appropriate corrective actions to repair degraded auxiliary feedwater

piping revealed by a through-wall leak on a pump minimum-flow orifice line. Technical

specification and ASME code class 3 requirements were satisfied. However, this event

revealed a weakness in scope of the flow-accelerated corrosion program in that only the

steam-driven pumps were included for monitoring. (Section M2.1)

Engineering

PSE&G restored the 22 steam generator steam flow channels II and Ill to an operable

status in a slow and deliberate manner, meeting all technical specification requirements

during the process. (Section E1 .1)

Plant Support

Based upon a review of selected items and procedures, the inspectors concluded that

PSE&G's method for tracking Emergency Preparedness corrective actions was very good

and that the self-assessment program provided good feedback to the staff. The timeliness

of resolving some identified issues was weak. (Section P1)

The emergency response facilities and equipment were in a good state of operational

readiness. Surveillance tests and inventories were performed as required and discrepancies

were resolved in a timely manner. Expenditure of resources to improve equipment.and

facilities demonstrated PSE&G's commitment to support and maintain the emergency

preparedness program. Overall, the inspectors considered this area to be very good.

(Section P2)

PSE&G emergency plan changes were adequately reviewed in accordance with 10 CFR

50.54(q). PSE&G planned to review, evaluate/rewrite the emergency plan implementing

procedures for conformance to other station procedures and to improve the review

process. The inspectors also concluded that letters of agreement with offsite agencies

were in place. (Section P3)

PSE&G conducted emergency response training and drills as required. Based upon overall

good performance during the drills and the March 1998 biennial full-participation

emergency exercise, the inspectors concluded that training for the ERO was effective.

(Section P5)

The department reorganization and hiring of a manager with extensive EP experience

enhanced the EP program. The inspectors concluded that the positive findings during this

inspection were an indication that the program had significantly improved since the last

inspection. (Section P6)

Quality Assurance audits of the emergency preparedness (EP) program were thorough and

  • the reports were useful to PSE&G management in assessing the effectiveness of the EP

program and providing enhancement recommendations. This area was assessed as

excellent. (Section P7)

iii

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_j

TABLE OF CONTENTS

EXECUTIVE SUMMARY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ii

TABLE OF CONTENTS .............................................. iv

I. Operations

01

02

OS

...................................................... 1

Conduct of Operations ..................................... 1

01 . 1 Unit 1 Reactor Startup and Power Ascension . . . . . . . . . . . . . . . . 1

01.2 Unplanned Unit 2 Load Reduction ........................ 4

Operational Status of Facilities and Equipment ..................... 5

02.1

125 Volt DC (VDC) Distribution System Walkdown ............ 5

02.2 Update on Service Water Biofouling ....................... 6

Miscellaneous Operations Issue ............................... 7

OS.1

(Closed) Inspector Followup Item 50-311197-03-02 ............ 7

OS.2 (Closed) Violation 50-311/97-07-01 ....................... S

OS.3 (Closed) LER 50-272/9S-002-00,9S-002-01 ................. S

II. Maintenance .................................................... 9

M 1

Conduct of Maintenance . . . . . . . . . . . . . . . . . . . . ................ 9

M 1 . 1 General Comments ................................... 9

M1 .2 Emergency Diesel Generator On-line Maintenance ............ 10

M2

Maintenance and Material Condition of Facilities and Equipment . . . . . . . 1 3

M2.1

11 Auxiliary Feedwater Pump Minimum Flow Line Leak ........ 13

MS

Miscellaneous Maintenance Issues . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

MS.1

(Closed) VIO 50-272&311 /96-0S-02,96-0S-03, 50-311 /96-1 S-02

............................................... 14

MS.2 (Closed) LER 50-272/97-013-00 ........................ 15

Ill. Engineering ..................................................... 16

E1

Conduct of Engineering .................................... 16

E1 .1

22 Steam Generator Steam Flow Transmitter (Update) ... : ..... 16

IV. Plant Support .................................................. 17

P1

P1 .1

Effectiveness of Licensee Controls in Identifying, Resolving and

Preventing Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1 7

P2

Status of EP Facilities, Equipment, Instrumentation and Supplies . . . . * . . 18

P3

EP Procedures and Documentation . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

P5

Staff Training and Qualification in EP . . . . . . . . . . . . . . . . . . . . . . . . . . 19

P6

EP Organization and Administration ........................... 20

P7

Quality Assurance in EP Activities ............................ 21

SS

Miscellaneous Security and Safeguards Issues ................... 22

SS. 1 Operational Security Response Evaluation for Hope Creek and Salem

............................................... 22

FS

Miscellaneous Fire Protection Issues .......................... 22

FS.1

Fire Protection Inspection for Hope Creek and Salem .......... 22

iv

V. Management Meetings .......... : ................................. 22

X1

Exit Meeting Summary .................................... 22 ,

INSPECTION PROCEDURES USED ...................................... 23

ITEMS OPENED, CLOSED, AND DISCUSSED ............................... 23

LIST OF ACRONYMS USED ........................................... 24

v

Report Details

Summary of Plant Status

Unit 1 began the period in Mode 4, and transitioned to Mode 3 on March 17, 1998.

Reactor startup began and criticality was achieved on April 7, 1998. The unit reached

Mode 1 on April 12, 1998 and 100% power on May 3, 1998.

Unit 2 began the period at approximately 50% power during a power ascension following a

unit forced outage. 100% power was achieved on March 17, 1998. Power was reduced

to 60% on March 24, 1998 in response to an unplanned loss of the 21 steam generator

feed pump, and later restored to full power the next day. On April 18, 1998, operators

reduced power and removed the unit from the offsite electrical network following the

unplanned inoperability of a service water cooling loop. Following resolution of the service

water issues, the unit. was synchronized to the offsite network on April 11, 1998. 100%

power was reached on April 13, 1998, and remained at that level for the balance of the

inspection period.

I. Operations

01

Conduct of Operations .

01 .1

Unit 1 Reactor Startup and Power Ascension

a.

Inspection Scope (71707. 71715)

On April 1, 1998, based on the recommendation of the Salem Assessment Panel

(SAP), the NRC modified Confirmatory Action Letter .(CAL) 1-95-009 to permit*

PSE&G to restart Salem Unit 1 . NRC resident and regional inspectors conducted

augmented inspection coverage of the Unit 1 reactor startup and low power physics

testing from April 7 - 11, 1998 .. Additionally, the resident inspectors closely

monitored subsequent power ascension activities through the end of the report

period, including the "hold point" testing and assessments at 25%, 50%, and 90%

power, as dictated by the CAL.

b.

Observations and Findings

Salem operators entered Mode 2 and achieved criticality at Unit 1 on April 7, 1998,

and then raised power to 1 o-s amperes in the intermediate range in order to conduct

low power physics testing. During this period, the inspectors observed that the

control room operators exhibited good use of procedures and, clear

c*ommunications. Additionally, good managerial and quality assurance department

oversight was noted, and control room distractions were kept to a minimum. Pre-

evolution briefings frequently incorporated lessons learned from the Unit 2 startup in

August 1997.

