ML18100A583

From kanterella
Jump to navigation Jump to search
Forwards Initial SALP Repts 50-272/91-99,50-311/91-99 & 50-354/91-99 for Period of 911229-930619.Concerned W/ Adequacy & Timeliness of Utils Mgt Response to Significant Events
ML18100A583
Person / Time
Site: Salem, Hope Creek  PSEG icon.png
Issue date: 09/01/1993
From: Martin T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To: Miltenberger S
Public Service Enterprise Group
Shared Package
ML18100A584 List:
References
NUDOCS 9309080031
Download: ML18100A583 (55)


See also: IR 05000272/1991099

Text

Docket Nos. 50-272

50-311

50-354

SEP

Public Service Electric and Gas Company

ATIN: Mr. Steven E. Miltenberger

I 1993

Vice President and Chief Nuclear Officer

Post Office Box 236

Hancocks Bridge, New Jersey 08038

Gentlemen:

SUBJECT:

INITIAL SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

(SALP) REPORT NOS. 50-272/91-99, 50-311/91-99, AND 50-354/91-99

On July 29, 1993, an NRC SALP Board conducted a review to evaluate the performance of

activities associated with the Salem and Hope Creek Generating Stations for the period

between December 29, 1991 and June 19, 1993. The results of these respective assessments

are documented in the enclosed Initial SALP reports. As previously agreed, we will hold a

. management meeting to discuss these SALP findings on September 17, 1993, at the

Salem/Hope Creek Processing Center. You should be prepared to discuss these assessments

and your plans to improve performance. In accordance with NRC policy, this meeting will

be open for public observation.

During this issessment period, we concluded that activities at the Salem and Hope Creek

Stations have been performed in a safe manner. We noted that the functional areas common

to both stations, i.e., Emergency Preparedness and Security, continued to exhibit excellent

performance. However, we observed a declining trend in Emergency Preparedness,

primarily as a result of your failure to maintain the staffs ability to develop correct

Protective Action Recommendations, as demonstrated during training, drills and exercises.

With respect to the fire protection program, which is also common to both stations, a

weakness was noted in the management oversight of the firewatch program activities,

particularly contractor performance.

Relative to Hope Creek, the overall performance continues to be excellent with strong

management oversight in the functional areas of Operations, Maintenance/Surveillance,

Radiological Controls, and Safety Assessment/Quality Verification. We observed improved

performance of Engineering and Technical Support compared to the last period. The

performance at Hope Creek continues to exhibit strengths in overall operator safety

consciousness, management oversight and control, safety assessment and quality review.

/

\\

Public Service Electric and

Gas Company

2

Relative to the Salem facility, we concluded that your performance during this period was,

good, which was consistent with our previous assessment. We noted that you improved the

performance of Radiological Controls such that the functional area is considered excellent.

However, during this period, the Salem facility had a substantial number of operational

challenges. For example, nine reactor trips occurred, of which six were attributable to a

variety of component failures. Further, during this period, Salem Unit 2 experienced

significant events involving the Overhead Annunciator System and the Rod Control System,

which followed a significant event at the end of the last SALP period involving a turbine-

generator failure.

Additional management attention is warranted to reduce the frequency of operational

challenges at the Salem facility. In a recent meeting, we discussed your plans to further

evaluate the root causes for these events and to ascertain if there were any common

underlying performance issues. We expect that a status of your assessment will be discussed

at our meeting.

Finally, we are concerned with the adequacy and timeliness of PSE&G's management

response to significant events. Our concern is not with your ability to critically evaluate and

assess identified problems, but rather the consistency of your management evaluation and

decision-making process for initiating such actions. We note that once your attention was

focused on evaluating and assessing the issues, your organization performed very

comprehensive and thorough assessments, accomplished excellent root cause analyses, and

determined effective corrective actions. Although we acknowledge your staff initiated and

conducted extremely thorough and comprehensive assessments and root cause evaluations

concerning the performance of contracted firewatches and the morale of security personnel,

examples of such responsiveness are limited.

Upon completion of our discussion of these SALP findings on September 17, 1993, we

request that you provide written comments, including any correction of factual information,

within 20 days of the date of that meeting. The enclosed reports and your responses will be

placed in the NRC Public Document Room.

Your cooperation with us is appreciated.

Sincerely,

Original Sil!n&:f By:-

Ti1omas T. Martin

Thomas T. Martin

Regional Administrator

Public Service Electric and

Gas Company

Enclosures:

3

I.

Salem Generating Station, Initial SALP Report Nos. 50-272/91-99 and 50-311/91-99

2.

Hope Creek Generating Station, Initial SALP Report No. 50-354/91-99

cc w/encls:

J. J. Hagan, Vice President, Nuclear Operations

C. Schaefer, External Operations - Nuclear, Delmarva Power & Light Co.

C. Vondra, General Manager - Salem Operations

R. Hovey, General Manager - Hope Creek Operations

F. Thomson, Manager, Licensing and Regulation

R. Swanson, General Manager - QA and Nuclear Safety Review

J. Robb, Director, Joint Owner Affairs

A. Tapert, Program Administrator

R. Fryling, Jr., Esquire

M. Wetterhahn, Esquire

P .J. Curham, Manager, Joint Generation Department,

Atlantic Electric Company

Consumer Advocate, Office of Consumer Advocate

William Conklin, Public Safety Consultant, Lower Alloways Creek Township

K. Abraham, PAO (27)

The Chairman

Commissioner Rogers

Commissioner Remick

Commissioner de Planque

Institute for Nuclear Power Operations (INPO)

Public Document Room (PDR)

Local Public Document Room (LPDR)

Nuclear Safety Information Center (NSIC)

NRC Resident Inspector

State of New Jersey

Public Service Electric and

Gas Company

bee w/encls:

4

Region I Docket Room (with concurrences)

bee via E-Mail:

J. Taylor, EDO

A. Ramey-Smith, DEDO

J. Lieberman, OE

S. Bajwa, NRR/DRIL/RPEB

M. Boyle, NRR

S. Dembek, NRR

J. Stone, NRR

Region I Staff (Refer to SALP Drive)

  • RI:DRP
  • RI:DRP
  • RI:DRSS

JWhite

EWenzinger WHehl

8/ /93

8/ /93

8/ /93

'f RI:NRR

KRI:NRR

'/RI:NRR

MBoyle

JS tone

SDembek

8/ /93

8/ /93

8/ /93

  • RI:DRS

CMiller

8/ /93

1/RI:DRA

WKane

8/ /93

  • RI:DRP

~RI:DRP

TJohnson

WLanning

8/ /93

8/ /93

r.

TMartin

f/I 193

OFFICIAL RECORD COPY

  • See Previous Concurrence Page

a: salem.int

a: hopecrek.int

4

bee w/encls:

Region I Docket Room (with concurrences)

bee via E-Mail:

J. Taylor, EDO

D. Wheeler, OEDO

J. Lieberman, OE

S. Bajwa, NRR/DRIL/RPEB

M. Boyle, NRR

S. Dembek, NRR

J. Stone, NRR

Region I Staff (Refer to SALP Drive)

  • RI:DRP
  • RI:DRP
  • RI:DRSS

JWhite

EWenzinger WHehl

8/ /93

8/ /93

8/ /93

'f'RI:NRR

'RI:NRR

JRI:NRR

MBoyle

JS tone

SDembek

8/ /93

8/ /93

8/ /93

  • RI:DRS

CM ill er

8/ /93

r

t

  • RI:DRP

TJohnson

8/ /93

r

TMartin

"'//93

OFFICIAL RECORD COPY

  • See Previous Concurrence Page

RI~

WLanning

8/r93

a:salem.int

a:hopecrek.int

4

bee w/encls:

Region I Docket Room (with concurrences)

bee via E-Mail:

J. Taylor, EDO

D. Wheeler, OEDO

J. Lieberman, OE

S. Bajwa, NRR/DRIL/RPEB

M. Boyle, NRR

S. Dembek, NRR

J. Stone, NRR

Region I Staff (Refer to SALP Drive)

!

8'\\ >>

81,f/93

'.

-

\\_ ....

\\_\\'

RI:DRA

WKane

8/ /93

RI:RA

TMartin

8/ /93

OFFICIAL RECORD COPY

RI:DRP

WLanning

817193

ENCLOSURE 1

INITIAL DRAFf SALP REPORT

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

REPORT NOS 50-272/91-99

50-311/91-99

PUBLIC SERVICE ELECTRIC AND GAS COMPANY

SALEM GENERATING STATION UNITS 1 AND 2

ASSESSMENT PERIOD:

DECEMBER 29, 1991 - JUNE 19, 1993

9309080033 930901

PDR

ADOCK 05000272

O

PD~

BOARD MEETING DATE:

JUL y 29' 1993

TABLE OF CONTENTS

I.

INTRODUCTION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

II.

SUMMARY OF RESULTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

II.A

Overview . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

Il.B

Facility Performance Analysis Summary . . . . . . . . . . . . . . . . .

4

Il.C

Unplanned Unit Trips . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

ill.

PERFORMANCE ANALYSIS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

ill.A

Plant Operations

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

ill.B

Radiological Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

ill.C

Maintenance/Survei11ance . . . . . . . . . . . . . . . . . . . . . . . . .

11

ill.D

Emergency Preparedness . . . . . . . . . . . . . . . . . . . . . . . . .

15

ill.E

Security and Safeguards . . . . . . . . . . . . . . . . . . . . . . . . . .

15

ill.F

Engineering and Technical Support . . . . . . . . . . . . . . . . . . .

15

ill.G

Safety Assessment/Quality Verification . . . . . . . . . . . . . . . . .

18

IV.

SITE ACTIVTI1ES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

22

IV .A

Licensee Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

22

IV .B

NRC Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . .

23

Attachment: SALP Evaluation Criteria, Performance Categories and Trends

i

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an integrated NRC

staff effort to collect availab1e observations and data periodical1y, and to eva1uate 1icensee

performance on the basis of this information. The program is supplemental to normal

regulatory processes used to ensure compliance with NRC rules and regulations. It is

intended to be sufficiently diagnostic to provide a rational basis for allocating NRC resources

and to provide meaningful feedback to the licensee's management regarding the NRC's

assessment of their facilities' performance in each functional area.

An NRC SALP Board, composed of the staff members listed below, met on July 29, 1993,

to review the observations and data on performance, and to assess licensee performance in

accordance with the guidelines in NRC Management Directive 8.6 "Systematic Assessment of

Licensee Performance," dated September 28, 1990. The SALP Evaluation Criteria utilized

by the Board are attached.

This report is a combined assessment for Sa1em Units 1 and 2 for the 18 month period of

December 29, 1991, through June 19, 1993. The Sa1em SALP Board members were:

CHAIRMAN:

W. D. Lanning, Deputy Director, Division of Reactor Projects (DRP), Region I (RI)

MEMBERS:

M. L. Boyle, Acting Director, Project Directorate 1-2,

Office of Nuclear Reactor Regulation (NRR)

C. W. Hehl, Director, Division of Radiation Safety and Safeguards (DRSS)

T. P. Johnson, Senior Resident Inspector, Salem/Hope Creek, RI

J. C. Stone, Project Manager (Salem), NRR

C. L. Miller, Acting Deputy Director, Division of Reactor Safety (DRS)

E. C. Wenzinger, Chief, Projects Branch No. 2, DRP, RI

2

OTHERS IN ATTENDANCE:

J. R. White, Chief, Reactor Projects Section 2A, DRP, RI

T. H. Fish, Resident Inspector, Salem/Hope Creek, RI

S. T. Barr, Resident Inspector, Salem/Hope Creek, RI

J. G. Schoppy, Resident Inspector, Salem/Hope Creek, RI

S. M. Pindale, Resident Inspector, Oyster Creek, RI

H. K. Lathrop, Resident Inspector, Calvert Cliffs, RI

B. J. McDermott, Reactor Engineer, DRP, RI

R. L. Nimitz, Senior Radiation Specialist, FRPS, DRSS, RI

C. Z. Gordon, Senior Emergency Preparedness (EP) Specialist, EP Section, DRSS, RI

S. Dembek, Project Manager (Hope Creek), NRR

R. R. Keimig, Chief, Safeguards Section, DRSS, RI

J. H. Lusher, EP Specialist, DRSS, RI

L. H. Bettenhausen, Chief, Operations Branch, DRS, RI

J. P. Durr, Chief, Engineering Branch, DRS, RI

S. A. Morris, Reactor Engineer, DRP, RI

J. I. Zimmerman, Project Engineer, NRR

M. J. Davis, Performance Evaluator, NRR

R. J. Summers, Project Engineer, DRP, RI

L. S. Cheung, Senior Reactor Engineer, DRS, RI

3

II.

