ML18094A621

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SALP Rept 50-354/88-99 for 880116-890430
ML18094A621
Person / Time
Site: Salem, Hope Creek  PSEG icon.png
Issue date: 04/30/1989
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18094A618 List:
References
50-354-88-99, NUDOCS 8908180151
Download: ML18094A621 (32)


See also: IR 05000354/1988099

Text

..

INITIAL SALP REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

REPORT NO.

50~354/88-99

PUBLIC SERVICE ELECTRIC AND GAS COMPANY

HOPE CREEK GENERATING STATION

Enclosure 2

ASSESSMENT PERIOD:

JANUARY 16, 1988 - APRIL 30, 1989


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I.

INTRODUCTION

II.

BACKGROUND .

TABLE OF CONTENTS

II.A Licensee Activities ......... .

II.B Direct Inspection and Review Activities

III. SUMMARY OF RESULTS ............ .

III.A Overview

. . . . . . . .

. . . . . . .

III.B Facility Performance Analysis Summary.

III.C Reactor Trips and Unplanned Shutdowns.

IV.

PERFORMANCE ANALYSIS ...

IV.A Operations .. * ....

IV.B Radiological Controls ..

IV.C Maintenance/Surveillance ......... .

IV.D Emergency Preparedness* (Common with. Salem).

IV.E.Security (Common with Salem) ...... .

IV. F Engi neeri ng/Techni ca 1 Support . . . . .. .

IV.G- Safety Assessment/Quality Verification ..

SUPPORTING DATA AND SUMMARIES

A.

Enforcement Activity ... * ..... .

8.

Inspection Hour Summary . . .

. .. .

C.

Licensee Event Report Casual Analysis

Attachment 1: * SALP Criteria

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2

I. - INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) is an integrated

NRC staff effort to collect available observations and data on a periodic

basis and to evaluate licensee performance on the basis of this

information.

The SALP program is supplemental to normal regulatory

processes used to ensure compliance with NRC rules and regulations. It

is intended to be sufficiently diagnostic to provide a rational basis for

allocating NRC resources and to provide meaningful feedback to the

licensee's management regarding the NRC's assessment of their facility's

performance in each functional area.

This report is the NRC 1s assessment of Public Service Electric & Gas

(PSE&G) Co.'s safety performance at the Hope Creek Generating Station for

the period January 16, 1988 through April 30, 1989.

The PSE&G programs

and personnel in the functional areas of security and emergency

preparedness overlap between the Hope Creek and Salem stations.

Accordingly, the SALP Board assessed these two functional areas at Hope_

Creek and Salem over similar assessment periods and provided a combined

assessment for each functional area.

These combined assessments are

duplic.a-Ced in both the Hope Creek and Salem SALP Reports.

An NRC SALP Board, composed of the staff members listed below, met on

July 12~ 1989, to review the observations and data on performance and to

asses*s PSE&G 's performance in accordance with the guidance in NRC Manual

Chapter 0516, "Systematic Assessment of Licensee Performance".

The

guid_ance and evaluation criteria are summarized in Attachment 1 to this

report~ The Board's findings and recommendations were forwarded to the

NRC Regional Administrator for approval and issuance.

Board Chairman

Samuel Collins, Deputy Director, Division of Reactor Projects (DRP)

Board Members

B. Boger, (Acting) Director, Division of-Reactor Safety (DRS)

M. Knapp, Director, Division of Radiological Safety & Safeguards

(DRSS)

J. Linville, Chief, Reactor Projects Branch No. 2, DRP

P. Swetland, Chief, Reactor Projects Section No. 28, DRP

G. Meyer, Senior Resident Inspector, Hope Creek

W. Butler, Director, Project Directorate (PD) I-2, Office.of

Nuclear Reactor Regulation (NRR)

C. Shiraki, Project Manager, PD I-2, NRR

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Other Attendees:

. David Allsopp, Resident Inspector, Hope Creek

Ronald Bellamy, Chief,. Facilities Radiological Safety & Safeguards

Branch, DRSS

Robert Bores, Chief, Effluents Radiological Protection Section, DRSS

Richard Conte, Chief, Boiling Water Reactor Section, DRS

Jason Jang, Senior Radiation Specialist, DRSS

Paul Kauffman, Project Engineer, Projects Branch No. 2, DRP

Ronald Nimitz, Senior Radiation Specialist, DRSS

Jack Strosnider, Chief, Materials & Processes Section, DRS

Robert Winters, Reactor Engineer, DRS

II.

BACKGROUND

II.A Licensee Activities

This assessment period began on January 16, 1988, with the reactor at full

power.

On February 13, 1988, Hope Creek began the first refueling outage,

which was completed in 63 days .. On April 15 the unit was returned to service.

~ive reactor scrams occurred in the following seven months, which resulte~ in

forced outages of short duration.

On Februq.ry 18, 1989, Hope Creek began a

two week mid-cycle outage.

Following return to service on March 7, the

reactor continued power operations through April 30, 1989, the end of the

period.

The reactor trips and unplanned shutdowns which occurred during the

period are described in Section III.C.

Early in* the assessment period, Steven Miltenberger was promoted to Vice

President and Chief Nuclear Officer.* On August 29, 1988, Stanley LaBruna was

promoted from General Manager - Hope Creek Operations to Vice President -

Nuclear Operations, and Joseph Hagan was promoted from Maintenance Manager to

General Manager ~ Hope Creek Operations.

On March 7, 1989,. and Apri 1 22, 1989, PSE&G management met with Re*gi on I

personnel.to describe Hope Creek accomplishments, organizational efforts to

improve performance, and planned initiatives.

II.B Direct Inspection and Review Activities

Two NRC resident inspectors were assigned to the site throughout the

assessment period with the currently assigned Senior Resident Inspector

assuming his duties on March 13, 1988.

Regional

inspecto~s performed routine

inspections throughout the period~ with added inspection emphasis during the

scheduled outages.

In addition, a special inspection of Emergency Operating

Procedures was performed in September 1988, and a Regulatory Effectiveness

Review was performed in April 1989.

NRC performed a total of 4007 hours0.0464 days <br />1.113 hours <br />0.00663 weeks <br />0.00152 months <br /> of

inspection during the period, which equates to 3120 hours0.0361 days <br />0.867 hours <br />0.00516 weeks <br />0.00119 months <br /> on an annualized

basis.

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III. SUMMARY OF RESULTS -

III.A Overview

Hope Creek programs continued to mature and exhibit a steady improvement in

performance.

PSE&G demonstrated a conservative, safety conscious approach in

all functional areas, and the sound management philosophies, good administrative

programs and skillful personnel achieved good results.

Performance in the

operations and radiological control functional areas improved sufficiently to

merit Category 1 ratings.

Excellent performance continued in the security

area.

The plant's operating record was good.

The operators did not initiate any

plant trips and responded correctly and promptly to operational events. The

previously identified weaknesses regarding licensed operator staffing and

housekeeping were effectively addressed.

The radiological -controls. program demonstrated good ALARA performance,

effective control of work activities, and strong radioactive effluent and

transportation controls.

PSE&G initiatives to reduce radiation exposure of

workers were commendable.

Good management support of the radiulogical -controls

and chemistry- programs was evident.

Performance in the emergency preparedness area, an area evaluated for Hope

Creek and Salem in a combined manner, decreased to. a Category 2 rating based

primarily on the weaknesses identified during the Salem-based full participation

exercise and on the inability of the Sal em Techn i ca 1 Support Center to meet

habi tabi f; ty requirements.