Several problems were noted during the reactor physics testing, largely stemming

from weak operations support from other departments. For example, the inspectors

2

witnessed a "control rod swap" reactivity measurement pre-evolution briefing

conducted by reactor engineers which lacked clarity and caused confusion among

reactor operators. The control room supervisor frequently stopped the briefing to

ensure that all questions and concerns were properly addressed. Additionally, an

equipment deficiency associated with an out-of-calibration pure water flow

integrator caused operators to over-dilute the reactor coolant system during the

test; which necessitated a subsequent unplanned boration to compensate for the

error. However, the boric acid volume recommended by the reactor engineer on

shift was incorrect because it was based on a faulty interpretation of control rod

worth tables. Because of a conservative operational practice to borate and dilute in

increments that were half the recommended volumes, the effect of this boration

error was minimized.

The inspectors also observed a weakness in operations support during the execution

of a boron endpoint determination test. This test, conducted in accordance with

procedure 51 .RE-RA.ZZ-0005 (0), required three separate attempts in order to be

successfully completed~ Specifically, operators experienced difficulty preventing

power from exceeding 95 % of the indicating scale on the reactivity computer during

the test. This issue was due primarily to coordination problems between the

operator performing the required reactivity manipulations and the reactor engineer

directing the evolution.

A final example involved a chemistry department recommended lithium hydroxide

addition to the reactor c;:oolant system to adjust plant pH levels. While Unit 1 was

still at 1 o-s amperes for physics testing, operators approved the chemical addition.

In order to understand the impact this addition would have on reactivity, chemistry

technicians informed the operators that approximately 10 gallons of pure water

would be added to the plant. After the addition was completed, operators promptly

identified that reactor power was increasing at a rate greater than expected, and

added boric acid to reduce power back to the desired level. Based on volume

control tank level changes, operators computed that nearly 90 gallons of pure water

had been injected during the chemical addition. The discrepancy between the

expected and actual water volumes, which caused a greater than anticipated

reactivity excursion, was later attributed to insufficient system operating knowledge

by the involved chemistry technicians.

Because of the self-revealing nature of the above .issues, PSE&G operations

management and quality assurance inspectors were promptly aware of the

concerns, and responded appropriately to each. Corrective action requests were

initiated both to document each of the discrete issues and to integrate all of the

concerns associated specifically with reactivity management into a single

comprehensive review. As each issue was identified, plant supervision placed a

hold on further Unit 1 evolutions until the causes were understood and interim

corrective measures were implemented. Additionally, these and other issues were

discussed at length at the PSE&G management review committee meeting

conducted at the 25 % power hold point .

_i

3

Following completion of the reactor physics testing, operators slowly and

deliberately raised reactor power to 25% in accordance with procedure TS1 .SE-

SU.ZZ-0001 (0), Startup and Power Ascension Sequence, and S1 .OP-IO.ZZ-

0003(0), Hot Standby to Minimum Load. Unit 1 achieved Mode 1 on April 12,

1998, and was later synchronized to the offsite electrical network on April 17,

1998. Several emergent secondary plant issues were promptly and effectively

addressed during this period, including minor steam and water leaks, a small fire,

and an inadvertent CARDOX initiation in the main generator exciter housing. The

inspectors observed main turbine overspeed trip testing, generator loading, and

reactor core flux mapping during this period. All of these evolutions were

thoroughly briefed, properly supervised, and implemented with successful results.

On April 18, 1998, members of the SAP held a conference call with PSE&G

management to review the station's request for release from the 25% power hold

point. During the call, the SAP discussed PSE&G's internal assessments of Unit 1

startup issues and test results, including all of the issues described above. During

the post-call caucus, the SAP concluded that PSE&G's assessment was sufficiently

self-critical and that adequate plans were either completed or in place to implement

needed corrective actions. As a result, the.SAP recommended and the Regional

Administrator subsequently approved a release from the 25 % hold point.

On April 23, 1998, with Unit 1 at 47% power, operators successfully completed a

planned 10% load swing test. This test verified that the newly in$talled dig.ital

feedwater control system was capable of properly responding to small load

changes. No problems were noted during this test. On April 24, 1998, the SAP

held another conference call with PSE&G management to discuss release from the

50% power hold point. With the exception of a status update of recent service

water system biofouling concerns (see Section 02.2 of this report), no significant

equipment or human performance issues were raised during the conference call. As

such, later that day, the Regional Administrator approved a release from the 50%

hold point .

. On April 30, 1998, the inspectors witnessed the conduct of a 25% load rejection

test from an initial 88 % power level, again conducted to verify the performance of

the digital feedwater control system. Operators prepared for this evolutions by

conducting dynamic training in the Unit simulator. While the feedwater controls

responded appropriately to the planned transient, operators observed apparently

abnormal control rod speed fluctuations with the rod control system in "automatic."

Upon recognition of this issue, operators promptly placed the control rods in

"manual" until the cause of the unexpected response could be understood and

corrected. During the following week, the inspectors observed maintenance

technicians and engineering personnel implement a well controlled and

comprehensive rod control system troubleshooting plan and transient response

evaluation.

On May 1, 1998, the NRC SAP members held another conference call with PSE&G

management, this time to discuss a requested release from the 90% power hold

point. Discussions during this call primarily centered on the apparent rod control

c.

4

system anomalies experienced during the 25 % load rejection testing. Based on

PSE&G management's planned actions to promptly evaluate and correct this

apparent rod control problem, and to discuss the final assessment of this issue with

the SAP prior to commencing a planned 40% load reduction and feed pump trip

test, the NRC released Unit 1 from the 90% power hold point and permitted PSE&G

to raise power to 100%. On May 3, 1998, Salem operators achieved 100% power

at Unit 1.

At the conclusion of the report period, only the 40% load reduction and feedwater

pump trip test from 90% power remained outstanding in the Unit 1 restart and

power ascension test plan. The modified NRC CAL 1-95-009 remained in effect

until PSE&G successfully completed these tests and performed a comprehensive

assessment of the startup test plan and any "lessons learned." The inspectors

independently concluded that overall, PSE&G's implementation of the Unit 1 restart

plan was an improvement over the Unit 2 restart (see NRC Inspection Report 50-

311 /97-15), as indicated by fewer emergent equipment deficiencies and test

coordination errors.

Conclusions

Overall, Salem plant management and staff controlled the Unit 1 reactor startup and

power ascension test activities well. The operating crews were attentive, used

excellent communication skills, and responded appropriately to plcmned and

emergent events and issues. Reactor engineering and chemistry department

support, as well as pre-evolution briefings, were usually of good quality although

some deficiencies were observed during low power physics testing. Strong

management and quality assurance oversight was indicated by continuous on-site

presence during restart activities and a willingness to halt further plant evolutions

following the identification of emergent issues. Good self-assessment capability

was evident during hold point release discussions with the NRC Salem Assessment

Panel.

01 .2 Unplanned Unit 2 Load Reduction

a.