SUMMARY OF RESULTS

Il.A

Overview

On July 29, 1993, the SALP board met to discuss PSE&G's performance at Salem during the

period from December 29, 1991 to June 19, 1993. The board conc1uded that the licensee

had operated the Salem units safely and that operator response to operational events was

excellent. The overall performance in the Operations area was good. However, weaknesses

were noted in the decisions to restart Unit 2 following the rod control system problems, in

the failure to follow procedures resulting in the loss of Unit 2 annunciators, and in the

inadequate oversight of the fire protection program.

PSE&G continued to implement effective radiological controis and ALARA programs during

this period. The SALP board noted improvements in this functional area inc1uding strong

management support and oversight. Quality Assurance audits in this area were of very good

quality.

The board conc1uded that the Salem maintenance and surveillance programs contributed to

the safe operation of the two units during the assessment period. In general, a declining

number of personnel errors in both maintenance and surveillance indicated improving

performance. However, the number of transients induced by component failures and the

significant problems with the rod control system raise questions regarding the overall

effectiveness of the maintenance and engineering support functions.

The SALP board determined that PSE&G maintained a genera11y strong and effective

emergency preparedness (EP) program. However, the board was concerned with an apparent

decline in the ability of the licensee to make correct initial Protective Action

Recommendations during training, drills and annual exercises. This concern resulted in the

board's assessment of a declining trend for this area. The board also conc1uded that PSE&G

continued to maintain an effective and performance-oriented security program during this

period. Overall, licensee performance in both EP and security remained exce11ent.

Engineering and technical support organizations provided good support for refueling and

maintenance outages, and strong performance in addressing day-to-day problems. The SALP

board noted that training programs for engineering personnel were exce11ent but that

weaknesses were observed in the licensee's non-conformance, erosion/corrosion, and fire

protection programs. Although the root cause training program was viewed as a strength,

the board noted that the threshold for initiating actual root cause investigation was not dear

or consistent.

PSE&G management continued to provide generally effective management support.

Significant Event Response Team (SERT) reviews of major events have been effective.

However, the board noted that in several instances, PSE&G failed to initiate adequate root

cause evaluation or assessment of abnormal conditions. NRC interaction with PSE&G

management was needed in a number of cases in order for full evaluation and corrective

4

action to be taken in a timely manner. Once initiated, comprehensive assessment, root cause

analysis and effective corrective actions were implemented. Outage planning and training

programs in all areas were considered strengths.

Il.B

Facility Performance Analysis Summary

Rating, Trend

Rating, Trend

Functiona] Area

Last Period

This Period

1.

Plant Operations

2

2

2.

Radiological Controls

2, Improving

1

3.

Maintenance/Surveillance

2

2

4.

Emergency Preparedness

1

1, Declining

5.

Security

1

1

6.

Engineering/Technical Support

2

2

7.

Safety Assessment/Quality

2

2

Verification

Previous Assessment Period: August 1, 1990 through December 28, 1991

Present Assessment Period: December 29, 1991 through June 19, 1993

Il.C

Unplanned Unit Trips

1.

6/8/93

Power

Level

100%

Root Cause

Grass content at circulating

water suction

Functional Area

SA/QV

Unit 1 automatically tripped following massive intrusion of sea grass into the

circulating water suction area. Four of five operating circulating pumps tripped

during cleaning of their trash racks, causing loss of vacuum, turbine trip, and

2.

3.

4.

5.

6.

7.

5

subsequent reactor trip. Root cause was determined to be less than adequate

management sensitivity to the possible consequences of rack Cleaning and incomplete

implementation of corrective actions from a previous similar event.

5/28/93

Subcritical

Component failure

Maintenance/

Surveillance

Unit 2 was manually tripped by the operators per abnormal operating procedures

when control bank "C", group 1 rods (four rods) fell into the core during dilution to

criticality for post refueling startup. A rod control system integrated circuit card

failure was attributed to a degraded solder trace.

3/16/93

100%

Random Component failure

NIA

Unit 2 automatically tripped from 100% power due to a low-low level condition on

No. 24 steam generator. A failed pressure control switch in the condensate polishing

system led to a low suction condition for No. 22 steam generator feed pump and

subsequent feed pump trip.

2/16/93

100%

Component failure

NIA

Unit 1 automatically tripped from 100% power due to an over-temperature delta

temperature signal caused by a faulty gain selector switch. This signal was received

with another channel already in the tripped position for ongoing channel calibration.

1/28/93

100%

Component failure during

troubleshooting

Maintenance/

Surveillance

Unit 2 operators manually tripped the reactor from 100% power in response to the

inadvertent loss of both operating steam generator feedwater pumps. A technician

was manipulating recorder test leads in the feedwater control cabinet when both feed

pumps automatically tripped. A loose module test jack was the cause.

1/16/93

13%

Random Component failure

NIA

Unit 1 operators manually tripped the reactor from 13% power in response to an

inadvertent opening of all turbine bypass (steam dump) valves. The transient was

initiated after a component in the control system failed.

9/3/92

100%

Personnel error - equipment

operator operated wrong

component

Maintenance/

Surveillance

8.

9.

6

Unit 2 tripped from 100% power due to the opening of the "A" reactor trip breaker.

A non-licensed equipment operator was to assist in surveillance testing of the trip

breakers. He mistakenly opened the cabinet of the "A" trip breaker instead of the

"A" trip bypass breaker.

5114192

15%

Lack of training/incorrect

assessment of feedwater control

system

Operations

Unit 2 tripped from 15% power due to a low-low level condition in the No. 23 steam

generator while personnel were troubleshooting feedwater level control problems.

While returning feedwater valves to their normal position, a transient occurred which

caused level to drop below the reactor trip setpoint. Operator's incorrect assessment

and lack of training associated with feedwater level control caused the event.

4/26/92

4%

Random Component failure

NIA

Unit 2 tripped from 4% power due to a low-low level condition in the No. 24 steam

generator. The low-low condition occurred while operators were transferring feed

from auxiliary feedwater to the main feedwater pump. A failed component in the

auto/manual feedwater control station caused sluggish valve response to both

automatic and manual control demand signals.

7

ID.

PERFORMANCE ANALYSIS

ID.A

Plant Operations

ID.A.1

Analysis

The previous SALP rated the Salem Plant Operations functional area as Category 2; mixed

operator performance characterized that SALP period. The assessment noted a continued

effective effort in maintaining a low number of reactor trips attributed to operations

personnel. Daily supervision and management oversight of plant operations were good.

Weaknesses were evident in the reactor operator training programs, and corrective actions*

for identified weaknesses were at times incomplete.

During this assessment period, PSE&G operated the Salem units safely. On several

occasions, station and operations management made conservative decisions to shut down the

Salem units to accommodate various repair and/or testing activities. Examples included a

Unit 2 shutdown to investigate erosion/corrosion concerns, a mini-outage at Unit 1 for

secondary plant maintenance, and a Unit 2 shutdown to repair a main generator stator water

leak. In addition, the licensee periodically reduced power to accomplish various activities,

such as condenser circulator cleaning and a Unit 1 primary system temperature detector

replacement that required a containment entry. In one case, involving discrepant

performance of the Salem Unit 2 rod control system during multiple successive restart

attempts, initial management response was not sufficient to understand and determine the

cause of the rod control system failures and the associated safety significance of the event.

Operators effectively responded to reactor trips and other operational transients. In some

instances, prompt and effective operator actions averted the necessity for reactor trips. One

example included a Unit 2 steam generator feedwater pump trip while operating at full

power, where prompt operator response prevented a unit trip. The personnel error rate

decreased during this SALP period, which was the result of aggressive management

attention.

The licensed and non-licensed operator. training programs were well developed, implemented

and strongly supported by management. Operations and training department personnel

worked well together in assuring that a well trained, qualified, and competent operating staff

existed. Candidates for initial and requalification license examinations were well prepared

and knowledgeable. All candidates passed NRC exams given during the period. Weaknesses

were noted in the area of simulator modeling and the quality of job performance measures.

The licensee initiated actions to address these weaknesses. Overall, the licensed operator

requalification and initial qualification programs were strong and well managed.

Nine unplanned reactor trips occurred for both units during the period. Although these trips

challenged the operations staff, most of the trips were the result of component failure or

environmental conditions. This compares to five and six reactor trips in the last two

assessment periods, respectively. A personnel error by a non-licensed operator (as discussed

8

in the surveil1ance section) who entered the Unit 2 reactor trip breaker cubicles on September

3, 1992, to re-familiarize himself with breaker operation in preparation for a Unit 1 test

caused one reactor trip. The root cause for the May 14, 1992 Unit 2 reactor trip was an

incorrect understanding and a lack of training by operations personnel of the design

capability of the feedwater regulating bypass valve. In all cases, safety systems functioned as

designed. Component aging, particularly in feedwater control systems, appears as a principal

contributor.

The operations department effectively transitioned to 12-hour shift rotations. The five

operating shifts were staffed adequately, utilizing an extra senior licensed operator to

supervise the work control group. One extra licensed operator was added to the shift

complement, and reduced the administrative burden in the control room during the Unit 2

outage.

Operations supervision and management oversight and attention to daily unit operations

continued to be good during the assessment period. Daily operational and outage meetings

provided an effective forum for the exchange of relevant operational information among the

various station groups and management levels. Those meetings maintained direct and

effective communications between operations and station management.

Licensed operators demonstrated a genera11y good safety perspective and awareness of plant

conditions. The operators generally displayed good adherence to procedures and sufficient

attention to detail during activities. The completion of the operations procedure upgrade

project has resulted in an improved quality of station procedures, and this contributed to a

positive procedure adherence trend. However, an apparent isolated instance of incomplete

procedures and failure to use procedures contributed to a Unit 1 loss of the overhead

annunciator (ORA) system. PSE&G initiated corrective action to previously identified

emergency and abnormal operating procedure deficiencies. The responsiveness of PSE&G

personnel was thorough, as indicated through administrative enhancements, including

verification and validation process strengthening.

Operations support of refueling outage activities was very good. Reactor core alteration

activities were conservatively conducted. The licensee demonstrated a good safety

perspective during outage periods by ensuring safety equipment availability and by

conducting independent reviews of the outage sequence. Operators performed unit startup

activities in a safe and deliberate fashion. Operators' performance and control during

reduced reactor coolant system inventory operations were strong. Licensed operators were

generally well trained on modifications prior to unit startup from outages. One exception

was that the control room ORA system modification training did not adequately train the

operators to routinely verify proper system operation.

The fire protection program was good and staffed with dedicated fire protection personnel

from the Site Protection group, who responded to fire and first aid emergencies. Plant and

site management strongly supported the fire protection program.

However, some

distinctions affecting Salem included weaknesses involving procedure problems, fire water

9

system knowledge shortcomings by plant personnel, and improper storage of combustible

materials. Further, due to equipment and maintenance difficulties, both Salem fire pumps

were inoperable for an extended period. However, the licensee implemented timely

compensatory measures in accordance with regulatory requirements. The licensee's

investigation of a self-identified instance of misconduct by a firewatch revealed a more

extensive weakness in oversight and control of contract personnel performing roving

firewatch duties. More than one-half of the firewatch personnel annotated their logs to

indicate they had inspected areas when, in fact, they had not. The licensee's corrective

actions were prompt and comprehensive in assessing and resolving this deficiency.

