ML18082A189

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IE Insp Repts 50-272/79-32 & 50-311/79-37 on 791118-1215.No Noncompliance Noted.Major Areas Inspected:Plant Operations, Including Tours of Facility,Log & Record Review,Review of Licensee Events,Ie Circulars & Bulletins & Followup Items
ML18082A189
Person / Time
Site: Salem  PSEG icon.png
Issue date: 02/20/1980
From: Dante Johnson, Keimig R, Norholm L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML18082A188 List:
References
50-272-79-32, 50-311-79-37, NUDOCS 8004170293
Download: ML18082A189 (20)


See also: IR 05000272/1979032

Text

U. S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

50-272/79-32

Report Nos.

50~311/79-37

50-272

Docket Nos.

50-311

REGION I

DPR-70

License Nos.

CPPR-53

Priority -----

Category

c

81


Licensee:

Public Service Electric and Gas Company

80 Park Place

Newark, New Jersey

07101

Facility Name:

Salem Nuclear Generating Station - Units land 2

Inspection At:

Hancocks Bridge, New Jersey

I'nspection Conducted:* November 18 - December 15, 1979 and Januar 9, 1980

Inspectors:

Approved by:

Section

Inspection Summary:

~- z" .. F°t:J

date

~- 21J- r~

date

date

2-~t)-/"4

date

Inspections on November rn*.:.*oecember*15~ *1979 and.January 9, 1980 (Combined .

Report Nos. *50.:.272179.:.32 and*so.:.311;79.:.37)

Unit l Areas Inspected: *Routine inspections by the resident*insp~ctor of plant

operations including:

tours of the facility; log and record reviews; review of

licensee events; IE Bulletins and Circulars; implementation of licensing commit-

ments; and, followup on previous inspection items.

The inspections involved 49.

inspector-hours by the NRC resident inspector and 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> by a regional based

inspector.

  • Results£

Ohe item of noncompliance was identified. (Infraction - failure to

follow procedures, Details 7).

Region I Form 12

(Rev. April 77)

'.t

.. ..

Unit 2. Areas Inspected:

Routine inspections by the resident inspector of plant

preoperational testing including:

tours of the facility; IE Bulletins and

Circulars; reportable items under 10 CFR 50.55(e); followup on previous

inspection items; and, preparedness for issuance of an operating license.

The inspections involved 15 inspector-hours by the NRC resident inspector.

Results.:

No items of* noncompliance were identified .

l.

2 .

"DETAILS

Persons Contacted

S. LaBruna, Maintenance Engineer .

A. Meyer, Site QA Engineer

E. Meyer, Project QA Engineer

.

H. Midura, Manager - Salem Generating Station

P. Mo ell er, Associate Engineer

W. Reuther, Site QAD

F. Schna~r, Station Operating Engineer

R. Silverio, Assistant to the Manager

J. S~illman, Station QA Engineer

J. Zupko, Chief Engineer

The inspectors also interviewed and talked with other licensee personnel

during the course of the inspections including management, clerical,

maintenance, operations, performance, quality assurance, and construction

personnel.

Status of Previous Inspection Items

(Closed) Unresolved Item (272/77-24-02):

Placement of fire hose in

outdoor hose houses.

The inspector verified through observation that

hose houses were adequately equipped with fire fighting gear and were

fitted with breakaway locks.

(Closed) Follow Item (272/78-29-03): Resolution of DR PD-0607.

The

inspector reviewed documentation tracking repair of a Hagan Comparator

Module.

This module had been the cause of an inoperable pressurizer

pressure channel.

Resolution of the DR included repair of a cold solder

joint and a design change to improve voltage regulation.

The inspector

had no further questions.

(Closed)" Unresolved. Item (272/79-18-05): Nuclear Review Board Charter

rev1s1on.

The inspector reviewed NRB Charter, Revision 5, dated September

25, 1979 and noted that it was now consistent w.ith Technical Specifications

Section 6 in the area of audit coverage and membership for the NRB.

The

inspector had no further questions.

(Closed) Follow Item (272/79-22-04): Evaluation of insulation weight

omission in seismic analysis calculations. The inspector reviewed calcula-

tions made on the pipe section irr question with and without insulation

weight taken into consideration. The stress values obtained were not

significantly different. It was further noted that the insulation had

been added for personnel protection due to the proximity of the pipe to a

walkway.