Improving trends were noted in the functional areas of maintenance/surveillance,

engineering/technical support, and safety assessment/quality verification.

In

these areas, the general programmatic approach was determined to be acceptable,

meaningful PSE&G initiatives were underway, and inconsistent performance and

personnel errors were being addressed~

The challenge for Hope Creek i~to continue to apply r1s1ng standards to the

established programs, to complete the initiatives underway, and to address the

isolated personnel errors and equipment failures which have occurred during

thi*s assessment period.

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III.8

Facility Performance Analysis Summary

Functional Area

-Last Period

This Period

Trend

(12/1/86-1/15/88)

(1/16/88-4/30/89)

Plant Operations

2

1

Radiological Controls

2

1

Maintenance/Surveillance

1/2*

2

Improving

Emergency Preparedness

1

2

Security

1

1

Engi neeri ng/T_echni ca 1

2

2

Improving

Support

Safety Assessment/

2**

2

Improving

Quality Verification

Rated as separate functional areas.

A simi*lar area {Assurance of Quality) was assessed last period.

Also,

the functional .area of Licensing Activities, which was assessed as

Category 2 during the last period, is currently included in this

functional area.

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III.C

6

Reactor Trips and Unplanned Shutdowns

Event Description

Power

Date

Level

Root Cause

Functional Area

1.

While shutdown~ reactor trip occurred due to an Intermediate Range

Monitor (IRM) spike.

The spike resulted from electrical interference due

to welding near the IRM electrical cabinets.

No control rods moved.

3/21/88

0%

Personnel error

Maintenance

2.

While shutdown a reactor trip occurred due to an IRM spike concurrent

with a half scram from unrelated surveillance testing.

The IRM spike was

suspected to have occurred due to jarring of the support for the IRM

electrical cabinets.

One control rod~oved .

.. 3/30/88'

  • Q%;

Personnel error

Maintenance

3.

A manual reactor trip was initiated because of the loss of all

circulating water pumps to the main condenser due to an e~ectronic

failure. in the multiplexed pump control signals.

4/30/88

. 80%

Component failure

NA

4.

The reactor tripped automatically on low reactor vessel level, because

one -0f the two operating reactor feed pumps tripped. A Secondary

Condensate Pump (SCP) had tripped when a preventive maintenance tagout

removed power from its auxiliary oil pump and inadvertently removed power

from the SCP controls.

5/5/88*

100%

Personnel error/Design

Maintenance

5.

The reactor tripped automatically fo 11 owing a turbine trip during

functional testing of the turbine thrust bearing wear detector. A

mechanical failure in the wear detector linkage caused the turbine trip.

8/26/88

100%

Component failure*

NA

6.

The reactor tripped automatically on low reactor vessel' level when the

three reactor feed pumps tripped simultaneously on a false signal of high

discharge pressure. A failed electronic component had caused the false

pressure signal.

10/15/88

100~

Component failure

NA

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  • Event Description

Power

Date

Level

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7

Root Cause

Functjonal Area

7.

The reactor tripped automatically following a turbine trip caused by

arcing in the collector of the main generator exciter.

11/1/88

100%

Component failure

NA

8.

While shutdown the reactor tripped on an alternate rod insertion signal~

During instrumentation modifications, the procedure did not specify that

a trip signal be reset in a Redundant Reactivity Control System (RRCS)

channel prior to work on another RRCS channel.

No control rods moved.

2/22/89

0%

Procedure inadequacy

Maintenance

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IV.

PERFORMANCE ANALYSIS

IV.A

IV .A.1

Operations

Analysis

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(1486 hours0.0172 days <br />0.413 hours <br />0.00246 weeks <br />5.65423e-4 months <br />, 37%)

The previous SALP rated Operations as Category 2.

That assessment concluded

that Hope Creek displayed a conservative and safety conscious attitude toward

plant operation.

Licensed operator performance was very good with the

exception of isolated attention to detail errors related to operational

control of equipment.

Non-licensed operator performance while generally

adequate had more frequently shown the need for improvement in the areas of

overall plant knowledge and attention to detail related to control of

equipment in the field.

During this assessment period,-PSE&G operated the reactor in a conservative,

safety conscious manner, and the results were good.

There were no reactor

trips initiated by opera-tors or to-which operators contributed. The responses

of operators to reactor trips and transients were timely, thorough, well

coordinated, and technically correct.

Prompt actions by operators prevented

reactor trips in some instances, e.g., loss of vessel level control in April

1988.

PSE&G had committed and continued to commit resources to upgrade plant

operations*.

Specifically, manpower resources were provided such that each

operating shift had three Senio~ Reactor Operator (SRO) licensed individuals

(one above technical specification requirements), the Operations manpower

budget wa-s increased to enable a pipeline into licensed operator :;tatus, an

- SRO-licensed individual was added to supervise- the work control group

during regular maintenance hours, and additional Operations support staff was

provided.

Further, the work control area was relocated outside the control

room to minimize. distractions to the control room,- and. the Operations

Department offices were relocated adjacent to the control room.

Plant operations were well supported by the Training Department.

All five SRO

license candidates=and-three of four Reactor Operator (RO) candidates passed

the license examinations, a good performance.

In addition, prior to reactor

startups the on duty Ros* were given simulator refresher training on reactor

startups immediately before taking the shift, if they had not recently

restarted the reactor.

Licensed operators' plant awareness, safety perspective, and professional

control room demeanor were consistently evident.

Plant operations were well

supported by detailed plant procedures.

Shift. turnovers were formal and in-

cluded thorough briefings of the relief crew.

~untrol room access was strictly

controlled, and activities were limited to those directly related to plant

operations.

Continued management support resulted in further reductions in the

number of normally energized control room overhead annunciators.

An -Operator's

thoroughness during testing resulted in the early detection of a control room

ventilation system problem resulting from a modification.

The use of overtime

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was properly controlled.* The performance of non-licensed equipment operators

in general was good and continued to improve over the previous assessment

period.

However, during an NRC operator license examination walkthrough, the

examiner noted minor examples of plant condition discrepancies, which had

apparently been overlooked by non-licensed operators.

An NRC emergency operating procedure (EDP) inspection determined that the EOPs

were technically correct and could be accomplished effectively by using

existing equipment, controls, and instrumentation.

The operators were well

trained on the EOPs and used the EOPs properly in all applicable instances.

Overall, the EOPs were found to be fully capable of performing their intended

purpose.

A high 1eve1 of management attention to ope rat ions was evident on a daily

basis.

An operational perspective of plant problems and work prioritization

was well understood by the station general manager and department managers,

and was enhanced by the daily morning briefing conducted by the Senior Nuclear

Shift Supervisor (the Senior). This approach proved effective in ensuring

good interd.epartmental communication and in resolving problems.

Isolated instances of personnel errors in Operations continued.

The errors were

generally of minimal significance, occurred in different areas, and were

committed by different people. Acceptable, appropriate corrective actions

were taken for each error, but the incidence of errors remained an area for

improvement.

Specifically, operational errors included disabling an incorrect

valve, overlooking a valve's return to service, losing track of installed

electrical jumpers, a cleanup system isolation due to deviating from a procedure,

failing to fully- close a valve that resulted in an 8,000 gallon spill onto the

torus-room floor, and _erroneously placing two battery chargers into service on

one battery.

The frequency of personnel errors has continued to decrease

compared to earlier assessment periods.

PSE&G has developed an approach to

these issues and continued to evaluata the previous corrective actions and

potential additional corrective actions.