Summary

PSE&G operated the Salem units safely. Operator response to reactor trips and other

operational transients was excellent. Operations supervision and management .oversight of

day-to-day unit operations activities were good. Operations personnel generally demonstrated

a good safety perspective. However, the licensee decided to restart Unit 2 before the rod

control system problems were fully understood; and failure to follow procedures combined

with a design problem resulted in a loss of Unit 2 annunciators. Operations support for

refueling outages was very good. The PSE&G fire protection program exhibited

programmatic and performance weaknesses.

ill.A.2

Performance Rating: Category 2

ill.A.3

Board Comments:

None

ill.B

Radiological Controls

ill.B.1

Analysis

The previous SALP rated the functional area of radiological controls at Units 1 and 2 as

Category 2; improving. The radiological controls program was considered good. Staffing

and training were good, as wer~ radwaste processing, storage and transportation activities.

ALARA efforts and performance were commendable. Confirmatory measurements, effluent

controls, and the Radiological Environmental Monitoring Program (REMP) were effectively

implemented.

The radiological controls and chemistry programs were challenged during the current

assessment period. Refueling outages were performed at both units; personnel made periodic

entries into the Unit 1 containment, with the reactor at power; and minor fuel leaks, which

were detected at both units, required monitoring. The NRC's reviews of these activities

determined that the radiological controls and chemistry programs were effectively

implemented. There was strong management and supervisory oversight of on-going activities

and proactive involvement in radiation protection and chemistry programs. These were

evidenced by excellent steam generator (SG) chemistry controls, responses to SG chemistry

10

excursions, and the responses to minor fuel leaks on both units. Challenging 1992 goals for

radiation dose, personnel contamination events, and solid radwaste volume were met. Goals

for 1993 continue to be challenging and are being met. Planning and procedure development

for implementation of the revised 10 CFR Part 20 were very good.

The radiological controls organization and staffing levels were stable. There was very good

use of station radiological controls personnel to oversee contractor activities, a good level of

expertise within the organization, and minimal use of overtime. The outage radiological

controls organizations were well defined.

Overall, radiation protection and chemistry personnel were generally well trained and very

knowledgeable of their respective duties. However, early in the period the NRC identified

that personnel transferred from the Hope Creek site to support outage activities at Salem *

were not provided training on Salem specific radiation protection procedures. Appropriate

personnel were subsequently trained on Salem specific procedures in a timely manner.

Radiation workers received appropriate and timely training. For example, a new course

titled "Integrated Training" was implemented at both Salem and Hope Creek Stations. The

course involved radiation workers and radiological controls personnel planning and

performing work activities together under realistic conditions on a mock-up. The majority of

radiation protection and maintenance personnel attended the course .. The course was

considered a very good initiative. There were excellent pre-job briefings and explicit

guidance specified on radiation work permits.

The overall internal and external exposure controls programs were strong, and control of

radiological work activities was commendable. An effective access control system using

state-of-the-art computer supported equipment continued to be maintained. There were no

internal or external exposures in excess of NRC limits and overall administrative controls of

personnel exposure were effective. For example, the internal exposure controls for steam

generator work were such that the majority of work was conducted without the need for

respiratory protection. The weaknesses associated with quality control of dosimetry,

identified during the previous period, were corrected. Weaknesses in exposure records

controls, identified by NRC early in the period, were also corrected. All dosimetry issues

were closed. The radiological occurrence report system was wen supported by management

and effective in identifying root causes and corrective actions for radiological problems.

The ALARA program continued to be strong throughout the period. NRC independent

review of work activities indicated commendable planning and preparation, use of

appropriate exposure goals, and very good oversight of on-going activities from an ALARA

standpoint. Aggregate personnel radiation exposure continues to be among the lowest in the

industry. Emergent work received appropriate *reviews and ALARA controls.

Overall, the radioactive material and contamination control programs were strong. Isolated

lapses in contamination controls were aggressively pursued and root causes were identified

and corrected. Radiological Control Area and containment housekeeping improved during

the period and contaminated floor areas were reduced significantly. In addition, the

11

radioactive waste handling, storage and transportation programs were strong and well

managed. Plans have been established for interim on-site storage of radioactive waste in the

event of delays in finalization of compact efforts by the State of New Jersey.

The Radiological Effluent Control Program (RECP) and the REMP continued to be effective

during this period. Personnel exhibited good knowledge of all RECP areas including effluent

controls, radiation monitoring systems (RMS), and off-site dose calculations. Comparisons

of projected off-site doses between the licensee and the NRC PCDOSE computer code were

in excellent agreement. Procedures were detailed, concise and well written and resulted in

effective implementation of the RECP and REMP. The initiative to develop and issue RMS

manuals to assist in maintenance of the RMS, as well as the efforts to upgrade the RMS,

were noteworthy. These actions indicated not only a clear understanding of technical issues,

but also a proactive approach to maintaining the RMS. The meteorological monitoring

program was effective.

Overall quality assurance (QA) oversight of program areas was very good. Special audits of

dosimetry program matters were conducted to verify quality and independent assessors

continued to be used to monitor outage activities. QA audits of effluent and environmental

monitoring programs were thorough and of sufficient technical depth to probe for

programmatic weaknesses. Findings were promptly resolved. Early in the period, the NRC

identified a weakness in the area of audits of personnel qualifications. It was not clear that

personnel qualifications of all appropriate groups were being systematically audited. Baseline

audits were immediately initiated by the QA group and no unqQalified personnel were

identified.

Summary

PSE&G implemented effective radiological controls and ALARA programs. There was

strong management support and strong supervisory and management oversight of program

areas. External and internal exposure controls were effective, as were contamination

controls, storage and handling of radioactive material, and radioactive waste transportation

activities. The confirmatory measurements and effluent controls program, as well as the

REMP continued to be effective. QA audits were of very good quality.

ID.B.2

Performance Rating: Category 1

ID.B.3

Board Comments:

None

m.c

Maintenance/Surveillance

ID.C.1

Analysis

The previous SALP assessment rated the Maintenance/Surveillance area as Category 2.

12

Personnel errors and inattention to detail resulted in problems in both maintenance and

surveillance. A number of improvements in such areas as plant material condition and fewer

missed surveillances had been noted in the previous assessment. Weaknesses were noted in

the area of material control and procurement.

Maintenance

The Salem maintenance program contributed to the continued safe operation of both Salem

units during the assessment period. Maintenance department management was directly and

effectively involved in the oversight of routine maintenance activities during power

operations and during forced and refueling outages. PSE&G employed a fixed shift work

schedule, providing balanced work activity impact and contributing to maintenance planning

efficiency. Pre-outage system walkdowns were initiated to improve outage efficiency. Plant

management screened work to be done during planned maintenance outages of safety-related

equipment to achieve a net safety gain. Safety system availability was maintained high, also

demonstrating management's safety conscious control of the maintenance program. A new

work standards monitoring program provided for proper management review of maintenance

activities.

Maintenance Department staff adequately supported plant operations. Non-supervisory

personnel were technicaJly knowledgeable of routine preventive and corrective activities;

their training and experience remained a strength. Maintenance first-line supervisors

provided generally good oversight. Personnel errors resulted in one engineered safety

feature actuation early in the period, a partial loss of off-site power later in the period, and a

small number of non-cited violations throughout the period. However, the number of

reportable events (including surveillance-related events) due to personnel error decreased

from 24 in the previous SALP period to 12 in this period.

Two reactor trips resulted from maintenance activities. In one case, control rods dropped

because of a degraded solder trace from maintenance on a rod control printed circuit card.

Another trip resulted from installation of test equipment in a feedwater control cabinet which

had a loose module test jack. These maintenance-related trips and the continuing problems

due to personnel error reduced the effectiveness of the maintenance program.

The conduct of routine maintenance activities was good. Coordination between maintenance

and operations to schedule and accomplish work activities was effective and improving.

Indicators of good maintenance performance included dec1ining trends in the corrective and

preventive maintenance backlogs, in the number of industrial safety events, in the number of

plant leaks and in the number of required radiation monitoring system work orders.

13

Continued improvement in both units' materiaJ condition was also noted. The Salem

RevitaJization Project has positively impacted the plant material condition. Aggressive

management attention in this area was evident. The Procedure Upgrade Program, nearing

completion for I&C and Maintenance procedures by the end of the period, was a positive

effort.

Salem has established and maintained a very good preventative maintenance (PM) program.

Improvements in the PM program are continuing, and as a result, deferred PMs have been

reduced significantly. Much of this program's success is attributable to a close working

relationship between engineering, operations and maintenance.

Salem performed three refueling outages; one at Unit 1 and two at Unit 2. Outage planning

activities and outage conduct were strong. Outage meetings and good inter-departmental

cooperation resulted in better daily work coordination and more efficient accomplishment of

outage work. The delegation of some inservice inspection and balance-of-plant outage work

to PSE&G Site Services reduced the dependency on contractors for those efforts and

addressed a weakness from a prior SALP report. Good performance was noted during the

outages in the restoration of the Unit 2 turbine generator, the service water piping

replacement at both units, the erosion/corrosion work at Unit 1, and the 10-year overhaul of

a11 three emergency diesel generators at Unit 2.

Deficiencies were observed in PSE&G's troubleshooting effort involved with the Unit 2 rod

control system following that unit's refueling outage at the end of the period. Maintenance

and troubleshooting activities were not wen controlled. Since root cause determination

policy and expectations were not well established, these activities initially did not identify

design and physical circuit problems. Consequently, corrective actions were not effective.

Further, PSE&G staff members responsible for maintenance of the rod control system did

not recognize that some exhibited system defects were outside of the system design basis

(e.g., the observation that one of the control rods withdrew from, instead of inserting into,

the core on an "insert demand signal"). Several rod control system failures and anomalies

were experienced without reaJizing that the defects were related. This led to an attempt to

restart the plant without understanding the cause or nature of the failures or the significance

of the anomalous performance. After NRC directed attention to this area, including the

formation of an Augmented Inspection Team, the licensee initiated a thorough and

comprehensive investigation of the rod control system deficiencies, and resolved the issues.

The licensee continued improvement in the area of spare parts procurement and availability.

The procurement program also included commercial grade component dedication. The new

integrated and automated warehouse was placed into operation during the period. A

computerized data base was widely used by the staff and was effectively integrated into the

procurement program. This system enabled the procurement activities to be processed

efficiently, and the procurement backlogs to be substantially reduced.

14

Surveillance

During this period the Salem surveillance program was safely and properly implemented and

confirmed the operability of safety-related equipment. The maintenance information system

was effectively used to schedule and track the completion of a large number of required

surveillance activities at both units. Technical Specification surveillances were completed

within the required periodicity, with four isolated exceptions. The missed surveillances were

not indicative of any program weakness and were properly addressed by PSE&G upon their

discovery. The four missed surveillances decreased from nine during the previous SALP

period. Technicians demonstrated a good level of knowledge during the performance of the

surveillance and inservice test activities.

Communications and coordination between technicians and control room operators were

good. Despite the association of one reactor trip with the performance of a reactor trip

breaker surveillance procedure and two engineered safety feature actuations, management

attention has reduced the number of personnel errors committed during surveillance test

performance. A design change involving the 4kV vital bus test points significantly reduced

potential for these kind of errors. The Procedure Upgrade Program continued to improve the

quality of surveillance procedures. However, an operations surveillance test was inadequate

to assure that the overhead annunciator system display was verified to be functioning on a

regular basis and contributed to a loss of annunciator event in December, 1992.

The inservice inspection and testing efforts were again well performed; a noted strength was

the performance of steam generator tube inspections during refueling outages. Unit 2's

second 10-year ISi interval program has been enhanced as a result of PSE&G's assuming its

preparation and control instead of delegating this responsibility to an ISi vendor, as was done

during the first 10-year interval. PSE&G responded well to the increased surveillance test

requirements following the restoration of the Unit 2 turbine generator and the placing of that

equipment into service.

Summary

The Salem maintenance and surveillance programs contributed to safe operation of the two

Salem units during the assessment period. Continued reduction of personnel errors in both

maintenance and surveillance activities was noted. A number of other trends indicated

continuing improvement. Three refueling outages were performed with strong planning and

implementation. However, a significant event still resulted from personnel error and

maintenance activities that were not well controlled. Improvements were noted in

procurement and material control.

m.C.2

Performance Rating: Category 2

ill.C.3

Board Comments: None

15

ID.D

Emergency Preparedn~

m.D.1

Analysis

This area is common for the Artificial Island site, refer to Hope Creek SALP report 50-

354/91-99, Section ill.D.1 for details.

