ML18095A524

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SALP Rept 50-354/89-99 for May 1989 to Jul 1990 Period
ML18095A524
Person / Time
Site: Salem, Hope Creek  PSEG icon.png
Issue date: 10/09/1990
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18095A523 List:
References
50-354-89-99, NUDOCS 9010180103
Download: ML18095A524 (75)


See also: IR 05000354/1989099

Text

ENCLOSURE

INITIAL SALP REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

REPORT NO. 50-354/89-99

PUBLIC SERVICE ELECTRIC AND GAS COMPANY

HOPE CREEK GENERATING STATION

ASSESSMENT PERIOD:

MAY 1, 1989 - JULY 31, 1990

BOARD MEETING DATE:

SEPTEMBER 19, 1990

9010180103 901009

~DR

ADOCK b5000272

Q

PDC

I.

INTRODUCTION . . .

II.

SUMMARY OF RESULTS

A.

Overview ...

TABLE OF CONTENTS

B.

Facility Performance Analysis Summary

III. PERFORMANCE ANALYSIS ...

1

3

3

4

5

A.

Plant Operations .. *.

5

B.

Radiological Controls

8

C.

Maintenance and Surveillance. . . .

.

.

.

.

10

D.

Emergency Preparedness (Common With Salem) ...... 15

E.

Security and Safeguards (Common With Salem)

17

F.

Engineering and Technical Support . . . . .

19

G.

Safety Assessment and Quality Verification.

22

IV.

SUPPORTING DATA AND SUMMARIES .....

A.

B. c.

D.

Licensee Activities.

. .....

Inspection and Review Activities.

Significant Licensee Meetings ..

Plant Trips and Unplanned Shutdowns

Table 1 - Inspection Hours Summary

Table 2 - Enforcement Summary

Table 3 - Licensee Event Reports Summary

Attachment 1:

SALP Evaluation Criteria

25

25

25

26

26

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) is an integrated

NRC staff effort to collect observations and data to periodically evaluate

licensee performance on the basis of this information.

The SALP process

is supplemental to normal regulatory processes used to ensure compliance

with NRC rules and regulations.

SALP is .intended to be sufficiently

diagnostic to provide a rational basis for allocating NRC resources and to

provide meaningful feedback to the 1 icensee 1 s management to improve the

quality and safety of plant operations.

An

NRC SALP Boa rd, composed of the staff members 1 i sted be 1 ow, met on

September 19, 1990 to review the collection of performance observations

and data and to assess the 1 icensee 1 s performance at the Hope Creek

Generating Station. This assessment was conducted in accordance with the

guidance in NRC Manual Chapter 0516,

11Systematic Assessment of Licensee

Performance

11 *

This report is the NRC 1s assessment of Public Service Electric and Gas

(PSE&G) Co. 1 s safety performance at the Hope Creek Generating Station for

the period May l, 1989 through July 31, 1990.

The SALP Board for the Hope Creek Generating Station assessment consisted

of the following individuals:

Chairman:

C. Hehl, Director, Division of Reactor Projects (DRP)

Members:

R. Blough, Chief, Projects Branch 2, DRP

P. Swetland, Chief, Reactor Projects Section 2A, DRP

T. Johnson, Senior Resident Inspector, DRP

W. Butler, Director, Project Directorate I-2, Office of Nuclear Reactor

Regulation (NRR)

C. Shiraki, Project Manager, NRR

M. Knapp, Director, Division of Radiation Safety and Safeguards (DRSS)

J. Durr,

Chief,

Engineering Branch, Division of Reactor Safety (DRS)

Others in Attendance:

J. Stone, Project Manager, NRR

S. Dembek, Project Manager, NRR

S. Barr, Resident Inspector, DRP

S. Pindale, Resident Inspector, DRP

K. Lathrop, Resident Inspector, DRP

C. Anderson, Chief, Plant Systems Section, DRS

J. Jang, Senior Radiation Specialist, DRSS

2

Others in Attendance (Continued)

R. Nimitz, Senior Radiation Specialist, DRSS

J. Joyner, Division Project Manager, DRSS

W. Pasciak, Chief, Facilities Radiation Protection Section, DRSS

J. Noggle, Radiation Specialist, DRSS

C. Conklin, Senior Emergency Preparedness Specialist, DRSS

C. Amato, Emergency Preparedness Specialist, DRSS

R. Keimig, Chief, Safeguards Section, DRSS

R. Albert, Physical Security Inspector, DRSS

P. Ray, Operations Engineer, Performance Evaluation Branch, NRR

A. Almond, General Engineer, Director's Office, NRR

3

II

SUMMARY OF RESULTS

II.A Overview

PSE&G successfully operated the Hope Creek reactor in a safety conscious

manner, effectively completed their second refueling and maintenance out-

age, and exhibited excellent performance by support groups.

Strong licen-

see management involvement and oversight were evident in a 11 fun ct i ona l

areas, as was excellent performance at the worker and supervisory levels.

Strong and effective self-assessment by supervision, management and inde-

pendent assessment groups was noted.

Critical, technically sound problem

i dent if i cation, root cause analysis and corrective action programs were

also evident in all functional areas.

As a result, the plant operations,

radiological controls, and security/safeguards functional areas maintained

a superior level of performance.

In addition, the emergency preparedness,

engi neeri ng/techn i cal support and safety assessment/quality veri fi cation

functional areas achieved this high level of performance during this

period.

However, some isolated personnel errors persisted in most func-

tional areas.

The maintenance/surveillance functional area received the same SALP per-

formance rating noted during the last assessment period.

Improvements are

needed in worker attention to detail and procedural compliance, in the

spare parts procurement and material control programs, and in reactor trip

rate reduction.

Significant licensee corrective measures in this area

were evidenced and an

improving trend in this area at the end of the'

period was noted.

In summary, the licensee achieved an overall superior level of perform-

ance.

It is important that the licensee recognize the challenge to mai~

tain this performance level by continuing the aggressive, safety conscious

attitude and approach to nuclear, radiological and personnel safety, from

the worker level through corporate management.

II. B

4

Facility Performance Analysis Summary

Functional

Rating, Trend

Rating, Trend

Area

Last Period

This Period

Plant Operations

1

1

Radiological Controls

1

1

Maintenance/Surveillance

2, Improving

2, Improving

Emergency Preparedness

2

1

Security and Safeguards

1

1

Engineering/Technical

Support

2, Improving

1

Safety Assessment/

Quality Verification

2, Improving

1

Previous Assessment Period:

January 16, 1988 through April 30,

1989

Present Assessment Period:

May 1, 1989 through July 31, 1990

III

III.A

III.A.1

5

PERFORMANCE ANALYSIS

Plant Operations

Analysis

The previous SALP rated Hope Creek operations as Category 1.

That

assessment concluded that the operating staff continued to display a

conservative and safety conscious approach to plant operation.

There

was

an

excellent operating

record with

no

operationally caused

reactor scrams.

The operators were ski 11 ful and kn owl edgeab 1 e, and

properly responded to transients.

PSE&G

improved the support of

operations with increased staffing in both onshift and support roles.

The need for reduction in personnel errors rep.resented the primary

area for improvement.

During this assessment period, the reactor was operated in a conser-

vative and safety conscious manner.

Operators ski 11 fully performed

their duties during unit startups, shutdowns and transients.

There

were four reactor scrams during the period and none were caused by

operators.

However, two of these scrams occurred during main turbine

testing from the contro 1 room, and a reactor operator error contri b-

uted to one of these scrams.

Operator response to reactor scrams and

plant transients was exemplary.

In

sev~ral instances, prompt actions

by operators prevented plant transients and possible reactor scrams

due to *a feedwater heater isolation, a loss of instrument air event

and reactor feedwater pump trips.

PSE&G

has

committed resources to upgrade p 1 ant operations.

Each

operating shift continues to have three Senior Reactor Operator (SRO)

licensed individuals

(one

above Technical

Specification

require-

ments).

The operations staffing includes a pipeline into licensed

operator status to recover losses from attrition.

A separate SRO

1 i censed i ndi vi dua 1 supervises the work control group during regular

maintenance hours.

There are a

to ta 1 of 36

1 i cen sed operators,

including 25 onshift and 11 in staff and training positions.

Plant operations were adequately supported by the Training Depart-

ment.

Simulator refresher training on reactor startups continues to

be given to the ROs and SROs immediately before taking their shift.

Three of five SRO license candidates and four of four Reactor Oper-

ator (RO) candidates passed their initial license examinations.

The

RO/SRO requalification program was determined to be satisfactory with

four of four ROs and eight of ten SROs passing an NRC administered

exam.

The failure rate for these initial and requalification SRO

exams indicates weaknesses in licensee and candidate preparation.

6

Deficiencies also existed in methods for simulator evaluations, in

exam grading and in poor quality of licensee submitted exam material.

Licensed operators' plant awareness, safety perspective, and profess-.

ional control

room

demeanor w.ere

consistently evident.

However,

mi nor weaknesses were noted in the routine performance of periodic

contra l boa rd wa l kd.own s and with the procedures that establish the

requirements such as the a 11 owed contra l room mobility for the RO/

SRO.

For example, the SRO was a 11 owed to enter the computer room

where he would be out of sight of.control room alarms/indications.

The licensee was responsive to these NRC .concerns and adequately

addressed these mi nor weaknesses.

Pl ant opera ti ans were wel 1 sup-

ported by detailed procedures, and procedura 1 adherence was good.

Shift turnovers: were formal and inc 1 uded thorough briefings of the

relief crew.

Control room access was controlledi and activities were

limited to those directly related to plant operations.

A high number

cif lit annunciator alarms was noted upon

~he completion of a~d prior

to startup from the second refueling outage.

Aggressive management

attention resulted in significant reductions in these lit annuncia-

tors.

The use of overtime was properly controlled.

Good performance

of non-licensed equipment operators was noted during observations

made

on

pl ant tours, and *during eqlii pment testing and operation.

The licensee has implemented

revision~ to the emergency procedure

guidelines in their emergency operating procedures (EOPs).

The oper-

  • ators effectively used the EOPs as evidenced by

observations of

actual plant transients and scrams, and *during simulator training.

Overa 11, the EOPs continued to be fully capable of performing their

intended purpose.

Strong plant management oversight and a.ttention to operations was

evident on a daily basis.

An operational perspective of plant prob-

lems and work prioritization was well understood and was enhanced by

daily meetings.

The licensee has been effective in ensuring good

interdepartmental

communication

and

in

resolving

problems.

The*

senior

nuclear

shift

supervisor

has

direct

access

to

plant

management.

Instances of personnel errors in Operations continued. *The- errors

were of minor safety significance, occurred during operational, main-

tenance

and

testing activities and were

committed by different

peop 1 e.

The errors were . most preva 1 ent during the outage peri ad

early in the SALP period.

Acceptable, appropriate corrective actions

were taken for each error.

Management meetings with each shift dur-

ing the refueling outage were held to ensure operators understood

III.A.2

III.A.3

7

expectations.

All operations related outage activities were stopped

during these meetings.

Safety, procedure compliance, proper brief-

ings and communications, and reversing the short term negative trend

in personnel errors were demonstrated to be more important to manage-

ment than meeting the outage schedule.

There were fewer errors in

the latter portion of this assessment period, and the frequency of

significant personnel

errors has decreased compared

to

previous

assessment periods.

PSE&G's aggressive approach has continued to

reevaluate previous corrective actions and the potential for addi-

tional corrective actions.

Plant housekeeping has improved during the period.

Plant area paint-

ing is nearing completion.

This activity has reduced the contamin-

ated floor space, particularly in the high pressure coolant injection

and reactor core isolation cooling rooms.

Equipment operators can

make their rounds with only minimal contamination protective cloth-

ing.

The assignment of housekeeping area responsibilities has been

effective in providing

11 ownership

11 of specific plant areas.

The overall fire protection program was effective.

Dedicated fire

protection personnel performed we 11

and were kn owl edgeab le, which

demonstrated an effective training program.

The fire brigade was

staffed by the Site Protection group personnel, which minimized the

reliance on operators to respond to fir~ and first aid related emerg-

encies.

Appropriate operator involvement in emergencies was pro-

vided.

The preventive maintenance and surveillances of fire protec-

tion equipment were effective.

Fire protection equipment upgrades

included a new ambulance, incident command vehicle, and other items.

Overa 11, pl ant and site management aggressively supported the fire

protection area.

In summary, the Hope Creek reactor was operated skillfully and in a

conservative and safety conscious manner.

Reactor operator error

contributed to one of four reactor scrams that occurred during the

period.

Strong management and supervisory oversight and involvement

occurred at all levels from the senior reactor operator through the

station general manager.

An aggressive approach by management has

been effective in reducing the number of personnel errors.

Senior

reactor operator failure rate during licensing and requalification

exams was higher than normal.

Performance Rating

Category:

1

Trend:

NA

Board Comments

None

-- ---- ---------------------------------,

III.B

III.B.1

8

Radiological Controls

Analysis

The previous SALP rated the functional area of radiological controls

as Category 1 and concluded that PSE&G maintained and implemented an

effective radiological controls program.

No significant weaknesses

were identified during the last assessment period.

During the current assessment period, the radiological controls pro-

gram continued to be effective and well managed.

NRC observations

throughout the period, which included the second refueling outage,

continued to indicate a good level of management involvement and con-

trol of the radiological controls program.

PSE&G supervisors and

managers actively observed ongoing work activities and plant condi-

tions through formal

review processes.

The

licensee's internal

review processes such as quality assurance audits and surveillances

and internal self-assessments provided effective oversight of program

activities.

The review processes were generally performance based

and used technical experts where appropriate.

The licensee's approach to the resolution of technical issues was

good as evidenced by the licensee's response to and resolution of

technical

problems associated with two

operational

events.

For

example, the licensee's response to a higher than expected crud burst

during refueling was appropriate and well managed.

In addition, late

in the assessment period the liquid radwaste processing system backed

up, causing overflows of several tanks into in-plant dikes.

The

licensee's technical review of the overflow event was extensive and

continuing at the end of the assessment period.

The overflows did

not result in any onsite or offsite radiological concerns.

This was

an isolated event, and the licensee's response to this event was

determined to be appropriate.

The licensee's enforcement history during the period was good.

No

NRC violations were cited.

The licensee effectively detected an

isolated problem with a High Radiation Area door being left open and

implemented

appropriate corrective actions.

PSE&G's

ability

to

self-identify and implement appropriate corrective actions remains a

strength.

Staffing throughout the period continued to be good, both for routine

operat1ons and outage periods. Well qualified personnel continued to

fill key positions within the organization.

Reliance on contractor

support was minimized by use of temporary support from the Salem

station and the corporate radiological controls group.

The staff,

including contractors, received appropriate training and qualifica-

tion testing to perform assigned tasks.

9

There were no unplanned external whole body radiation exposures dur-

ing the assessment period.

Engineering controls were effectively

used to control airborne radioactivity, and no significant intakes of

airborne radioactivity occurred during the assessment period.

Over-

all external and internal exposure controls were effective.

The licensee instituted several engineering changes to reduce ISI

personnel radiation exposure.

These changes are:

(1) the replace-

ment of cont rci l blade pins and ro 11 ers with others made of non-

ste l lite materials prior to startup; (2) the use of zinc injection to

reduce cobalt plate-out; and (3) the reduction of feedwater iron from

approximately 11.8 parts per billion (ppb) during the first fuel

cycle to 3-5 ppb during the second cycle.

The

station ALARA

(As

Low As

Reasonably Achievable) organization

effectively planned for outage radiological work activities.

Expos-

ure goals were reasonable.

ALARA

initiatives,

such

as

use

of

robotics and video cameras were evident throughout the outage.

The

use of the computerized radiation work permit system in conjunction

with the automated dosimetry access contra l system was effective in

tracking and controlling exposure.

The licensee aggressively pur~ued

power reductions to minimize occupational exposure during steam plant

maintenance activities.