Inspection Scope (93702)

b.

The inspectors reviewed Salem Unit 2 operators response to a March 24, 1998

event involving an electrical power transient affecting steam generator feed pump

(SGFP) controls.

Observations and Findings

An unexpected electrical power spike resulted in the momentary partial loss of non-

vital 115 volt AC power. This event in turn caused a shutdown of the 21 SGFP,

which lost governor control power. Operators acknowledged the associated

overhead alarm, observed that the 21 SGFP speed was lowering, and initiated a

manual main turbine generator load reduction to 60% power. Based on operator

interviews and a review of narrative logs, the inspectors determined that plant

c.

5

operators correctly followed alarm response and abnormal operating procedures to

stabilize the plant. The inspectors found the impact of this event on plant safety *

minimal, in that all plant systems responded as designed to the transient and no

safety systems were challenged as a result. Operators returned Unit 2 to full power

on March 25, 1 998 after Jesting all affected equipment to verify continued proper

operation. At the conclusion of the report period, PSE&G had not determined the

root* cause for this electrical transient event, but also concluded that all plant

equipment functioned as designed in response to the transient.

Conclusions

Operators responded promptly and effectively to an unexpected transient associated

with the 21 steam generator feed pump while a 100% power. All plant equipment

functioned as designed during the transient ..

02

Operational Status of Facilities and Equipment

02.1

125 Volt DC (VDC) Distribution System Walkdown

a.

b.

Inspection Scope (71707)

The inspectors conducted a comprehensive wal!<down of the accessible portions of

the 125 VDC electrical distribution system. The inspectors reviewed the Updated

Final Safety Analysis Report (UFSAR), Technical Specifications (TS), Configuration

Baseline Documentation, and TS surveillance procedures for background

information.

Observations and Findings

Material condition and housekeeping of 125 VDC batteries and associated busses

were acceptable at both Salem units. System configuration was consistent with

UFSAR system descriptions, and was properly aligned for existing plant conditions.

The inspectors reviewed procedures S1 (52).0P-ST.125-0001, "Electrical Power

Systems 1 25 VDC Distribution," and determined that the procedure adequately

verified system operability requirements specified in plant TS at the appropriate

frequency. Some minor discrepancies were noted and brought to the attention of

system engineering. For example, two cells on the 28 125 VDC battery had plates

which were slightly bowed. Actions taken to address these items were timely and

appropriate.

c.

Conclusions

The 125 volt DC electrical distribution system was properly aligned for existing

plant conditions at Unit 1 and 2. Material condition and housekeeping were

acceptable. Adequate surveillance test procedures were implemented to verify

system operability .

6

02.2 Update on Service Water Biofouling.

a.

Inspection Scope (40500. 92901, 92902, 92903)

b.

The inspectors reviewed PSE&G's response and actions taken to address degraded

service water system (SW) strainers. Related SW brofouling issues were previously

discussed in NRC Inspection Report 50-272 & 311/98-01.

Observations and Findings

On April 3, 1998, maintenance technicians identified one missing filter disk and five

cracked filter disk retaining rings during an internal inspect.ion of 23 SW pump

discharge strainer (Unit 2). A similar inspection of 14 SW strainer (Unit 1) also

revealed one missing disk and approximately forty cracked retaining rings. No

adverse temperature trends were identified in any SW cooled heat exchangers.

PSE&G engineers attributed the cause of the cracked rings to excessive torque

during installation. The plastic retaining rings were installed using an air impact

wrench, with no specific torque requirement. Strainer manufacturer, S. P. Kinney

Engineers, Inc., indicated that factory installation of the rings is "hand tight plus an

additional one half of one turn." Maintenance procedure SC.MD-PM.SW-0003,

"Service Water Auto Strainer Adjustment, Inspection, Repair, and Replacement," did *

not specify a particular method of ring installation. Air wrenches were used to

expedite the task, since hand installation requires several days to complete. PSE&G

management decided to overhaul each Unit 1 and 2 SW strainer ( 12 total) and

install each new retaining ring by hand. The inspectors verified that the noted

maintenance procedure was modified to specify hand installation of the retaining

rings.

On April 8, 1998, with Salem Unit 2 at 100%, operators declared one of the two

service water (SW) loops inoperable due to both the 24 and 25 SW pump strainer

motors tripping on overload. This rendered the associated pumps inoperable.

Technical Specification 3. 7.4 requires two operable SW loops, and the action

statement allows 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> to restore the inoperable SW loop to an operable status

before a unit shutdown is required. At the time of event, one of the. three strainers

in the opposite SW loop was also unavailable due to pre-planned corrective

maintenance. An NRC inspector was in the control room at the time of this event

and observed. that plant operators acted appropriately in response to the observed

conditions. At the time of the event, Salem Unit 1 was in Mode 2 with low power

physics testing in progress; no effects on the Unit 1 SW system were observed.

_ Within three hours of this event, PSE&G management elected to reduce power and

take Unit 2 off-line for further investigation and repairs of the strainers, well before

the expiration of the 72-hour TS allowed outage time. Subsequent inspections of

the affected strainers revealed that they were clogged with excessive amounts of

grass and debris. Though the root cause evaluation for this event was not yet

completed by the end of the report period, several corrective actions were

implemented, including: overhauling the SW strainers, replacing the strainer motor

overload heaters, and adjusting all of the traveling screen spraywash nozzles. By

c.

7

the* end of the report period, all of the Unit 1 and Unit 2 SW strainers had been

overhauled, and most overload heaters were replaced with higher capacity

overloads. The remaining overload heaters have been scheduled for replacement.

The inspectors reviewed the overload sizing calculations, and no problems were

noted. The inspectors also determined that the overload modification would not

negatively impact electrical loading during accident conditions.

Conclusions

PSE&G's actions to address and correct the cause of missing service water (SW)

strainer filter disks and cracked filter disk retaining rings were appropriate and

promptly implemented. Unit 2 control operators responded promptly to the clogging

of two SW pump discharge strainers in the SW same loop. PSE&G management's

decision to take Salem unit 2 off-line for strainer repairs was appropriate, and

corrective actions were adequate.

08

Miscellaneous Operations Issues

08.1

(Closed) Inspector Followup Item 50-311 /97-03-02: Management Commitment

Process

a .

b.

Inspection Scope (92702)

The inspectors reviewed and assessed a recent revision to the commitment

management program procedure as a follow up to a similar review performed while

evaluating Salem Unit 1 and Unit 2 for restart readiness.

Observations and Findings

As part*of the restart action plan, Salem staff evaluated the commitment

management process and subsequently instituted corrective actions to correct

program deficiencies. One of these tasks, a revision of the commitment

management program procedure, was not completed at the time NRC staff was

inspecting the commitment process for restart readiness, and was therefore left

open pending a review and assessment of the final procedure. PSE&G issued the

revised commitment management procedure, NC.NA-AP.ZZ-0030(0) in May 1997.

The inspectors reviewed the document and determined that the procedure and

program modifications were acceptable. This item is closed.

c.