ID.D.2

Perf onnance Rating: Category 1, Declining

ID.D.3

Board Comments: None

ID.E

Security and Safeguards.

ID.E.1

Analysis

This .area is common for the Artificial Island site, refer to Hope Creek SALP report 50-

354/91-99, Section ill.E.1 for details.

ID.E.2

Perfo~nce Rating: Category 1

m.E.3

Board Comments: None

ID.F

Engineering and 'J'echnical Support

ID.F.1

Analysis

The previous SALP rated Engineering and Technica1 Support as Category 2. The previous

assessment indicated that the control and limitations of temporary modifications improved.

Also improved was the quality of work performed by the onsite system engineers and in the

Salem Qualified Reviewers Program. Progress was observed in, the Salem RevitaJization

Project and the Configuration Baseline Project, two of the engineering enhancement projects.

Weaknesses were noted in the responses to NRC generic communications.

Engineering and Technical Support for Salem is provided by the corporate engineering,

known as Engineering and Plant Betterment (E&PB), and the onsite system engineering

organization. These groups effectively provided technical support for refueling and

maintenance outage activities. E&PB handles major engineering efforts such as plant

modifications and design bases reconstitution. The onsite engineering group supports

operations, maintenance, testing and minor design change activities. These groups are well

staffed with experienced personnel in various engineering disciplines. Both engineering

organizations communicated and interfaced well with the station and outage groups on a daily

basis. Reactor engineering generally provided strong support to the Salem station during

refueling, reactor startup and power ascension testing activities.

16

The licensee has an exce11ent program for controlling design changes and plant modifications.

The "workbook" used in the design change process provides easy-to-follow guidance to the

preparer of plant modification packages. The modification packages reviewed were of good

quality. They were thorough and contained adequate safety reviews. However, the licensee

made minor changes to the facility as described in the UFSAR without determining if there

was an unreviewed safety question involved as required by procedures. There were no other

identified cases of the licensee failure to fo1low the 10 CFR 50.59 implementation procedure.

While these failures to follow procedures did not result in safety problems, the finding

indicates a potential weakness in the licensee's 10 CFR 50.59 program.

The loss of the overhead annunciator (OHA) system on Unit 2 and failure to recognize that

loss for 90 minutes had several root causes, some that were engineering in nature. The

multi-microprocessor OHA system that was recently installed failed to provide the necessary

human-machine interface. The system also gave higher priority to other actions besides

providing alarm indications to the operators and did not provide indication of failure. The

engineering staff performed little software review of the OHA modification. In addition, the

staff's knowledge of the OHA system and the associated new technology was less than

adequate. Only after NRC directed attention to this area, including the formation of an

Augmented Inspection Team, did the licensee initiate a thorough and comprehensive

investigation to determine the cause and effect resolution.

As a result of concerns identified during an NRC inspection, PSE&G further identified

significant programmatic weaknesses in the site Erosion/Corrosion (E/C) Program. The

licensee used incorrect criteria in determining minimum wall thickness. Subsequently,

numerous piping erosion conditions involving non-safety related feedwater piping were

dispositioned incorrectly for both Salem units. E&PB subsequently implemented substantial

programmatic improvements to correct the E/C Program to an acceptable condition.

Concerns were also identified by the NRC with regard to the licensee's Appendix R

program.

It was determined that the fire barrier systems were not installed in accordance

with the tested configuration. In response to the inoperable status of these fire barrier

systems, due to the lack of proper qualification test data to substantiate the design of the in-

plant configuration, the licensee had to institute hourly fire watch patrols in the plant areas

containing the questionable fire barrier systems.

The licensee has an excellent training program for E&PB staff and onsite system engineering

personnel. A typical system engineer receives substantial theory-based training, including

thermodynamics, heat transfer, and fluid mechanics. Recent enhancements to the E&PB

training program have advanced towards a more performance/application oriented approach.

In addition, the licensee has an excellent Root Cause Analysis and Decision Making course

designed for members involved in problem solving and incident investigations. However, the

threshold for initiating root cause investigations was not clear or consistent.

--~

17

Several longer standing design and hardware concerns represent challenges to the reliable

operation of the facilities. For example, control room operators entered Technical

Specification 3.0.3 on several occasions due to design problems associated with the analog

rod position indication system. Automatic main steam line isolations continued to occur

during plant heatup due to design deficiencies. In addition, some reactor trips were caused

by random failures of plant hardware. On the positive side, the engineering organi:zations

implemented several system design modifications and other actions to address long-standing

concerns. Examples included the safeguards equipment cabinets (load sequencers),

pressurizer power operated relief valves, service water and radiation monitoring systems (in

progress), and vital/non-vital switchgear transformers.

The engineering organi:zations proactively identified and addressed a number of technical

problems in a timely manner. These included auxiliary feedwater system excessive flow, a

longer than expected overall response time for the containment spray system, a potential

overload condition associated with the emergency diesel generators, and a condition outside

the design basis for the control air containment isolation valves.

System engineers generally exhibited strong performance in addressing day-to-day problems.

The system engineers effectively evaluated safety-related pump failures, and switchgear

transformer failures. System engineer performance, however, demonstrated some control

and coordination weaknesses while troubleshooting problems with an emergency diesel

generator, which resulted in an engine overspeed trip.

The licensee's response to recent failures in the rod control system indicated the following

weaknesses: (1) the lack of a site wide root cause determination policy; (2) the lack of

supervision and control over vendor activities; (3) PSE&G's inadequate understanding of the

depth and capabilities of the vendor's circuit card testing program; (4) the less than adequate

control over the vendor's non-like-for-like replacement of the rod control system digital

group counters; (5) the lack of control of the vendor's troubleshooting; and (6) the lack of

appropriate troubleshooting rigor. However, the licensee allocation of resources for each

individual event was adequate. Furthermore, after the initiation of the NRC's AIT, the

upper management oversight and the investigation of the event by the Significant Event

Response Team (SERT) were considered strengths.

Engineering and Plant Betterment has initiated an aggressive program to substantially reduce

the engineering work request (EWR) backlogs for both Salem and Hope Creek. They were

successful in reducing the backlog during this period.

The licensee has separate programs for controlling nonconformance reports (NCR) in each

division. The NRC identified weaknesses in this area due to lack of interface between

individual programs. For example, a fire damper, which provides ventilation to the station

battery to prevent hydrogen accumulation reaching the ignition limit, failed to the closed

position (due to damaged fusible link) and remained closed for more than 18 months. The

E&PB NCR, which identified the deficiency, was closed without assuring either: 1) that the

safety impact of the deficiency was properly addressed and the deficiency corrected, or 2)

18

that the nonconformance was addressed by site engineering.

The quality of the technical content of licensee submittals has appeared to level off with some

room for improvement still remaining. Of the ten amendments approved during the SALP

period, four required significant information to be submitted before approval. The responses

to various generic letters required significant revision before satisfactory resolution of these

issues were achieved. Other requests from the licensee, such as relief requests from ASME

Code requirements have been generally acceptable.

The erosion/corrosion monitoring program for high energy piping has shown improvement

from an administrative control standpoint. Both units have their own respective

administrative procedures. Predictive analyses are more appropriate and conservative than

past evaluations.

Summary

Engineering and Plant Betterment and the onsite system engineering provided good technical

support for refueling and maintenance outages. System engineering exhibited strong

performance in addressing day-to-day problems. The modification packages reviewed were

of good quality, with a few exceptions. The training program provided for E&PB staff and

system engineering personnel was determined to be excellent. Several operational problems

were caused by long-standing design and hardware concerns. The engineering organization

implemented several system design modifications to address some long-standing concerns.

However, coordination weaknesses were observed in troubleshooting emergency diesel

generator problems and the root cause determination and troubleshooting associated with the

rod control system failures. Both E&PB and system engineering have initiated aggressive

programs to reduce substantially the engineering backlogs. Weaknesses were observed in the

licensee's non-conformance, erosion/corrosion, and fire protection (Appendix R) programs.

ID.F.2

Performance Rating: Category 2

ID.F.3

Board Comments:

None

ID.G

Safety A~ent/Quality Verification

m.G.1

Analysis

The previous SALP rated this area as Category 2. That assessment noted that management

continued to be involved in problem resolution and the assurance of nuclear safety. Groups

that provide independent reviews were effective and provided safety conscious reviews of

licensee activities. A continuing concern with personnel errors, procedure compliance, and

licensee submittals was noted.

During this period, performance at both Salem units was good. Cooperation, communication

and coordination between the different departments at Salem continued to improve. There

19

were, however, indications that personnel error and lack of procedure adherence continue to

exist.

The Station Operations Review Committee (SORC) properly performed their Technical

Specification required duties and provided conservative and effective review of design

changes, post-trip reviews and significant events. However, in the case of the rod control

system problems at Unit 2, late in the SALP period, SORC did not perform well in that

multiple startup attempts were permitted without requiring the root cause of the problems to

be determined. Some weaknesses were identified in the IO CFR 50.59 process as discussed

in the Engineering and Technical Support section.

The licensee properly implemented the Significant Event Response Team (SERT) process in

order to provide an independent assessment of all reactor trips and other major events. The

NRC found the SERT reviews to be effective, and SERT recommendations were

appropriately received and considered by plant management.

The PSE&G on-site Safety Review Group (SRG) and Station Quality Assurance (SQA)

performed effectively in reviewing Salem station activities. SRG provided consistently good

shutdown risk assessments for three refueling outages and maintained good independence

from the station staff. SQA provided good coverage of routine and non-routine activities at

Salem, and produced effective monthly reports and appropriately performed all audits

required by Salem Technical Specifications.

Outage planning and preparation developed into a strength during this assessment period.

Outage work was well controlled, inter-department coordination was very good, and

emergent issues were properly addressed in the three refueling outages which occurred

during the period and during the forced outages of the period. Management involvement and

control of the outage work were evident.

Salem station management, including the General Manager and individual department heads,

generally provided effective and conservative oversight of station activities. This

management involvement was provided in daily meetings with senior nuclear shift

supervision and through management accountability meetings. The Salem General Manager

conducted informative State-of-the-Station meetings to convey expectations to plant

personnel. Corporate management also provided a highly visible presence at the station.

However, when the station was challenged by significant events, management response was

not as effective. In some cases, management was not promptly informed of the event (loss

of overhead annunciators) or did not appreciate the significance of the event (rod control

system anomalies). As a result, management response was initially inadequate. However,

once these conditions were understood and recognized, management took conservative,

thorough, and comprehensive actions, and brought the issue to a timely resolution.

20

PSE&G has an excellent root cause analysis and decision making training program designed

for personnel involved in problem solving and incident investigation; however, management

has not effectively developed the criteria or expectations for when the root cause of an event

must be determined prior to the resumption of normal plant operations. This contrast in the

quality and ability of the program versus its implementation was demonstrated most notably

in the licensee's failure to identify root cause in their handling of the Unit 2 rod control

system problems.

The licensee's corrective action program generally functioned well, but there were signs of

reduced effectiveness. The weaknesses were noted in troubleshooting activities associated

with the emergency diesel generator, rod control system and overhead annunciators. In

addition, inadequate oversight of contractors and vendors led to less than full knowledge of

the overhead annunciator system and rod control system maintenance activities. This

contributed to a delay in the root cause determination of these events. The erosion/corrosion

program as implemented at Salem had significant programmatic weaknesses. Jn all of these

cases, once the deficiency was identified by NRC, PSE&G management took immediate and

appropriate actions.

Training programs implemented by PSE&G in all areas were well developed and effective.

Of particular note were the training of licensed and non-licensed operators, radiation

protection personnel, safeguards and security personnel and on-site and off-site engineering

personnel. This training and the strong results of the licensee's procedure upgrade program

have resulted in improvements in the areas of reduced personnel errors and procedure

adherence.

The quality of the technical content of licensee submittals (e.g., amendment requests,

responses to NRC generic communications, and other licensee initiated requests) is

occasionally deficient. Of the ten amendments that were approved, four required significant

additional information to be submitted before approval. Responses to three generic letters

required significant revision before satisfactory resolution of the issues was achieved.