Also, an in-depth post-outage ALARA report

was developed to document strengths and weaknesses encountered during

the outage.

Areas for improvement were tracked to ensure resolution

prior to the next outage.

The licensee performed ALARA reviews for

outage work that accounted for about 90% of the aggregate exposure

sustained during the outage.

Overa 11, the licensee's efforts to

maintain

occupational

radiation

exposure

ALARA

have

been

very

effective.

The radiological liquid and gaseous effluent monitoring and control

programs were effective.

Liquid

and

gaseous

effluent

sampling,

analysis, and reporting were good.

Air cleaning and effluent/process

radiation monitoring systems were well maintained, tested, and cali-

brated.

The

licensee's

effluent

control

training

program

for

technicians was very good.

An effective Radiological Environmental Monitoring Program was imple-

mented.

Sampling and ana lyt i cal procedures were upgraded, and an

effective QC program was in pl ace to assure the quality of sample

analysis.

The meteorological monitoring system was properly cali-

brated* and maintained.

Audi ts performed by the Quality Assurance

Division were thorough, and audit-identified deficiency items were

adequately resolved in a timely manner by the licensee.

III.8.2

III .8.3

III. C

III.C.1

10

The solid radwaste/transportation program continues to be very good.

The unique radwaste processing system (asphalt solidification and

dewatering system) has been effectively operated, with no incidents,

violations or problems at the disposal sites.

The quality assurance

(QA) program for radwaste was determined to be excellent with notable

strength in the area of QA surveillances.

The licensee 1 s training

program, especially for the Radwaste Operators, was excellent.

The

l icensee 1 s

performance with respect to NRC

standard chemical

measurements was good.

In addition, the results of the radiological

sample measurements comparisons indicated that all the measurements

were in agreement under the NRC criteria used for comparing results.

Disagreements initially encountered in the measurement of an air

particulate filter and

a

charcoal

cartridge

~ere resolved.

The

licensee's QA program for chemical and radiological measurements is a

noted strength.

In summary,

PSE&G continued to maintain and implement an effective

radio l ogi cal contra ls program.

Management support and oversight of

the

program were

good.

Overall

radiological controls, including

staffing, to support routine and outage work activities were good.

The licensee's initiatives in the ALARA area continue to indicate a

proactive approach to reducing aggregate exposure over the life of

the

plant.

Programs

such

as

radwa~te processing and

shipping,

effluent monitoring and control and environmental monitoring continue

to be well managed.

Performance Rating

Category:

1

Trend:

NA

Board Comments

None

Maintenance/Surveillance

Analysis

The last SALP rated the Hope Creek maintenance/surveillance func-

tional area as a Category 2, Improving.

That assessment concluded

that the maintenance organization effectively managed preventive and

corrective maintenance and was staffed with technically knowledgeable

and experienced personnel.

Strengths noted included an improvement

11

in the control of maintenance work as evidenced by the decrease. in

the number of maintenance-related reactor trips, and the adequacy and

detail of the plant 1 s surveillance test procedures.

The SALP noted

the reduction of the number of personnel errors and missed surveil-

lances as the areas requiring improvement.

Maintenance:

The Hope Creek maintenance program is well organized, and the licen-

see has demonstrated good performance in this area including overall

adherence to procedures in maintenance work, and appropriate over-

sight of maintenance activities.

Both unit and individual systems

availability have been maintained at a high level. Senior management

was noted to be directly and intimately involved *in plant maintenance

activities.

Management oversight has been effective through the

di re ct use of maintenance performance i ndi ca tors and a maintenance

tracking system.

Daily planning meetings demonstrated the ability of

plant management to adjust maintenance priorities and to review and

correct adverse trends. Additionally in this area, the licensee has

been acquiring risk assessment data to be used for prioritizing main-

tenance activities. This activity has only recently been in it i c;ited

at Hope Creek and is a positive indication of management 1 s safety-

conscious control of maintenance work at the plant.

The most significant strength of the maintenance organization is its

stab 1 e and we 11-tra i ned staff.

The maintenance work force operates

under the direction of good supervision, and utilizes proven mainten-

ance procedures.

The maintenance training program was effective and

demonstrated very well-defined qualification criteria for personnel.

However,

not a 11 maintenance personne 1 had comp 1 eted this forma 1

training program.

The training center continued to provide extensive

electrical and mechanical training facilities. Overall, the mainten-

ance staff was highly knowledgeable in their respective areas of

responsibility.

For times when the Hope Creek maintenance staff

needs to be supplemented, the licensee has established an effective

control for contracted maintenance personnel by using the Contractor

Control Sheet to track contractor personnel and their training,

indoctrination and qualification.

Maintenance faci 1 it i es were generally we 11 contro 11 ed, equipped and

maintained. The layout and utilization of these facilities were well

planned, organized and controlled throughout the plant to accommodate

the maintenance activities and the movement of materials and equip-

ment.

The administrative controls over procurement, receipt, inspec-

tion, storage and issuance of materials were generally adequate for

ensuring that maintenance materials were available when needed and

..

12

are issued properly for their intended use.

A weakness in ma i nten-

ante support activities was noted, however, concerning the availabil-

ity of replacement parts.

A slow requisition process resulted in a

large number of -routine maintenance requests being delayed because

they were awaiting parts.

At the end of the assessment period, the

licensee

had

recently dedicated additional

resources

with

sole

responsibility for material control to. improve performance in this

area.

The l icensee

1 s routine management oversight and feedback system has

worked well to assure safe and reliable plant operations.

A strength

of the system is the Managed Maintenance Information System (MMIS).

MMIS riot only provides a wide range of information, such as equipment

history, recurring task scheduling, real time job status and parts

inventory, but is widely used* by pl ant personnel , is easily access-

ible~ and usable.

During the assessment period, Hope Creek completed o_ne refueling and

several forced outages.

The maintenance planning and outage organ-

izations functioned well in scheduling all required tasks and coor-

dinating the team work required of the different work groups to

a~complish those tasks.

The unit uhderwent its second refueling out-

age during September through November 1989, with a 11 major efforts

successfully completed and without the ,occurrence of any maintenance

related safet~ system actuations br other significant incident~.

The

maintenance organization functioned effectively during a two week.

forced outage following

the March 19, 1990

reactor

scram.

With

little notice or preparation time, the maintenance department per.;..

formed successful repairs on a feedwater drain cooler that had been

isolated and had been preventing. the unit from operating at full

power.

S~veral events occurred during the period related to improper system

restoration following maintenance on the system.

One event occurred

in September 1989 and resulted in a core spray pump being operated

for 45 minutes with both the minimum fl ow and full fl ow test lines

isolated.

A second event occurred in June 1990 when a Reactor Water

Cleanup (RWCU) isolation was caused by an RWCU pump being started

with two discharge drain valves open, which resulted in a high rlif-

ferential

flow

signal.

Additional

examples

of

improper

system

restoration included the failure to reconnect the air supply to the

air operated drain valves, which contributed to the January 6, 1990

turbine and reactor trip, and a faulty ci rcul at i ng

water system

a 1 i gnment which resulted in

a

1 arge amount of salt water being

rel eased to and contaminating the 1 i quid effluent radwaste system.

The licensee received one maintenance-related violation during the

assessment period, resulting from several instances of maintenance

work*procedures not being properly followed.

Notwithstanding the weaknesse~ identified in this area, the licensee

has managed and performed a high number of maintenan~e acti~ities in

a commendable manner.

13

Surveillance:

The Hope Creek survei 11 ance program was conservatively and effec-

tively managed and

implemented throughout the assessment period.

Surveillance tests were scheduled and tracked effectively through the

MMIS, which provided good coordination of the Operations, Mai nten-

ance, Radiation Protection, Chemistry and Site Protection Departments

for the performance of the surveillance program.

This inter-depart-

ment coordination and cooperation were strengths of the Hope Creek

program.

Another asset of the surveillance program was the surveillance test

procedures themse 1 ves, which continued to be well written, accurate

and complete.

The procedure revision backlog noted in the previous

SALP report was eliminated during this SALP period, and the licensee

is now ~head of schedule in the required review of surveillance pro-

cedures.

An additional positive aspect of the surveillance program

is the implementation by the licensee of a policy whereby_ all _sur-

veillance procedures which affect safety system redundancy or initia~

tion -are performed on the night shift.

The policy* results in the

surveillances being performed in a more controlled atmosphere, with

fewer distractions for the test performer.sand the onshift plant

operators.

However, the policy is implemented only between May and.

September, primarily to reduce the risk of a plant scram during the

day when the electrical distribution grid is more strained.

Although the nu~ber of surveillance rel~ted incidents decreased from

  • the pri'or SALP cycle, the predominant cause of the incidents con-

tinued to be personnel error; including inadequate admi.nistrative

contra ls.

Three survei 11 ance t_ests were missed during this SALP _

period, one* due to a computer malfuncti.on and two due to personnel

error.

Personnel error was also the attributable cause of the three

calibration* errors which occurred over the course of the assessment

period.

One calibration error resulted in an

engineered safety

feature actuation, whi 1 e another resulted , in a licensee i dent i fi ed,

Technical Specificatton violation.

The licensee took effective and

timely corrective action fo-r all six of these incidents, but atten-

tion to detail remained the primary area for improvement in the rou-

tine ~urveillance program.

Two rea.ctor scrams* occurred at Hope Creek during the SALP cycle dur-

ing surveillance testing.

In December 1989 and again in January

1990, the reactor scrammed due to a main t_urbine trip.

The first

scram was due to a main turbine thrust bearing wear detector failure,

and the second was ca!Jsed by a high water l eve 1 trip of a moisture

III.C.2

III.C.3

14

separator.

The root cause of the first event was management's fail-

ure to implement a modification recommended as a result of a previous

similar event.

The root cause of the second event included poor

calibration of the normal and emergency separator drain path controls

combined with an operator procedural noncompliance while the surveil-

lance test was being performed.

The licensee ultimately implemented

adequate corrective actions, yet this is another example of the need

for better attention to detail in the surveillance area.

The inservice inspection (ISI) program at Hope Creek was well admin-

istered and effectively implemented.

Staffing levels, including the

use of ISI contractors were good.

The licensee exhibited good con-

trol over ISI vendors, part of which was the performance of multiple

quality assurance surveillances of vendor activities.

A notable

strength existed in the licensee's ISI personnel and contractors who

were well qualified to perform ultrasonic testing of intragranular

stress cracking corrosion (IGSCC) susceptible piping.

Hope Creek has

been effectively operating plant equipment in a manner which achieves

optimum primary water chemistry which in turn is part of an overall

effort to reduce the susceptibility of austenitic stainless steel

piping systems to IGSCC.

Licensee management has also demonstrq.ted

an

active concern and sensitivity to efforts regarding personnel

exposure during ISI and surveillance activities.

ISI results have

been well documented, complete, easily retrievable, and able to be

trended by comparison with previous data.

In summary, the Hope Creek station has carried out successful main-

tenance and surveillance programs.

The programs have been adequately

scheduled, planned and implemented.

The strengths of the program lie

in management, a well-trained and experienced staff and good proced-

ures.

Weaknesses in the area continued to be found in the procure-

ment process, post-maintenance system restoration, and in the per-

sonnel errors which have contributed to the noted pl ant events and

scrams.

Hope Creek's maintenance and surveillance program is a good

one, but improvements need to continue to resolve these weaknesses.

Performance Rating

Category

2

Trend:

Improving

Board Comments

None

III.D

III.D.l

15

Emergency Preparedness

Analysis

The Emergency Pl an for Art ifi ci al Is 1 and covers both Hope Creek and

Salem Nuclear Generating Stations, therefore the assessment of emerg-

ency preparedness is a combined evaluation of both facilities* emerg-

ency response capabilities.

During the previous SALP period, this area was rated Category 2.

This rating was based on weaknesses identified during a Salem based

full-participation exercise, some actual event classification prob-

lems, and delays in ensuring that the Salem Technical Support Center

could meet NRC design requirements.

Strengths noted included a high

level of management involvement in emergency preparedness activities,

responsiveness to NRC concerns, and an overall effective emergency

preparedness training program.

Management involvement in emergency preparedness was effective and

extensive.

Executives and plant managers maintain emergency response

organization position qualification, review and approve plan and pro-

cedure changes, participate in drills and exercises, resolve audit

noncompliance issues, exercise oversight functions, and interface

with Delaware and New Jersey State and County government personne 1.

Management oversight includes a review of call-in test results and

emergency preparedness training rescheduling.

The licensee successfully completed a partial-participation emergency

preparedness exercise conducted at the Salem facility during this

assessment period.

PSE&G 1 s emergency response actions were success-

ful in providing for the health and safety of the public.

Overall,

licensee performance was excellent and noted to be improved since the

last period.

Resolution of technical issues continues to be very good and demon-

strates a commitment to quality.

For example, as a result of an NRC

concern, the licensee completed a review of default iodine to noble

gas ratios as a function of release pathway, and determined the

values were consistent with accident data and emergency off-gas sys-

tem design and specifications. A four hour, default release duration

time has been developed and accepted by the States.

User friendly

personal computer software has been developed for the back-up dose

assessment program.

Relating to deficiencies in the previous assess-

ment,

the Technical

Support Center ventilation

system

has

been

16

upgraded to meet NRC design requirements.

Innovative program activ-

ities in-progress include development of site Emergency Action Levels

(EALs) for natural phenomena and security events to replace individ-

ual station EALs, a single Event Class-ification Guide for all three

units, and a simplified EAL description for use in the initial con-

tact message sent to the States.* Another example of resolving iden-

tified concerns was apparent in review of the licensee 1 s corrective

actions following loss of the NRC Emergency Notification System (ENS)

when it was accidentally disconnected from an uni nterruptab le power

supply (UPS) in May 1990.

The licensee 1 s communications staff has

aggressively

pursued

upgrading

the

Salem

Telephone

Switch

Room

(location of the ENS UPS connection).

Staffing in the emergency preparedness area is stable with a well-

qualified staff_ available to maintain an effective emergency pre-

paredness program.

Personnel

with operations backgrounds -are on

staff who develop demanding operations based scenarios for drills and

exercises.

Management* s attention t6 qua-1 ity was effective as demonstrated by

the following items.

Effective licensee audits and reviews for ~ach

unit were completed by independent audit groups.

Among other things,

drills were observed and the State/County/licensee interface was

determined to be adequate.

There were no significant findings and

the licensee/off-site interface was proactive.

Emergency Department

-p~rsonnel with licensee _e~ecutives and managers attended almost 100

meetings with State and County personnel.

The public alerting system

is tested daily, and is well maintained with availability at 99.5%, a

value which exceeds Federal Emergency Management Agency standards.

Independent and redundant siren activating systems are installed and

maintained in each State ..

The licensee has an effective emergency preparedness training pro-

gram.

Responsibility for emergency preparedness training has been

assigned to *the Emergency Preparedness Department.

Two qualified

emergency

preparedness trainers

have

been

transferred

from

the

Nuclear Training Center to the Emergency Preparedness Department to

support this effort.

Weekly, on-the-job, mini training drills for

each site have resumed and nine day-long drills are.also scheduled.

Over

1,000

licensee

personnel

have

been

trained

for

Emergency

Response Organization (ERO) positions. There are at least three per-

sonnel qualified for each key

ERO decision-making and management

position.

A dedicated emergency preparedness training facility has

been placed in service.

Engineers assigned to the Technical Support

- Center and the Emergency Operations Facility are given an overview

of Emergency Plan Implementing Procedures and Core Damage Assessment

Procedures.

III.0.2

III.D.3

III. E

IILE.1

17

The effectiveness of the training program was al so demonstrated !:Sy

response to twelve actual conditions requiring classification, and

the strong exercise performance.

This re so 1 ves the previous SALP

concern regarding event classification.

Observations of training

drills indicated active involvement

from licensed .senior reactor

operators dedicated to drill scenario deve 1 opment.