The inspector.had no further questions on this item.

4

(Closed) Open Itein (311/79-03-13):

Environmental preservation controls

ror records storage in accordance with ANSI N45. 2 .* 9.

The licensee had

addressed this concern by storing duplicate records in a records storage

facility at Iron Mountain.

Transmittal on a routine basis was verified.

  • . The inspector had* no furthe.r questibns.

.

.

(Open) Unresolved Item (272/78""29-0l):

Evaluation of several vital

inverter failures during 1978.

The inspector reviewed an engineering

evaluation dated September 18, 1979, which concludes that, while the

inverters meet design criteria, modifications or replacement to improve

reliability would be desirable. This item remains open pending licensee

imp.lementation o.f an appropriate inverter improvement program.

Unit l

3.

Shift Logs and Operating. Records

a.

The inspector reviewed the following plant procedures to determine

the licensee established requirements in this area in preparation

for a review of selected logs and records.

AP-5, Operating Practices, Revision 9, April 23,. 1979;

AP"-6, Operational Incidents, Revision 6, February 22, 1979;

AP-13, Control of Lifted Leads and Jumpers, Revision 3, February

22, 1979;

Operations Directive Manual; and,

AP-15, Tagging Rules, Revision 0, April 13, 1979.

The* inspector had. no .questions tn this area.

b.

Shift logs and operating records were reviewed to verify that:

.

.

.

Control room log sheet entries are filled out and initialled;

Auxiliary fog sheets are filled out and initialled:

Log entries involving abnormal conditions' provide sufficient

  • detail to communicate equipment status, lockout status, cor-

rection* and restoration;

Log book reviews are.being conducted by the staff;

Operating orders do not conflict with Technical Specification

requirements;

5

Incident reports detail no violation of Technical Specification

LCO or reporting requirement; and,

Log's and records were maintained in accordance with Technica,l

Specifications and the procedures in 3.a above.

c.

The re.view included the fo.llowing plant shift logs and operating

records as indicated and discussed with licensee personnel:

Log No. l - Control Room Daily Log, November 16, 17, 19, 20,

25-27, 29, December 1-6,. 8-13;

  • Log No. 3 - Control Console Reading Sheet, November 16, 17, 19,

20, 25-27, 29, December l-6, 8-13;

Night Orders, October 29 - December 10, 1979

4.

Plant Tour

a.

Durihg the* course of the inspections, the inspector made observations

and conducted multiple tours of:

(l) Control Room

(2) Relay Room

(3) Auxiliary Bi.J.ilding

(4) Vital Switchgear Rooms

(5} Turbine Building

(6) Yard Areas

(7) Radwaste Building

(8) Control Point

b.

The following determinations we.re made:

(l) Monitoring instrumentation:

The inspector verified that selected

instruments were functional and demonstrated parameters within

Technical Specification limits.

(2). Valve positions.

The inspector verified that selected valves

were in the position or condition required by the Technical

Spec.i fi cations for the applicable p 1 ant mode .

(3)

(4)

(5)

(6)

(7)

6

Radiatian controls. The inspector verified by observation that

control point procedures and posting requi.rements were being

followed.

Plant housekeeping conditions.

Observations relative to plant

housekeeping and fire hazards identified no notable conditions

except for Auxiliary Building elevation 122'.* A considerable

accumulation of outage-related items has collected in this

~rea. Cleanup is in progress.

Fluid leaks.

No fluid leaks were observed which had not been

identified by station personnel with corrective action initiated,

as necessary.

Piping vibration.

No excessive piping vibration was noted

during the plant tours.

Selected pipe hangers and seismic restraints were observed and

no adverse conditions were noted.

(8). Technical specifications. Through log review and observations

during tours, the tnspector verified compliance with selected

Technical Specification Limitin~ Conditions for Operation.

The

following parameters were sampled frequently:

RHR flow rate,

Boric Acid Storage Tank levels and concentration, emergency and

off s.ite power availability, source range nuclear instrumentation,

system operability verification prior to Mode Changes.

(9) Control room annunciators.

Selected lit annunicators were

discussed with control room operators ta verify that the reasons

for them were understood and corrective action, if required,

was being taken.

(10) By frequent observation through the inspection including s.hift

turnovers., the inspector verified that control room manning*

requirements of 10 CFR 50.54(k.) and the Technical Specifications

were* being met.