Housekeeping improved, and efforts were underway to complete painting of the

remainder of the plant. *Further, the storage and availability of ladders was

upgraded, and platforms for better access to equipment were noticeably

improved.

The fire protection program was well staffed, well equipped, and well

organized.

Fire protection personnel were knowledgeable, which demonstrated

an effective training program.

The fire brigade was staffed by fire

protection personnel, which minimized the reliance on operators to respond to

emergenci~s. Appropriate operator involvement in emergencies was provided.

The preventive maintenance and surveillances of fire protecti0H equipment were

effective, although more aggressive monitoring of fire door operability was

needed.

Once identified, all discrepancies were promptly corrected.

Overall,

management properly supported the fire protection area.

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In summary, the Hope Creek operating staff continued to display a conservative

and safety conscious approach* to plant operation and had an excellent

operating record with no operationally caused reactor trips.

The operators

were skillful and knowledgeable and properly responded to transients.

PSE&G

improved support of operations with increased staffing in both onshift and

support roles.

The need for reduction in personnel errors represented the

primary area for improvement.

IV.A.2

Performance Rating

Category 1

IV.A.3

Recommendations

None

IV.B

Radiological Controls . (452 hours0.00523 days <br />0.126 hours <br />7.473545e-4 weeks <br />1.71986e-4 months <br />, 11%)

IV.B.1

Analysis

The previous SALP rated Radiological Controls as Category 2 (improving).

The

radiological programs were effective and well coordinated. Areas for

improvement were audits, review of radiological incidents, ALARA goals and

review of on-going work from an ALARA perspective.

During thjs.assessment period, an effective radiological controls program was

imp 1 emented and maintained.

The program was cont ro 11 ed by we 11 deve 1 oped and

disseminated policies and proceduresA

The responsibilities and authorities of

the routine non-outage radiological controls organization were adequately

defined.

Weaknesses in the definition of responsibilities for the outage

radiological controls organization, identified early .in this assessment

period, were corrected.

PSE&G recently reorganized the in plant radiological

controls group to provide for enhanced oversight of the program in addition to

improving ALARA planning and goal setting.

Required records (e.g. radiation

survey and personnel training records ) for the various areas of the

radiological control*s program were well maintained.

Staffing levels to support outage and non-outage radiological controls

activities were good.

PSE&G used personnel from the corporate radiological

controls group and the Salem Station to augment the staff during outages.

This minimized reliance on contractor support.

Communications between

radiological controls personnel and other plant personnel were *good.

PSE&G's program used for routine training and qualification of radiological

controls personnel and radiation workers was well defined and implemented.

The special program used to train and qualify contractor radiological controls

personnel for outages was of good quality and appropriately implemented.

A

program to provide continuing training for the radiological controls staff was

well defined and implemented.

Previous weaknesses in maintaining personnel

qualification records and in implementing the continuing radiological controls

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personnel training program, wh1ch were identified last period, were corrected.

The radiation protection and chemistry training programs were INPO accredited

during this SALP period.

The quality of audits, surveillances and assessments of this area have

improved.

Observations found these to be performance oriented and continuing

to improve throughout the assessment period.

PSE&G* used outside technical

specialists, where appropriate, to audit selected technical areas.

NRC

observations indicated radiological controls supervisory personnel and

managers monitored* on-going work performance.

Overall PSE&G response to NRC

identified concerns was good as demonstrated by timely resolution of the

issues, such as improvement in ALARA goals, improvement in the review of

on-going work and improvement in audit quality.

The weaknesses in the tracking, trending and closure of radiological

occurrences, a problem identified last period. were corrected. Station

management actively reviewed radiological occurrences.

NRC review of PSE&G

action on self-identified problems indicated PSE&G took aggressive corrective

actions to address these matters.

The few isolated radiological events that

have occurred in this area were promptly reported, analyzed and corrected.

The external and internal exposure control programs were well defined and,

with some exceptions, effectively implemented.

The radiological controls

deficiencies identified in this area, e.g., poor contamination control, were

attributable to isolated instances of poor performance by radiological

controls technicians.

NRC observations during the mid-cycle outage late in

the peri o_d indicated imp roved performance.

The program to minimize airborne radioactivity and to issue and control

respiratory protection equipment was particularly noteworthy.

The program

used state-of-the-art techniques with an effective computerized system.

PSE&G

evaluation of. radiological conditions during the first movement of spent fuel

was commendable.

This was evidenced by excellent radiological evaluations to

verify shielding. integrity during spent fuel movement.

PSE&G 1 s control of and

minimization of contamihated* areas were good.

Industrial safety concerns including heat stress, use of safety lines and

improper use of scaffolding were identified at Salem Station.

In response,

PSE&G took action to preclude these problems at Hope Creek.

Some isolated NRC

observations, e.g., use of untagged scaffolding, were noted during the mid-

cycle outage.

These examples indicated the need for continued attention *

to industrial safety at Hope Creek.

The ALARA- program was effective. Station aggregate exposure since initial

startup was commensurate with plant radiological operations and ~ompared

favorably with industry averages.

Aggressive oversight and control of major

exposure tasks were noted.

Previously identified weaknesses in goals

development and exposure tracking were corrected.

AL.ARA goals were considered

challenging.

Lessons learned were effectively used for AL.ARA planning

purposes.

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PSE&G continued to aggressively pursue dose reduction actions and initiatives

that could reduce aggregate exposure over the life of the facility.

For

example, a semiautomatic control rod drive removal system was installed and

operationally tested for exposure* reduction during routine system maintenance,

and robots were purchased and used where needed to minimize personnel

exposure.

Water chemistry was closely monitored, and the imminent

implementation of hydrogen water chemistry is a positive initiative to address

pipe cracking and associated operational and radiological problems.

Fuel

performance has been good.

These initiatives will aid in maintaining

exposures ALARA in the future.

Also, PSE&G used zinc injection to minimize cobalt-60 buildup on primary

piping.

However, some higher than expected radiation fields caused by zinc-65

were encountered.

PSE&G continues to evaluate the reason for the unexpected

fields.

A formalized cobalt reduction program was under development at the

end of the assessment period to provide further reduction of the station's

radiation source term.

Staffing in the ALARA area was good.

PSE&G placed radiological controls

personnel in the planning and scheduling department to evaluate work packages

and interface between work :~roups and the radio l ogi ca 1 contra 1 s group.

This*

improved ALARA planning.

Improvement was observed in the areas of calibration of the liquid and gaseous

monitors, effluent control equipment, and effluent control procedures which

were identified as significant weaknesses in the previous assessment.

An

effectivs program for controlling radioactive effluent releases from the site

was in place.

Effluent ~ampling, analyses, and reporting were good.

Air

cleaning systems were w~ll maintained and tested.

The review of the

radiological environmental monitoring program (REMP) indicated an adequate

program was in place.

Timely, thorough corrective actions were taken regarding

violations for failure to audit an REMP area and for an inadequate downscale

trip fcnction on a liquid effluent monitor.

The QA audits covered the stated

objectives and were thorough~ and-corrective actions were prompt and effective.

PSE&G has an effective solid radioactive waste processing, preparation,

packaging and shipping program.

Overall, PSE&G management controls, waste

processing procedures, QA audits and training in the area of radwaste were

adequate.

During this assessment period PSE&G completed a major accomplishment

in this area: the testing of a new asphalt solidification/dewatering system to

ensure that a suitable waste form for disposal was provided and key process

parameters were identified.