Ope rat i ans Sup-

port Center ~nd Technical Support Center personnel were observed to

implement effective problem identification and resolution.

The licensee successf~lly used the Hope Creek and Salem simulators to

enhance training effectiveness during emergency drills.

To enhance

the training effectiveness of these facilities, emergency communica-

tion systems duplicating those in the control rooms were installed in

each simulator.

In summary, the licensee maintains a strong and effective emergency

preparedness

program.

Management

remains

involved with. a demon-

strated

commitment to* quality.

Technical

issues

are

generally

promptly resolved and appropriate response is given to NRC initia-

tives.

The Emergency Preparedne~s Program staff is stable and well

quali,fied

to

maintain

an

effective

program.

Training *is well

developed and is effective as demonstrated by exercise' performance

and. response to actual conditions requiring classifiCation.

A good

working relationship is maintained with ,the States and Counties_ wi_th

regular meetings, and frequent drills.

Performance Rating

Category:

1

Trend:

NA

Board Comments

None

Securtty and Safeguards

Analysis

.The Security Plan for Artificial Island covers both Hope Creek and

Salem Generating Stations, therefore the assessment a*f security and

safeguards is a combined evaluation.

During the previous assessment period, the licensee's performance was

rated as Category 1.

Noted were an excellent enforcement history,

the continued implementation of an effective and performance-based

program, kn owl edgeab 1 e and experienced security. supervisory person-

ne 1,

and management

1 s. i nvo 1 vement in and support for the program.

18

During this assessment period, the licensee continued to implement a

high quality and very effective program, and management's attention

to and

involvement

in

the

program

remained

evident.

The

site

security supervisor and his staff are well-trained and qualified

professi ona 1 s who have been vested wi.th the necessary authority to

ensure that the security program is carried out effectively and in

conformance with NRC regulations.

The site security manager and his

staff continued to actively participate in

the Region I

Nuclear

Security Association and other groups

engaged

in

nuclear

plant

security matters.

They also maintained excellent rapport and effec-

tive communication channels with the plant staff who exhibit respect

and a good attitude toward the program.

Staffing of the contract security force was consistent with program

needs.

Early in this assessment period, the security force attrition

rate was high (24 percent).

Licensee and contractor efforts through

personal incentives were

successful

in

reducing this rate to

9

percent by the end of this period.

The licensee was responsive to identified concerns.

This was evident

by the approach to several potential weaknesses during the period

which primarily involved system and equipment aging.

As a result,

the licensee promptly initiated a comprehensive evaluation of all

systems and equipment and developed appropriate plans and a timely

schedule for upgrading and/or replacing the affected equipment.

In

addition, the licensee implemented a well managed fitness-for-duty

program in response to new NRC requirements during the period.

The

licensee's policy has been clearly stated and widely disseminated

among both emp 1 oyees and contractors.

It was found to be aggress-

ively implemented by knowledgeable personnel, and processing facil-

ities and procedures were exce 11 ent.

These efforts represented a

proactive management approach that continually seeks to improve the

effectiveness of the entire security program.

The

security force training and requalification program is well-

developed and administered by an experienced staff of two full-time

and five part-time instructors, and a supervisor.

Facilities are

provided on-site for training and requalifications and were well-

equipped and well-maintained.

During this

period,

the

licensee

established additional oversight of the contractor's training and

requalification program by providing a full-time licensee represen-

tative to administer the program.

III.E.2

III.E.3

I I I. F

III.F.1

19

The licensee 1s event report procedures were found to be clear and

consistent with the NRC 1 s reporting requirements.

Only one report-

able safeguards event was identified during the assessment period.

This event involved the loss of power to the security system and was

properly compensated for by the security force.

The licensee

1 s

report was cl ear and concise, and indicated an appropriate response

to the event.

During the assessment period, the licensee submitted three rev1s1ons

to the security program plans under

the

prov1s1ons

of

10

CFR

50.54(p).

These revisions were of high quality and technically

sound, and reflected well-developed policies and procedures.

The

licensee

also

updated

all

Physical

Security

Plan

implementing

procedures.

In summary, the licensee continued to maintain a very effective and

performance-based security program that exceeds regulatory re qui re-

ments.

The licensee's ongoing program to identify and correct poten-

tial weaknesses

in systems and equipment during this period are

commendable and demonstrated the licensee's commitment to maintain an

effective and high quality program.

Performance Rating

Category:

1

Trend:

NA

Board Comments:

None

Engineering/Technical Support

Analysis

The previous SALP rated Engineering and Technical support as Category

2, Improving.

The previous assessment indicated significant changes

within the corporate engineering department ( Engineering and Pl ant

Betterment, E&PB).

These changes were intended to improve engineer-

ing interaction with the plant staff. These changes included: estab-

lishment of Project Matrix Organization,

rev1s1on of the Design

Change Process, implementation of an Engineering Work Request System,

use of a Project Management System, and improved responsiveness of

E&PB to site needs.

Inconsistencies iri the quality of engineering

work from E&PB were noted to remain and a concern was

i dent i fi ed

early in the assessment period regarding reduced experience levels

within the systems engineering group.

20

During this SALP period, evidence of improved performance was noted

in the E&PB.

The Project Matrix Organization and the new design

change control process worked well.

The other changes appeared to

function properly.

Communication between E&PB and the plants also

improved through daily morning meetings,

and

regular weekly and

monthly meetings.

An improvement in the consistency of the quality

of work from E&PB and improvements in the performance of the systems

engineering group were observed.

The E&PB was mainly involved in the design process and less involved

i n d a il y p 1 a n t act i v i t i e s .

The o v e r a 11 de s i g n p r o c e s s with i n E& PB

was well controlled and contained appropriate checks and balances.

There was an emphasis on nuclear safety as evidenced by discussions

with E&PB personnel related to upgrading of procedures and implemen-

tation of new initiatives, such as the Configuration Baseline Docu-

mentation project, which is intended to reconstitute the design basis

for many of the major plant systems.

The design change process pro-

cedures were observed to be clear and detailed.

The procedures ade-

quately addressed design interface, design process and corrective

action process requirements with appropriate 1eve1 s of review and

verification specified.

Satisfactory performance and documentation

of cross discipline reviews were noted.

Calculations contained in

the modification packages were technically correct and performed in

accordance with applicable procedures .* A new workbook procedure has

been developed to improve the existing design change package process

and to improve configuration management control.

The workbook was sufficiently detailed to control the design process

and post-modification testing.

The drawings affected by modifica-

tions were accurate and appropriately reviewed and approved.

A new

prioritization program is under development to

improve

workload

prioritization and resource allocation.

The E&PB organization support of plant problems is noteworthy.

For

example, engineering support following a reactor scram and electrical

transient

was

thorough

and aggressive.

This

included

immediate

response,

root cause analysis

and investigations,

and corrective

actions.

Also,

metallurgical

evaluations for plant defects were

noted as being satisfactory, as was Hope Creek 1 s implementation of

the guide 1 in es of Generic Letter 90-05,

11 Gui dance for Performing

Temporary Non-Code Repair of ASME Code 1, 2, and 3 Piping,t' in affec-

ting repairs to the service water system.

The

E&PB organization

works well with Onsite System Engineering.

However, one example of a

poor design change package was associated with the core spray system

flow instrumentation not meeting the ASME Section XI instrument range

requirements.

The

licensee is properly addressing this concern.

21

The onsite system engineering group is staffed with experienced and

knowledgeable personnel.

Evidence of good system engineering support

for station activities includes:

(1) location of a packing leak in

the drywell and its prompt isolation; (2) maintenance trending, dis-

position for degraded equipment, and procedure generation; (3) active

participation in a scram reduction program by review of Hope Creek

and other plant events and near misses; and (4) thorough root cause

determination and incident report fo 11 owup.

The 1 i censee has been

aggressive in identifying and following

up

on engineering related

deficiencies.

10

CFR Part 21 evaluations and associated notifica-

tions such as HPCI/RCIC drain pot level switch qualification were

appropriately executed.

System engineering aggressively pursued cor-

rective actions associated with Rosemount transmitters.

The licen-

see* s operating experience. feedback (OEF) program has been effec-

tively implemented.

For example, vendor information regarding design

problems with Terry Turbine overspeed trip devices was reviewed and

addressed by the station in a timely and adequate manner.

Also, the

station is conducting weekly meetings to discuss current industry OEF

information.

Early in the period, a high turnover rate was noted for system e~gi

neers.

This had the potential for reducing the overall experience

level.

The licensee continued to implement their pipeline program to

train new system engineers.

Improvements in system engineering site

experience and the addition of new system engineers were noted to

reduce the turnover rate later in the assessment period.

These

individuals provided good day-to-day support of plant operations.

Engineering analyses in support of proposed licensing amendments were

technically viable and sound from a safety standpoint and on only a

few

occasions,

required

additional

information.

The

licensee 1 s

responses to Generic Letters and Bulletins usually addressed al 1

required aspects of the issues with little or no prompting.

The

engineering

staff

1 s

performance

indicated

good

interdepartmental

communications.

The licensee aggressively pursued solutions to a high failure rate

for the Bailey Solid State Logic Modules.

The licensee has been able

to

reduce

the

failure

rate

of these modules.

The statistical

analyses of failure rates for the modules were conservative.

The inservice inspection (IS!) program is generally well administered

and showed a high degree of licensee control over its IS! vendors.

An example is the diversified QA surveillances performed on a number

of vendor activities.

IILF.2

III.F.3

III.G

III.G.l

22

In summary, corporate engineering (E&PB), de'sign change control, com-

munications between E&PB and the plant have all improved.

The engi-

neering support was excellent for license amendments and replies to

generic correspondence.

The engineering staff possesses good tech-

nical knowledge and competence and closely monitors areas that have

been problems in the past.

They are responsive to the daily needs of

the station and prompt to respond with sufficient support.

Performance Rating

Category:

1

Trend:

NA

Board Comments

None

Safety Assessment/Quality Ver1ficatiori

Analysis

The previous SALP rated Safety Assessment/Quality Verification as

Category 2, Improving.

The safety conscious approach *instilled. by

plant management and exercised by Hope Creek personnel was commend-

able.

Problem

identification

was

excellent,

and

problems

were

promptly addressed and corre.cted.

PSE&G licensing activities were

generally

complete

and

timely.

Numerous

personnel

errors

had

occurred in all functional areas, and continued management attention

was deemed necessary.

Overall during this SALP period, individual performanc;:e was excel-

1 ent.

First and second 1 i ne supervisors were di re ct ly involved in

the field.

However, early in the period, isolated personnel errors

continued in all functional areas which resulted in further manage-

ment attention.

The errors were of low safety significance, and were

promptly reported and corrected.

During the refue 1 i ng outage, *the

operations department concluded that the rapid pace of outage activ-

ity was

contributing to the personne 1 errors and stopped outage

activities to couhsel the department to take the time required to do

the job right.

In addition to being willing to halt work to empha-

size the importance of quality work, it is to management's credit

that undue

schedular pressures are not exerted bn

the workers.

Another tool being utilized to emphasize the importance that manage-

ment places on quality output is a training session on attention to

detail, which "includes an effective video tape presentation.

Fewer

  • personne 1 errors occurred during the second ha 1 f of the assessment

period.

23

Station management,

including department managers and the general

manager, was di-rectly involved in providing effective station over-

sight on a daily basis.

The Senior Nuclear Shift Supervisors were

held accountable for plant operations, and they had direct access to

station management.

Effective daily meetings gave an operational

perspective to plant problem/work prioritization, and to tracking and

trending of information.

When a high number of 1 it contro 1 room

annunciator

alarms were present,

station management aggressively

dedicated resources and* successfully reduced the number.

Corporate management was also involved in station activitie~. Their

presence was observed onsite and in the plant during normal and off-

normal working hours.

Nuclear services,

engineering and quality

assurance (QA) management were also in'volved in their departments'

activities.

Corporate, plant, QA, and nuclear services management

personnel

responded

to

the site when

several

unplanned

scrams

occurred during evening hours.

The licensee has an effective program for problem identification.

Incident Reports continued to be used to identify and resolve these

p 1 ant prob 1 ems

and off-norma 1 events and for tracking corrective

actions to completion.

PSE&G continued to analyze a:nd trend the

. Incident Reports and LERs; their analyses* demonstrated a steadily

decreas.i ng .frequency.

The s*tation Operations Review Committee (SORC) provided consistent,

effective

review' of significant plant

issues,

including design.

changes, post-scram reviews, and reportp.b 1 e events.

After the off-

s i te marsh fire* on

March 19, 1990

and

the *resultant* 'electrical

transient and scram, the SORC met severa.l times to review the root

causes, corrective actions arid course .of action bE;!fore implementa-:-

tion, a good indication of the SORC's ~roactive role.

PSE&G has instituted an event review process .entitled "Significant

Event Response Team (SERT)".

A SERT 1s initiated by* the

gener~l

manager and is a real time,

independent review. of any unplanned

reactor* scram

or

other

major

plant

event.

SERTs

effectively

developed the sequence of events, determined root cause(s) and recom-

mended corrective actions for the four reactor scrams that occurred

during the reporting period.

The Human Performance Eva 1 uati on Sys-

tem; a detailed*analysis method for dete~mining root causes in inci-

dents involving personnel errors is also utilized by the licensee.

24

The Quality Assurance Department, the Onsite Safety Review Group

(SRG), and the Offsite Safety Review Group provided effective, inde-

pendent review of plant activities.

These groups also participated

in SERT activities and root cause training.

The station QA organiza-

tion provided effective day-to-day review of station activities,

including resolution of problems, and was well integrated into the

station 1 s organization.

The QA organization has developed and used

performance based surveillances for several station activities.

QA

involvement in the area of radwaste processing was

considered a

strength.

The

SRG

has been aggressive in reviewing and assessing

plant performance.

This included a twenty-four hour coverage of con-

trol room activities for a two week period.

Two of four scrams during the period were attributed to this func-

tional area.

A December 30, 1989 main turbine trip and reactor scram

were caused by failure of the thrust bearing wear detector trip by-

pass linkage during testing.

The root cause analysis determined that

plant management failed to aggressively implement modifications that

were recommended after a similar failure and scram in 1986.

Also the

March 19, 1990 scram which resulted from an offsite marsh fire, had

previously been identified by the licensee as a potential problem,

yet appropriate actions or contingency plans were not developed to

cope with them.

.

Twenty-seven licensing actions were processed.

The quality of the

technical evaluations was good, indicating that PSE&G

has a good

understanding of the technical issues, is aware of and participates

in industry groups, and uses acceptable approaches to problem solu-

tions.

The licensee 1 s response to Generic Letter 88-01 regarding

stainless steel piping was timely and adequately addressed the issues

in the letter.

PSE&G

has developed

and effectively implemented

Hydrogen Water Chemistry in the plant as a result of their review and

followup to the generic letter.

During the assessment period, a small leak was detected in the Hope

Creek service water piping, and plant management proposed to perform

a non-code repair in accordance with the

newly

re 1 eased Generic

Letter 90-05.

This was the first application of the provisions of

Generic Letter 90-05,

and

numerous discussions were

required to

arrive at a satisfactory resolution.

Although the licensee and the

NRC staff had differing views as to the best technical approach for

effecting the temporary non-code repair, PSE&G 1 s decision to adopt

the provisions of the Generic Letter was a positive action that

allowed the issue to be satisfactorily resolved.

III.G.2

III.G.3

25

In summary, Hope Creek, continues to be a well run, safety conscious

organization.

Management is heavily involved on a daily basis, and

makes its safety conscious attitude known throughout the plant.

The

review teams are candid and effectively determine root cause of

events.

The

licensee effectively identifies

problem

areas

and

ensures prompt and effective corrective actions.

How_ever, isolated

personne 1 errors continue to be an area meriting addi ti ona 1 manage-

ment attention.