Conclusions

PSE&G appropriately revised the process by which license commitments are tracked

and managed .

8

08.2 (Closed) Violation 50-311197-07-01.: Failure to establish containment integrity

within eight hours

a.

Inspection Scope (92702)

The inspectors performed an on-site review and verification of PSE&G's corrective

actions for the subject Notice of Violation.

b.

Observations and Findings

In the violation response letter dated June 13, 1997, PSE&G management

attributed the event cause to inadequate tracking of i.noperable equipment. In

response, PSE&G provided electrical systems technical specifications refresher

training to licensed operators, and enhanced the technical specifications action

statement tracking log. The inspector reviewed the refresher training and the

  • revised tracking log and determined these corrective actions were reasonable and

complete. This item is closed.

c.

Conclusions

The PSE&G staff developed and implemented timely and reasonable corrective

actions for a Notice of Violation involving a failure to promptly establish

containment integrity .

08.3 (Closed) LER 50-272/98-002-00,98-002-01: Auxiliary building ventilation excess

flow damper found wired open with spring removed

a.

Inspection Scope (90712. 92700)

The inspectors performed an on site review of LER 50-272/98-002-00. LER 50-

272/98-002 Supplement 1, which documented the results of an evaluation

performed to determine the safety significance of this issue. The inspectors

reviewed and discussed the noted evaluation with PSE&G design engineers.

b.

Observations and Findings

The circumstances surrounding the initial discovery and corrective actions related to

this issue were previously discussed in NRC Inspection Report 50-272 & 311 /97-

21 . No new issues were identified in this LER and all stated corrective actions have

been completed. As such, this LER is closed.

Based in part on a discussion with PSE&G design engineers, the safety significance

evaluation completed for this event was deemed to be reasonable. Specifically, this

event had limited safety significance since the control room and offsite dose

consequences were bounded by the loss of coolant accident and steam line break

analyses. This LER supplement is closed .

c.

9

Conclusions

Corrective actions for LER 50-272/98-002-00were reasonable and complete. The

safety significance evaluation performed for this event, documented in LER

Supplement 1, was also acceptable.

/

II. Maintenance

M 1

Conduct of Maintenance

M 1 . 1 General Comments

The inspectors observed all or portions of the following work activities and technical

specification surveillance tests:

  • * * *
  • *
  • * * * * *
  • * * * * * * * * *

WiO 980311218:

W/O 980315118:

W/O 980315129:

W/O 971005022:

W/O 990131032:

W/O 971228015:

W/O 980331158:

W/O 910529001: *

15 Service water strainer - inspect and check clearness

Ultra-sonic test of 12 AFW minimum-flow orifice area

Ultra-sonic test of 22 AFW minimum-flow orifice area

22 Charging pump lube oil heat exchanger - open, clean

and inspect

22 Charging pump gear box heat exchanger - open,

clean and inspect

22 Charging pump, clean and repack couplings

16 Service water strainer inspection/retaining ring

replacement

12 Containment hydrogen analyzer - replace hydrogen

sensor

W /0 980408061 :

25 Service water pump strainer backwash valve -

W/O 980408059:

W/O 971216022:

W/O 970605093:

W/O 980312302:

W/O 980320186:

w /0 98051 6040:

inspect

24 Service water pump strainer - open and inspect

28 EOG lube oil heater - remove, clean, and inspect

28 EOG switch replacement

14 SW strainer grass and clearance inspection

13 SW strainer grass and clearance inspection

Radiography test of 11 SW53 ( 13 CFCU inlet check

valve)

W /0 980328091 :

Repair 25 SW strainer (seized)

W/O 980312297:

23 SW strainer grass and clearance inspection

W /0 98041 2104:

2A EOG fuel oil leak repair on 9R fuel pump

W /0 960513198:

2C EOG oil leak repair on 6L cylinder

S1 .RE-RA.ZZ-0005: Boron endpoint determination

51.IC-FT.NIS-0014: 1N36functional test

S 1 . IC-CC. RCP-0018: 1 PT546 (pressurizer pressure channel 2) calibration

S1 .IC-CC.RCP-0023:1 PT474(pressurizer pressure channel 4) calibration

S2.MO-FT.4KV-0002:2Bvital bus undervoltage testing

S2.0P-SO.OG-0002: 28 EOG 15-minute post-maintenance run

10

The inspectors observed that the plant staff performed the maintenance activities

effectively and in accordance with the standards defined by the station maintenance

program. Salem plant staff also completed the noted surveillance tests safely, and

effectively proved the operability of the associated systems. Minor deficiencies

noted by the inspectors were referred to and promptly corrected by the PSE&G

staff.

M1 .2 Emergency Diesel Generator On-line Maintenance

a.

Inspection Scope (71707,62707 ,92901 ,92902)

The inspectors reviewed the limiting condition for operation (LCO) maintenance plan

for the April 14, 1998 28 emergency diesel generator (EOG) planned maintenance

outage, observed implementation of associated work activities, and interviewed

PSE&G management concerning the plan. The inspectors also reviewed

documentation for the March 13, 1998 1 B EOG outage, and the April 21, 1998 2C

EDG planned maintenance outage.

b.

Observations and Findings

1 B EOG Outage:

At 4:41 a.m. on March 18, 1998, the 1 B EDG service water inlet i.solation valve

failed to open within its allowed time period during a technical specification

surveillance test. Operators appropriately declared the diesel inoperable and

initiated a work order to troubleshoot the problem. The work order was finalized

and tags were hung at 3:31 p.m. to commence work. However, the work was not

authorized to begin until 10:40 p.m., a delay of about seven hours. Additionally,

after work completion, the tag release was authorized at 11 :53 p.m., but the tags

were not cleared until 2: 12 a.m. the next morning, resulting in another two-hour

delay. The EOG retest was completed at 3:19 a.m. on March 19.*

The inspectors agreed with PSE&G's subsequent assessment that oversight of this

emergent work item was weak. PSE&G documented this issue in a corrective

action request and concluded that the primary cause for the ineffective management

was the lack of an established single point of contact to coordinate the work.

Additionally, operations and maintenance personnel were insensitive to the urgency

of returning safety equipment to an operable status, and the need to minimize

unavailabi.lity time for maintenance rule requirements.

28 EDG Outage:

At 5:47 a.m. on April 14, 1998, operators removed the 28 EOG from service for

planned on-line maintenance. PSE&G developed an LCO maintenance plan for this

outage in accordance with procedure SC.SA-SD.ZZ-0011 (Z), "Work Management

Manual (WMM)." The inspectors noted that the content of the plan was thorough

and met the standards of the WMM, including an assessment of the plan's impact

on both overall plant risk and maintenance rule performance criteria.