Sum mazy

PSE&G management continues to be involved in station activities and have genera1ly

provided effective management support. In several significant instances (e.g., the overhead

annunciator event, the rod control system problem, and the issue involving erosion/corrosion

of system piping), the licensee failed to initiate adequate root cause evaluation or assessment

of the abnormal condition. However, once management attention was directed to these

issues, the licensee initiated very thorough and comprehensive efforts to understand and

resolve the issues. SERT reviews of major events have been effective and recommendations

have been accepted by licensee management. Outage planning has developed into a licensee

strength. Training programs in all areas have been found to be effective with only minor

weaknesses noted. Prior weaknesses in personnel errors and procedure adherence were

effectively addressed. The quality of routine license submittals is occasionally deficient.

m.G.2

m.G.3


21

Performance Rating: Category 2

Board Comments:

The NRC is concerned with the adequacy and timeliness

of PSE&G's management response to significant events and to the cha11enges

presented by numerous component failures and several unreso1ved design

issues at Salem.

22

IV.

SITE ACTIVITIES

IV .A

Licensee Activities

Unit 1

The unit began the period at full power. On January 21, 1992, the unit was shut down when

three circulators were lost due to a control power cable failure. The unit was restarted on

January 27, 1992.

Unit 1 operated until it was shut down for its tenth refueling outage on April 4, 1992. The

unit remained in an outage to repair linear indications identified on three of the four steam

generator feedwater nozzles and to replace portions of turbine building feedwater piping due

to minimum pipe wall concerns. The unit was returned to service on August 16, 1992.

Unit 1 remained at power until December 24, 1992, when the unit was removed from service

due to a loss of circulating water pumps as a result of excessive debris and increased sodium

levels in the steam generators as a result of failed condenser tubes. Power operation

resumed on December 29, 1992, and continued until January 16, 1993, when control room

operators initiated a manual reactor trip from 13% power following the failure of the steam

dump system. The unit was being shut down at the time for control rod position indication

system maintenance. Following completion of the related repair activities, the unit was

restarted on January 21, 1993.

An automatic reactor trip occurred from 100% power during nuc1ear instrumentation testing

on February 16, 1993. A spike occurred on another channel (loop 11 Tave) resulting in a

two of four coincident Over Temperature Delta-Temperature reactor trip. The unit restarted

on February 22, 1993.

The unit operated at power until it automatically tripped from 100% power on June 8, 1993,

when four of five circulators tripped due to large sea grass intrusion. The unit remained shut

down at the end of the SALP period.

Unit 2

The unit began the period in its sixth refueling outage fo1lowing the November 9, 1991,

turbine generator failure. Unit 2 was restarted on April 19, 1992.

A reactor trip from 4 % power occurred on April 26, 1992. The unit was restarted on May

3, 1992, and on May 14, 1992, a trip from 15% power occurred. Both of these trips

occurred on low-low steam generator level due to problems with the feedwater level control

system. The unit was restarted on May 18, 1992.

On June 18, 1992, the licensee shut down Unit 2 due to feedwater pipe wall thinning caused

by erosion/corrosion. The unit was restarted on July 15, 1992, and continued to operate

23

unti1 September 3, 1992, when an automatic reactor/turbine trip occurred from fu11 power.

The cause of the trip was determined to be a non-licensed operator error. The unit was

restarted on September 6, 1992.

Unit 2 operated at power until January 28, 1993, when control room operators manua11y

tripped the unit from 100% power, immediately following the loss of both operating steam

generator feed pumps caused by a loose test connector. The unit was restarted on January

31, 1993.

The unit operated at power until March 16, 1993, when the unit automatica11y tripped from

100% power on low steam generator level caused by a failed pressure control switch in the

condensate polishing system. The licensee then began the unit's seventh refueling outage.

Several aborted post refueling startups occurred during the period May 24 - June 4, 1993.

This included a manually initiated reactor trip on May 28, 1993, when one control rod bank

dropped into the core. The unit remained shut down at the end of the period while rod

control system problems were investigated.

IV .B

NRC Inspection Activities

Four NRC resident inspectors were assigned to Artificial Island during the assessment

period. NRC team inspections were conducted in the following areas:

Salem 2 restart readiness after a six month outage to repair/replace the turbine

generator from March 22 - May 2, 1992.

Motor Operated Valve Inspection on May 4-8, 1992.

Emergency Preparedness Inspection conducted on October 27-29, 1992, to observe

the Artificial Island annual exercise.

Augmented Inspection Team to review a loss of annunciators event at Unit 2 from

December 14-23, 1992.

Fire Protection Appendix R Inspection on May 17-21, 1993.

Augmented Inspection Team to review Unit 2 rod control abnormalities from June 5-

28, 1993.

ATTACHMENT 1

SALP EVALUATION CRITERIA. PERFORMANCE CATEGORIES AND TRENDS

The following evaluation criterion were used, as applicable, to assess each functional area:

1.

Assurance of quality, including management involvement and control.

2.

Approach to the identification and resolution of technical issues from a safety

standpoint.

3.

Enforcement history.

4.

Operational and construction events (including response to, analyses of, reporting of,

and corrective actions for).

5.

Staffing (including management).

6.

Effectiveness of training and qualifications program.

The performance categories used when rating licensee performance are defined as follows:

Category 1. Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in a superior level of performance. NRC wiII consider reduced

levels of inspection effort.

Cate~ory 2. Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in a good level of performance. NRC will consider maintaining

normal levels of inspection effort.

Category 3. Licensee management attention to or involvement in nuclear safety or

safeguards activities resulted in an acceptable level of performance; however, because of the

NRC's concern that a decrease in performance may approach or reach an unacceptable level,

NRC will consider increased levels of inspection efforts.

Category N. Insufficient information exists to support an assessment of licensee

performance. These cases would include instances in which a rating could not be developed

because of insufficient licensee activity or insufficient NRC inspection.

The SALP Board may assess a performance trend, if appropriate. The trends are:

Improving: Licensee performance was determined to be improving during the assessment

period.

Declinin~: Licensee performance was determined to be declining during the assessment

period and the licensee had not taken meaningful steps to address this pattern.

Trends are normally assigned when one is definitely discemable and a continuation of the

trend is expected to result in a change in performance during the next assessment period.

- - - --------

--

ENCLOSURE 2

INITIAL DRAFT SALP REPORT

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

REPORT NO 50-354/91-99

PUBLIC SERVICE ELECTRIC AND GAS COMPANY

HOPE CREEK GENERATING STATION

ASSESSMENT PERIOD:

DECEMBER 29, 1991 - JUNE 19, 1993

BOARD MEETING DATE:

JUL y 29' 1993

TABLE OF CONTENTS

I.

IN'TRODUCTION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

II.

SUMMARY OF RESULTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

II.A

Overview . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

II.B

Facility Performance Analysis Summary . . . . . . . . . . . . . . . . .

4

III.

PERFORMANCE ANALYSIS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

III.A

Plant Operations

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

III.B

Radiological Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

III.C

Maintenance/Surveillance . . . . . . . . . . . . . . . . . . . . . . . . .

10

III.D

Emergency Preparedness . . . . . . . . . . . . . . . . . . . . . . . . .

12

III. E

Security and Safeguards . . . . . . . . . . . . . . . . . . . . . . . . . .

14

III.F

Engineering and Technical Support . . . . . . . . . . . . . . . . . . .

16

III.G

Safety Assessment/Quality Verification . . . . . . . . . . . . . . . . .

18

IV.

SITE ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

21

IV.A

Licensee Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

21

IV.B

NRC Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . .

21

Attachment: SALP Evaluation Criteria, Performance Categories and Trends

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an integrated NRC

staff effort to collect available observations and data periodically, and to evaluate licensee

performance on the basis of this information. The program is supplemental to normal

regulatory processes used to ensure compliance with NRC rules and regulations. It is

intended to be sufficiently diagnostic to provide a rational basis for a11ocating NRC resources

and to provide meaningful feedback to the licensee's management regarding the NRC's

assessment of their facilities' performance in each functional area.

An NRC SALP Board, composed of the staff members listed below, met on July 29, 1993,

to review the observations and data on performance, and to assess licensee performance in

accordance with the guidelines in NRC Management Directive 8.6, "Systematic Assessment

of Licensee Performance," dated September 28, 1990. The SALP Evaluation Criteria

utilized by the board are attached.

This report is an assessment for the Hope Creek Generating Station for the 18 month period

from December 29, 1991, to June 19, 1993. The Hope Creek SALP Board members were:

CHAIRMAN:

W. D. Lanning, Deputy Director, Division of Reactor Projects (DRP), Region I (RI)

MEMBERS:

M. L. Boyle, Acting Director, Project Directorate I-2,

Office of Nuclear Reactor Regulation (NRR)

S. Dembek, Project Manager (Hope Creek), NRR

C. W. Hehl, Director, Division of Radiation Safety and Safeguards (DRSS)

T. P. Johnson, Senior Resident Inspector, Salem/Hope Creek, RI

C. L. Miller, Acting Deputy Director, Division of Reactor Safety (DRS)

E. C. Wenzinger, Chief, Projects Branch No. 2, DRP, RI

2

OTHERS IN A ITENDANCE:

I. R. White, Chief, Reactor Projects Section 2A, DRP, RI

T. H. Fish, Resident Inspector, Salem/Hope Creek, RI

S. T. Barr, Resident Inspector, Salem/Hope Creek, RI

I. G. Schoppy, Resident Inspector, Salem/Hope Creek, RI

S. M. Pindale, Resident Inspector, Oyster Creek, RI

H. K. Lathrop, Resident Inspector, Calvert Cliffs, RI

B. I. McDermott, Reactor Engineer, DRP, RI

R. L. Nimitz, Senior Radiation Specialist, FRPS, DRSS, RI

C. Z. Gordon, Senior Emergency Preparedness (EP) Specialist, EP Section, DRSS, RI

J. C. Stone, Project Manager (Salem), NRR

R. R. Keimig, Chief, Safeguards Section, DRSS, RI

I. H. Lusher, EP Specialist, DRSS, RI

R. J. Summers, Project Engineer, RI

L. H. Bettenhausen, Chief, Operations Branch, DRS, RI

I. P. Durr, Chief, Engineering Branch, DRS, RI

S. A. Morris, Reactor Engineer, DRP, RI

I. I. Zimmerman, Project Engineer, NRR

M. I. Davis, Performance Evaluator, NRR

L. S. Cheung, Senior Reactor Engineer, DRS, RI

3

II.

SUMMARY OF RESULTS

II.A

Overview

On July 29, 1993 the SALP board met to discuss PSE&G's performance at Hope Creek

during the period from December 29, 1991 to June 19, 1993. The board concluded that the

licensee had operated Hope Creek in a safe and conservative manner. Operator training was

a strength and the operator error rate remained low, contributing to a decreased reactor

scram rate. PSE&G provided effective management oversight and attention to a11 operational

activities. A weakness was noted in management's oversight of firewatch program activities,

a common function affecting Salem and Hope Creek.

The licensee continued effective implementation of their state-of-the-art radiological controls

program. The SALP board noted that management support and control, staffing levels,

quality assurance oversight, and ALARA were program strengths.

PSE&G demonstrated superior results in maintenance program implementation at Hope

Creek, and very good results in surveillance testing. Continued management involvement in

improving program performance and correcting identified problems was evident. The SALP

board also noted specific improvements in procurement and material control during this

period.

The SALP board determined that PSE&G maintained a generally strong and effective

emergency preparedness (EP) program. However, the board was concerned with an apparent

decline in the ability of the licensee to make correct initial Protective Action

Recommendations during training, drills, and annual exercises. This concern resulted in the

board's assessment of a declining trend for this area. The board also concluded that PSE&G

continued to maintain an effective and performance-oriented security program during this

period. Overall, licensee performance in both EP and security remained excellent.

Engineering and technical support for the Hope Creek station improved during this SALP

period. The board noted improvements in the licensee's program for contro11ing design

changes and plant modifications, MOV program implementation, training of the engineering

staff, and reduction of engineering backlogs. Although the root cause training program was

viewed as a strength, the board noted that the threshold for initiating actual root cause

investigation was not clear or consistent.