Performance Rating

Category:

1

Trend:

NA

Board Comments

None

IV

SUPPORTING DATA AND SUMMARY

IV.A LICENSEE ACTIVITIES

BACKGROUND

The assessment period began May 1, 1989, with the Hope Creek reactor at

ful 1 power.

Automatic reactor scrams occurred on August 30, 1989, on

December 30, 1989, on January 6, 1990 and on March 19, 1990.

These scrams

are further described in Section III.C.

Other than these four scrams,

there were

no

unplanned shutdowns during the assessment period.

On

September 16, 1989, the Unit shutdown for its second refueling outage.

The Unit restarted on November 16, 1989.

At the end of the period, the

Unit had operated continuously for 124 days.

IV.B NRC Inspection and Review Activities

Two

NRC resident inspectors were assigned to the site throughout the

assessment period.

Regional

inspectors performed

routine

inspections

throughout the period, with added inspection emphasis during the schedule

outage.

In addition, a special inspection of the Maintenance Program was

performed in October 1989, and a Fitness For Duty inspection was performed

in March 1990.

Also, a team inspection was conducted to review perform-

ance

during

the

annual

emergency

preparedness

exercise

on

October 14, 1989.

NRC performed a to ta 1 of 3165 hours0.0366 days <br />0.879 hours <br />0.00523 weeks <br />0.0012 months <br /> of inspection dur-

ing the period, which equates to 2453 hours0.0284 days <br />0.681 hours <br />0.00406 weeks <br />9.333665e-4 months <br /> on an annualized basis.

26

IV.C Significant Licensee Meetings

A meeting was held on February 28, 1990, at Hope Creek Generating Station

to conduct a mid-SALP review and evaluation of licensee performance.

IV.D Reactor Scrams and Unplanned Shutdowns

Event Description

Date

Power

Root Cause

Functional Area

1.

The reactor was manually scrammed when half of the control rods inserted

due to a failed solder joint in the scram air header connection to one

control rod drive.

The solder joint had been inadequately installed dur-

ing plant construction.

8/30/89

81%

Component failure,

inadequate installation

NA

2.

The reactor automatically scrammed due to a turbine trip caused by the

failure of the main turbine thrust bearing wear detector trip bypass link-

age during surveillance testing.

Management had not aggressively imple-

mented modifications that were recommended after a similar failure and

scram in 1986.

12/30/89

100%

Component failure,

inadequate corrective

actions

Safety Assessment/

Quality Verification

3.

The reactor automatically scrammed due to a main turbine trip caused by a

high level in the A moisture separator during surveillance testing.

Al-

though calibrated per the vendor's recommendation, the normal and emerg-

ency drain systems were poorly tuned.

This, when combined with an oper-

ating error, caused the moisture separator level to rise uncontrollably.

1/6/90

96%

Inadequate level

contra 1 system

maintenance, operating

error

Maintenance/

Surveillance

4.

The reactor automatically scrammed on low reactor level due to loss of the

condensate and feedwater pumps when an offsite marsh fire caused an elec-

trical bus transient.

Although an electrical transient was predictable

from previous marsh fire events, the licensee did not implement effective

measures to prevent recurrence.

3/19/90

100%

Marsh Fire,

electrical system

transient; inadequate

corrective actions

Safety Assessment/

Quality Verification

TABLE 1

Inspection Hours Summary

Hope Creek Generating Station

May 1, 1989 - July 31, 1990

Annualized

Functional Area

Hours*

Hours

% of Time

A. Plant Operations

1375

1066

43

B.

Radiological Controls

283

219

9

c.

Maintenance/Surveillance

964

747

30

0.

Emergency Preparedness

80

62

3

E.

Security and Safeguards

144

112

5

F.

Engineering/Technical

Support

191

148

6

G.

Safety Assessment/

Quality Verification

128

99

4

TOTALS

3165

2453

100

  • Does not include operator licensing hours.

TABLE 2

Enforcement Summary

Hope Creek Generating Station

May 1, 1989 - July 31, 1990

Functional Area

A.

Plant Operations

B.

Radiological Controls

C.

Maintenance/Surveillance

0.

Emergency Preparedness

E.

Security

F.

Engineering/Technical

Support

G.

Safety Assessment/

Quality Verification

TOTALS

Number/Severity of Violations

Level IV

1

1

TABLE 3

Licensee Event Re2ort

Hope Creek Generating Station

May 1, 1989 - July 31, 1990

Number by Cause

Functional Area

A

B c

D

E x

Subtotal

-

-

-

-

-

A.

Operations

2

1

1

1

B.

Radiological Controls

1

1

c.

Maintenance/Surveillance

4

2

2

3

0.

Emergency Preparedness

E.

Security and Safeguards

F.

Engineering/Technical

2

3

1

Support

G.

Safety Assessment/

1

Quality Verification

TOTALS

10

2

1

4

7

1

This analysis includes LERs 89-12 through 89-26, and 90-01 through

90-11.

Cause Codes:

A.

B. c.

0.

E. x.

Personnel Error

Design, manufacturing or installation

Unknown or external cause

Procedure inadequacy

Component failure

Other

5

2

11

6

1

25

Root causes assessed by the SALP Board may differ from those listed in

the LER.

Table 3 (Continued)

2

Cl early, the above causal analysis shows that personnel errors remained the

major contributor to reportable events.

PSE&G's analysis also showed personnel

errors to be the major contributor, but to a lesser extent than last period.

These errors involved six violations of Technical Specifications (all PSE&G

identified).

PSE&G analyses, including the Human Performance Evaluation System

(HPES), have not identified any common root causes for the personnel errors.

Personnel at various working levels were involved, from technicians to proced-

ure writers to engineers to supervisory licensed operators.

The next significant causal factor was component failure.

Review of these

failures did not determine any shortcomings in the preventive maintenance

program.

ATTACHMENT 1

SALP Criteria

Licensee performance is assessed in selected functional areas, depen'ding on

whether the facility is in a construction or operational phase.

Functional

areas normally represent areas significant to nuclear safety and the environ-

ment.

Some functional areas may not be assessed because of little or no

licensee activities or lack of meaningful observations in that area.

Special

areas may be added to highlight significant observations.

The following evaluation criteria were* used, as applicable, to assess each

functional area:

1.

Assurance of quality, including management involvement and control;

2.

Approach .to resolution of technical issues from a safety standpoint;

3.

Enforcement h1story;

4.

Operational and construction events (including response to, analyses of,

reporting of, and corrective actions for);

5.

  • Staffing (including management); a~d

6*.

Effectiveness of training and qualification program.

Ori the basis of the _SALP Board assessment, each functi9nal area evaluated is

rated according to three performance categories. The definitions of these per-

formance categories are gi~en below~

Category 1 .

. Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in a superior level of performance.

NRC*

will consider reduced levels of inspection effort.

Category 2.

Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in a good level of performance.

NRC will

  • consider maintaining normal levels of inspection effort.

Attachment 1

2

Category 3.

Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in an acceptable level of performance; how-

ever, because of the NRC 1 s concern that a decrease in performance may

approach or reach

an unacceptable level,

NRC will consider increased

levels of inspection effort._

Category N:

Insufficient information exists to support an assessment of 'licens~e per-

formance.

These cases would include instances in which a rating could not

be developed because of insufficient licensee activity or insufficient NRC

inspection.

The SALP Board may assess a functional area to compare the 'licen.see's perform-

ance during a portion of the assessment period to that during an* entire period

in order to determine a performance trend.

Gene.rally, performance in the

latter part of a SALP period is- compared to the performance of' the entire

period.

Trends in performance from one period to the next may ~lso be noted.

_The tren~ categories used by t~e SALP Board are as 'follows:

- Improving:

Licensee performance wa~ determined to be improving._

.

Declining:

Licensee performance was - determined to be dee H n i ng

and the -

licensee had not satisfactorily addressed this pattern.

A trend is assigned only when, in the opinion of the SALP Board, the tre_nd is

significant enough to be. considered_ indicative- of a likely change in the per-

formance

category in the near .future.

For example,

a classification of

ncategory 2, Improving" indicates the cl ear potent i a 1 for "Category 1" perform-

ance in the next SALP period.

It should be noted that Category 3 performance, the lowest category, represents

acceptable, although minimally adequate, safety performance.

If at any time

the NRC toncluded that a licensee was not achieving an adequate leve1 of safety

performance, .it would then be incumbent upon NRC to take_ prompt appropriate

action in the interest of public health and safety.

Such matters would- be

dea 1 t *with independently from, and on a more urgent schedule than, the SALP

process.

ENCLOSURE

INITIAL SALP REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

REPORT NOS. 50-272/89-99

50-311/89-99

PUBLIC SERVICE ELECTRIC AND GAS COMPANY

SALEM GENERATING STATION

UNITS 1 AND 2

.

ASSESSMENT PERIOD:

MAY 1, 1989 - JULY 31, 1990

BOARD MEETING DATE:

SEPTEMBER 20, 1990

901018014~ 901009

F

    • [-1R

ADOCK

h~ru)Q?7 2

. '** - - PDC

0.

..

I.

INTRODUCTION . . .

II.

SUMMARY OF RESULTS

A.

Overview ...

TABLE OF CONTENTS

B.

Facility Performance Analysis Summary

III. PERFORMANCE ANALYSIS ...

1

3

3

4

5

A.

Plant Operations. . .

5

  • B.

RadiOlogical Controls

-9

C.

Maintenance and Survei 11 ance. .

.

. . . . .

13

D.

Emergency Preparedness (Common With Hope Creek) .

17

E.

Security and Safeguards (Common With Hope. Creek).

20

F.

Engineering and Technical Support . . . . . .

22

G.

Safety Assessment and Quality Verification.

25

IV .. SUPPORTING DATA AND SUMMARIES ......*

A.

Licensee Activities.

. .....

8.

Inspection and Review Activities.

C.

Significant Licensee Meetings ..

D.

Reactor Trips and Unplanned Shutdowns

Table 1 - Inspection Hours Summary

Table 2 - Enforcement Summary

Table 3 - Licensee Event Reports Summary

Attach~ent 1~

SALP Evaluation Criteria

.*

29

29

30

31

31

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) is an integrated

Nuclear Regulatory Commission (NRC) staff effort to collect observations

and data to periodically evaluate licensee performance on the basis of

this information.

The SALP process is supplemental to normal regulatory

processes used to ensure compliance with NRC rules and regulations.

SALP

is intended to be sufficiently diagnostic to provide a rational basis for

allocating NRC resources and to provide meaningful feedback to the licen-

see's management to improve the quality and safety of plant operations.

An

NRC SALP Board, composed of the staff members listed below, met on

September 20, 1990, to review the collection of performance observations

and data and to assess the licensee's performance at the Salem Generating

Station.

This assessment was conducted in accordance with the guidance

in

NRC

Manual

Chapter

0516,

11Systematic

Assessment

of

Licensee

Performance.

11

This report is the NRC 1 s assessment of the licensee's safety performance

at the Salem Generating Station, Units 1 and 2 for the period May 1, 1989

through July 31, 1990.

The SALP Board for the Salem Generating Station assessment consisted of

the following individuals:

Chairman:

C. Hehl, Director, Division of Reactor Projects (DRP)

Members:

R. Blough, Chief Projects Branch 2, DRP

P. Swetland, Chief, Reactor Projects Section 2A, DRP

T. Johnson, Senior Resident Inspector, DRP

W. Butler, Director, Project Directorate I-2, Office of Nuclear Reactor

Regulation (NRR)

J. Stone, Project Manager, NRR

M. Knapp, Director, Division of Radiation Safety and Safeguards (DRSS)

J. Durr, Chief, Engineering Branch, Division of Reactor Safety (DRS)

Others in Attendance:

S. Pindale, Resident Inspector, DRP

S. Barr, Resident Inspector, DRP

A. Lopez, Reactor Engineer, DRS

C. Anderson, Chief, Plant Systems Section, DRS

D. Bessette, Acting Chief, Operational Programs Section, DRS

2

Others in Attendance (Continued)

J. Jang, Senior Radiation Specialist, DRSS

R. Nimitz, Senior Radiation Specialist, DRSS

J. Joyner, Division Project Manager, DRSS

C. Conklin, Senior Emergency Preparedness Specialist, DRSS

C. Amato, Emergency Preparedness Specialist, DRSS

R. Keimig, Chief, Safeguards Section, DRSS

R. Albert, Physical Security Inspector, DRSS

P. Ray, Operations Engineer, Performance Evaluation Branch, NRR

J. Caldwell, Regional Coordinator, Office of the Executive Director for

Operations

C. Woodard, Reactor Engineer, DRS

A. Almond, General Engineer, Director's Office, NRR

3

II.

SUMMARY OF RESULTS

II.A Overview

PSE&G was successful in improving performance in the functional areas of

plant operations and emergency preparedness during the assessment period.

Good management involvement, supervisory oversight, and individual per-

formance resulted in a reduced reactor trip and personnel error rate.

The

emergency preparedness functional area achieved a superior level of per-

formance.

An effective, performance based security program resulted in

maintaining a superior level of performance in the security/safeguards

functional area.

Very good performance by corporate engineering was noted, while mixed per-

formance of the onsite

system engineering group was observed.

As

a

result, the engineering and technical support functional area did not

a chi eve the high level of performance that was predicted in the last

assessment.

Although a large number of maintenance and surveillance activities were

successfully completed during this assessment period, there were signifi-

cant performance weaknesses noted.

These weaknesses included a

large

maintenance backlog, recurring missed surveillance tests, inservice test-

ing program deficiencies and poor material condition of the plants.

An

overall rating of Category 2 was assigned, however, the SALP Board gave

serious consideration to a lower rating.

The licerisee 1 s prior recognition

of the i dent i fi ed problems and the achievement of sma 11 but measurable

progress toward resolution of these weaknesses were critical factors in

the Board's determination.

However, as a plant ages the challenges of

maintaining equipment reliability and readiness increase.

The declining

trend in this area reflects the gravity of the Board's concern over per-

formance in this area and the need for marked progress in correcting the

identified weaknesses.

Some improvements in the safety assessment/quality verification functional

area were noted such as better supervisory involvement and oversight,

development of significant event response teams, and effective review by

the independent safety review groups.

Weaknesses were identified in the

effectiveness of licensee corrective action

programs.

In particular,

there was a lack of effective interim measures to address continuing pro-

cedural inadequacies and degrading material conditions notwithstanding the

long term significant remedial initiatives which were in process.

Although the licensee has achieved discernible improvement in some aspects

of each fun ct i ona l area, the overa 11 performance in maintenance and sur-

vei 11 ance, engineering/technical support, and safety assessment/quality

verification

has

not

improved.

Continued

management

attention

and

aggressive prosecution of remedial initiatives is needed to attain

a

uniform, high level of performance.

4

II.B Facility Performance Analysis Summary

Functional

Area

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency Preparedness

Security and Safeguards

Engineering/Technical

Support

Safety Assessment/

Quality Verification

Previous Assessment Period:

Present Assessment Period:

Rating, Trend

Rating, Trend

Last Period

This Period

3

2

2

2

2

2, Declining

2

1

1

1

2, Improving

2

2

2

January 1, 1988 thr~ugh April 30, 1989

May 1, 1989 through July 31, 1990

I I I.

III.A

III.A.I

5

PERFORMANCE ANALYSIS

Operations

Analysis

The previous SALP rated Salem operations as Category 3.

That assess-

ment identified weaknesses in the area of supervisory oversight of

routine day to day operations.

The number of plant trips and fre-

quency of personnel errors had increased.

Operations management did

not always provide adequate guidance to the operators for non-routine

evolutions, however, operator response to plant transients was very

good.

Procedure establishment, use and compliance required continued

station management attention.

Some root cause analyses and correc-

tive action determinations lacked aggressiveness and thoroughness,

especially in cases related to possible operator errors.

The licen-

see had instituted actions to improve performance in these areas with

mixed results.

The planning and work control processes were noted as

strengths as was the fire protection program.