11

PSE&G planning personnel recognized about 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> after the on-line outage

began that EOG service water (SW) valves were inappropriately tagged and the heat

exchanger drained. Plant operators were promptly informed after discovery of this

issue. Specifically, a biofouling inspection of the SW jacket water/lube oil heat

exchanger was originally planned as part of EOG outage work scope, but was later

removed from the scope three weeks prior to the work. This change in scope was

not effectively communicated to the operations department staff, and as a result,

the EOG SW system was unnecessarily tagged out and drained, delaying the

implementation of other necessary work. Additionally, the Salem staff also

determined that appropriate fire protection impairments had not been prepared for

the SW outage, nor was there a scheduled activity for a required jacket water

chemistry sample. These issues further delayed the completion of this non-required

work activity.

The inspectors observed various individual maintenance activities conducted during

the outage and noted that workers used approved procedures, had copies of work

orders and prints at the work site, and maintained work areas in a neat and orderly

manner. Temporarily installed scaffolding was structurally sound and had the

required permit attached! The inspectors observed that work supervisors frequently

toured the work area.

On April 15, PSE&G personnel identified an equipment tagging "near miss" during

the 28 EOG outage. Specifically, the day shift l&C supervisor rec~ived a turnover

from the night supervisor that a partial tag release could be executed for a diesel

control power breaker. This breaker had a red blocking tag attached due to various

electrical work being performed. The supervisor authorized the temporary release

without reviewing all activated work orders that were in progress. At the time, l&C

technicians were performing maintenance activities which were protected by this

tag. An alert electrical supervisor monitoring work in the 28 EOG room observed

the l&C work in progress and stopped the operator from releasing the tag.

The inspectors noted that PSE&G's administrative procedure NC.NA-AP.ZZ-0015,

"Safety Tagging Program," requires that "responsible individuals ensure that

personnel protected by safety tags are notified and clear of the equipment when

authorizing a tag release." The inspectors concluded that the failure to implement

this step of the procedure was a violation of TS 6.8.1, which requires that

procedures be implemented for control of safety-related equipment. PSE&G

corrective actions for this event included counseling the individuals involved in the

improper tagging release, and re-emphasis on the need for tagging process

adherence to craft personnel during a weekly department meeting. This self-

identified and corrected violation is being treated as a Non-Cited Violation consistent

with Section Vll.8.1 of the NRC Enforcement Policy. (NCV 50-311/98-03-01 ).

All pre-planned 28 EOG maintenance was completed at 1: 12 a.m. on April 16, yet

blocking tags were not removed until about 9:00 a.m., resulting in another eight

hour delay. The inspector noted that there was no clearly designated coordinator of

the LCO plan to ensure its timely completion. Also, operators were not sufficiently

sensitive to the priority of returning the 28 EOG to an operable status, and as such

c.

12

did not pursue blocking tag removal. in a timely manner. This unnecessarily delayed

post-maintenance testing, and resulted in the 28 EDG not being returned to

operability until 5:18 p.m. on April 16. The actual overall outage duration was 59

hours, or 82% of the 72-hour TS allowed outage time (AOT), while the planned

duration was 60% of the AOT. PSE&G management understood and recognized

that this on-line maintenance would result.in exceeding the 28 EDG maintenance

rule performance criteria, however, the noted delays unnecessarily extended the

diesel's unavailability. The 28 EDG will now be classified category a(1) under the

maintenance rule, which requires that specific performance goals be established and

monitored.

PSE&G management also recognized the poor execution of the 28 EDG planned

outage and aggressively implemented corrective actions. A level two action request

was initiated to evaluate the inadequate preparation for and execution of the work.

An outage critique was held on Friday, April 17, to capture lessons learned,

especially since the 2C EDG was scheduled for a similar outage the following week.

Additionally, the planning supervisor issued a memorandum with specific

expectations for the preparation and implementation of LCO maintenance plans,

including the formation of work week teams to oversee LCO maintenance, deadlines

for plan and prerequisite signoffs, and specific guidance concerning tagging

implementation.

2C EDG Outage:

Operators removed the 2C EDG from service at 5:46 a.m. on April 21, 1998 for

planned on-line maintenance. "Critical path" for the outage was equipment

calibration by l&C personnel. This work was turned over to the "12-hour shift"

maintenance crew so that the work could be pursued around the clock. However,

the 1 2-hour crew was not familiar with the scheduled instrument calibration

procedures and required assistance from day shift l&C technicians who were.

Additionally, the 12-hour shift technicians were diverted from the critical path work

to assist in maintenance on a boric acid transfer pump, for which there was no TS

limiting condition for operation. Further, the commencement of work was delayed

about three hours due to tagging inefficiencies. Overall PSE&G determined that

these delays resulted in a 2C EOG outage duration of 59 hours6.828704e-4 days <br />0.0164 hours <br />9.755291e-5 weeks <br />2.24495e-5 months <br /> instead of the

scheduled 42 hours4.861111e-4 days <br />0.0117 hours <br />6.944444e-5 weeks <br />1.5981e-5 months <br />.

PSE&G management recognized the noted deficiencies during the conduct of a

critique of the 2C EOG planned maintenance and initiated an action request to

  • document the assessment. Corrective actions were still being developed at the

conclusion of the inspection report period.

Conclusions

PSE&G determined tha.t the lack of clear ownership for and coordination of recent

emergency diesel generator (EDG) on-line maintenance outages resulted in

unnecessary delays in work completion, extending the overall equipment

unavailability time. Inadequate tagging controls during the 28 EDG outage resulted

in an electrical breaker blocl<ing tag being released while personnel were actively

working on equipment supplied by that breaker.

-1

. -I

13

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1

11 Auxiliary Feedwater Pump Minimum Flow Line Leak

a.

Inspection Scope (92902, 92903)

On March 14, 1998, an equipment operator identified a through-wall leak on the

discharge weld of the 11 auxiliary feedwater (AFW) pump minimum-flow line orifice.

The inspectors reviewed PSE&G's actions to correct this degraded condition and

ensure that redundant trains of equipment were not similarly degraded.

b.

Observations and Findings

PSE&G determined that the leak from the 11 AFW orifice was approximately 25-30

drops per minute on the outlet of the minimum-flow orifice, where a stainless steel

coupling is welded to the downstream carbon steel pipe. When the leak was

discovered, the 11 AFW pump was in service, but was not required to be operable

in accordance with technical specifications (TS). Engineers determined that the root

cause of the leak was cavitation at the discharge of the minimum-flow orifice.

Technicians repaired the 11 AFW orifice weld and examined the equivalent piping

for the 12 AFW pump by using ultrasonic testing. Since these re~ults were

acceptable, Unit 1 operators proceeded with a mode change from mode 4 to 3, an

operating condition which requires AFW to be operable. Subsequently, engineers

recommended a radiographic test of the 12 AFW line to provide a clearer picture of

the affected area of pipe. This test revealed that the wall thickness on the 1 2 AFW

pipe was .085 inches, less than minimum wall thickness of . 14 7 inches, contrary to

the earlier ultrasonic examination. Operators declared the 12 AFW train inoperable

and entered the 72-hour TS 3. 7 .1.2.a action statement to initiate repairs.