In addition, the inspector observed that

frequent tours were made by shift supervision.

c.

The following acceptance criteria were used for the above items.

(1) Technical Specifications

(2) Operations Directives Manual

(3)

Inspector Judgement

d.

Except as noted above, the inspector had no questions relative to

observations during plant tours.

7

5.

Licensee Event Reports CLER' s)

a.

In Office Review of Licensee Event Reports

The .inspector reviewed LERs submitted to the *NRC:RI office to verify

that details of the event were clearly reported, including* the

accuracy of the description of cause and adequacy of corrective

action.

The inspector determined whether further information was

required from. the licensee, whether generic implications were involved,

and* whether the event warranted onsite followup.

The following LERs

were reviewed:

  • --

79-36/0lT, 4 KV Vital Bus Differential Relays Seismic Deficiency

--

79-37/03L, Source Range Nuclear InstrumentationChannel N-32

Inoperable

  • --
  • --
  • --.
  • --*
  • --

.. *--

  • --

79-38/03L, Containment Air Particulate Detector Inoperable

79-39/03L, Inadvertent Entry Into Refueling Mode 6

79-41/0lT, Loss of Eddy Current Template- Plug Assembly Inside

the Reactor* Coolant System

79-42/03L, Fire Barriers Inoperable

79-43/0lT, Auxiliary Feedwater Pumps Discharge Valves Closed

During Surveillance Testing

79;...44/03L, Damaged Fue.l Assemblies

79-45/0lT, Imperfections in Component Cooling Pump Impellers

79;...46/0lT, Linear Indications in Steam Generator Feedwater

. Nozzle Welds

.

.

79-47/03L, Failed Spid~r Fingers on Six (6) Control Rods

  • --
lc;.._
  • --
  • --

79-50/0lT, Steam Generator Water Level Instrumentation Deficiency

79-52/0lT, Steam Generator Rate of Rise Restriction

79-55/0lT, Possible Malfunction of Containment Ventilation

Isolation Valve

79-56/0lT, RHR Pump Exceeds Design Runout Flow

b.

8

  • --

79-58/0lT, Qualification of Control Systems for Adverse Environ-

mental Conditions

  • --

79-60/03L, Loss of Safeguards Manual Initiation/Reset Functions

  • --

79-6T/03L, Open Electrical Penetration Fire Barrier with No Fire

Watch

  • --

79-53/03L, Loss of Fire Suppression Systems

  • --

79-64/0lT, Low Pressure C02 Storage Tank Level Less Than Required

by Technical. Specifications

  • --

79-65/03L, Failure to Submit Temporary Changes to Station Procedures

to SORG for Review within 14 Days

  • --

79-66/03L, Meteorological Tower Instrumentation Inoperable

Onsite Licensee Ev~nt FOllowup

For those LERs selected for onsite followup (denoted by asterisks in

detail Paragraph 5.a), the inspector verified that the reporting

requirements of Technical Specifications and Regulatory Guide 1.16 had

been met, that appropriate corrective action had.been taken, that the

event was reviewed by the licensee as required.by AP-4, 6, and 7, and

that continued operation of the facility was conducted in accordance

with Technical Specification limits. The following findings relate ta*

the LERs reviewed on site*:

-.-

79-36/0lT, The initial corrective action taken consisted of

disconnecting the trip function provided by the suspect relays.

The relays have been replaced. with qualified substitutes (NRC

Inspection Report 50-272/79-25 refers).

79-39/03L, Reactor head removal is accomplished using Maintenance

nepartment Procedure* MSC,. Reactor Vessel Head and Interna 1 s

Removal and Installation. This event was caused by a failure on

the part of maintenance personnel to inform the shift supervisor

when that portion of the procedure was reached which actually

called for head detensioning and removal.

This action places the

plant in Mode 6.

The procedure has been modified (Revision ll,

dated June 25, 1979) to require a senior shift supervisor signoff

to indicate that the plant is ready to enter Mode 6.

79-41/0lT, This event resulted from failure to account for one

of 34 black plastic plugs (2" long, l" diameter) used to secure

a template inside the steam generator primary side during eddy

current testing of tubes.

The plug is assumed to have remained

inside the reactor coolant system boundary.