The licensee continued to perform well in the area of Safety Assessment and Quality

Verification during this period. First line supervision and management oversight were very

good, as was the independent review provided by the On-site and Off-site Safety Review

Groups and by Station Quality Assurance. Performance by individuals was strong, as

evidenced by a reduction in the personnel error rate.

4

Il.B

Facility Performance Analysis Summary

Rating, Trend

Rating, Trend

Functional Area

Last Period

This Period

1.

Plant Operations

1

1

2.

Radiological Controls

1

1

3.

Maintenance/Surveillance

2, Improving

1

4.

Emergency Preparedness

1

1, Declining

5.

Security

1

1

6.

Engineering/Technical Support

2

2, Improving

7.

Safety Assessment/Quality

1

1

Verification

Previous Assessment Period: August 1, 1990 through December 28, 1991

Present Assessment Period: December 29, 1991 through June 19, 1993

5

III.

PERFORMANCE ANALYSIS

ID.A

Plant Operations

ID.A.1

Analysis

The previous SALP rated Hope Creek operations as Category 1. That assessment concluded

that PSE&G operated the Hope Creek reactor conservatively with nuclear safety as the top

priority. Operator errors remained low, however, the frequency of automatic reactor scrams

was a concern. Strong management and supervisory oversight of, and involvement in,

operations were evident. The licensee conducted its third refueling outage effectively. An

effective training program was noted; though, the failure rate for initial Reactor Operator

license examinations near the end of the period indicated weak preparation.

During this assessment period, PSE&G operated the reactor in a professional and safety

conscious manner. Well-trained operators ski11fully performed their duties during unit

startups, shutdowns, and transients. For the two reactor scrams that occurred during the

period, operator performance was not a causal factor. During a loss-of-offsite power and a

failure of reactor feedwater pump automatic control, prompt and effective operator actions to

restore equipment and to deal with power reductions mitigated these plant transients and thus

averted plant scrams. The licensee completed an event-free 300 day run in the middle of

1992 when the unit was shut down for a scheduled mid-cycle outage.

The licensee exceeded the minimum Technical Specification shift staffing requirements for

Senior Reactor Operators (SRO) and Reactor Operators. Additionally, SRO licensed

individuals supervised the work control group continuously. SRO licensed personnel

provided field support for day shift operational activities.

Plant management maintained effective and thorough oversight and attention to an operational

activities on a daily basis. Daily status meetings were used to provide an operational

perspective of plant problems and work prioritization with the focus on nuclear safety, as

was evidenced by the timely and thorough followup to a boron dilution problem in the

standby liquid control system, the initiation of a timely shutdown for failure of three torus-to-

drywell vacuum breakers, and a very proactive approach to shutdown risk management.

The licensed and non-licensed operator training programs were well developed, effectively

implemented, and received strong management support. Candidates for initial and

requalification license examinations were well-prepared and knowledgeable. There were no

license examination failures during this period, indicating that corrective measures taken as a

result of weak performance on license examinations in the previous period had been

effective. Training facilities and materials were excellent, and the licensee's use of the

simulator for training, event analysis, drills, and observations of performance was a strength.

The requalification program identified weaknesses related to evaluation standards in the

operating portion of the examination and administrative procedures and controls for use of

the scenario examination bank during training. These weaknesses involved administrative

procedures and controls, and linkage between simulator scenarios and conditions.

6

The professional control room demeanor, nuclear safety perspective and knowledge of plant

activities of the licensed operators continued to be a strength. Operating procedures were

detailed and accurate. Operations managers implemented a number of procedure

enhancements to promote continued improvement. For example, SRO licensed personnel

author, review, and perform safety screening responsibilities for operations department

procedures, which has resulted in a decrease in the procedure revision request backlog.

Overtime usage was properly controlled. The personnel error rate was very low.

The licensee's implementation of the Emergency Operating Procedure (EOP) program was

very good overall. Several long-standing issues involving procedure implementation levels

were acceptably resolved. The licensee continued to improve the administrative procedures.

ROs and non-licensed operators demonstrated thorough knowledge and attention to detail in

the operation and testing of equipment and systems. Equipment operator effectiveness was

enhanced during the period by the implementation of a computerized equipment surveillance

log system, which simplified data collection and also provided improved data review and

trend analysis capabilities.

Concerned with a higher-than-expected number of scrams over the previous periods, the

licensee conducted a thorough investigation into the root causes of the scrams and

implemented a number of corrective actions during this period. During the current period

one scram occurred due to equipment problems and one due to contractor personnel error.

Licensee actions have effectively reduced the scram rate from that observed during the

previous period.

The fire protection program was good and staffed with dedicated fire protection personnel

from the Site Protection group, who responded to fire and first aid emergencies. Plant and

site management supported the fire protection program. The licensee's investigation of a

self-identified instance of misconduct by a firewatch revealed a more extensive weakness in

oversight and control of contract personnel performing roving firewatch duties. More than

half of the firewatch personnel annotated their logs to indicate they had inspected areas when

in fact they had not. The licensee's corrective actions were prompt and comprehensive in

assessing and resolving this deficiency once it was identified.

Overall, plant housekeeping was very good. Improvements continued during the period,

including facility painting, resealing of floor surfaces, using sticky pads to prevent dirt and

hot particle spread, and implementing a clean bootie program for selected work groups.

These activities positively reflected the level of support provided by management and

contributed significantly to plant cleanliness and housekeeping conditions.

The licensee effectively prepared for Hope Creek's fourth refueling outage, including a very

thorough shutdown risk assessment. Work performance during the outage was very good,

with minimal rework required. However, personnel errors contributed to two potentially

safety-significant events: an inadvertent loss of reactor cavity inventory and a short-term loss

of shutdown cooling. However, the licensee took prompt corrective actions to preclude

recurrence. The unit was returned to service in a safe and efficient manner.

7

Summary

PSE&G operated the Hope Creek unit in a professional and safety conscious manner, and the

frequency of abnormal events remained low. Strong management oversight and attention to

all operational activities were noted. The fourth refueling outage was effectively planned and

executed. Operator training was strong, as evidenced by the examination results and field

observations. Weaknesses were noted in management's oversight of firewatch program

activities.

ID.A.2

Performance Rating: Category 1

ID.A.3

Board Comments:

None

ID.B

Radiological Controls

ID.B.l

Analysis

The previous SALP rated the functional area of radiological controls as Category 1. NRC

reviews during the previous period determined that radiological controls staffing levels were

excellent, effective measures were taken to minimize personnel exposure, and radiological

work activities were effectively managed. The environmental monitoring and effluent

controls programs were effectively implemented as were the radwaste processing, handling

and shipping programs.

NRC reviews during the current period identified that there was a high degree of

management and supervisory oversight of radiation protection and chemistry activities. For

example, NRC reviews of outage activities identified very good work planning and control, a

high degree of radiation protection involvement in on-going activities, and excellent efforts at

minimization of ambient radiation dose rates and aggregate personnel radiation exposure

through successful implementation of the hydrogen water chemistry, iron reduction, and

depleted zinc injection programs. Although the 1992 goals for radiation dose and personnel

contaminations were slightly exceeded, the licensee performed very well in keeping exposure

As Low As Reasonably Achievable (ALARA). An aggressive refueling outage dose goal

was met despite emergent work. Planning and procedure development for implementation of

the revised 10 CFR Part 20 was very good.

The radiological controls organization was well defined, well staffed, and augmented, as

appropriate, to support outage work activities. There was minimal use of overtime and a

very good level of technical expertise within the organization. Late in the period the

radiological controls group was re-organized and the position of radiation

protection/chemistry manager was eliminated and replaced with direct reporting managers for

each organization. The re-organization was performed in a controlled manner and no

negative effects were identified by the close of the period. Appropriately qualified personnel

continued in responsible positions.

8

The training and qualification program continued to be a strength. Radiation workers

received appropriate and timely training. A new course titled, "Integrated Training," was

implemented at both Hope Creek and Salem Stations. This course involved radiation

workers and radiological controls personnel planning and performing work activities together

under realistic conditions on a mock-up. The majority of radiation protection and

maintenance personnel attended the course. The NRC considered the course a very good

initiative. Radiation protection and chemistry personnel were well trained and very

knowledgeable. A well defined initial qualification program for both permanent radiation

protection personnel and contractor radiological controls personnel was maintained.

However, an NRC review determined that the radiation protection technician staff were not

always reviewing required reading material (e.g., procedure changes). Enhanced supervisory

oversight of required reading activities was immediately initiated including supervisor

verification of completion.

The internal and external exposure control programs were effective and overall control of

radiological work activities was commendable. There were no internal or external personnel

exposures in excess of NRC limits and overall administrative controls of personnel exposure

were effective. An effective access control system using state-of-the art computer supported

equipment continued to be maintained. The weaknesses associated with quality control of

dosimetry, identified during the previous period, were corrected. Also, NRC identified

weaknesses in exposure records controls, identified early in the period, were also corrected.

Radiation protection personnel demonstrated excellent containment entry controls and

appropriately responded to the inadvertent reactor cavity inventory loss and standby liquid

control system boron loss.

The radiological occurrence report program, well supported by

management, was effective in identifying root cause and corrective actions for radiological

problems.

A strong radioactive material and contamination control program was implemented. The

licensee continues to maintain very good programs for monitoring and control of Zinc-65, a

difficult to detect radionuclide. Late last period, aggressive monitoring detected minor

migration of this contamination outside the radiological controlled area boundary into the on

site sewage system. The contaminated sewage was isolated and properly disposed of, and

appropriate corrective actions were implemented to preclude recurrence. Station

housekeeping continued to be noteworthy. Total contaminated area square footage was

rigorously controlled.

The radioactive waste processing, handling, storage and transportation programs continued to

be effective and well coordinated. Plans have been established for interim on-site storage of

radioactive waste in the event of delays in finalization of state compact efforts.

9

The ALARA program continued to be effective in maintaining personnel radiation exposure

low. Exposure goals were found to be challenging, planning and preparation was effective,

and very good oversight of on-going activities from an ALARA standpoint was performed.

The licensee continued to aggressively implement long term exposure reduction initiatives

(e.g., snubber reduction, iron reduction, hydrogen water chemistry, and robotics). A

working group, with BWR vendor representatives, was established to plan and implement

innovative shut-down techniques to maximize clean-up of radioactivity in the reactor coolant

during shutdown. Emergent work received appropriate reviews and ALARA controls.

The Radiological Effluent Control Program (RECP) and Radiological Environmental

Monitoring Program (REMP) continued to be effectively implemented during this assessment

period.

Licensee personnel exhibited good knowledge of all RECP areas including effluent

controls, radiation monitoring systems (RMS) and off-site dose calculations. Comparisons of

projected off-site doses between the licensee and the NRC PCDOSE computer code were in

excellent agreement. Procedures were detailed, concise and well written and resulted in

effective implementation of the RECP and REMP. Effluent RMS calibrations were excellent

and exceeded industry practices. The meteorological monitoring was effectively

implemented. Reactor coolant chemistry was excellent with a very low fission product

activity level.

Overall quality assurance (QA) oversight of program areas was very good. Special audits of

dosimetry program matters were conducted and independent assessors continued to be used to

effectively monitor outage activities. QA audits of effluent and environmental monitoring

programs were thorough and of sufficient technical depth to probe for programmatic

weaknesses. Findings were promptly resolved. Early in the period, the NRC identified a

weakness in the area of audits of personnel qualifications. It was not clear that personnel

qualifications of all appropriate groups were being systematically audited. The QA group

immediately initiated baseline audits and no unqualified personnel were identified.

Sum mazy

The licensee continued to maintain and implement an effective state-of-the art radiological

controls program. There was excellent support and control by management and effective

QA oversight. Staffing levels continued to be very good, and the ALARA program was

effective in reducing personnel exposure. The internal and external exposure control

programs were well maintained and effectively implemented as were the environmental and

effluent controls programs. Radwaste processing, handling, and shipping programs also

continued to be well maintained and effectively implemented.

ID.B.3.2

Performance Rating: Category 1

ID.B.3.3

Board Comments:

None

10

m.c

Maintenance/Surveillance

m.C.1

Analysis

The previous SALP rated the maintenance/surveillance functional area as Category 2,

Improving. Program strengths included effective management involvement, a stable, well-

trained staff, and well-written procedures. Weaknesses involved material procurement,

occasional lapses in attention to detail, and continued personnel error initiated plant events.