PSE&G technicians also performed an ultra-sonic test of the same piping for the 22

AFW (Unit 2) pump. This inspection revealed an acceptable wall thickness of .235

inches, and no cavitation damage like that found on the Unit 1 pumps, likely due to

the fact that the Unit 2 AFW pumps are newer and have less run time than the Unit

1 pumps. Also, PSE&G design engineering performed a calculation which showed

that .040 inches of wall thickness was sufficient to withstand the design pressure

at the orifice outlet. Based on this information, inspections of the 21 and 23 AFW

pumps were scheduled for August and September 1998, respectively.

Based on the activities associated with the 11 AFW pump orifice leak, PSE&G

determined that only the steam-driven AFW pump (13 and 23) discharge piping was

included in the FAC program. However, the motor-driven pumps had greater run

times since they are normally operated during unit shutdowns. PSE&G revised the

FAC program scope to include monitoring all the AFW pumps discharge and

minimum flow line piping .

c.

14

Conclusions

PSE&G implemented appropriate corrective actions to repair degraded auxiliary

feedwater piping revealed by a through-wall leak on a pump minimum-flow orifice

line. Technical specification and ASME code class 3 requirements were satisfied.

However, this event revealed a weakness in scope of the flow-accelerated corrosion*

program in that only the steam-driven pumps were included for monitoring.

MS

Miscellaneous Maintenance Issues

M8.1 (Closed) VIO 50-272&311/96-08-02,96-08-03,50-311 /96-18-02

a.

Inspection Scope (92702)

b.

Based on an on-site review and verification of corrective actions, the inspectors

assessed PSE&G's response to the previously-cited violations described below ..

Observations and Findings

VIO 50-272&311 /96-08-02: failure to perform post maintenance testing (PMT). In

a letter dated September 9, 1996, PSE&G attributed the cause of this violation to

personnel error and improper procedure use for controlling PMT work. In response,

Salem staff reviewed the event with maintenance personnel and r.evised the work

management desk guide, SC.MD-DG.Z-0001 (Z), to clarify PMT requirements. The

inspector reviewed the revised desk guide and determined that the corrective action

was implemented. This item is closed.

VIO 50-272&311 /96-08-03: inadequate safety-related material storage. In a letter

dated September 9, 1996, PSE&G attributed the cause of this violation to a failure

to follow procedures and inadequate implementation of management expectations.

In response, Salem staff revised the material handling procedure, NC.NA-AP.ZZ-

0018(0), to add sufficient detail regarding the proper storage of material. The staff

also completed a follow up self assessment in October 1996, which verified that

personnel were properly storing material. The inspector reviewed the results of the

assessment and the noted procedure revision and determined that these corrective

actions were reasonable. This item is closed.

VIO 50-311/96-18-02: lack of containment closure during refueling. In a letter

dated March 20, 1997, PSE&G attributed the cause of this violation to inadequate

implementation of outage scheduling and risk management requirements. In

response, PSE&G staff implemented a continuing training program on outage risk

management, to be administered to outage management and planning and

scheduling personnel. The staff also revised the containment closure procedure,

S1/S2.QP-ST.CAN-0007,to incorporate the posting of penetration areas to restrict

work in those areas during core alterations, and to provide clarification of criteria for

determining that a system is intact. The inspector reviewed the training program

and procedure revisions and determined that these corrective actions were

. appropriate. This item. is closed.

c.

15

VIO 50-311197-14-03: failure to follow technical specification 6.8. 1 procedure.

The inspectors reviewed PSE&G's response to the Notice of Violation (NOV), dated

September 12, 1997, regarding test equipment left installed on the 2A emergency

diesel generator. Licensee Event Report 50-272/97-013-00,also describes the

circumstances and corrective actions associated with this issue. See section M8.2

below for the inspector's review and assessment.

Conclusions

PSE&G responses to the previously-identified issues were timely arid reasonable.

The inspectors verified that all committed actions were completed.

M8.2 (Closed) LER 50-272/97-013-00:failure to meet technical specification 3.8.1.1

action b

a.

Inspection Scope (92700, 92901, 92902. 92903)

b.

On July 2, 1997, following surveillance testing, the 2A emergency diesel generator

(EOG) was inappropriately declared operable with electrical test equipment still

installed in the EDG control cabinet. This issue was discussed in NRC Inspection

Report 50-272 & 311/97-14and dispositioned as a cited violation. The inspectors

performed an on-site review the corrective actions specified in this licensee event

report (LER) .

Observations and Findings

After this issue was identified, a follow-up surveillance test was performed

satisfactorily, and the test equipment was removed. PSE&G attributed the cause of

this event to human error. Operators did not perform the surveillance test

restoration completely, in that they left test equipment connected to support

subsequent work. Station administrative procedures allow omitting procedure steps

(i.e. marking them "not applicable"), if the partial performance does not change the

intent of the procedure. In this case, the intent of the procedure was changed

because the pre-test condition was not fully restored. Following this event, Salem

management re-emphasized the expectations concerning procedure use to all plant

personnel. The inspectors determined that the operations department guidance for

procedure use was revised to require the concurrence of two operators, at least one

of whom shall be a supervisor, before a procedure step is determined to be "not

applicable."

Additionally, the EDG surveillance test equipment was modified by installing safety-

related fuses to separate the Class IE equipment from the test equipment. The

inspector reviewed and discussed the fuse selection calculation with Salem design

engineering personnel and did not note any problems. Adequate controls were

established for maintaining safety-related fuses in the test equipment. The

inspectors also reviewed the 10 CFR 50.59 safety evaluation for considering the

EDG system operable with temporary test equipment connected. The safety

evaluation was adequate. This LER is closed.

c.

16

Conclusions

Corrective actions taken to address the deficiencies identified following the improper

restoration of a Unit 2 emergency diesel generator were adequate. Associated

design calculations and safety evaluations were thorough.

Ill. Engineering

E 1

Conduct of Engineering

E1. 1

22 Steam Generator Steam Flow Transmitter (Update)

a.

Inspection Scope (92902, 92903)

b.

c.

The failure of the 22 steam generator (SG) steam flow transmitter for channels II

and Ill was documented in NRC Inspection Report (IR) 97-18 and updated in IR 97-

21 . The inspector followed up on subsequent licensee actions to correct this

persistent problem.

Observations and Findings

PSE&G technicians replaced the low side sensing line during the recent Unit 2

forced outage. Inspection of the old sensing line revealed that the drain hole which

carries condensation back to the main steam line was plugged with debris. PSE&G

concluded that this was evidently the root cause for the high steam flow indications

which these channels had been exhibiting. Operators monitored these channels

after returning Unit 2 to power operation and noted normal indications, consistent

with other steam flow channels. The channels were successfully tested by a

special test procedure to ensure that they would respond appropriately to power

changes. PSE&G then restored the channels to operation, and removed the forced

values to the digital feed water system.

Conclusions

PSE&G restored the 22 steam generator steam flow channels II and Ill to an

operable status .in a slow and deliberate manner, meeting all technical specification

requirements during the process .

P1

a.