During this assessment period, both reactors were generally oper~ted

in a conservative and safety conscious manner.

Examples of conserva-

tive licensee operations include extension of shutdowns for both

units to fully evaluate emergency core cooling system (ECCS)

con-

cerns, and the shutdown of one unit when a potential main steam iso-

lation valve (MSIV) fast closure concern was identified.

Operator

response to reactor trips and plant transients was good.

In several

instances prompt actions by operators prevented transients or reactor

trips due to feedwater problems, loss of circulators, and steam dump

system failures.

Specific exceptions include an operations initiated

loss of residual heat removal

(RHR)

event while shutdown due to

operator error and an inadequate procedure, poor initial Station

Operations Review Committee (SORC) response to an engineering iden-

tified single failure vulnerability associated with the low pressure

safety injection system, and non conservative interpretation and use

of Technical Specification 3.0.3.

The licensee has been successful in reducing the frequency of auto-

matic reactor trips.

During the current assessment there were a

total of 6 trips (4 at power and 2 while shutdown) for both units.

This compares to 16 trips last assessment.

During the assessment

period, Unit 1 did not experience a reactor trip for over 10 months

and Unit 2 for over one year.

One of the six reactor trips during

this assessment period was attributed to a personnel error by a

licensed operator.

An

effective licensee trip reduction program

included

11 scram-a-gram

11

information

notices,

warning

signs

for

reactor trip sensitive areas,

a new troubleshooting procedure and

independent verification of trip sensitive procedural steps.

6

PSE&G has committed resources to upgrade pl ant operation.

A second

operating engineer, a dedicated radwaste engineer, and an emergency

operating procedure coordinator were added to the operations staff.

In addition to the three senior reactor operators (SROs) required for

each shift, a number of replacement candidates were hired to pursue a

goal of five SROs for each shift crew.

Two additional SRO-licensed

individuals now supervise the work control group during regular main-

tenance

hours.

Operations -

maintenance interface for equipment

tagging is satisfactory.

There are a total of 45 licensed operators,

including 38 on-shift and seven in staff and training positions.

Plant operations were generally well

supported

by

the

Training

Department.

One exception was the response to the loss of RHR event,

where both the station and the training department were not aggress-

ive in obtaining training assistance following the potentially sig-

nificant plant event.

Simulator refresher training before each unit

restart continues to be given to the reactor operators (ROs) and SROs

immediately before taking their shift and is considered a strength.

The station instituted improved procedures to control the training

process,

and also established a master training matrix to track

individual qualifications and to facilitate the maintenance of train-

ing records.

Six of six SRO license candidates anq six of seven RO candidates

passed their initial license examinations.

The RO/SRO requalifica-

tion program was excel lent with seven of seven ROs and six of six

SROs tested passing an NRC administered requalification exam.

Direct

involvement of operations management personnel

has had a positive

effect on the requalification program success.

Licensed operators 1 plant awareness, safety perspective, and profess-

ional control room demeanor were consistently evident.

Shift turn-

overs were formal and included thorough briefings of the relief crew.

Control room access was controlled, and activities were limited to

those di re ct ly related to pl ant operations.

Good performance of

non-licensed equipment operators was noted during NRC observations

made on plant tours, and during licensee equipment testing and oper-

ation.

However, operator overtime was at times not properly control-

led in that proper management approval for exceeding administrative

guidelines was not obtained.

The licensee has increased the number

of licensed operators to reduce the amount of overtime and has

initiated corrective actions

to ensure

appropriate

approval

is

obtained.

Overal 1, there has been a reduction in the personnel error rate.

This is reflected in root causes for LERs

and licensee incident

reports.

This can be attributed to increased accountability of per-

sonnel, effective management oversight of activities, and implemen-

tation of worker performance standards.

7

Procedural

inadequacy continues to

be

a

leading root cause for

events, including the loss of RHR event during the Unit 1 refueling

outage.

A procedural

upgrade project (PUP)

continues to be

an

important initiative; however, program implementation has encountered

problems as discussed in Section III.G.

Operators effectively used Emergency Operating Procedures (EOPs) as

evidenced during simulator observations, and actual unit transients

and trips; as well as during the NRC EDP team inspection.

EOPs were

well written, usable by operators and well maintained.

However, a

concern was identified regarding excessive responsibilities placed

on the one RO who operates the controls while the other RO reads the

EOPs.

The licensee plans to resolve this issue by modifying RO/SRO

command and control responsibilities.

Weaknesses were also noted

with respect to abnormal operating procedures (AOPs) and some alarm

response procedures.

The lack of a good procedure verification pro-

gram resulted in AOPs con ta i ni ng many 1 ongstandi ng errors including

labeling problems and missing information.

Consequently, successful

performance of these procedures relies heavily upon operator know-

1 edge and experience.

Licensee

Operations

Department event

and

problem evaluation

and

response were usually prompt and comprehensive.

Improvements in root

cause analysis and self-assessment were noted.

Management attention

and the root cause training

program have been effective.

Also,

implementation of the Significant Event Response Team initiative has

been

effective

in

providing

timely,

independent,

detailed,

and

thorough root cause analyses.

However, there were isolated instances

where

i nterna 1 incident reports were not written when re qui red by

station procedures.

Examples include boric acid transfer pump fail-

ures

and

a

spurious

steam dump

system actuation,

which nearly

resulted in a reactor trip.

Also, early in the period, there were

several instances where the licensee failed to make timely 10 CFR

50.72 reports.

Improvements were noted later in the period.

Strong plant management oversight and attention to operations were

evident on a daily basis.

There was an operational perspective of

plant problems,

and work prioritization was well

understood

and

enhanced by daily meetings.

The licensee has been effective in

ensuring good interdepartmental communication and in resolving prob-

lems.

The senior nuclear shift supervisor has direct access to plant

management.

Pl ant housekeeping

has shown

some

improvement during the period.

Plant area decontamination activities have reduced the contaminated

floor space, particularly in the ECCS rooms.

Equipment operators can

make their rounds with only minimal contamination protective cloth-

ing.

Overall, however, material condition of* the plant was weak

(Section III.C).

Licensee initiatives in progress to improve the

degraded

conditions

were

not

sufficient

to

display significant

improvements.

II .A.2

III.A.3

8

The overall fire protection program was satisfactory.

Dedicated fire

protection personnel

performed well

and were knowledgeable, which

demonstrated an effective training program.

The fire brigade was

staffed by site protection personnel, which minimized the reliance on

operators to respond to emergencies.

Appropriate operator involve-

ment in emergencies was provided.

The preventive maintenance and

surveillances of fire protection

equipment were effective.

Fire

protection equipment upgrades included a new ambulance, incident com-

mand vehicle, and other items.

However, the fire protection program

experienced implementation problems at Sal em.

For example, a weak-

ness was identified in the apparent tolerance for and the lack of

timely resolution for a long term condition at Salem where some fire

doors did not always close securely.

This condition was due to

imbalances in the plant 1 s ventilation system.

Some interim compen-

satory measures were taken by the plant to monitor these doors during

the rounds of roving fire watches; however, doors that were not part

of the route for the watches often went unmonitored.

In response to

NRC concerns, a task group was formed to investigate the root cause

of this problem and to formulate corrective actions.

A second weak-

ness was related to improper control of combustible material

in

safety related areas.

The licensee was aggressive in addressing.and

correcting this concern.

In

summary,

improvement in management involvement and supervisory

oversight, in reduced reactor trip and personnel error rate, and in

root cause analysis initiatives were noted.

Emergency operating pro-

cedures are considered a strength; however, weaknesses were noted

relative to abnormal operating procedures.

Good operations manage-

ment and training department involvement has resulted in a successful

operator

requalification

program.

The

licensee

has

committed

resources to improving plant operations.

Performance Rating

Category:

2

Trend:

NA

Board Comments

None

III. B

III.B.1

9

Radiological Controls

Analysis

The previous SALP rated the functional area of radiological controls

as Category 2.

The NRC 1 s review during the last assessment period

identified that performance for inplant radiation protection activ-

ities had declined early in the period and that the licensee's cor-

rective actions and self-assessments were initially ineffective in

improving overal 1 performance.

NRC observations toward the end of

the

last assessment

period found that management attention

had

resulted in significant performance improvement.

The radiological

controls organization was

reorganized and a new ALARA group was

established during the last period.

The licensee's performance in

the areas of radwaste transportation, effluent monitoring and control

were adequate, and radiological confirmatory measurements was good.

During the current assessment period, direct NRC observations of Unit

2 refueling activities indicated that outage activities were well

planned and effectively controlled.

The licensee established and

implemented an effective outage radiological controls organization

which minimized the use of contractor personnel acting in supervisory

roles.

All major radiological work activities performed during the

outage (e.g., steam generator work activities) were directly super-

vised by a licensee radiological controls supervisor.

In addition,

the staffing levels to support outage and non-outage work activities,

including the training of personnel, were good and the new ALARA

organization continued to provide aggressive oversight of outage

radiological work activities.

During the Unit 2 outage, the licensee experienced operational prob-

lems with emergency ~ore cooling systems at Unit 1, necessitating a

concurrent mini-outage at Unit 1.

The licensee established a special

organization to review and plan the Unit 1 work activities in order

to prevent distraction of personnel supporting the Unit 2 outage.

This indicated a good level of management

involvement in outage

activities.

No degradation of radiological controls was identified.

The licensee also experienced an operational event at Unit 1 which

resulted in generation of High Radiation Areas in various portions

of the Auxiliary Building.

The event, which caused a high crud burst

during full-flow testing of emergency core cooling systems, was well

responded to by the licensee.

No unplanned exposures occurred and

the crud was quickly cleaned up.

Corrective actions were taken to

prevent recurrence.

However, the event did indicate test planning

process weaknesses that failed to predict and prevent occurrence of

the crud burst.

10

NRC observations during the current assessment period found that the

licensee 1 s oversight of radiological program activities has improved

relative to the last assessment period.

For example, an independent

radiological assessor was reporting findings to management during the

Unit 2 outage and QA was active in identifying concerns.

The 1icensee 1 s enforcement hi story during the assessment period has

generally been good.

However, there were two NRC i dent i fi ed prob-

1 ems.

One

involved lack of performance of an audit of radwaste

activities and one involved two examples of failure to adhere to

radiation

protection

procedures.

The

problems

were

properly

addressed by the licensee.

In addition, the licensee identified a

number of problems that included a worker leaving the site with a

contaminated shoe, identification of contaminated tools in a storage

area located outside the radiological controlled area (RCA), radio-

active material stored in offsite warehouses, and one individual who

exceeded administrative external exposure guidelines through per-

sonnel error in use of exposure control computers.

Review of the

NRC

and licensee identified problems indicated the

problems were attributable to inattention to detail by the *licensee

and

weaknesses

in

procedures.

The

radioactive and contaminated

material control problems did not result in any unplanned or unmon-

itored exposures of personnel

and thi; licensee 1 s response to the

events was timely, comprehensive, and effective.

Good support and

involvement in resolving the event by the corporate radiological con-

trols group were evident.

The licensee had not yet implemented all

long term corrective actions at the end of the assessment period for

the radioactive material control problems.

The problems with release, control and handling of radioactive mate-

rial outside formally defined RCAs

indicated the need to provide

enhanced procedures.

The 1 icensee has been attempting to improve

procedures, but this effort was progressing slowly.

The licensee has

initiated action to improve these efforts.

The licensee 1 s radiological occurrence program exhibited a number of

significant weaknesses which minimized the effectiveness of this pro-

gram for identifying, tracking, and resolving self identified radio-

logical problems.

NRC review found that root cause analysis of the

problems was weak, problems were not always categorized properly, and

corrective actions for problems were not always identified.

Examples

of this weakness included the contamination control problems.

11

With the exception of the previously mentioned administrative limit

problem, there were no

unplanned externa 1 who 1 e

body or i nterna 1

exposures resulting from work activities.

Access controls to HRAs

were effective and enhanced through the use of

11 ta 1 king si gns

11 which

automatically inform personnel of access control

requirements to

HRAs.

The licensee has installed digital signs at the entrance to

the RCA to inform workers of important information.

NRC observations

indicated improvement in industrial safety, but housekeeping con-

tinues to be in need of attention.

Observations of numerous candy

wrappings in the RCA continue to indicate lack of worker sensitivity

to the potential of ingestion of radioactive material.

The

licensee's controls for

steam generator work, a significant

radiological work activity, were commendable.

Of particular note was

the use of multiple, redundant monitoring methods to monitor and

control the exposure of personnel working on steam generators.

Performance in the ALARA area was very good and improved over pre-

vious assessment periods.

Exposure of station and contractor per-

sonnel

was closely tracked, monitored and reported by use of the

computerized radiation work permit and automated dosimetry acc;:ess

control system.

Potential emergent work was anticipated and planned

(e.g. possible extended work scope for steam generator inspection and

maintenance).

The licensee performed A LARA

reviews for work that

accounted for about 95% of the aggregate exposure sustained during

the outage.

A LARA goals were reasonable and effectively used to

monitor ongoing work but person hour estimating could be improved.

Overall performance in the ALARA area has been effective.

The licensee has an effective solid radwaste/transportation program.

The training provided to radiological controls personnel involved in

the radwaste program continues to make a positive contribution to the

effectiveness of the program.

NRC reviews of the radiological effluent monitoring and control pro-

gram indicated calibration of effluent and process monitors was per-

formed acceptably during the assessment period.

However, there were

about 32 Emergency Safety Feature ( ESF) actuations due to spurious

Radiation Monitoring Systems (RMS) signals.

The licensee had estab-

1 i shed short and 1 ong term projects to upgrade the RMS during the

previous assessment period.

The projects are on schedule with the

installation of a central process unit in 1990 and replacement of ESF

RMS in .1991.

III.B.2

III.8.3

12

NRC reviews performed during this assessment period indicated weak-

nesses in the licensee's maintenance of safety related ventilation

systems particularly charcoal filter systems.

For example, the NRC

identified that the licensee did not take measurements to verify the

relative humidity of the Auxiliary

Building

Ventilation

System.

Other systems,

such as the Control

Room ventilation systems, were

found to have failed inplace surveillance testing with no explanation

as to possible causes.

Also,

the licensee 1 s response to an

NRC

identified issue related to testing of the air cleaning systems,

including humidity measurements, identified early in the assessment

period remained open, ~ith the licensee not anticipating closeout of

the issue before the end of 1990.

An effective Radiological Environmental Monitoring Program (REMP) was

implemented.

Sampling and analytical procedures were upgraded and an

effective QC program was in place to assure the quality of sample

analysis.

One problem was identified in the area of an unmonitored

liquid radwaste release, but there was no impact on the public health

and safety or environment and the licensee took effective corrective

actions for the occurrence.

The meteorological monitoring system was

properly calibrated and maintained.

Audits of these areas performed

by the Quality Assurance Division were thorough and audit identified

deficiency items were adequately resolved in a timely manner by the

licensee.

In

summary,

the licensee implemented a good radiological controls

program with a good 1eve1 of management i nvo 1 vement in the program.

Efforts in organization, staffing, training and qualification have

improved performance.

The

licensee

1 s

ALARA activities were very

good.

Weaknesses exist in the radiological occurrence report program

and personne 1 attention to deta i 1 is in need of improvement.

A 1 so,

problems

with

radioactive material

control

indicated a

need to

improve procedural controls.

The radwaste handling, transportation,

and environmental monitoring programs were effective.

The licensee

has performed adequately in the area 6f liquid and gaseous effluent

controls.

Performance Rating

Category:

2

Trend:

NA

Board Comments

None

III. C

III.C.1

13

Maintenance and Surveillance

Analysis

The last SALP assessment rated the Maintenance and Surveillance func-

tional area a Category 2.

Identified strengths included the initia-

tive to develop work standards; maintenance planning, pre-staging and

oversight during refueling outages; and the assignment of additional

resources

to

prevent missed

surveillances.