Hope Creek continued its aggressive water chemistry control program, which

received good plant management support.

Chemistry related parameters such as

conductivity, chlorine, and condenser in-leakage were continually kept low.

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  • In summary, PSE&G maintained and implemented an effective radiological

controls and chemistry program.

ALARA performance relative to comparable

facilities was good.

PSE&G initiatives to reduce radiation exposure of

workers were commendable.

Overall radiological controls for work activities

were effective.

Performance in the areas of radioactive effluent controls and

transportation was generally strong.

Management oversight of the program was

good.

Effective corrective actions were taken for self-identified and NRC

identified problems.

PSE&G's overall performance in these areas indicated

good management commitment to and support of the radiological controls

program.

IV.B.2

Performance Rating

Category 1

IV.B.3

Recommendations

  • None

IV.C

Maintenance/Surveillance (1143 hours0.0132 days <br />0.318 hours <br />0.00189 weeks <br />4.349115e-4 months <br />, 29%)

IV.C.1

Analysis

The previous SALP rated Maintenance as Category 1 and Survei *,lance as

Category 2.

The SALP concluded that the maintenance organization was

effectiv~y implementing corrective and preventive maintenance.

The

surveillance program was assessed as utilizing procedures of high quality, but

the assessment encouraged improvement in the attention to detail area to

reduce the number of personnel errors and missed surveillances.

Maintenance:

The Maintenance Department continued to effectively manage maintenance

activities. Management involvement was commendable, especially the first

line supervisors, who were frequently evident at the work locations, were

informed regarding the problems, and resolved problems effectively. The

managers exercised a conservative approach to problem resolution, and status

meetings between managers were well controlled and focused on problem

resolution.

Work activities were well planned and coordinated which minimized

equipment out-of-service time.

The availability of safety equipment was very

good, with a minimum number of corrective maintenance problems on major safety

equipment.

Equipment outages were largely preventive maintenance.

The

utilization of a forced outage schedule allowed effective planning and maximum

repU:i"':!°"effort when the unit was unexpectedly shutdown.

Maintenance activities*

continued to be well controlled and received an appropriate level of

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supervisory attention.

The Maintenance Department was adequately staffed with

skillful. well trained personnel and provided an appropriate level of detailed

procedures for their use~

There were four reactor trips which resulted from component failures.

The

four failures involved multiplexed circulating water pump controls, turbine

bearing wear detector, feedwater pump controls, and the collector of the main

generator exciter.

None of the failures indicated problems within the

preventive maintenance program, and PSE&G took effective corrective actions to

prevent continued reactor trips from similar component failures.

Four maintenance related reactor trip system actuations occurred, three of

which had minimal safety significance as the reactor was already shutdown.

All four trips were related to the control of maintenance work; one trip

resulted from improperly removing an auxiliary oil pump from service to

perform preventive maintenance, one trip resulted from a procedure inadequacy

regarding resetting of logic system trip signals during transmitter

modifications, and two trips occurred due to we*lding and lifting adjacent to

electronic cabinets~ Cl early, the operators who authorized the auxiliary oil

pump tagout and work in proximity of operating electronics cabinets

sharr,d responsibility for these trips. Nonetheless, Detter planning

and control of maintenance work would reduce cha 11 enges to the operators and

to safety systems.

The maintenance planning and outage organizations were effective and an

integral part of the performance of the work, both during outages and routine

operation_.

The planning group was properly supported by management, in that

the* staffing was adequate, and the assigned personnel had experience in

operations, maintenance, and radiological protection.

The managed maintenance

information system (MMIS) continued to be an effective scheduling and tracking

system. for all corrective and preventive maintenance.

MMIS is an on-line

computer based program that. integrates th~ master equipment list, equipment

history, recurring task scheduling, real time job status, and ~arts inventory.

Early in the assessment period Hope Creek completed its first refueling outage

in 62 days. *The station personnel generally worked well together and

accomplished many task~ effecttvely .. Some problems occurred in modification

work, and twi"ce control of electrical jumpers was lost, although the impact on

safety was minimal.

Hope Creek completed a successful scheduled mid-cycle maintenance outage in

April 1989, which lasted 17 days.

Effective interdepartmental coordination

and planning was evident as the station implemented approximately 60 design

changes and responded effectively to emerging problems.

The station completed

all procedure revisi-O"ns associated with the design changes prior to returning

the unit to operation.

Outage management control was enhanced by use of an

outage management team, which consisted of an overall outage manager and shift

managers.

The smooth functioning outage and the significant work accomplished

in a short period of time demonstrated a highly effective team.

--.-

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15

  • The training center maintained extensive electrical and mechanical training

facilities, both INPO accredited. Both electrical and mechanical technicians

in the field have demonstrated technical knowledge and skill in accomplishing

assigned tasks.

At the end of the period the electrical and maintenance

organizations were fully staffed and did not utilize any contractor personnel.

Surveillance:

The surveillance program encompa~sed approximately 5000 surveillance tests

performed annually within the Operations, Maintenance, Chemistry, Radiation

Protection and Site Protection Departments.

The computerized system (MMIS)

described above scheduled all periodic surveillance tests and enabled the

generally effective control of the surveillance program.

There were five

instances where surveillance tests were missed primarily due to personnel

error. The missed tests had minimal safety significance, were identified by

PSE&G, and typically involved poor recognition of the effect of .changing plant

conditions on required surveillance tests.

Effective corrective actions were

implemented for the*mtssed surveillances.

In general, surveillance test procedures were well written, accurate and

compl~te. Inadequate surveillance testing procedures were responsible for a

Nuclear Steam Supply Shutoff System (NSSSS) channel A isolation and a loss of

shutdown cooling for twelve minutes.

Also, early in the period, there was one

surveillanc~ test which did not adequately demonstrate operability of the

liquid radwaste radiation monitor.

This appeared to be an isolated case, as*

no other test was found to inadequately test a system.

Technicians freely

provided feedback and recommended procedure revisions to improve procedures

based on field experience~ These improvements have contributed to a

.

significant backlog of procedure revisions (approximately 600) which have been

implemented at a rate of 15-20 a week.

This was a positive initiative which

warranted continued PSE&G emphasis to provide for timely disposition of

procedure revtsions ..

There were two incidents which could have been prevented with improved

attention to detail or better training.

The incidents involved the

misapplication of test* equipment, which resulted* in a cleanup system

isolation, and an,.incorrect a~i.gnment on an ECCS logic tester, which caused a

C channel ECCS isolation. Other personnel errors involved a procedure

deviation, which caused a HPCI isolation; an NSSSS isolation, which was

generated when a test equipment meter lead became grounded in a steam leak

detection cabinet; and an inadequate return to service of a ventilation

instrument.

Effective corrective actions were taken for each of the errors,

including personnel disciplinary actions, remedial training, and procedure

improvements.

The rate of personnel errors continued to decline compared to

previous assessment periods, but represented an area for improvement.

The Inservice Test (IST) program was generally good with several strengths and

weaknesses noted.

The strengths includ~d a comprehensive IST program submittal

.

.

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16

to NRC staff with relatively few issues that required resolution 9 a comprehensive

review team that established a documented program basis~ and generally well

prepared test procedures.

Good engineering practice and conservatism were

evident in the pump reference values, which were traceable to the FSAR, the

valve stroke time limits derived from actual stroke times 9 and the actions

taken to resolve the safety relief valve (SRV) setpoint drift and pilot valve

sticking.

The weaknesses included the delay in establishing an IST

coordinator and a few instances of failure to disseminate IST applicable NRC

Bulletins and Information Notices to all affected parties.