Maintenance

During this period, the Hope Creek maintenance program demonstrated superior

performance. The program was staffed with skillful, well-trained personnel. Procedure

quality and adherence were strong, and effective management oversight of activities was

present. Results from the maintenance program were excellent. Previous weaknesses

regarding procurement, attention to detail, and personnel errors were effectively addressed

and corrected.

Management supported specialized training, including the use of PSE&G's extensive

electrical and mechanical training facilities. Excellent procedure adherence and strong

direction from line management and supervision contributed to the high quality of work and

low error rates. Management at all levels, from first line supervision through department

and plant management, was observed in the field providing the appropriate oversight.

Maintenance program implementation provided excellent results. The quality of corrective

maintenance work was excellent, including a very low rework rate. There were no

maintenance initiated reactor scrams, and reportable events attributable to maintenance were

minor.

Effective maintenance planning and implementation resulted in a low maintenance backlog.

Equipment forced outages were rare and of short duration, an indication of an effective

preventive maintenance program. Based on NRC observation, safety-related equipment

availability was excellent.

PSE&G addressed previous weaknesses in procurement and personnel errors, and improved

the maintenance program in other areas. As previously noted, personnel errors were low and

significantly reduced from the previous period. Results improved in procurement as

demonstrated by adequate spare parts which properly supported work efforts. Management

strengthened their approach on planned equipment outages to ensure that a net safety gain

would be achieved during any planned and executed equipment/system outage. Based on

NRC inspection and observation, these initiatives were effective and demonstrated a safety-

conscious attitude.

11

The licensee continued improvement in the area of spare parts procurement and availability.

The new integrated and automated warehouse was placed into operation during the period

and provided effective support in efforts to reduce the corrective maintenance backlog and to

support refueling outage activities. For example, during the unit's fourth refueling outage,

the licensee ensured spare parts availability in order to complete scheduled tasks on time.

Additionally, parts were available for emergent work such that no negative impacts to

scheduled activities or outage duration occurred.

Hope Creek completed a scheduled mid-cycle outage, a refueling outage, and several forced

outages during this SALP period. Strong maintenance planning and outage organizations

conducted these outages safely and effectively. A strong safety-conscious attitude was

demonstrated during shutdown risk and equipment outage reviews. Emergency diesel

generator overhauls and control rod drive replacements were effectively and safely

conducted.

A wiring error caused by maintenance personnel was not corrected during motor-operated

valve work, and resulted in an unplanned reactor cavity inventory loss. This personnel error

was caused by inadequate wiring diagrams and tabulations, weak communications, and poor

working practices. PSE&G appropriately responded to this event and initiated effective

corrective actions.

Surveillance

The Hope Creek surveillance program was effectively implemented and demonstrated very

good results. Strong oversight by management and good cooperation among departments

contributed to a successful surveillance program. Surveillance tests were effectively

scheduled and tracked by the central planning organization using the maintenance information

system. Two surveillances were missed: one due to a personnel error and one due to a

procedure inadequacy. The frequency of these errors has continued to decrease over the last

few assessment periods.

The surveillance test program effectively demonstrated system operability. Surveillance

procedures were generally well written, appropriate and complete. Procedure weaknesses

were identified and immediately corrected. Implementation and review of surveillance

procedures were competently performed. A few instances of lack of rigor in post-test

reviews and comparisons with design data were noted. These were corrected upon

identification.

The number of surveillance caused events continued to decrease compared to previous

periods. There were no surveillance initiated reactor scrams as compared to two last period.

A total of 7 personnel errors occurred in the surveillance area (out of 9,000 surveillance

activities) which resulted in Licensee Event Reports; this total was fewer than last period.

Four engineered safety feature actuations were caused by personnel errors during surveillance

testing. Corrective actions for these events were thorough and timely. PSE&G completed a

design change to improve testability. This change provided better identification of test points

and relocated these test points to prevent inadvertent actuations.

12

The inservice inspection program continued to be well planned and implemented with

appropriate quality assurance department oversight. The feedwater nozzle ultrasonic

examinations and snubber examinations used state of the art technology and specially trained,

qualified technicians. The erosion/corrosion program was improved. PSE&G corrected the

prior identified weaknesses in the predictive analysis of erosion/corrosion rates by

establishing a programmatic standard for the erosion/corrosion monitoring program.

Sum mazy

Hope Creek demonstrated superior results in maintenance and very good results in

surveillance testing. Management involvement in improving program performance and

correcting identified problems was evident. Program strengths included effective, detailed

procedures, skillful staff, and excellent oversight by managers and supervisors. Although

some personnel errors occurred, they were at a decreased rate as compared to previous

periods. A maintenance caused wiring error resulted in an unplanned reactor cavity level

loss. Improvements were noted in procurement and material control.

m.c.2

Performance Rating: Category 1

m.C.3

Board Comments:

None

m.D

Emergency Preparedness (Hope Creek and Salem - Combined Assessment)

ill.D.1

Analysis

During the previous SALP, Emergency Preparedness (BP) was rated Category 1. That rating

was based on strong management involvement and commitment to BP, a highly qualified EP

staff, a thorough and innovative training program, and excellent support of off-site agencies.

PSE&G's Emergency Response Organization (ERO) was well qualified as evidenced by

effective exercise performance.

During this SALP period, the licensee responded to two events at Salem and two events at

Hope Creek. The Salem events were low river level and transportation of a contaminated

injured person to the local hospital; Hope Creek had an Emergency Core Cooling System

(ECCS) initiation with vessel injection and inoperability of primary containment. In each

case, PSE&G correctly classified these events as Unusual Events and properly implemented

the Emergency Plan. Notifications of on-site and off-site response organizations were

timely.

Salem Unit 2 also experienced a loss of Control Room overhead annunciators (OHAs) on

December 13, 1992. Operators restored the OHAs within two minutes of recognition of

their loss. However, this event involved the unidentified (for about 90 minutes) existence of

a condition defined as an emergency, and subsequent notification of cognizant

13

organizations was not accomplished until after repeated prompting by the resident inspector.

At the end of the SALP period, licensee classification and reporting of this event was still

under licensee and NRC review.

PSE&G's performance in the October 1992 full-participation exercise at Salem was very

good. Under a challenging scenario, strengths were identified in Emergency Response

Facility command and control, Technical Support Center engineering assessment, Operational

Support Center prioritization and management of repair tasks, and Emergency Operations

Facility (EOF) dose assessment. One exercise weakness was identified: the initial

(sheltering) protective action recommendation (PAR) was not consistent with this General

Emergency. That was corrected by an upgraded PAR (for evacuation). PSE&G conducted

numerous other drills during the period, including an assembly and accountability drill in the

protected area and an unannounced off-hours callout of the ERO. These were well

coordinated by the BP Department and showed excellent PSE&G initiative.

Management support of EP was evident. Senior managers met periodically with the

Manager, EP for program status reports. Senior staff were qualified in upper-level ERO

positions. EP staff regularly met with state and local officials to discuss EP issues. A very

good working relationship with off-site agencies was indicated. This was evident at a

PSE&G-sponsored forum for New Jersey State and local officials, FEMA, and the NRC to

discuss emergency response roles and relationships.

Independent licensee audits of the EP program were of good quality and resulted in minor

recommendations for program enhancement. The corrective action system was effective and

appropriately used by BP staff to track outstanding items to resolution.

BP training effectiveness was demonstrated during NRC-observed table-top walk-through

scenarios with shift crews from Salem and Hope Creek. Overall, crews worked together and

responded well. However, weaknesses were identified in making emergency classifications

and protective action recommendations (PARs), and in providing complete information to the

NRC. For example, the loss of containment was not recognized, this resulted in a different

classification than was specified in the Event Classification Guide and in non-conservative

PARs/PAR upgrades. Additionally, PSE&G Emergency Action Levels for fission product

boundary failures did not clearly address the loss of the containment boundary. PSE&G

committed to addressing these concerns through training and procedure revisions. The

effectiveness of the licensee's actions has not yet been inspected.

EP staffing was a strength. The program was administered by a stable staff of fourteen,

including a very good mix of well qualified and responsible senior reactor operator, health

physics, and maintenance personnel. The ERO was also fully staffed, with managerial

positions filled by experienced senior personnel.

PSE&G successfully implemented the Emergency Response Data System (EROS) in February

1993. Emergency Response Facilities were maintained in a very good state of readiness.

Appropriate equipment and supplies were available. Surveillances were completed at

prescribed frequencies and instrumentation was calibrated. Noteworthy improvements were

14

made to the prompt notification system (siren) hardware and software. All communications

equipment was found to be consistent with licensee procedures. However, portable

respirators were found stored inside the radiological controlled area instead of in designated

Control Room/Operational Support Center lockers.

Summary

PSE&G maintained a generally strong and effective EP program. Senior management

commitment to EP was evident through program involvement and qualification in key ERO

positions. EP was well staffed, with a good discipline mix. The Emergency Plan was

effectively implemented during four Unusual Events. Licensee response to the December

1992 loss of the Salem 2 control room OHAs resulted in non-classification and non-reporting

of a defined emergency which remains under NRC review. Training was generally good, but

table-top exercises, and emergency drills and exercise performance indicated a need to

improve procedural guidance and training in event classification and PAR formulation.

Facilities were maintained in good operational readiness.

ill.D.2

ill.D.3

ill.E

ill.E.1

Performance Rating: Category 1, Declining

Board Comments:

NRC was concerned with the licensee's ability to make

accurate and consistent PARs.

Security and Safeguards (Hope Creek and Salem - Combined A~ment)

Analysis

The previous SALP rated this area Category 1. That rating was based on the licensee's

maintaining an effective, performance-based security program which, in many areas,

exceeded regulatory requirements; and demonstrating sensitivity in effectively managing

events that challenged the performance of the security organization. In addition, audits and

self-assessments of the security organization, program upgrades and enhancements were

indicative of excellent support from both corporate and station management for the security

program.

During this SALP period, corporate and station management acted prudently and responsibly

in contracting for an independent review of station security and other support programs

following the off-duty suicide of a security-force member. The comprehensive, in-depth

review did not show any work-related culpability. Throughout the period, there were no

appreciable adverse results from the incident on the morale or performance of the security

organization.

Station security management demonstrated initiative in evaluating the effectiveness of the

security program and in enlisting the support of corporate and station management for

program improvements and enhancements. This initiative was evident by the licensee's

efforts to enhance tactical training by additional contractor support. The training involved

15

defensive strategy, full-scale contingency drills and tabletop analyses of numerous scenarios

of the design basis threat. Further initiative was shown in coordinating a security drill

among state and local law enforcement agencies, and the security force. The drill was well-

planned and executed. It also provided the law enforcement agencies with valuable insight of

security procedures and station layout. In addition, excellent management support,

throughout the period, was evident for the systematic upgrade of the aging assessment aids

and other program enhancements.

The licensee also maintained aggressive, effective audit and self-assessment programs

throughout the period. These programs were instrumental in identifying potential weaknesses

such as the improper control of safeguards information, and fitness-for-duty (FFD) problems

and assisting the licensee in implementing corrective measures before problems developed.

Excellent rapport with other plant groups also helped minimize the number and extent of

problems.

The FFD program was generally well implemented and comprehensive. However,

programmatic problems were identified relative to personnel with infrequent, unescorted

station access and training for newly appointed supervisors who were responsible for

implementing certain aspects of the FFD program. While the licensee identified these

problems, they were not effectively resolved before coming to NRC attention. Despite these

programmatic problems, the program proved effective in identifying personnel who did not

meet FFD requirements. For example, the licensee took effective corrective actions when a

supervisor on a tour identified a security officer who failed to meet FFD parameters.

Staffing for the security organi7.ation was appropriate. This was evident during the

unplanned outage following the turbine failure at Salem and three planned refueling outages,

two at Salem and one at Hope Creek. Each of the outages required only a small amount of

overtime for security personnel.