Weaknesses

included

inconsistent use of procedures, insufficient documentation of trou-

bleshooting activities, failure to follow procedures and inattention

to detail resulting in severa 1 p 1 ant events, and multi p 1 e missed

surveillances.

Maintenance:

During this assessment period, the licensee implemented a satisfac-

tory maintenance program.

A large volume of maintenance activities

was

successfully implemented, however specific observations often

indicated several areas for continued improvement and management

attention.

The goals and objectives of the maintenance program were

we 11

defined.

There was a good l eve 1 of maintenance management

involvement and supervisory oversight in daily activities.

Some pro-

cedure content and usage deficiencies continued to exist during this

assessment period.

The licensee has stressed procedure compliance

and i dent i fi cation of procedure inadequacies.

Work in progress has

occasionally been stopped by workers and first line supervisors due

to procedure problems, indicating that licensee management's efforts

to identify procedure weaknesses have been communicated to the staff.

Early in the SALP period, work standards were issued to employees for

the purpose of improving work, procedural compliance and industrial

safety

practices.

Written

planning

standards were

subsequently

issued to enhance maintenance planning.

Although the work standards

improvement program is in its early stages, its development is con-

sidered to be a good licensee initiative.

The turnover rate experienced by the maintenance organization is low

and is indicative of a stable staff.

Maintenance workers are com-

petent, trained and qualified.

Qualification criteria are well-

defined and documented for both licensee and contractor workers.

The

training center continues to provide extensive electrical and mech-

anical training facilities.

When the existing modular training pro-

gram was initiated in 1987, many craft personnel were

11 grandfathered 11

with the intent of eventually being formally trained.

However,

reviews of training records did not support fulfillment of this plan.

Additionally, there was not an aggressive effort to satisfy yearly

training requirements for mechanical maintenance, apparently due to

increased work loads from unit outages.

Overall, however, the main-

tenance

staff

was

highly

knowledgeable

in

their

areas

of

responsibility.

14

Maintenance department staffing was

adequate to properly support

significant maintenance activities.

Staffing additions during this

SALP *period

included

supervisors,

planners

and craft personnel.

Also, each unit now has an outage manager.

However, the maintenance

backlog of overdue corrective and preventive maintenance was large.

Initiatives taken to increase productivity, improve scheduling, up-

grade work

planning,

and increase staffing were demonstrated to

increase maintenance productivity.

However, the monthly work order

production rate has increased proportionally to the increased pro-

ductivity.

The work order production increase was partly due to

recent

management

goals

to

improve

plant

materiel

condition

deficiencies and worker sensitivity in

identifying deficiencies.

The aging of any plant causes the challenge of material condition

maintenance to increase over time.

The number of deficient plant

material and area conditions such as steam and water leaks, equipment

corrosion, and service water pipe integrity was indicative of years

of insufficient attention to facility and equipment status.

Par-

ticular concerns included inadequate maintenance of the watertight

features of the service water valve galleries and the steam and water

leaks in the containment penetration rooms in both units.

Recent NRC

findings,

such as main

steam isolation valve detent problems and

material condition deficiencies that are not identified by the licen-

see staff indicate an apparent toler.an~e of equipment deficiencies.

The licensee has shown some recent improvement (e.g., Unit 2 service

water valve rooms) in this area and has assigned a special task force

to address material condition and equipment improvements.

Despite

the existence of these problems, the plants have been maintained and

operated in a safe manner.

Maintenance activities are at times impaired due to the control and

availability of spare parts.

The licensee had previously recognized

these parts problems and recently dedicated additional resources with

sole responsibility for material control to improve performance in

this area.

The spare parts problems represented a major contributor

to a large maintenance backlog.

The licensee is developing a reliability centered maintenance (RCM)

program.

Based on a licensee assessment that the existing number of

preventive maintenance (PM) activities is excessive, implementation

of the

RCM

program is expected to adjust the

PM

program

scope,

schedule and workload accordingly.

The licensee's self initi~ted RCM

program has been in progress for about three years.

Significant

increases in

RCM program resources have been provided by licensee

management in mi d-1989.

The program is planned to be performed in

two phases and is expected to cover about 30 systems.

The RCM pro-

gram is currently in its early stages of implementation.

15

Effective management involvement and oversight resulted in successful

comp 1 et ion of two unit refue 1 i ng outages and severa 1 forced outages

during the assessment period.

Core alterations, reactor vessel work,

and other refueling activities were well supported by operations.

Reactor coolant system midloop operations were wel 1 planned, pro-

cedur-al ized and implemented.

Periodic outage meetings were effec-

tive in communicating priority activities and problem areas to all

members of the dedicated outage team.

Maintenance procedure deficiencies continued during this assessment.

The station's expanded procedure upgrade project (PUP) was initiated

in mid-1989 to fully address procedural deficiencies. Only two main-

tenance procedures had been completely processed and issued at the

end of the assessment period.

The NRC identified examples where com-

p 1 ex maintenance activities were conducted without comp 1 ete, suf-

ficiently detailed and

approved procedures,

including emergency

diesel generator and main steam isolation valve mechanical latching

mechanism (detent) maintenance.

Two reactor trips were attributed to maintenance activities conducted

prior to this assessment period; one due to ineffective actions for a

previous event, and the other due to an inadequate maintenance pro-

cedure.

Ex amp 1 es of p 1 ant events caused by maintenance activities

during the current assessment period in~lude the failure of an emerg-

ency lighting inverter due to inadequate maintenance and an inadver-

tent safety injection signal, which occurred when a maintenance tech-

nician used a drawing for the opposite safety train while performing

maintenance work.

At times, the licensee did not effectively control and supervise con-

tractor maintenance.

Severa 1 findings were identified during this

assessment period relative to procedural noncompliance by contractors

and indicated the need for increased management attention.

Examples

include work on a feedwater regulating valve without proper work

authorization and the failure to implement administrative procedure

requirements

for temporary installations.

The

licensee recently

modified their contractor procedures including enhanced work standard

requirements and procedural familiarization.

Increased direct over-

sight by PSE&G personnel was provided. Toward the end of the assess-

ment period, improvements were noted re 1 at i ve to contractor contro 1.

However, continuing problems were noted.

16

Surveillance:

During this assessment period, surveillance testing was usually con-

ducted in a well controlled manner by knowledgeable personnel with

usually appropriate supervision.

A large number of surveillance

testing activities were

successfully completed.

The surveillance

program administrative procedure was modified to clarify personnel

responsibilities, to assign indivi~ual surveillance coordinators, and

to formally assign a Technical Specification (TS) Administrator to

coordinate related station activities.

Surveillance test procedures

continued to contain human factors and technical deficiencies.

Weak-

nesses were identified in the administration of the Inservice Testing

Program.

There were seven missed surveillances this period, predominantly due

to past inadequate administrative controls related to TS amendment

issuance.

This compares with 12 missed surveillances during the last

assessment period.

Missed surveillances have been a long-standing

problem at Salem for which numerous TS

surveillance reviews and

audits have been performed, including a computer data base review and

a limited review of recent

TS

amendments.

Technical

procec;iure

reviews to identify additional missed TS requirements have not yet

been completed.

The continued missed TS survei 11 ances due to past

inadequate administrative controls indicate that the previous licen-

see actions taken to identify the problems have been too narrowly

focused and ineffective.

Licensee management recently directed a

more comprehensive review of TS surveillance requirements against

existing surveillance procedures to resolve this issue.

Several surveillance procedures contained deficiencies, some of which

resulted in plant events.

Human factors deficiencies contributed to

the May 20, 1989 loss of residual heat removal (RHR) event and emerg-

ency core cooling systems flow calculation errors.

The licensee is

addressing these types of procedural inadequacies in their ongoing

PUP efforts.

In an effort to reduce plant trips, early in the assessment period

the licensee instituted an independent peer review of critical steps

for reactor protection system and ESF testing.

This action appeared

to have been effective in preventing trips during surveillance test-

ing; no reactor trips occurred during surveillance testing.

However,

three engineered safety feature (ESF) actuations occurred during sur-

veillance testing.

Two were due to inadequate procedures and one was

due to personnel error.

III.C.2

III.C.3

III.D

III.D.1

17

There are indications that the Inservice Testing (IST) program was

not effectively. administered.

Pump vibration testing was not repeat-

able due to a combination of unmarked vibration reading points and

unclear component drawings in test procedures, and weaknesses were

evident relative to evaluation of questionable and unsatisfactory

test results (e.g. auxiliary feedwater and

boric acid transfer

pumps).

Weaknesses were also identified concerning trending of sur-

veillance test data.

In summary, the maintenance organization implemented a satisfactory

program.

Work standards, management involvement, and the RCM initia-

tive were licensee strengths.

Maintenance weaknesses include the

large maintenance backlog, the quality of some procedures, control of

contractor maintenance, and control and availability of spare parts.

A poor overall material condition of the plant was a significant

weakness sourced in a prolonged period of insufficient attention to

maintaining the plant.

Licensee efforts to improve this area have

been

slow;

meanwhile,

the challenge to

the maintenance

program

increases with plant age.

A large number of surveillance testing

activities were conducted in a well controlled fashion by knowledge-

able and experienced personnel.

Some surveillance test procedl)res

continue to contain deficiencies.

Although no reactor trips were

caused by

personnel errors, such errors resulted in other pl ant

events. Weaknesses were identified in the administration of the IST

program.

Missed surveillances continued to be identified due to

ineffective previous actions.

Performance Rating

Category:

2

Trend:

Declining

Board Comments

Although the overall assessment was that a Category 2 rating was

appropriate,

several

weak

areas

continue to exist without

significantly

effective

measures

to

improve

performance.

Increased management attention is warranted.

Emergency Preparedness

Analysis

The Emergency Plan for Artificial Island covers both Hope Creek and

Salem Nuclear Generating Stations, therefore the assessment of emerg-

ency preparedness is a combined evaluation of both facilities' emerg-

ency response capabilities.

18

During the previous SALP period, this area was rated Category 2.

This rating was based on weaknesses identified during a Salem based

full-participation exercise, some actual event classification prob-

lems, and delays in ensuring that the Salem Technical Support Center

could meet NRC design requirements.

Strengths noted included a high

level of management involvement in emergency preparedness activities,

responsiveness to NRC concerns, and an overa 11 effective emergency

preparedness training program.

Management involvement in emergency preparedness was effective and

extensive.

Executives and plant managers maintain emergency response

organization position qualification, review and approve plan and pro-

cedure changes, participate in drills and exercises, resolve audit

noncompliance issues, exercise oversight functions, and interface

with Delaware and New Jersey State and County government personnel .

Management oversight includes a review of call-in test results and

emergency preparedness training rescheduling.

The licensee successfully completed a partial-participation emergency

preparedness exercise conducted at the Salem facility during this

assessment period.

PSE&G 1 s emergency response actions were

succc~ss

ful in providing for the health and safety of the public.

Overall,

licensee performance was excellent and noted to be improved since the

last period.

Resolution of technical issues continues to be very good and demon-

strates a commitment to quality.

For example, as a result of an NRC

concern, the licensee completed a review of default iodine to noble

gas ratios as a function of release pathway, and determined the

values were consistent with accident data and emergency off-gas sys-

tem design and specifications. A four hour, default release duration

time has been developed and accepted by the States.

User friendly

personal computer software has been developed for the back-up dose

assessment program.

Relating to deficiencies in the previous assess-

ment, the Technical Support Center ventilation system has been up-

graded to meet NRC design requirements.

Innovative program activ-

ities in-progress include development of site Emergency Action Levels

(EALs) for natural phenomena and security events to replace individ-

ual station EALs, a single Event Classification Guide for all three

units, and a simplified EAL des-cription for use in the initial con-

tact message sent to the States.

Another example of resolving iden-

tified concerns was apparent in review of the licensee 1 s corrective

actions following loss of the NRC Emergency Notification System (ENS)

when it was accidentally disconnected from an uni nterruptab le power

supply (UPS) in May 1990.

The licensee

1 s communications staff ras

aggressively pursued

upgrading

the

Salem

Telephone

Switch

Room

(location of the ENS UPS connection).

19

The licensee successfully used the Hope Creek and Salem simulators to

enhance training effectiveness during emergency drills.

To enhance

the training effectiveness of these facilities, emergency communica-

tion systems duplicating those in the control rooms were installed in

each simulator.

Staffing in

the emergency preparedness area is

stable with a well-qualified staff available to maintain an effective

emergency preparedness program.

Personnel with

operations back-

grounds are on staff who develop demanding operations based scenarios

for drills and exercises.

Management's attention to quality was effective as demonstrated by

the following items.

Effective licensee audits and reviews for each

unit were completed by independent audit groups.

Among other things,

drills were observed and the

State/County/li~ensee interface was

determined to be adequate.

There were no significant findings and

the licensee/off-site interface was proactive.

Emergency Department

personnel with 1 icensee executives and managers attended almost 100

meetings with State and County personnel.

The public alerting system

is tested daily, and is well maintained with availability at 99.5%, a

va 1 ue which exceeds Federa 1 Emergency Management Agency standards.

Independent and redundant siren activating systems are installed.and

maintained in each State.

The licensee has an effective emergency preparedness training pro-

gram.

Responsibility for emergency preparedness training has been

assigned to the Emergency Preparedness Department.

Two qualified

emergency

preparedness trainers have

been

transferred

from

the

Nuclear Training Center to the Emergency Preparedness Department to

support this effort.

Weekly, on-the-job, mini training drills for

each site have resumed and nine day-long drills are also scheduled.

Over

1,000

licensee personnel

have

been

trained for

Emergency

Response Organization (ERO) positions. There are at least three per-

sonnel qualified for each key

ERO decision-making and management

position.

A dedicated emergency preparedness training facility has

been placed in service.

Engineers assigned to the Technical Support

Center and the Emergency Operations Facility are given an overview of

Emergency Plan Implementing Procedures and Core Damage Assessment

Procedures.

The effectiveness of the training program was also demonstrated by

response to twelve actual conditions requiring classification, and

the strong exercise performance.

This re so 1 ves the previous SALP

concern regarding event classification.

Observations of training

drills indicated active involvement from licensed senior reactor

operators dedicated to drill scenario development.

Operations Sup-

port Center and Technical Support Center personnel were observed to

implement effective problem identification and resolution.

III.0.2

III.D.3

III. E

III.E.l

20

In summary, the licensee maintains a strong and effective emergency

preparedness

program.

Management

remains

involved with a demon-

strated

commitment

to

quality.

Technical

issues

are

generally

promptly resolved and appropriate response is given to NRC in it i a-

t i ves.

The Emergency Preparedness Program staff is stable and well

qualified

to

maintain

an

effective

program.

Training

is well

developed and is effective as demonstrated by exercise performance

and response to actual conditions requiring classification.

A good

working relationship is maintained with the States and Counties with

regular meetings, and frequent drills.

Performance Rating

Category:

1

Trend:

NA

Board Comments

None

Security and Safeguards

Analysis

The Security Plan for Artificial Island covers both Hope Creek and

Salem Generating Stations, therefore the assessment of* security and

safeguards is a combined evaluation.

During the previous assessment period, the licensee's performance was

rated as Category 1.

Noted were an exce 11 ent enforcement hi story,

the continued implementation of an effective and performance-based

program, kn owl edgeab le and experienced security supervisory person-

nel ,

and management

1 s

involvement in and support for the program.

During this assessment period, the licensee continued to implement a

high quality and very effective program, and management* s attention

to and involvement in the program remained evident.

The site secur-

ity supervisor and his staff are well-trained and qualified profess-

ionals who have been vested with the necessary authority to ensure

that the security program is carried out effectively and in compli-

ance with NRC regulations.

The site security manager and hjs staff

continued to actively participate in the Region I Nuclear Security

Association and other groups engaged in nuclear plant security mat-

ters.