The inspector

9

reviewed an analysis of potential effects from continued unit

operation with the plug in the system. * The analysis concludes

that no detrimental effects will be realized from the presence

of this plug.

NRR concurs in this conclusion as documented in*

the safety analysis accompanying license Amendment 20, dated

October 30, 1979.

79"".'43/0lT, The inspector verified that the associated surveillance

test procedure had been modified to preclude isolation of

redundant pumps du.ring operability testing Of Auxiliary Feedwater

Pumps.* In addition,- this LER and a letter to NRR dated November

1, 1979, commits to locking open manually operated Auxiliary

.

-Feedwater Valves.

The inspector verified that procedure revisions

have been made to lock open the following valves:

lAFl, 11-13AF3,

ll-14AF10, 11-14AF20, 11-14AF22, and 11-14AF86.

Field verifica-

. tion of valve position and locks was also conducted by the

inspector.

The inspector had no questions.

79-44/03L, Followup on this event is documented in NRC Inspection

Repo-rts 50-272/79-15 and 79-18.

Fuel assembly grid strap

-damage is also addressed in the safety evaluation accompanying

Ticens~ Amendment 20, dated October 30, 1979 .

79-46/0lG, As a result of NOE indications found in carbon steel

component cooling pump impellers, the licensee has elected to

replace the impellers with stainless steel. This has been

accomplished on Unit 1.

The inspector had no further questions.

79-46/0lT, Cracking in the feedwater nozzle to piping weld in

all four steam generators was identified. All have been repaired.

Details of findings, repa.irs, and further evaluation are discussed

in the licensee 1 s responses to IE Bulletin 79-13 dated July 12,

August 24, and November 15, 1979 and. in NRC Inspection Report

50-272/79-24.

79-47/03L, Fo.llowup on this event is discussed* in NRC Inspection

Report 50-272/79-18.

The significance of control rod finger

separation is also addressed in the NRC safety analysis accorn-

panyi.ng Amendment 20 to the facility operating license.

--

79-48/0lT, Visible wear marks were observed on steam generator

tubes adjacent to the tube lane blocking device on steam generator

No.s. 11 , 13, and 14.

Eddy current testing confirmed wa 11

thicknes.s degradation in five tubes.

Since motion of the tube

lane blocking device appeared to have been caused by improper

installation, reassembly was done under the direction of vendor

personnel. A 11 adjacent tubes in the affected steam generators

were plugged.

10

79-50/0lT, The inspector verified that the steam generator

level trip has been raised to 11% to account for level errors

induced by an a*cci dent environment.

The potenti a 1 for 1eve1

errors has been brought to the attention of operators via

memorandum, however, no procedural change has been made to

incorporate this concern. This item is unresolved pending a

modification to operating procedures (272/79-32-01).

79-52/0lT, The licensee raised a concern that a license re-

striction on feedwater flow rate, based on water hammer consid-

erations, limited the flow to a rate less than that assumed in

. the safety analysis for auxiliary feedwater*.

License Amendment

22, dated* November 20, 1979,. removes the license condition

related to steam generator level rate to rise. The inspector

verified that station emergency procedures have been changed to

remove any restriction on feedwater flow rate whenever loss of

secondary heat sink is threatened.

Flow rate considerations to

avoid water hammer conditions are retained in operating instruc-

tions for those situations where total loss of heat sink is not

imminent.

The inspector had no further questions *.

79-55/0lT, In responding to NRR concerns, the licensee could

not demonstrate that containment ventilation butterfly valves

would close within design time intervals with a design differential

pressure across them.

In correspondence to NRR dated November

21, 1979, the licensee confirms a commitment to keep the four

36

11 purge valves shut at all times, except when required to

perform tests pursuant to the Technical Specificattons, and to

modify the operators on the 10

11 pressure/vacuum relief valves

to meet design closure specifications. The inspector verified

that administrative controls have been applied to the large

valves to preclude operation in Modes l through 4.

In addition,

vendor modifications to the 10

11 valves have been completed to

11short--stroke

11 the valves such that the full open position is

600.

79-56/0lT, Analysis related to RHR pump NPSH indicated that RHR

pump runout conditions would be experienced if, while in the

post-accident recirculation mode, one RHR pump is used to supply

two SI pumps, two charging pumps, and two cold legs directly.

Resolution was achieved by reducing the size of a downstream

flow measuring orifice such that system flow resistance increased

enough to prevent single pump runout.