17

IV. Plant Support

Conduct of Emergency Preparedness (EP) Activities

Effectiveness of Licensee Controls in Identifying, Resolving and Preventing Problems

Inspection Scope (82701)

The inspectors reviewed PSE&G's process for identifying, tracking and resolving EP-

related items.

b.

Observations and Findings

c.

The EP staff utilized an automated corrective action tracking system maintained by

the Quality Assurance group. PSE&G used the system as a mechanism for

reporting conditions requiring corrective action, program enhancement and

drill/exercise issues. The program was maintained by the EP Corrective Action

Coordinator who tracked items and ensured corrective actions were timely and

adequate. This was a good initiative because prior to mid-1997, the EP staff used

several different tracking systems. It was evident during this inspection that having

one system with a dedicated coordinator provided continuity and immediate

attention, and provided EP management with continual oversight of EP-related open

items .

While reviewing past action item reports, the inspectors noted that some of the

issues discussed in the previous NRC inspection had not been resolved in a timely

manner. For example, a lapse in respirator qualifications was identified by the NRC

in late 1996 and the issue, although improved, was not ye~ fully resolved. The

backup diesel generator located in the Emergency Operations Facility (EOF) has

been found to be inadequately maintained in the past two internal audits. Also,

Emergency Action Level (EAL) charts were not adequately updated to reflect the

NUMARC EAL classification scheme because of a burdensome review and approval

process. PSE&G personnel acknowledged these had to be coordinated with other

departments for resolution, and planned to better prioritize issues that required

resolution.

Additionally, PSE&G's EP Self-:assessment program had improved and was deemed

effective. Since January 1, 1997, PSE&G completed nine self-assessments. A

review of the corrective actions associated with the self-assessment findings

indicated that they were properly tracked and trended, and that corrective actions

were being effectively implemented to resolve programmatic weaknesses.

Conclusions

Based upon the review of selected items and procedures, the inspectors concluded

that PSE&G's method for tracking EP corrective actions was very good and that the

EP self-assessment program provided good feedback to the staff. The timeliness of

resolving some identified issues was weak.

18

P2

Status of EP Facilities, Equipment, Instrumentation and Supplies

a.

Inspection Scope (82701}

The inspectors conducted an audit of emergency equipment in the control room, the

operations support center (OSC), the technical support center (TSC), and the

emergency operations facility (EOF) to assess facility readiness. Also, the

inspectors reviewed documentation of equipment surveillance tests conducted since

the last EP program inspection for completeness and accuracy.

b.

Observations and Findings

EP equipment checklists were main.tained accurately. Radiological survey

instruments at the facilities were all within the designated calibration period. The

inspectors reviewed equipment surveillance tests and inventory checklists and

determined that they were completed as required, and that any discrepancies were

resolved in a timely manner. The inspectors reviewed the monthly communication

test records and determined that Emergency Response Organization responders

were timely and that EP management was proactive in retrieving station badges if a

responder failed to reply. PSE&G recently switched pager vendors and problems

have been identified in which not all the pagers activated when required. PSE&G

staff indicated that in these cases PSE&G verified that PSE&G would be able to

minimally staff the emergency facilities if activated at that time. flesolution of this

issue was being actively pursued.

The inspectors toured the new combined Hope Creek/Salem OSC and EOF. The

facilities were enlarged and the layout was much improved for accommodating the

needs of the emergency responders. PSE&G plans to combine the Hope

Creek/Salem technical support centers in 1999. These enhancements demonstrated

PSE&G's commitment to support the EP function.

Additionally, the inspectors determined through document reviews and discussions

with EP staff that the siren system was properly maintained and tested as required

by the Emergency Plan (E-Plan) and applicable procedures. Work orders generated

due to equipment malfunctions were tracked to completion and once a work request

was initiated, repairs were completed within 24-48 hours.

c.

Conclusions

The emergency preparedness facilities and equipment were in a good state of

operational readiness. Surveillance tests and inventories were performed as

required and discrepancies were resolved in a timely manner. Expenditure of

resources to improve equipment and facilities demonstrated PSE&G's commitment

to support and maintain the EP program. Overall, the inspectors considered this

area to be very good .

19

P3

EP Procedures and Documentation .

a.

  • Inspection Scope (82701 l

The inspectors assessed the process which PSE&G used to review and change the

E-Plan and implementing procedures (EPIPs). The inspectors also reviewed recent

EPIP/E-Plan changes to assess the impact on the effectiveness of the EP program.

Further, the inspectors verified that appropriate letters of agreement were in place

with offsite emergency agencies.

b.

Observations and Findings

The inspectors assessed the 10 CFR 50.54(q) (effectiveness review) process for E-

Plan changes and the annual E-Plan review process performed by the licensee. The

reviews were thorough, and met NRC requirements as well as commitments made

in the Updated Final Safety Analysis Report (UFSAR) and the E-Plan.

The inspectors conducted an in-office review of recent EPIP/E-Plan changes and

found the EPIPs lacked detail and clarity, and that paragraphs had been

inadvertently removed during the revision process. Also, the inspectors determined

that PSE&G was not routinely reviewing the EPIPs to ensure they were consistent

with E-Plan requirements and adequately described the current program. In*

addition, the inspector often found it difficult to determine the ad~quacy of changes

because the changes were not always identified and the basis for the change was

not easily understood. The EP Manager stated that an action item had been

initiated to completely rewrite the procedures for improving understanding and for

conformance with other station procedures. Also, PSE&G added an item to the

corrective action system to ensure that procedures will be reviewed on a biennial

basis. Also, changes would be prominently identified and explained when sent to

the NRC for review. The inspectors had no further questions.

The inspectors verified that agreement letters '(Vith offsite agencies and support

organizations were valid or were updated as required per the E-Plan.

c.

Conclusions

P5

a.

PSE&G emergency plan changes were adequately reviewed in accordance with 1 0

CFR 10.54(q). PSE&G planned to review, evaluate/rewrite the emergency plan

implementing procedures for conformance to other station procedures and to

improve the review process. The inspectors also concluded that letters of

agreement with offsite agencies were in place.

Staff Training and Qualification in EP

Inspection Scope (82701 l

The inspectors reviewed EP training records, training procedures, and the E-Plan

training requirements to evaluate PSE&G's emergency response organization (ERO)

training program.

b.

c .

20

Observations and Findings

The inspectors determined through a review of training lesson plans, training record

reviews, and discussions with ERO members, that the required EP training was

conducted in accordance with PSE&G's E-Plan and applicable procedures. The*

inspectors randomly selected 60 training records for the ERO staff and found that

the qualifications were current. Additionally, the inspectors reviewed the initial and

requalification EP lesson plans for fire brigade and security personnel and

determined, by a review of test documentation, that both organizations conducted

EP training in accordance with applicable procedures.