In addition,

following a modification to a check valve, the IST procedure lacked adequate

detail and acceptance criteria and the equipment operators were not trained in

the modified design.

Overall the IST program was properly implemented.

The Inservice Inspection (ISI) program was properly defined and implemented.

Local Leak Rate (LLRT) activities were properly administered and implemented

by the ISI group.

PSE&G 1s program for monitoring erosion=corrosion in

susceptible piping systems and components was good.

PSE&G reviewed 100% of

the ISI data as part of the program.

PSE&G's response to Generic Letter 88-01

on lntergranular Stress Corrosion Cracking was timely and add~essed all

required areas with no relief requested.

Overall the IS! program was

effective.

Measuring and test equipment (M&TE) was routinely controlled; however, one

finding indicated an instance where the lack of M&TE control prompted the

need for additional effort to ensure all M&TE is properly calibrated prior to

use.

In summary, the* maintenance organization continued to effectively manage

preventive and corrective- maintenance.

The maintenance, planning and outage

organizations were well trained and productively coordinated to minimize

degraded equipment.

Better control of maintenance work was demonstrated

  • during the mid-cycle outage, with no reactor trips versus the three reactor

trips during the refueling outage.

The surveillance area was well staffed

with. technically knowledgeable and. experienced personnel.

Surveillance test

procedures were detailed and continued to be refined from in-plant

implementation feedback.

The reduction of the number of personnel errors and

missed surv~illances continued to represent. areas for improvement.

IV.C.2

IV.C.3

Performance Rating

Category 2; Improving

Recommendations

None

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IV.D

IV.D.1

Emergency Preparedness

Analysis

17

(136 hours0.00157 days <br />0.0378 hours <br />2.248677e-4 weeks <br />5.1748e-5 months <br />, 3%)

There is a consolidated Emergency Plan for the Artificial Island complex,

including the Salem and Hope Creek facilities.

Consequently, the assessment

of emergency preparedness is a combined evaluation of both facilities*

emergency response capabilities.

The previous SALP rated Emergency Preparedness as Category 1.

The licensee

had demonstrated strong emergency response capability during the Hope Creek

based exercise.

No exercise weaknesses or areas for improvement were

identified. There was no Salem-based exercise.

The licensee had maintained a

strong management awareness of and commitment to emergency preparedness.

One

weakness was identified regarding the adequacy of the Salem staff response to

pager call-in tests. *

During this assessment.period, a Salem based full-participation exercise took*

place which involved Delaware and New Jersey. It included an ingestion

pathway response in New J~rsey. There was no full-scale exercise for Hope

Creek.

Two routine emergency preparedness inspections were conducted and the

Resident Inspector observed several training* drills.

During the* full-participation exercise two weaknesses were identified by the

NRC.

One weakness involved the. fact that the Control Room and Technical

Support Center staffs did not recognize postulated containment failure for an

hour and_forty minutes.

The other weakness involved a communication problem;

the Emergency Response Manager did not inform- the Emergency Operations

Facility staff that recovery conditions had been attained.

In addition,

several other areas of lesser significance were identified.

Remedial drills

demonstrated effective corrective action for all identified exercise

weaknesses with on~ exception,. recognition of containment failure, which will

be evaluated in a future exercise.

In other areas, corrective actions have been completed regarding pager call-in

response.

Management also responded to NRC concerns and took steps to improve

. the quality of dose projection. calculations and field monitoring techniques.

Sixteen Unusual Events (UEs) were declared during this assessment period.

Licensee response to the events was generally in accordance with procedures;

however, some areas for improvement were identified.

Two similar events at

Salem were classified differently (one as a UE and one not classified),

indicating inconsistent interpretation and use of EAL classification

procedures by the operators.

The procedures have been revised to provide

clarification.

On two other occ*asions, inaccurate or incomplete information

was provided to the NRC Headquarters Operations Officer. A Hope Creek UE was

declared 45 minutes after the event had begun.

Management recognized the need

for corrective action in these cases and reemphasized to the Senior Reac~or

Operators the importance of prompt, accurate declarations.

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18

A reorganization placed the Emergency Preparedness Department in the Nuclear

Services Department, which is iritended to enhance corporate involvement in

this area as the Nuclear Services Department General Manager (GM) has an

operations and emergency response background and has maintained close contact

with the emergency preparedness program (EPP).

Corporate management involvement

and interest in this area was evident by the considerable amount of effort by

the onsite Vice Presidents devoted to emergency preparedness issues, including

off-site interfaces.

Support of and cooperation with the states remained at a

high level.

One new staff position, requiring a radiation protection

background, was added to emergency preparedness.

Two senior reactor operators

are to be assigned full time to the EPP staff.

Emergency Preparedness Training (EPT) was a collaborative effort between EPP

and the Tr~ining Department (TD).

The TD was changing its approach to EPT:

additional trainers are being qualified; a modular methodology based on Job

Task Analysis will be used to ensure trainers have an adequate understanding

of emergency response organization staff needs; and the frequency of weekly

- training dril 1 s has been revised to one for each site every two weeks (on a .

trial basis). At least three persons were qualified for each position in the

Emergency Response Organization.

The licensee: recently affirmed that the Salem Technical Support Center (TSC),

an interim TSC per the Salem Unit 2 License, has not met NRC design require-

ments regarding ventilation. This is a condition which has existed for eight

years.

The* licensee committed to* resolve the deficiencies by October 1989.

Under the current situation, in the event TSC evacuation is required due to

uninhabitability, the Salem TSC staff will .relocate to the Hope Creek TSC.

  • In most areas the licensee demonstrated a high level of interest and

involvement in maintaining emergency response capability: the licensee had an

excellent Rumor Control organization, which could be manned by about 300

people on- two shifts;

an upgraded route alerting mechanism was developed; and

a VHS tape was developed to train offsite workers in radiological

self-protection. Siren* a-vailability was 98.5%.

Ten independent, redundant

and diverse offsite communication systems were in place.

The Emergency News

Center (ENC) was ldcated about 7.5 miles from the site. Although it was not

required, an alternate, Emergency News Center .has. been identified and logtstics

arranged to support activation, if necessary.

In summary, the licensee maintained a good Emergency Preparedness Program.

Management remained involved, was reasonably responsive to NRC concerns, and

maintained an adequate staff for the Emergency Response Organi~ation. An

effective training program has been maintained.

Salem staff performance

during the annual exercise was not at the same high level as that noted in the

previous Hope Creek exercise; however, it was acceptable.

There were isolated

event classification problems.

The licensee 1 s corrective actions with regard

to resolving TSC operability concerns are scheduled to be completed by October

1989.

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IV.D.2

IV.D.3

IV.E

IV.E.1

19

Performance Rating

Category 2

Recommenda.t ions

None

Security

(222 hours0.00257 days <br />0.0617 hours <br />3.670635e-4 weeks <br />8.4471e-5 months <br />, 5%)

Analysis

One security program covers Salem and Hope Creek, and the protected areas and

security staffs overlap.

Accordingly, this assessment of security applies to

both sites.

The previous SALP.rated the Salem and Hope Creek security program as

Category 1.

This rating was largely influenced by management's attention to

and involvement in the program, an effective self-appraisal program, a clear

understanding of NRC security objectives and a good enforcement history.

Management's attention to, and involvement in, assuring the implementation of

an effective security program remained evident.

The licensee was very

effec~ive in maintaining good support for the security program from other

functional groups at both stations.