The inspector verified

that the orifice modification had. been completed and the flow

instrumentation recalibrated.

79-58/0lT, A review of environmental qualifications indicated

that the following control systems could, if subjected to the

accident environment, have an impact on systems with protective

11

functions; pressurizer power operated relief valve controls,

steam generator power operated relief valve controls, main

feedwater controls, and automatic rod control. In a response

-dated October 4, 1979, to an NRR *request for information under

l 0 C_FR 50. 54( f), the licensee concludes that no modi fi cation

due to the above concerns is required, with the exception of

procedural cautions for the operator relating to steam generator

power operated relief valve misoperation which may occur on a

postulated high energy line break in a penetration area.

At

the conclusion of this inspection period, these procedure

changes had not been made..

This item is unresolved (272/79-32-02).

79*50/03L; The inspector verified by direct inspection and

review of records that a design change has been made to increase

the trip setpoint of circuit breakers providing safeguards

- reset power.

The inspector had no further questions.

79-61/03L, The inspector verified that maintenance contractor

personnel had again been notified of Maintenance Procedure M3Y

and Technical Specifications requirements relative to opened

fire barriers. Based on routine inspection observations, it is

concluded that the requirements are known to maintenance and

ope rat ions personnel.

No recurrence of this i tern has been

identified by the inspector;

79-63/03L, This is a repeated occurrence.

Administrative

controls imposed on the fire protecti~n cross-connect valve

with the Hope Creek site proved inadequate to prevent opening

of the valve and consequent drai ni.ng of the system volume below

Technical Specification limits. The inspector verified that

corrective action taken after this later event included instal-

lation of a positive locking arm and lock over the valve access

tube.

Direct knowledge of shift supervision and permission of

the Chief Engineer are now required to open valve 1FP30.

The

inspector had no further questions.

79-64/0lT, The inspector verified that changes to operating

logs have been made to raise the minimum CARDOX level to 75%.

Continual log reviews and observations relating to this specific

item have identified no recurrence.

Further concerns relative

to this item are documented in NRC Inspection Report 50-272/79-27.

79-65/03L, The inspector verified that the supervisor involved

had been reinstructed in on-the-spot change procedures.

Based

on the number of successfully executed on-the-spot changes,

this* appears to be an isolated case.

12

79-66/03L, To maintain continuity of meteorolog.ical tower

instrumentation the licensee i~ formulating plans to install*

surge protection aga.inst lightning strikes.

Pending implemen-

tation of an appropriate design change to improve meteorological

instrument .reliability, this item is unresolved (272/79-32-03).

c.

The following Licensee Event Reports required corrective action

pursuant to the license or Technical Specifications:

79-39/03L

.79-42/031

79-43/03L

79-61/03L

79*64/0lT

79-65/03L

The inspector had no further questions relative to the above LERs *

6.

Other Items

a.

As a result. of staff reviews, concerns were raised relative* to RHR

pump NPSH requirements in.the post-accident recirculation mode.

At

meetings with the staff on November 16, 1979 and November 21, 1979,.

it was determined that both Salem units would increase the number of

flow*holes in the containment sump cover, install anti-vortex baffles

in the sump, and raise the minimum NPSH level setpoint. All of

these modi fi cat ions were complete at the end of this report peri.od,

and before significant power* history had been added to the refueled

core.- on Unit l.

Thefospector had no questions re.lative to the above.

b.

On December* 10, 1979, the inspector participated in an audit conducted

by- the NRR Bulletins and Orders Task Force on site.

The subject of

this audit was implementation of NRR-approved Westinghouse guidelines

_to be used in developing small break loss of coolant accident procedures.

The audit included detailed procedures reviews and operator interviews.

The licensee had substantially followed the vendor guidelines in

modifying accident procedures. A number of comments were provided

to the licensee relative to omissions of some recommended steps ih

the procedure.

These are being evaluated by the licensee.

Some of

the comments have been incorporated. Others wi 11 not be, due to

c.

13

uniqueness in design, accident analysis considerations, or in response

to an effort to omit superfluous information from immediate action

steps in emergency instructions.

Some weaknesses were identified in operator knowledge of the TMI

accident scenario and the dynamics of saturated systems.

These will

be addressed in the licensee's continuing training program.