The inspectors verified that the required drills were conducted to evaluated medical,

radiation monitoring, and fire response. Since the last program inspection, PSE&G

increased the number of quarterly drills to 12, in addition to monthly tabletop

training for the operators. The PSE&G staff stated that the additional drills allowed

them to focus more on teamwork, and critique documentation indicated an overall

improvement in ERO performance. Also, the inspectors interviewed several Senior

Reactor Operators from both Hope Creek and Salem, and found that they spoke

positively of the additional table top drills because the repetitiveness provides them

with more confidence in making emergency classifications using the new NUMARC

Emergency Action Level (EAL) scheme, implemented in January 1997.

Conclusion

PSE&G conducted emergency response training and drills as required. Based upon

overall good performance during the drills and the March 1998 biennial full-

participation emergency exercise, the inspectors concluded that training for the ERO

was effective.

P6

EP Organization and Administration

a.

Inspection Scope (82701)

b.

The inspectors reviewed PSE&G's EP department staffing and management to

determine what changes had occurred since the last program inspection and

whether those changes had any adverse effect on the EP program.

Observations and Findings

Since the last NRC EP program inspection in August 1997, the EP program was split

from the radiation protection department and combined with corrective actions and

instructional technology departments. In March 1997, PSE&G hired a new EP

manager who has a broad knowledge of EP. Recently the EP section was fully

staffed with nine individuals. This included the addition of a supervisor for handling

offsite agency i~sues and two coordinators for corrective actions and training

oversight. This initiative was deemed to be good because it provided better

program ownership. Each supervisor was given a staff to support their mission .

Also, the Director of EP/Training, reports directly to the PSE&G Chief Nuclear

c.

21

Officer and President who appeared to be very supportive of the EP program and its

management.

Conclusions

The department reorganization and hiring of a manager with extensive EP

experience enhanced the EP program. The inspectors concluded that the positive

findings during this inspection were an indication that the program had significantly

improved since the last inspection.

P7

Quality Assurance in EP Activities

a.

Inspection Scope (82701)

b.

c.

The inspectors reviewed the 1996 and 1997 Quality Assurance (QA) audit reports

of EP to assess the effectiveness of the audits of the EP program.

Observations and Findings

During an interview with the lead QA auditor for the last EP-evaluation conducted

from November 3 to December 5, 1997, the inspectors determined that PSE&G had

expended significant resources to conduct the audit. Specifically, the audit

consisted of several person-weeks of effort and included an .independent technical

specialist. The inspectors reviewed the 1997 audit plan and checklists, which

covered 10 CFR 50.54(t) requirements, commitments in the E-Plan, and the

guidance in NUREG-0654, "Criteria for Preparation and Evaluation ~f Radiological

Emergency Response Plans and Preparedness in Support of Nuclear Power Plants".

The checklist used to implement the audit plan for the 1997 audit was thorough.

The 1996 and 1997 audit reports were of sufficient scope and depth to assess the

EP program, and addressed the areas specified in 10 CFR 50.54(t). Numerous

recommendations for program enhancement resulted. The recommendations were

not indicative of programmatic weaknesses and were incorporated by the EP

department. The inspectors verified that offsite officials were provided copies of

the audit report section pertaining to PSE&G's interface with offsite agencies and

that the reports were distributed to the appropriate licensee management.

Conclusions

Quality Assurance audits of the emergency preparedness (EP) program were

thorough and the reports were useful to PSE&G management in assessing the

effectiveness of the EP program and providing enhancement recommendations.

This area was assessed as excellent .

22

SS

Miscellaneous Security and Safeguards Issues

S8.1

Operational Security Response Evaluation for Hope Creek and Salem

NRC headquarters and regional inspectors conducted an on-site Operational Security

Response Evaluation at both the Hope Creek and Salem generating stations from

April 20, 1998 to April 24, 1998. The findings of this inspection will be

documented in NRC Inspection Report 50-272, 311, and 354/98-201.

FS

Miscellaneous Fire Protection Issues

F8.1

Fire Protection Inspection for Hope Creek and Salem

Region-based inspectors performed an inspection of the adequacy of the fire

protection program at the Hope Creek and Salem generating stations from March

23, 1998 to March 27, 1998. The findings of this inspection were documented in

NRC Inspection Report 50-354/98-02 for Hope Creek.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on May 11 , 1998. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified .

IP 37551:

IP 40500:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 82701:

IP 90712:

IP 92700:

IP 92702:

IP 92901:

IP 92902:

IP 92903:

IP 92904:

IP 93702:

23

INSPECTION PROCEDURES USED

Onsite Engineering

Effectiveness of Licensee Controls in Identifying, Resolving, and Preventing

Problems

Surveillance Observations

Maintenance Observations

Plant Operations

Plant Support Activities

Operational Status of the Emergency Preparedness

In-office Review of Written Reports of Nonroutine Events at Power Reactor

Facilities

On-site Followup of Written Reports of Nonroutine Events at Power Reactor

Facilities

Followup on Corrective Actions For Violations and Deviations

Plant Operations Followup

Maintenance Followup

Engineering Followup

Plant Support Followup

Event Followup

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened/Closed

50-311/98-03-01

50-272&311/98-81-01

50-272&311 /98-81-02

Closed

50-272&311 /96-08-02

50-272&311 /96-08-03

50-311 /96-18-02

50-311 /97-03-02

50-311 /97-07-01

50-311 /97-14-03

50-272/97-013-00

50-272/98-002-00

50-272/98-002-01

NCV

Failure to implement procedure step in safety

tagging program

NOV Failure to implement action request procedure

NOV Failure to implement corrective action procedure

VIO

Failure to perform post maintenance testing.

VIO

Inadequate safety-related material storage.

VIO

Lack of containment closure during refueling.

IFI

Management of commitment process.

VIO

Failure to establish containment integrity within

eight hours.

VIO

Improper restoration of emergency diesel

generator following testing.

LER

Failure to meet TS 3.8.1.1 Action B

LER

Auxiliary building excess flow damper found

wired open with spring removed

LER

Auxiliary building excess flow damper found

wired open with spring removed

AFW

AOT

CAL

CFCU

E-Plan

EAL

EOG

EOF

EP

EPIP

ERO

FAC

LCO

LER

NRC

osc

PDR

PMT

PSE&G

QA

RATI

SAP

SG

SGFP

SW

TS

TSC

UFSAR

voe

WMM

24

LIST OF ACRONYMS USED

Auxiliary Feedwater

Allowed Outage Time

Confirmatory Action Letter

Containment Fan Coil Unit

Emergency Plan

Emergency Action Level

Emergency Diesel Generator

Emergency Operations Facility

Emergency Preparedness

Emergency Preparedness Implementing Procedure

Emergency Response Organization

Flow-Accelerated Corrosion

Limiting Condition For Operation

Licensee Event Report

Nuclear Regulatory Commission

Operations Support Center

Public Document Room

Post Maintenance Testing

Public Service Electric and Gas

Quality Assurance

Restart Assessment Team Inspection

. Salem Assessment Panel

Steam Generator

Steam Generator Feed Pump

Service Water

Technical Specifications

Technical Support Center

Updated Final Safety Analysis Report

Volt DC

Work Management Manual