They also maintained excellent rapport and effective communi-

cation channels with the plant staff who exhibit respect and a good

attitude toward the program.

21

Staffing of the contract security force was consistent with program

needs.

Early in this assessment period, the security force attrition

.rate was high (24 percent).

Licensee and contractor efforts through

personal incentives were successful in reducing this rate to 9 per-

cent by the end of this period.

The

licensee

continued to demonstrate responsiveness to

several

potential weaknesses during the period.

These weaknesses primarily

i~volved system and

equipment aging.

As

a result, the licensee

promptly initiated a comprehensive evaluation of all

systems and

equipment and developed appropriate plans and a timely schedule for

upgrading and/or replacing the affected equipment.

In addition, the

licensee

implemented

a

well

managed fitness-for-duty program in

response to new NRC requirements during the per.iod.

The licensee's

policy has been clearly stated and widely disseminated among both

employees and contractors.

It was found to be aggressively imple-

mented

by

knowledgeable

personnel,

and processing facilities and

procedures were excellent.

These efforts represented a proactive

management approach that continually seeks to improve the effective-

ness of the entire security program.

The

security force training and requalification program is well-

developed and administered by an experienced staff of two full-time

and five part-time instructors, and a. supervisor.

Facilities are

provided on-site for training and requalifications and were well-

equipped

and well-maintained.

During this

period,

the

licensee

established additional oversight of the contractor's training and

requalification program by providing a full-time licensee representa-

tive to administer the program.

The licensee's event report procedures were found to be clear and

consistent with the NRC 1 s reporting requirements.

Only one report-

able safeguards event was submitted to the NRC during the assessment

period.

This report involved the loss of power to the security sys-

tem and was properly compensated for by the security force.

The

licensee's report was clear and concise, and indicated an appropriate

response to the event.

During the assessment period, the licensee submitted three revisions

to the security program plans under

the

prov1s1ons

of

10

CFR

50.54(p).

These revisions were of high quality and technically

sound, and reflected well-developed policies and procedurE;!s.

The

licensee

also

updated

all

Physical

Security

Plan

implementing

procedures.

III.E.2

III.E.3

III. F

III.F.1

22

In summary, the licensee continued to maintain a very effective and

performance-based security program that exceeds regulatory require-

ments.

The licensee's ongoing program to identify and correct poten-

tial weaknesses in systems and equipment during this period are com-

mendable and demonstrated the licensee's commitment to maintain an

effective and high quality program.

Performance Rating

Category:

1

Trend:

NA

Board Comments

None

Engineering/Technical Support

Analysis

The previous SALP rated Engineering and Technical Support as Category

2, improving.

The

previous assessment noted significant changes

within the corporate engineering department established to improve

engineering's interaction with the station staff.

Improvements were

noted in corporate/station engineering communications.

System engi-

neering was a strength.

Weaknesses included implementation problems

associated

with

station

modifications

and

inadequate

safety

evaluations.

During this SALP period, evidence of good performance was noted in

E&PB.

The Project Matrix Organization and the new design change con-

trol process worked well.

The other changes appeared to function

properly.

Communications between E&PB and the plants also improved

through daily morning, regular weekly and monthly meetings.

Several

new concerns were identified regarding the consistency of the quality

of work performed by the systems engineers and instances of inappro-

priate implementation of the temporary modification program.

The design change process is effective in plant modification imple-

mentation.

Design change process procedures were observed to be

clear and

detailed.

The

procedures adequately addressed design

interface, design process and corrective action process requirements

with appropriate levels of review and verification specified. Satis-

factory performance and documentation of cross discipline reviews

were noted.

Calculations contained in modification packages were

technically correct and

performed

in accordance

with applicable

23

procedures.

A new workbook

p~ocedure has been developed to improve

the existing design change package process and to improve configura-

tion management contra l.

The workbook was sufficiently detailed to

control the design process and post-modification testing.

The draw-

ings affected by modifications were mostly accurate and appropriately

reviewed and approved.

In addition, a new prioritization program is

under development to improve workload prioritization and resource

allocation.

The

E&PB organization works well with onsite system

engineering.

This* was evidenced during the followup of the Emergency

Core Cooling System (ECCS) flow problems.

The on site system engineering group supports operational, mainten-

ance, testing and design change activities.

Inconsistencies were

observed in the quality of work performed by the systems engineers.

For example, system engineer troubleshooting and corrective action

plans for radiation monitoring system deficiencies, main power trans-

former problems, main steam line isolation valve (MSIV) modification

errors, reactor coolant system check valve leakage, and feedwater

system and regulating valve timing problems were thorough and compre-

hensive.

However, system engineer followup of boric acid pump low

flow

problems,

initial

MSIV

drifting

indications,

and

initial

analysis of the RHR overpressurization event were poor. System engi-

neers are used as station qualified reviewers (SQRs).

The SQR pro-

cess, at times, was noted as a weaknes~. Examples include:

proced-

ure changes involving safety significant issues being processed by

the SQR; not maintaining the required SQR independence; and, not

implementing SQR training that was committed.

There have been several examples of inappropriate implementation of

the temporary modification program.

Some installed temporary changes

should have been processed as permanent modifications, some temporary

modifications were found to have been in place for excessive time

periods, and a required periodic review of temporary modifications by

the Station Operations Review Committee was missed.

A new control

procedure for temporary modifications (T-MOD) had been developed and

approved for use at Salem.

The training for the use of this new pro-

cedure was just completed at the end of the SALP period and the con-

trol of T-MODs at Salem is in a transition period for using the new

procedure.

The purpose of the new procedure is to provide clearer

guidance than the old one.

Engineering problem evaluations are generally adequate.

However, the

licensee 1 s response to discrepant system flow measurement devices was

initially too narrowly focused.

10 CFR Part 21 reviews and notifica-

tions are appropriately executed.

..

24

Technical support for refueling and maintenance outage periods and

for post outage recovery activities was noted as being effective.

Both E&PB and onsite system engineering participated in and inter-

faced with the outage organization on a daily basis.

Reactor engi-

neering was noted as providing strong support during fuel movement

activities, and during reactor startup and power ascension testing.

The licensee established project task forces led by E&PB managers to

address specific technical issues and problem areas.

These included

ECCS pump and flow problems and MSIV circuitry design.

These task

forces effectively integrated offsite, onsite and contractor engi-

neering groups.

The licensee 1 s site and corporate management were

actively involved in the resolution of these technical issues.

The technical justification for amendment requests was mostly satis-

factory and exhibited good responsiveness to NRC issues and concerns.

However, the technical justification that accompanied requests for

emergency changes to the Technical Specifications was not of the same

quality.

Examples included main steam isolation valve timing and

charging pump excess fl ow submittal s.

These changes required the

licensee to augment its application with significant amounts of addi-

tional information.

The technical information included in licensee

responses to NRC

Bulletins, Generic

Letters,

and other licensee

requests was generally timely and adequate with sufficient detail to

allow a determination concerning the acceptability of the licensee 1 s

action.

One exception was the response to Bulletin 88-04, Potential

Safety Related Pump Loss.

In that response the licensee did not

recognize that the existing system alignment made the Salem Unit 1

RHR

pumps

potentially susceptible to the

strong

pump/weak

pump

interaction.

The

licensee has maintained adequate control

over the inservice

inspection (ISI) Program, and has completed required inspections and

examinations for the first interval without undue recourse to exten-

sion and deferral requests.

The licensee has performed inspections

in excess of the technical specification requirements in all steam

generators to determine the operating condition of the generators,

and to assure safety and reliability of the NSSS

system.

Also,

recognizing the importance of the

11ALARA

11 concept, the licensee pro-

vided adequate training, controls, and maximum effective automation

for these inspections and examinations.

Forty-eight of 87 licensee event reports (LERs) were attributable to

this functional area.

The majority of these were due to radiation

monitoring system initiated actuations caused by design flaws.

PSE&G

is adequately addressing this area.

There were other LERs that were

identified by the licensee during their Configuration Baseline Docu-

mentation

(CBD)

project.

This design basis *reconstitution is a

III.F.2

III.F.3

III.G

III.G.1

25

positive licensee initiative (Section III.G).

Two of the six auto-

matic reactor trips during the period were attributed to the engi-

neering/technical support area.

The causes of these trips were a

personnel error leading to an unauthorized modification, and untimely

corrective actions for a previously identified inadequate modifica-

tion design.

In

summary,

the corporate engineering (E&PB)

performance, design

change control; communications between E&PB and the plants have been

very good.

Inconsistencies were observed in the quality of work per-

formed by the systems engineers.

There have been several examples

of misuse of the temporary modi fi cation program.

The requests for

license amendments were adequately supported with the exception being

those requests made under emergency circumstances.

Other licensee

submittals and responses to generic correspondence have been timely

and provided the requested information.

These exhibited adequate

management

support,

attention

to

detail

and

interdepartmental

communications.

Performance Rating

Category:

2

Trend:

NA

Board Comments

None

Safety Assessment/Quality Verification

Analysis

This area assesses the effectiveness of the licensee's programs pro-

vided to assure the safety and quality of plant operations and activ-

ities.

During the previous period the licensee was evaluated as

Category 2 in this functional area.

The last assessment noted that

licensee management generally displayed an adequate safety perspec-

tive, however, continued management attention to assure consistency

in the quality and timeliness in licensee submittals was needed.

To

correct a licensee recognized need for improved quality performance

and personnel accountability, enhanced management communication and

corrective action programs had been developed.

Implementation of

these programs had begun, but completion of the programs and con-

tinued management oversight was necessary.

26

At the beginning of this assessment period, a number of new programs

were instituted by the licensee to correct the noted concerns.

Cor-

porate and station management continue to be involved in the conduct

of operations and in the resolution of unplanned occurrences.

Sta-

tion management is directly involved in the daily oversight of unit

operations.

Corporate management was observed onsite and in the

plant during normal and off-normal working hours.

Senior Nuclear

Shift Supervisors were held accountable for unit operations and had

direct access to station management.

Daily meetings were held to

provide an operational perspective to unit problems and for work

prioritization.

First and

second line supervisors were directly

involved in field activities.

Worker performance during the period

was adequate.

Other than for routine material condition problems, (see Section

III.C.), the licensee had a generally effective program for problem

identification.

Plant deficiencies and events were documented using

incident reports.

These reports were discussed at shift turnover and

at the daily morning status and management meetings.

There were

several instances of late or poor 10 CFR 50.72 and 50.73 reports.

Examples include engineering safeguards feature actuations caused by

radiation monitoring systems and a residual heat removal (RHR) over-

pressurization

event.

Root

cause

determination

and

corrective

actions were generally adequate.

The ltcensee has implemented a root

cause training program.

There were several instances where initial

corrective actions were either incomplete or ineffective.

Examples

include

emergency

core

cooling

system

(ECCS)

pump

surveillance

deficiencies, overdue biennial procedure reviews, and late station

qualified reviewer training.

At the beginning of the period, management promulgated worker stand-

ards and provided training which has improved worker performance and

procedure compliance.

PSE&G has been successful in

reducing the

number of personnel errors and reactor trips.

An effective trip

reduction program included

11 scram-a-gram

11 notices, reactor trip warn-

ing signs on sensitive equipment, and independent verification of

trip sensitive surveillance procedures.

Two

reactor trips (both

while shutdown) were caused by personnel errors.

One was caused by

an operations error during atmospheric steam dump operation and the

other by an engineering and technical support error resulting from a

1987 plant modification.

Management

has been aggressive in disseminating and instilling a

safety conscious attitude among station personnel.

There have been

effective results as evidenced by the following conservative opera-

tions:

a voluntary unit shutdown because of main steam isolation

valve (MSIV) operability concerns; extending shutdowns for both units

to resolve ECCS concerns; successful reactor coolant system midloop

operation with detailed procedures and training; and voluntary unit

..

27

power reductions to avoid transients.

However, at times management

appeared to tolerate deficient conditions.

Examples of this toler-

ance include MSIVs drifting off their open latch; open fire doors;

and continuing degraded material condition of both

uni ts.

Al so,

worker overtime was, at times, not properly controlled by station

management.

Station Operations Review Committee (SORC) review of reactor trips,

design changes, significant technical issues, and reportable events

were usually thorough

and timely.

However,

there

were

several

occasions where SORC reviews were weak, such as (1) the failure to

identify an

RHR

system single failure vulnerability, (2) an

MSIV

closure circuit failure to "seal in", with a subsequent modification

providing an uncontrolled steam generator vent path to the environ-

ment, and (3) a non-conservative interpretation of Technical Specifi-

cation 3.0.3.

At Salem, personnel designated as Station Qualified Reviewers (SQRs)

are used to decide whether a safety evaluation and subsequent SORC

review is necessary.

Because of incomplete screening criteria and a

misunderstanding on the part of SQRs and station management,

?Orne

issues that should have been reviewed by SORC were not.

Included

were both procedure changes and facility changes.

This was a pro-

grammatic control

problem, but no safety issues were identified.

Licensee safety evaluations, when completed, were found to be of high

quality.

The Quality Assurance (QA) Department, the Onsite Safety Review Group

(SRG) and the Offsite Safety Review Group provided effective, inde-

pendent

review

of

plant

activities.

The

QA

organization

has

developed and used performance based surveillance of station activ-

ities.

QA

involvement

in

radwaste

processing

is

considered

a

strength.

Post trip reviews and other investigations by the SRG were

effective in determining root cause and providing good corrective

action recommendations.

In addition, PSE&G has instituted an event

review process entitled "Significant Event Response Team" (SERT).

A

SERT is initiated by the station general manager and is a real time,

independent review of any

unplanned reactor trips or other major

station event.

The

SERTs effectively developed the

sequence of

events, determined root cause(s) and recommended corrective actions.

In one instance, shortcomings associated with a SERT evaluation were

identified by PSE&G management and corrected.

The Human Performance

Evaluation System, a detailed analysis method for determining root

cause of incidents involving personnel error is also utilized by the

licensee.

28

Direct inspection of station activities through inspection hold

points by Quality Control (QC) has been significantly reduced over

the past several years.

Additionally, the administrative processes

to identify, document, and resolve adverse conditions were at times

not aggressively applied.

Examples include the reassembly of a main

steam drain valve with an unacceptable seating surface, and the fail-

ure to install the required washer kit and properly tighten flange

fasteners on service water system repairs.

Management attention in

this area is needed for assurance that those conditions are properly

evaluated.

PSE&G has revised their guidance for QC inspection and

hold points, and increased QA surveillance of maintenance activities.

The overall design process was well controlled and contained appro-

priate checks and balances.

There was an emphasis on nuclear safety

as evidenced by discussions with personnel related to upgrading of

procedures and implementation of new initiatives, such as the Con-

figuration

Baseline Documentation project, which is intended to

reconstitute the design basis for many of the major plant systems.

Inadequate station procedures continue to be a contributing root

cause for both reportable and non-reportable events.

PSE&G initiated

a procedure upgrade project (PUP) last assessment period and provided

additional resources this period.

The PUP was an important initia-

tive; however, the program has encount.ered implementation problems.

These included program scope changes, a variable resource allocation,

and re-definitions of an end product.

Also, the required biennial

reviews of existing procedures were not completed in a timely manner.

These

items

have

resulted in significant setbacks in

upgrading

station procedures.

Licensee

performance

in

routine

licensing

activities,

in

most

instances, has been adequate.

Requests for additional information

were necessary in over half the cases.

PSE&G is usually very respon-

sive to the requests for information.

Non-routine licensing activity

(i.e.,

emergency

requests,

exigent requests)

in

most

instances

required significant followup by the staff with PSE&G to obtain the

requisite additional information.

PSE&G

was

responsive to these

requests and provided the requested information in a timely manner.

PSE&G 1 s response to generic NRC correspondence (Bulletins, Generic

Letters) was generally timely and with sufficient information that a

judgement concerning the suitabi 1 ity of the position taken. by them

could be made.

In one instance PSE&G failed to recognize a possible

strong pump/weak pump interaction in the RHR system.