Frequent organization interactions a~d

good working relationships were apparent from the professional attitude of

employees toward the security program, as well as the attention given by the

maintenance group to the prevention and correction of problems with security

systems and equipment.

As further evidence of management's interest in an effective and quality

program, it was noted that all security shift supervisors, who provide

around-the-clock oversight of the contract*security force, attended a yearly

training course given by the licensee on regulatory and security program

requirements and objectives.

In addition, security management continued to

participate in the* Region I Nuclear Security Organization and in other nuclear

industry groups engaged in nuclear security related matters.

The licensee also continued to implement a self-initiated appraisal program

carried out by security management and supervisory personnel.

Adverse

findings were promptly resolved and provided to training personnel to factor

into the training program to prevent their recurrence.

The appraisal program

is in addition to the NRC 1 s required annual program audit that is conducted by

quality assurance personnel.

The last annual audit was very comprehensive in

both scope and depth.

Audit findings were distributed to appropriate

management personnel for review, and corrective actions for deficiencies were

prompt and effective. This also demonstrated the licensee 1 s desire to

implement an effective and quality security program.

'

20

During this assessment period, the licensee appointed a new site security

manager. The new security manager was promoted from within the existing

organization, and the transition went smoothly which was indicative of gaod

planning and effective management.

The security force contractor had effective management as was evidenced by

continuous onsite contractor management, steps taken to improve the security

program (e.g., employee benefits, training aids, and better equipment), and

the low turnover of personnel (about 7%).

The contractor also implemented

changes to its supervisory structure, which eliminated duplicate supervisory

positions between the licensee and the contractor.

Staffing of the security organization appeared adequate, as evidenced by a

limited use of overtime and a low backlog of work.

The installation and

maintenance of some state-of-the-art systems and equipment during this period

significantly reduced the use of compensatory posts for systems and equipment

failure and, thus, reduced the need for extensive overtime.

Both the

  • licensee's proprietary supervisors and the contractor's supervisors were well

trained and experienced, and exhibited a conservative and positive attitude

toward security.

Security force personnel were also well-trained and

exhibited high morale and professionalism in carrying out their duties.

The

licensee's efforts to establish and maintain such a professional image for the

security force was another indicator of the licensee's desire to implement a

quality security program.

It was also reflected by the generally excellent

state of cleanliness .in all security facilities ..

The train_i*ng and requalification program was well developed and carried out by

a Training Administrator and two full-time instructors.

In addition to

initial and ~equal.ification training, on-the-job performance evaluations were

conducted which test the proficiency of individuals on general and specific

security program requirements.

The on-the-job performance evaluations

provided management the ability to review. and enhance the performance and job

knowledge of security personnel and to correct deficiencies as they were

detected.

This was another initiative that was indicative of the licensee's

desire to implement an effective program.

Several minor deficiencies.were.identified that were promptly and effectively

corrected.

The licensee's good enforcement record during this period is

attributed to management's involvement in the security program, the continuing

self-appraisal program, comprehensive annual audits, and the security training

program.

The licensee submitted three security event reports pursuant to 10 CFR

73.71(c) during the assessment period.

One report in~olved an inadvertent

tailgating incident and the other two reports involved security guards who

were inattentive to duty.

The licensee's actions were prompt and effective in

each case.

During this period, the licensee also developed a program to

minimize the recurrence of inattentive guards; the program includes limiting

overtime and conducting organized discussions on topics such ~s proper

nutrition and physical fitness.

'* .. :: .. ls"**-,:;..

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21

An NRC Safeguards Regulatory Effectiveness Review (RER) of the Island reviewed

the protected area boundary and identified several potential weaknesses

associated with the Salem facility due to older equipment that the licensee

had planned to replace. The licensee was responsive to the RER findings and

implemented short-term corrective measures where necessary.

However, several

of the potential weaknesses were readily apparent to members of the RER team

and should have been identified and corrected by the security organization.

The licensee submitted one change to the contingency plan under 10 CFR

50.54(p).

This change was made to provide clarification to certain areas in

the plan.

This was indicative of the licensee desire to provide its security

force with unambiguous instruction. The change was clear and fully described

the issues. Prior to the submittal of this change, the licensee discussed the

change with Region I safeguards personnel at a licensee requested meeting.

In summary, .the licensee continued to implement a highly effective and quality

security program for Artificial Island.

Management interest in the program

remained evident through its continued support and attention. to program needs.

IV.E.2

Performance Rating

Category 1

IV.E.3

Recommendations

None

IV. F

Engi neeri ng/Techn.i cal Support

(382 hours0.00442 days <br />0.106 hours <br />6.316138e-4 weeks <br />1.45351e-4 months <br />, 10%)

IV.F.1

Analysis

The previous SALP rated Engineering and Technical Support as Category 2.

Signtficant inconsistency. was noted in the quality of engineering work from

the corporate Engineering and Plant Betterment (E&PB) Department.

A

reorganization had been implemented in* December 1987, at the end of the last

SALP period, with the. potential for: improved corporate engineering support of

plant activities. This late implementation of the reorganization did not

allow time for a meaningful evaluation of its effect during the previous

assessment period.

The station systems engineers were observed to perform a

valuable and effective function.

However, the role of.systems engineers needed

to be more clearly defined.

During this assessment period, significant changes were made to the corporate

engineu~~ng department (E&PB) and its interaction with the station. These

included:

implementation of an Engineering Work Request System; use of a

Project Management System; establishment of a Project Matrix Organization;

revision of the Design Change Process; more direct station input in

prioritizing engineering work; and, improved responsiveness of EP&B to site

needs.

-:,~::___ ~~** * : . * ~*

22

With the establishment of the new matrix organization, senior engineers are

designated as project managers.

They coordinate and are responsible for

design changes and other major projects from inception to completion.

This

has resulted in enhanced personnel accountability yielding an improvement in

control over design change and project development and implementation.

Plant

involvement has been accomplished by including the system and QA engineers on

project teams.

The E&PB's new project organization has provided better tracking of

engineering work within E&PB and enabled better coordination of technical

concerns, priorities and resources between Hope Creek and E&PB.

During the

two week mid-cycle outage late in the assessment period, a substantial amount_

of work was accomplished in an effective and efficient manner.

The E&PB

project organization contributed to this accomplishment as the design changes

were well organized and project personnel were present to ~esolve any

problems.

A preestablished workbook approachto design change package development has

been instituted during this SALP period.

This represented an improvement over

the previous, less formalized process.

The new design change procedures and

checklists enabled better configuration management control.

Improved

supporting information- in the design change packages is intended to aid field

i n s ta 11 at i on .

Overall, the modification work was acceptable under both the old and new

systems.

However, inconsistencies in the quality of engineering work from

E&PB were_ noted.

Engineering associated with feedwater flow measurement

calcul~tions and analyses supporting the Emergency Operating Procedures (EOPs)

were flawed. * Design *changes regarding venti-lation changes adjacent to the

control room, instrumentation relay replacements, and instrumentation tubing

supports had errors which needed corrective actions following turnover to the

station~ The full implementation of the upgraded design change process has

the potential to prevent such errors, but design changes unde~ this process

have only begun.to be installed.

The E&PB Nuclear Engi~eering Group effectively supported* plant operation,

. including. post"."refueling startup testing, :thorough. evaluations of secondary

plant efficiency, and resolution* of power oscillation concerns.

NRC review of the Mark I containment design found that resolutions of

previously identified issues were acceptable.

The supporting analyses were of

good quality and thorough.