A minor supervisory oversight problem was identified by the NRC late in the period when

security personnel were observed searching a vehicle contrary to the manner in which they

were trained. Generally, however, supervisory oversight of the security force was good, and

the security force continued to demonstrate attentiveness to security responsibilities and

responsiveness to identified problems. This was evident in the relatively smooth day-to-day

on-site operations and prompt and appropriate handling of security threats, such as a

telephone threat and the identification by x-ray of contraband material. The security force

also performed very capably on April 10, 1992, when an apparent lightning strike resulted

in a loss of the security computer and during a severe winter storm that occurred

March 12-15, 1993, that resulted in significant system degradations.

Training for the security force continued to be well-developed and generally well

administered. This was evident, throughout the period, by the high level of performance

indicated above and the small number of security personnel errors during the period.

16

The licensee's event reporting procedures were found to be clear and consistent with NRC

reporting requirements. One event, which involved the x-ray search detection of contraband

mentioned earlier, required prompt reporting to the NRC during this period. The licensee's

report was clear, concise and indicated appropriate responses. The licensee's event log was

found to be well maintained and utilized for tracking repetitive events.

During this period, the licensee submitted two revisions to the physical security plan and one

revision to the training and qualification plan. The revisions were of high quality,

technically sound and reflected well-developed policies and procedures.

Summary

In summary, the licensee continued to maintain a very effective and performance-oriented

security program. Corporate and plant management attention to and support for the program

remained evident throughout the period. Improvements to the program were made where

necessary, to maintain its effectiveness. Excellent rapport was maintained with other plant

groups, to minimize problems. The audit and self-assessment programs remained effective,

and enhanced program implementation. However, corrective actions were not always timely

as evidenced by the delay in resolving FFD problems. Staffing reflected program needs and

the training program was strong. Program plans and procedures were well-written and

understood by all concerned and reflected a thorough and comprehensive understanding of

regulatory requirements.

ID.E.2

Performance Rating: Category 1

ID.E.3

Board Comments:

None

ID.F

Engineering and Technical Support

ID.F.1

Analysis

The previous SALP rated Engineering and Technical Support as Category 2. The previous

assessment indicated weaknesses in engineering's development of the safety-related motor

operated valves (MOV) program in response to Generic Letter (GL) 89-10. Other

weaknesses were also observed in Hope Creek responses to the Station Blackout Rule, in the

initial root cause evaluation associated with the filtration, recirculation and ventilation system

(FRVS) heater fuse failures and in responses to the NRC regarding GLs. Despite these

weaknesses, Hope Creek was provided with strong technical support during the previous

SALP period.

Engineering and Technical Support for Hope Creek is provided by corporate engineering,

known as Engineering and Plant Betterment (E&PB), and the onsite system engineering

group. These groups effectively provided technical support for refueling and maintenance

outage activities. E&PB handles major engineering efforts such as plant modifications and

,.

17

design bases reconstitution. The onsite system engineering group supports operations,

maintenance, testing and minor design change activities. These groups are well staffed with

experienced personnel in various engineering disciplines.

The onsite system engineering group was well-staffed with experienced, knowledgeable and

wen-trained personnel. The licensee continued their eight-month system engineer training

program. Most of the system engineers have successfully completed this program and almost

all have received formal root cause analysis training. The system engineering group has

provided good support for safe and efficient plant operation as demonstrated by the progress

made on the implementation of the GL 89-10 MOV program and by their analysis and

resolution of a number of emergency diesel generator design and operability issues.

However, there was a recurring number of EDG jacket cooling water pump seal failures. A

contributing factor to these failures was inadequate system engineering review and root cause

determination.

E&PB worked well with the onsite system engineering group. Examples included the torus

to drywell vacuum breaker disc torquing analysis and the emergent snubber analysis work

during the fourth refueling outage. Several improvements to the design change process were

made to reduce paperwork and better focus on safety significant issues. For example, a

simplified "workbook" or design and review package was introduced that significantly

reduced design package preparation and review time. In response to previously identified

deficiencies in the GL 89-10 program, the licensee made noteworthy progress in

implementing program requirements. For example, during the unit's fourth refueling outage,

134 of 258 MOVs were statically tested and 23 dynamically tested. However, a wiring error

and inadequate followup by engineering and test personnel resulted in an unplanned reactor

cavity level decrease.

The modification packages reviewed were of good quality. They were thorough and

contained adequate safety reviews. However, the licensee made a change to the facility as

described in the UFSAR without determining if there was an unreviewed safety question

involved. Furthermore, there were other isolated cases of the licensee failing to follow its

10 CFR 50.59 implementation procedure. Individually, these failures to follow procedure

did not have safety significance; however, the finding indicates a continuing defect in the

licensee's 10 CFR 50.59 program.

The licensee had an excellent training program for E&PB staff and onsite system engineering

personnel. A typical system engineer received substantial theory-based training, including

thermodynamics, heat transfer, and fluid mechanics. Recent enhancements to the E&PB

training program have advanced towards a more performance/application oriented approach.

The Design Change Process training was being expanded to include examples of completed

packages; the Configuration Baseline Documentation (CBD) training has been revised to

emphasize the application of the CBDs and the maintenance of the documents due to

regulatory and operating experience reviews. In addition, the licensee has an excellent Root

Cause Analysis and Decision Making course designed for members involved in problem

solving and incident investigations such as licensee event reports (LER).

18

The licensee has initiated an aggressive program to pursue resolution of the Hope Creek

hydraulic control unit (HCU) accumulator lining pitting problem, although the safety

evaluation indicated that the pitting would not inhibit the movement of the piston during a

reactor scram. The licensee aggressively gathered information from other utilities and the

accumulator vendors to resolve this problem, and instituted a program to detect this problem

in the remaining HCUs during the refueling outage.

E&PB assumed responsibility for locating discontinued parts and effectively implemented a

program to develop new sources for parts and to provide equivalent replacements. E&PB

has also initiated an aggressive program to reduce substantially the engineering work request

(EWR) backlogs for both Salem and Hope Creek. Similar progress was made by the onsite

system engineering. For Hope Creek, the number of EWR backlogs was reduced by more

than one third.

As a result of concerns identified during an NRC inspection at Salem, PSE&G identified

significant weaknesses in the site Erosion/Corrosion (EiC) Program. E&PB subsequently

implemented substantial programmatic improvements. The current program meets the

industry standards and appears effective to monitor long term EiC issues.

Sum mazy

Hope Creek was provided with improving engineering and technical support by a competent,

experienced and stable corporate engineering organi7.ation, and a wen staffed and

knowledgeable onsite system engineering organii.ation. Noteworthy progress was observed

in implementing the MOV program. The modification packages reviewed were of good

quality. The training program provided for E&PB staff and system engineering personnel

was determined to be excellent. The licensee has implemented an effective procurement

program, which utilized a user-friendly computer database system. Both E&PB and system

engineering groups have initiated aggressive programs to reduce substantially the engineering

backlogs. Weaknesses were identified in the erosion/corrosion program and the

implementation of 10 CPR 50.59. Root cause programs were generally effective with some

minor errors noted.

ID.F.2

Performance Rating: Category 2, Improving

ID.F.3

Board Comments:

None

ID.G

Safety As.ses.sment/Quality Verification

ID.G.1

Analysis

The previous SALP rated this area as Category 1 and indicated that Hope Creek was a well

run, safety conscious facility. The licensee effectively identified problem areas, and ensured

prompt and effective corrective actions. The licensee's management of the third refueling

19

outage was a noteworthy strength. The licensee's MOY program and its responses to generic

issues were noted weaknesses. Personnel errors were noted in all functional areas. Safety

review committees and QA groups provided effective and independent oversight of activities.

Throughout this period, individual performance was very good. Direct supervision at the site

by first and second line supervisors and comprehensive management oversight of station

activities were strengths. The licensee has been successful in reducing the personnel error

rate; however, errors were observed in some functional areas, including one by a contractor

which resulted in a manual reactor scram. Another example involved a motor operated valve

(MOY) wiring error was not corrected per procedures, and resulted in an unplanned reactor

cavity level loss. Troubleshooting by contractor engineering and test personnel failed to

properly identify, document and correct the wiring error, and resulted in a drain down of

about 50,000 gallons. Licensee follow-up for this event included a thorough root cause

investigation and establishment of effective corrective actions.

The licensee's amendment and relief requests were generally of high quality, though

occasional lapses in clarity and omission of detail were noted. This was evidenced in the

licensee's request for a change to the licensing basis for the emergency diesel generator

(EOG) fuel oil storage and day tank minimum level requirements.

Notwithstanding this specific deficiency, the Station Operations Review Committee (SORC)

provided consistent and effective review of other significant plant issues, including design

changes, post-scram reviews and reportable events. The licensee's major event review

process, the Significant Event Response Team (SERT), effectively performed comprehensive

scram and event reviews. Recommendations generated from SERT reviews were promptly

acted upon by management and tracked in the licensee's Action Tracking System. As

discussed in the engineering section, the licensee root cause corrective action and 10 CFR

50.59 programs were generally very good, with only minor problems noted.

The On-site and Off-site Safety Review Groups (SRG) and Station Quality Assurance (SQA)

demonstrated effective independent reviews of Hope Creek issues. For example, SRG

performed a detailed and effective review of the shutdown risk for the fourth refueling

outage. SQA performed a thorough review of a temporary air compressor tie-in and

identified concerns and recommended effective corrective actions. Both the SRG and SQA

provided assistance to all SERT efforts.

The licensee took aggressive action to review its reportable events. Licensee Event Reports

were well written and accurate.

Hope Creek conducted its fourth refueling outage during the period. Outage preparations

were excellent. A number of shutdown risk initiatives were successfully performed. SQA

was effective during all phases of the outage, performing a large number of performance

based surveillance and hold point activities. Overall outage performance was good.

_

,*

20

Hope Creek station management, including the General Manager and department heads,

provided effective and safety conscious oversight of station activities on a daily basis. This

was evidenced in daily meetings with the senior nuclear shift supervision and operating crew

and in management accountability meetings. In addition, the General Manager conducted

informative State-of-the-Station meetings. Corporate management was highly visible relative

to Hope Creek station activities. Operations personnel exhibited a professional and

questioning attitude during the performance of their duties. A review of the Hope Creek

turbine generator overspeed protection system was comprehensive and displayed a

conservative approach to safety.

Summary

The licensee continues to perform well in this functional area. The licensee's first line

supervision management, SORC, and independent third part oversight was very good.

Individuals performed well, as evidenced by a reduction in the personnel error rate.

Excellent independent review and root cause determinations continued to be observed this

period. The licensee's performance in the fourth refueling outage was judged to be

excellent.

m.G.2

Performance Rating: Category 1

m.G.3

Board Comments:

None

---~- __ J

21

IV.

SITE ACTIVITIES

IV .A

Licensee Activities

The Hope Creek unit began the SALP period operating at full power. The unit completed a

300 day continuous run when PSE&G shut down the unit on March 6, 1992, for planned

mid-cycle outage.

The unit was restarted on March 17, 1992, and operated at power until May 26, 1992, when

PSE&G initiated a shutdown due to failure of drywell-to-torus vacuum breakers. The unit

restarted on May 31, 1992.

The unit operated until September 12, 1992, when PSE&G initiated a shutdown to commence

the fourth refueling outage. The unit was restarted from the refueling outage on November

6, 1992. A reactor scram was manually inserted when both reactor recirculation pumps

tripped due to a loss of room ventilation on December 3, 1992. The unit was restarted on

December 10, 1992.

On May 16, 1993, the unit automatically scrammed from 60% power on high reactor

pressure due to a failed electrohydraulic control relay. The unit was restarted on May 19,

1993.

Small power reductions were performed throughout the period to perform maintenance and

testing activities. At the end of the SALP period, the unit was operating at fu11 power.

IV .B

NRC Inspection Activities

Four NRC resident inspectors were assigned to Artificial Island during the assessment

period. Two of these resident inspectors were rotated with new residents assigned during the

period. NRC team inspections were conducted in the following areas:

Emergency Preparedness Inspection conducted on October 27-29, 1992, to observe

the Artificial Island annual exercise.

Electrical Distribution Safety Functional Inspection conducted January 13 - February

14, 1992.

Surveillance Test Program Inspection conducted during April 6-21, 1992.