(See Section

III.F.)

PSE&G has shown inconsistent performance in resolving the

open TMI Action Plan items.

For example, PSE&G was responsive in

adding the upgrade to the subcooling margin monitor to the Unit 2

refueling outage work list at a late date.

However, the post acci-

dent sampling system was to be upgraded by the end of March 1990.

While it was in a licensee tracking system it had not been properly

flagged and the due date was missed.

III.G.2

III.G.3

29

In summary, corporate and station management involvement in station

activities have improved.

Management continued to be involved in

problem resolution and the assurance of nuclear safety.

Initiatives

taken by management such as the SERT formation and their efforts in

instilling a safety conscious attitude among station personnel are

particularly noteworthy.

The two safety review groups, Onsite and

Offsite, have provided effective, independent review of plant activ-

ities.

SORC reviews, in some cases, have failed to identify safety

issues that required additional consideration.

The use of SQRs, in

some cases, have raised the threshold for SORC

review beyond the

expected threshold.

QC

involvement in station activities has not

been sufficient to assure that adequate independent review is being

maintained.

The material condition of the plants is poor and needs

management attention.

Inadequate procedures ar~ a frequent contrib-

utor to plant events and the implementation of the PUP was delayed.

Effective and timely implementation of the PUP is important to the

continued safe operation of the Salem units.

Closer attention should

be paid to the details provided in responses to generic correspond-

ence and to other licensing submittals.

Performance Rating

Category:

2

Trend:

NA

Board Comments

Licensee initiatives such as the PUP

and materiel condition

improvement

program

require

increased

and

more

aggressive

management attention to ensure completion.

IV.

SUPPORTING DATA AND SUMMARY

IV.A LICENSEE ACTIVITIES

BACKGROUND

The assessment period began May 1, 1989, with Unit 1 in its eight refuel-

ing outage and the Unit 2 reactor operating at full power.

Unit

1 was restarted and placed on-line on July 18, 1989.

Automatic reactor trips

occurred

at

Unit

1

on

June 9, 1989,

June 19, 1989,

April 3, 1990 and April 9, 1990.

These trips and other unit unplanned

shutdowns occurring during the assessment period are further detailed in

Section III.C.

Extended forced outages occurred April 11 -

June 7, 1990

(emergency core cooling system deficiencies) and July 22 - July 31, 1990

(main steam isolation valve concerns).

The unit remained shutdown at the

end of the assessment period.

  • -

30

A manual reactor trip was initiated at Unit 2 on June 10, 1989 and an

automatic reactor trip occurred on June 28, 1990.

These trips and other

Unit 2 unplanned shutdowns are further detailed in Section III.C.

On

March 31, 1990, the unit shutdown for its fifth refueling outage.

The

Unit restarted on June 24, 1990.

Extended forced outages occurred on

October 13 -

November 5, 1989 (main power transformer rep 1 acement) and

June 30 -

July 31, 1990 (main steam isolation valve concerns).

The Unit

remained shutdown at the end of the assessment period.

IV.B NRC Inspection and Review Activities

Two resident inspectors were assigned to the site throughout the assess-

ment period.

Regional inspectors performed routine inspections throughout

the period, with added inspection emphasis during the scheduled refueling

outages.

In

addition to the routine inspections,

the following

NRC

special and team inspections were conducted as follows:

May 22 through 26, 1989; Unit 1 Special Inspection to review the loss

of the residua 1 heat remova 1 system event that occurred during sur-

vei 11 ance testing.

May 27 through July 10, 1989; Special Inspection to review inadequate

response time testing of main and bypass feedwater regulating control

valves.

November 17 through 29, 1989; Special Inspection to review the iden-

tification of a single failure vulnerability in the emergency core

cooling system.

November 29 through December 1, 1989; Unit 1 Special Inspection to

review circumstances surrounding an entry into Technical Specifica-

tion 3.0.3 during a turbine volumetric flow test.

-

January 10

through 25, 1990;

Emergency Operating Procedures Team

Inspection.

March 12 through 15, 1990; Team Inspection of the Artificial Island

Fitness-for-Duty Program.

Apri 1 9 through 13 and Apri 1 23 through 27, 1990; Maintenance Team

Inspection.

31

April 11 through 18, 1990; Special Inspection to review circumstances

surrounding the m.iscalculation of safety injection pumps' flow rates

in the associated flow balance verification surveillance procedure.

~ay 14

through

25, 1990;

Integrated Performance Assessment

Team

Inspection.

IV.C Significant Licensee Meetings

An

Enforcement Conference was

held on July 26, 1989

in the NRC

Region I office to discuss potential violations associated with the

inoperability of the feedwater isolation system at both Salem units.

A

Severity

Level

IV

violation

was

subsequently

issued

on

August 9, 1989.

An Enforcement Conference was held on December 11, 1989 in the NRC

Region I office to discuss potential violations associated with the

i dent ifi cation of a sing 1 e failure vulnerability in the emergency

core cooling system and related licensee activities.

Circumstances

surrounding entries into Technical

Specification 3.0.3 were also

discussed at the meeting.

Three Severity Level

IV violations were

subsequently issued on January 8, 1990.

A Management

Meeting

was

held on

F~bruary 26, 1990

in the

NRC

Region I office to conduct a mid-SALP cycle review and evaluation of

licensee performance.

An

Enforcement Conference was

held on

May 18, 1990 in the

NRC

Region I office to discuss the circumstances related to the identi-

fication of miscalculations of emergency core cooling system flow-

rates during surveillance testing.

One Severity Level

IV violation

was subsequently issued on June 8, 1990.

IV.D Reactor Trips and Unplanned Shutdowns

Unit 1

Event Description

Date

Power

Root Cause

Functional Area

1.

An automatic safety injection/reactor trip occurred while in Mode 3 (Hot

Standby) due to a high steam line differential pressure condition. created

by internal steam line pressure oscillations.

A 1987 modification was

determined to have been implemented which installed an unidentified valve

(closed) in the common steam line drain header, which prevented draining

saturated water that had accumulated in the steam lines.

Neither the

comp uteri zed tagging system nor the associated system drawings reflected

the valve addition.

6/9/89

Shutdown

Personnel error

Engineering/Technical

Support

\\j_

32

Unit 1 (Continued)

Event Description

Date

Power

Root Cause

Functional Area

2.

An unplanned shutdown occurred due to an inoperable safeguards equipment

control (SEC) train lA.

The SEC failed the surveillance test and was

declared inoperable.

Licensee troubleshooting replaced some components.

Further testing proved operability.

6/18/89

20%

Component failure

Not Applicable

3.

The reactor tripped automatically on low-low steam generator water level

due to main steam isolation valve (MSIV) closure during a post-maintenance

surveillance test of MSIV bypass valves.

A design deficiency was identi-

fied in the MSIV continuity check circuitry, which al lowed voltage to

remain high for a sufficient time period and reset a latching relay, caus-

ing the MSIV inadvertent closure.

A Unit 2 reactor trip occurred from

full power due to the failure of the same relay approximately two months

earlier (previous SALP period). Subsequent to the reactor trip, an 8-day

unplanned shutdown commenced from Mode

3 on June 20, 1989 to repai.r a

leaking safety injection system check valve (No. SJ55).

6/19/89

45%

Untimely corrective

actions

Engineering/Technical

Support

4.

An unplanned shutdown was made due to the failure of the speed increaser

bearing on a safety injection charging pump.

The unit was cooled down

further to Mode 5 following the identification of a leaking safety injec-

tion system check valve (No. SJ56).

12/1/89

100%

Component failure

Not Applicable

5.

An unplanned shutdown was made due to an inoperable safeguards equipment

control (SEC) train lA.

The SEC actuated following testing and licensee

troubleshooting could not determine a specific cause.

The

licensee

declared the SEC

inoperable,

replaced the electrical chassis, tested

satisfactorily, and declared the SEC operable.

3/27/90

100%

Component failure

Not Applicable

6.

The reactor tripped automatically while in Mode 3 on low-low steam gener-

ator water level due to personnel error.

A licensed operator failed to

establish optimum operating conditions prior to transferring main steam

atmospheric dump control from one steam generator to another.

This was

aggravated due

to auxiliary feedwater flow indication abnormalities.

4/3/90

Shutdown

Personnel error, poor

supervisory oversight

Operations

f..

33

Unit 1 (Continued)

Event Description

Date

Power

Root Cause

Functional Area

7.

The reactor tripped automatically on low-low steam generator water level

due to the loss of one main feedwater pump.

The pump went to idle speed

due to the failure of the governor valve control linkage.

A pin bushing

in the linkage assembly was missing and an associated lock nut was found

installed backwards.

Subsequent to the reactor trip, an extended shutdown

commenced on April 11, 1990 due to emergency core cooling system fl ow

discrepancies.

4/9/90

90%

Inadequate procedure

Maintenance/Surveillance

8.

An unplanned shutdown was made to evaluate potential deficiencies asso-

ciated with the main steam isolation valves' ability to close under cer-

tain postulated conditions, and to resolve main

steam line isolation

circuitry deficiencies identified relative to the original circuit design.

7/22/90

100%

Event Description

Power

Date

Level

Inadequate design

Unit 2

Root Cause

Engineering/Technical

Support

Functional Area

1.

An

unplanned shutdown was made to resolve feedwater regulating -control

valve (FRV) response time testing inadequacies.

Inadequate surveillance

procedures prevented i dent i fi cation of design/performance problems with

the FRVs.

5/27/89

50%

Inadequate procedure

Maintenance/Surveillance

2.

The reactor was tripped manually after five of the six circulating pumps

had become inoperable due to high differential pressure across the asso-

ciated circulating water system screens.

A large accumulation of grass

and debris fo 11 owing a recent storm caused the high screen differential

pressure.

A periodic preventive maintenance activity to periodically

clean the lower portion of the intake trash racks was not established

following a similar event in 1983.

6/10/89

100%

Ineffective

corrective actions

Maintenance/Surveillance


-------

Event Description

Power

Date

Leve 1

34

Unit 2 (Continued)

Root Cause

Functional Area

3.

An unplanned shutdown was made to replace a degraded phase B main power

transformer.

Periodic monitoring identified an elevated total combustible

gas concentration, indicating the presence of an internal hot spot (700

degrees F).

10/13/89

90%

Component failure

Not Applicable

4.

An unplanned shutdown was made to repair a leak on a welded pipe cap on

the discharge side of the boron injection tank.

The cause of the leaking

joint was attributed to a defect in the root of the weld that occurred

during a modification.

1/17/90

100%

Modification

installation error

Maintenance/Surveillance

5.

The reactor tripped automatically on low steam generator level coincident

with steam/feed fl ow mismatch fo 11 owing a loss of feedwater caused by a

460 volt transformer failure.

A similar catastrophic transformer failure

occurred on Unit 1 about one week earlier,. however, significant opera-

tional problems were not experienced.

Subsequent to the reactor trip, an

extended unplanned shutdown was made to evaluate and resolve main steam

isolation valve fast closure circuitry deficiencies.

6/28/90

75%

Component failure

Not Applicable

  • '

TABLE 1

Inspection Hours Summary

Salem Generating Station

May 1, 1989 - July 31, 1990

Annualized

Functional Area

Hours*

Hours

% of Time

A.

Plant Operations

2912

2257

44

B.

Radiological Controls

303

235

5

C.

Maintenance/Surveillance 1340

1039

21

0.

Emergency Preparedness

151

117

2

E.

Security and Safeguards

243

188

4

F.

Engineering/Technical

Support

594

460

9

G.

Safety Assessment/

Quality Verification

959

743

15

TOTALS

6502

5039

100

  • Does not include NRC licensing staff hours.

.,

TABLE 2

Enforcement Summary

Salem Generating Station

May 1, 1989 - July 31, 1990

Number/Severity of Violations

Functional Area

Level IV

Deviation

A.

B.

C.

D.

E.

F.

G.

Plant Operations

4*

Radiological Controls

3*

Maintenance/Surveillance

7**

Emergency Preparedness

Security

Engineering/Technical

Support

1

Safety Assessment/

Quality Verification

5**

TOTALS

19

1

Violation cited two examples, one in operations and one in radiological

controls areas.

Violation cited two examples, one in maintenance/surveillance and one in

safety assessment/quality verification areas, and is therefore included

in both areas.

Functional Area

A.

Plant Operations

B.

Radiological Controls

TABLE 3

Licensee Event Reports

Salem Generating Station

May 1, 1989 - July 31, 1990

Number by Cause

A B

C D E

X

7

2

1

5

1

1

C.

Maintenance/Surveillance

8

4

7

2

1

D.

Emergency Preparedness

E.

Security

F.

Engineering/Technical

Support

G.

Safety Assessment/

Quality Verification

Tota 1 s

6

31

2

1 8

23

35

2

9 16

2

Subtotal

13

4

22

48

87

Includes Unit 1 LERs 89-18 through 89-37 and 90-01 through 90-20; and, Unit 2

LERs 89-10 through 89-27 and 90-01 through 90-30.

Cause Codes:

A.

Personnel Error

8. *oesign, manufacturing or installation

C.

Un known or externa 1 cause

D.

Procedure inadequacy

E.

Component failure

X.

Other

Root causes assessed by the SALP Board may differ from those listed in the

LER.

ATTACHMENT 1

Salp Criteria

Licensee performance is assessed in selected functional areas, depending on

whether the facility is in a construction or operational phase.

Functional

areas normally represent areas significant to nuclear safety and the environ-

ment.

Some functional areas may not be assessed because of little or no

licensee activities or lack of meaningful observations in that area.

Special

areas may be added to highlight significant observations.

The following evaluation criteria were used, as applicable, to assess each

functional area:

1.

Assurance of quality, including* management involvement and control;

2.

Approach to resolution of technical issues from a safety standpoint;

3.

Enforcement hi story;

4.

Operational and construction events (including response to, analyses of,

reporting of, and corrective actions for);

5.

Staffing (including management); and

6.

Effectiveness of training and qualification program.

On the basis of the SALP Board assessment, each functional area evaluated is

rated according to three performance categories.

The definitions of these

performance categories are given below:

Category 1.

Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in a superior level of performance.

NRC

will consider reduced levels of inspection effort.

Category 2.

Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in a good level of performance.

NRC will

consider maintaining normal levels of inspection effort.

>.; '

' .**

Attachment 1 (Continued)

2

Category 3.

Licensee management attention to and involvement in nuclear safety or

safeguards activities resulted in an acceptable level of performance; how-

ever, because of the NRC' s concern that a decrease in performance may

approach or reach an unacceptable level,

NRC will consider increased

levels of inspection effort.

Category N.

Insufficient information exists to support an assessment of licensee per-

formance.

These cases would include instances in which a rating could not

be developed because of insufficient licensee activity or insufficient NRC

inspection.

The SALP Board may assess a functional area to compare the licensee's perform-

ance during a portion of the assessment period to that during an entire period

in order to determine a performance trend.

Generally, performance in the

latter part of a SALP period is compared to the performance of the entire

period.

Trends in performance from period to the next may also be noted.

The

trend categories used .by the SALP Board are as follows~

Improving:

Declining:

Licensee performance was determined to be improving

Licensee performance was determined to be declining and the

licensee had not satisfactorily addressed this pattern.

A trend is assigned only when, in the opinion of the SALP Board, the trend is

significant enough to be considered indicative of a likely change in the per-

formance

category in the near future.

For example,

a classification of

"Category 2, Improvi ng

11 indicates the cl ear potential for "Category 111 perform-

ance in the next SALP period.

It should be noted that Category 3 performance, the lowest category, represents

acceptable, although minimally adequate, safety performance.

If at any time

the NRC concluded that a licensee was not achieving an adequate level of safety

performance, it would then be incumbent upon NRC to take prompt appropriate

action in the interest of public health and safety.

Such matters would be

dealt with independently from, and on a more urgent schedule than, the SALP

process.