Engineering personnel involved with this activity

were knowledgeable regarding the issues and their resolution.

Communications between**iJf'9anizations and at all levels from the engineers to

senior management were observed to be good regarding management control of

projects and tasks in E&PB.

Senior management is informed of the plant status

and site activities through formal monthly meetings with the department heads.

The General Manager of E&PB meets weekly with the functional managers for

discussions of department activities.

The functional managers met weekly with

their staffs.

. . .

~-.

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23

The EP&B staffing was noted to be generally adequate.

The staff was found to

be competent and knowledgeable in their areas of responsibility.

PSE&G strongly

supports participation in industry, owner groups and professional societies.

Progress was made toward better management of the various roles of the systems

engineers, a problem noted during the previous assessment period.

The systems

engineers have continued to provide responsive, effective engineering support

on day-to-day equipment problems.

This group remained a strength in the

organization. The systems engineers played significant roles in resolving

numerous plant problems, including loss of power to instrumentation optical

isolator panels, feedwater flow measurement errors, circulating water pump

control problems, and Rosemount transmitter problems.

The system engineering groups were staffed with experienced knowledgeable

engineers, who received six months of system and engineering training.

Further, PSE&G management staffed some unassigned positions to facilitate the

training and development of replacement systems engineers.

Nevertheless, the

overall e-xperience level of the system engineers has decreased due to the more

experienced engineers pursuing other opportunities, and more supervision of

the system engineers will be needed to maintain a consistent level of

performance.

In summary, PSE&G continues to make progress in addressing the engineering and

technical support deficiencies identified during the previous assessment

period. The*full potential of PSE&G* initiatives-was not yet achieved, and

inconsistencies in the quality of engineering work from E&PB remain.

The

system engineers continue to be an organizational strength, but reduced

experience.levels within the system engineering group could present a

challenge to their performance.

IV.F.2

IV.F.3

IV .G .

IV.G.l

Performance Rating

Category 2; Improving

Recommendations

None.

Safety Assessment/Quality Verification

(186 hours0.00215 days <br />0.0517 hours <br />3.075397e-4 weeks <br />7.0773e-5 months <br />, 5%)

Analysis

This new functional area combines the previous functional areas of Licensing

Activities and Assurance of Quality and assesses the effectiveness of PSE&G's

programs in assuring the safety and quality of plant operations and

activities.

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24

The previous SALP rated the Assurance of Quality functional area as Category 2

with an improving trend.

The report noted that PSE&G had established the

programs, procedures, and working environment to promote high quality, and

encouraged continued management attention to weak areas such as the

engineering department.

The previous SALP rated Licensing Activities, a

separate functional area, as Category 2 and noted the inconsistent quality of

licensing submittals regarding technical content and timeliness.

During this assessment period, PSE&G did a good job of addressing technical

issues in a straightforward manner.

PSE&G went beyond technical specification

requirements to ensure proper system operation; for example, all fourteen

safety relief valves (SRVs) were lift tested at power following replacement,

not just the required five SRVs, and the acceptance criteria for High Pressure

Coolant Injection (HPCI) System response time testing were reduced for low

pressure conditions.

After an acceptable HPCI overspeed test, the test was

repeated to confirm acceptability.

When a test engineer raised concerns

regarding the orientation of isolation valves in primary containment

ventilation* lines, the concern was expeditiously ra*ised to the plant

management level and corrective actions were initiated. These efforts

demonstrated a conservative, safety conscious approach to these issues.

PSE&G 1 s adherence to the concept of personal accountability was most

noticeable when observing the Senior Nuclear Shift Supervisors (the

Seniors"), the SRO licensed operators held accountable for plant operations

on each operating shift.

The Seniors ensured that they concurred with

decisions, such as technical specification interpretations, the acceptability

of equi pm_ent being returned to service, and courses of action.

Each morning,

the. department.managers attended a meeting ruil.by the Senior to discuss plant

status and plans~ which reinforced the Senior's responsibility and provided

the opportunity for him to have department managers address his concerns.

The

meeting provided ready accessibility from the operating crews to upper and

middle level management, as well as be-ing a* vehicle that quickly involved

engineering talent in operational problems.

However, as detailed in the individual functional areas, the PSE&G programs

have generally been well designed and properly supported with adequate staffs

of trained personnel, but the day:-to-day- implementation has resulted in

numerous personnel errors. These errors have had minor safety significance

and have been properly corrected.

The errors were variously caused by

technician error, inadequate procedure review, poor work practices, or a loss

of control of equipment.

Further, the errors affected a broad cross section

of the plant activities, including post-maintenance testing, workmanship, and

management oversight.

Frequently, the errors involved personnel errors

indicative of a lack of attention to detail, e.g., a technician checked off a

test step but did not place the switch in bypass*as specified, an instrument

was returned to service and verified despite a closed valve, etc.

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25

PSE&G has initiated the Human Performance Evaluation System (HPES), a detailed

analysis method for determining root causes in incidents involving personnel

errors. This analysis technique is intended to provide a thorough, innovative

analysis of personnel errors.

During the evaluation of the feedwater flow measurement errors that resulted

in the facility being operated slightly above its maximum licensed power

level, the engineering staff displayed a willingness and ability to analyze

data and events independent of the vendor representatives.

In this instance,

an engineer did not accept General Electric (GE) Company assurances that their

(GE's) calculations were correct and GE subsequently corrected the information

by issuing a Service Information Letter.

Good problem identification occurred both from within and from outside each

organizational element.

Numerous examples occurred in which personnel not

directly responsible for activities raised issues which were promptly elevated

to proper levels for resolution, including the orientation of containment

isolation valves on the torus and control room pressure differential.

Incident Reports continued to be used to identify and resolve plant problems

and off-normal events and for tracking corrective actions to completion.

Hope

Creek had 170 Incident Reports in 1988, 36 of which were reportable to the

NRC.

PSE&G continued to analyze and trend the Incident Reports; their

analyses demonstrated a steadily decreasing Incident Report frequency.

The Station Operations Review Committee (SORC) was composed of department

managers and provided consistent, effective review of significant plant

issues, i-ncluding design changes, post-trip reviews, reportable events, and

stat i*on-wide procedures.

During the opt i ca 1 i so 1 a tor failure, the SORC met

during the~night to review the course of action before its implementation, a

good indication of the SORC's role.

The Quality Assurance* Department, the Onsite Safety Review Group, and the

Offsite Safety Review Group provided effective, independent review of plant

activities.

The station quality assurance (QA) organization provided

day-to-day review in the quality control and in-process review areas and was

integrated into the station's resolution of problems.

As noted in the

individual functional.areas, the quality of auditing improved and provided an

effective, independent review of plant programs and activities.

Procurement

and receipt inspection were effective.

Station QA involvement in IS! and startup testing was apparent.

In the !SI

area QA performed surveillance of in-progress !SI contractor activities,

in-house reviews of contractor !SI procedures and audits at the contractor

facilities.

QA performed many surveillance activities during the post-

refueling startup testing program.

Sixteen licensing actions (amendments, relief requests, exemptions, etc) were

processed.

The qu_ality of the technical evaluations was _generally good, .

.i. *. ,-

.,

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_,.,.

26

indicating that PSE&G has a general understanding of the technical issues, is

aware of and participates in industry groups 9 and uses acceptable approaches

to problem solutions. Submittals generally reflected good planning and

effective assignment of priorities.

PSE&G 1 s responses to requests for

additional information or necessary corrections were usually prompt and well

handled.

The one exception dealt with a license change request concerning the

Filtration, Recirculation, and Ventilation System.

There was one instance of

an incomplete license change request dealing with an amendment to the

Technical Specification surveillance test intervals and allowable outage ti~es

for the reactor protection system.

These are viewed as exceptions to an

otherwise effective program.

The supplemental information was submitted

promptly and correctly.

PSE&G's response to regulatory initiatives (i.e. Generic Letters, Bulletins

and a TMI Action Plan update request) has been timely and complete.

Frequent

communications indicate that they commence work on their responses sufficiently

in advance that they are able to meet commitment dates without requesting

extensions.

In summary, the safety conscious approach.instilled by p~ant management and

exercised by Hrpe Creek personnel was commendable.

The personnel errors which

occurred in all functional* areas need continued management attention.

Problem

identification was excellent, and problems were promptly addressed and

corrected.

PSE&G licensing activities were generally complP.te and timely.

IV.G.2

IV.G.3

Performance Rating

Category 2; . I_mprov.i ng .

Recommendations

None

-- --

.

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27

SUPPORTING DATA AND SUMMARY

A.

Enforcement Activitl

Number of Violations bl Severitl Level

Functional Area

v

IV

III II

I

Dev.

Total

-

-

Plant Operations

2

2

Radiological Controls

Maintenance/Surveillance

2

1

3

Emergency Preparedness

0

Security

0

Engineering/Technical

1

2

3

Support

Safety Assessment/Quality

1

1

Verification

Other

l*

l*

Totals

1

7

1

0

0

1

10

A Severity Leve 1 III violation without a civil penalty was issued for

discrimination in 1985 by Bogan (PSE&G cont~actor) against an employee

for raising* safety concerns.

B.

Inspection Hour Summary*

Annualized

Actual

Hours_

Percent

Plant Operations

1486

1157

37% -

Radiological Control~

452

352

11%

Maintenance/Surveillance*

1143

890

29%

Emergency Preparedness

136

106

3%

Security

222

173

5%

Engineering/Technical Support 382

297

10%

Safety Assessment/Quality

186

145

5%

Verification

Totals

4007

3120

100%

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28

c.

Licensee Event Re~ort Causal Anal~sis

Functional Area

A

B c

D

E x

Total

Operations

7

7

Radiological Controls

2

2

Maintenance/Surveillance

15

1

13

29

Emergency Preparedness

Security

2

2

Engineering/Technical Support

4

4

8

Safety Assessment/Quality

Verification

Totals

30

4

1

13

48

This analysis includes LERs 88-02 through 89-11 and two safeguards LERs.

Cause Codes*

TyQe of Events

A.

Personne 1 Error. . . . . . . . . .

~O

Poor judgement

-

8

Lack of knowledge/training -

6

_Attention to detail

- 16

B.

Des.; gn/Man/Constr ./Install

4

C.

External Cause ...

D.

Defective Procedure.

1

E.

Component Fa i 1 ure.

13

X.

. Other.

. ...

-

Total.

48

  • Root causes assessed by the.SALP Board may differ from those listed in the

LER.

Overall, the number of LERS declined from 57 last SALP period (411 days) to 48

during this assessment period (471 days); this represents annual rates of 50.6

for last period and 37.2 for this period, a reduction of over 26%.

Also, this

number of LERs compared favorably with other units of similar construction and

vintage.

Clearly, the above causal analysis shows that personnel errors remained the

major contributor to reportable events.

PSE&G's analysis also showed

personnel errors to be the major contributor, but to a lesser extent; over the

assessment period, PSE&G attributed 21 *events to personnel er~or. These

errors caused at least half of the events in each functional area and involved

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29

six violations of Technical Specifications (all PSE&G identified and only one

cited).

p*sE&G analyses, including the Human Performance Evaluation System

(HPES), have not identified any common root causes for the personnel errors.

Personne-1 at. various working lev.els were involved, from technicians to procedure

writers to engineers to supervisory licensed operators.

The next significant causal factor was component failure.

Review of these

failures did not determine any shortcomings in the preventive maintenance

program,

.

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Attachment 1

SALP CRITERIA

Licensee performance is assessed in selected functional areas, depending on

whether the facility is in a construction, or operational phase.

Functional

areas normally represent areas significant to nuclear safety and the

environment.

Some functional areas may not be assessed because of little or

no licensee activities or lack of meaningful observations.

Special areas may

be added to highlight significant observations.

The following eval~ation criteria were used, as applicable, to assess each

functional area:

1.

Assurance of quality, including management involvement and control;

2.

  • Approach to. resolution of technical issues from a safety standpoint;

3.

Responsiveness to NRC initiatives;

4.

Enforcement history;

5.

Operational and construction events (including response to, analyses of,

reporting of, and corrective actions for);

6.

Staffing (including management); and

. .

. . .

.

7.

Effecti¥eness of trai~ing and qualification: program.

On the basis of the NRC assessment, each functional area evaluated is rated

according to three performance categories.

The definitions of these

performance categories are:

Category* l:

Licensee management attention and involvement are evident and

pl ace emphasis on superior* performance of nuclear safety or safeguards

activities, with the resulting performance substantially exceeding regulatory

requirements.

Licensee resources are ample and effectively used so that a

high level of plant and personnel performance is being achieved.

Reduced NRC

attention may be appropriate.

Category 2:

Licensee management attention to and involvement in the

performance of nuclear safety or safeguards activities is good.

The licensee

has attained a level of performance above that needed to meet regulatory

requirements..

Licensee re::;ources are adequate and reasonably a 11 ocated so

that good plant and personnel performance are being achieved.

NRC attention

should be maintained at normal levels.

_:**:. ; ':.
...

. ...... ' .....

Attachment 1

-2-

Category 3:

Licensee management attention to and involvement in the

performance of nuclear safety or safeguards activities are not sufficient.

The licensee's performance does not significantly exceed that needed to meet

minimal regulatory requirements.

Licensee.resources appear to be strained or

not effectively used.

NRC attention should be increased above normal levels.

The SALP Board may assess a functional area* and compare the licensee's

performance during a portion of the assessment period (generally the latter

part) to that during an entire period in order to determine a performance

trend.

Generally, performance in the latter part of a SALP period is compared

to the performance of the entire period.

Other trends in performance from one

period to the next may also be noted.

The trend categories used by the SALP

Board are as follows:

Improving:

Licensee performance was determined to be improving near the close

of the assessment period.

Declining:

Licensee performance was determined to be declining near the close

of the assessment period and the licensee had not successfully addressed this

pattern.

A trend is assigned only when, in the op1n1on of the SALP Board, the trend is

significant enough to be considered indicative of a likely change in the

performance category in the near future.

For example, a classification of

"Category "2~ Improvi-ng

11 indicates the clear potential for "Category 1

11

performance in the next SALP period.

It should be noted that Category 3 performance, the lowest category,

represents acceptable, although minimally. adequate, safety performance.

If at

any time the NRC concluded that a licensee was not achieving an adequate level

of safety performance, it would then be incumbent upon NRC to take prompt

appropriate action in the interest of public health and safety.

Such matters

would be dealt with independently from, and on a more urgent schedule than,

the SALP process.

It should be also noted that the industry continues to be subject to rising

performance expectations.

NRC expect£ each licensee to actively use

  • industry-wide and plant-specific operating experience in order to effect

performance improvement.

Thus, a licensee's safety performance would be

expec~ed to show improvem~nt over the years in order to maintain consistent

SALP ratings.

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