The inspector had no further questions in this area at this time.

The NSSS vendor, Westinghouse, had identified to the licensee and

the NRC staff a concern relative to rod control system response to a

dropped rod. * The postulated event involves a dropped rod in the

vicinity of a power range nuclear instrument detector.

Simultaneous

fa.ilure of the power auctioneering circuit could result in rod

withdrawal in response to the indicated drop in reactor power.

This

could result in an over power condition. It was agreed that automatic

rod control would be used only at less than 90% power.

Above 90%

power, automatic rod control would not be used unless Bank D rods

were at least at 215 steps.

The inspector verified that the licensee had incorporated the above*

requirements into operating procedures before returning Unit 1 to

critical operation.

The inspector had no further questions in this area.

7.

Unauthorized Tag Out of Diesel Generator (Reference: LER 79-71/03L)

.In preparation for adding lube oil to the A, B and C emergency diesels,

the automatic initiation lockout switches for the_co, Fire Suppression

System for the three diesel areas are tagged out as a safety precaution.

However, the diesel lockout switches were also tagged out at the same

time, rendering all three diesel generators inoperable.

This condition

existed for a period of 16 minutes on October 31, 1979.

Technical Specification 3.8.12 requires that with less thahthe minimum

AC electrical power sources operable, suspend all operations involving

core alterations or positive reactivity changes until the minimum required

AC electrical power sources are returned to an operable status.

During

the 16 minutes the diesels were inoperable, the plant was being maintained

in Mode 5 (cold shutdown) with no core alterations or reactivity changes

involved.

The cause of this occurrence was personnel error in that an individual

not authorized or familiar with Technical Specification requirements,

approved a tagging request without the knowledge of the responsible Shift

Supervisor.

14

The above actions were in violatio.n of Technical Speci.fication 6.8.1

requirements in that administrative controls established by Administrative

Procedure AP-2, "Station Organization", Section 5~14, AP-15, "Tagging

Rules

11

, Section6.0 and Operating Department Memo (OM-15) were not followed.

Thi~ is an item of noncompliance~ Infraction level.

Unit 2

7. * Plant Tour

a .. * .. The inspector conducted periodic tours of all accessible areas in

the plant. During these tours, the following specific items were

evaluated:

(1)

(2)

(3)

(4)

(5)

Hot Work.

Adequacy of fire prevention/protection measures

used.

Fire Equipment.

Operability and evidence of periodic inspection

of fire suppression equipment.

-

Housekeeping.

Minimal accumulations of debris and maintenance

of requ.i red cleanness levels in systems under or f o 11 owing

testing.

Equipment Preservation.

Maintenance of special preservative

measures for installed equipment as applicable.

Component Tagging.

Implementation and observance of equipment

tagging for safety or equipment protection. Authorized logs

for 5 components were selected for review.

(6) Maintenance.

Corrective maintenance in accordance with esta-

blished procedures.

(7) Instrumentation.

Adequate protection for installed instrumen"."

tat ion.

(8) .Cable Pulling.

Adequate measures taken to protect cable from

damage while being pulled~

(9) Communication.

Effectiveness of public address system in all

areas of the site.

(10) Equipment Controls.

Effectiveness of jurisdictional controls

in precluding unauthorized work on systems in test or which

have been tested .

15

(ll) Logs.

Completeness of logs maintained and resolution of identi-

fied problems.

(12) Foreign Material Exclusion.

Maintenance of controls to assure

systems which have been cleaned and flushed are not r*eopened to

admi't foreign material.

(13) Security .. Implementation of security provisions.

Particular

.attention to. maintenance of Unit 1 protected area boundary.

(14) Testing.

Spot-checks of testing in progress were made.

b.

. The following comment applies to observations made during the tours

of the plant.

During one tour, it was noted that the floor plates at elevations

100 1 and 84 1 in the Auxiliary Building had been removed.

This

provides access from a Unit 2 (unprotected) location on elevation

84

1 to Unit 1 vital areas on elevation 100 1 and 64 1 *

The

inspector questioned the effectiveness of a single armed guard

placed at elevation 100 1 to monitor the perimeter* opening.

A

guard was subsequently placed at elevation 84 1 , providing more

positive access control at the point of entry into Unit 1

areas.

The inspector* had no further questions in this area.

8.

Reports of Significant D~ficiencies

Reports of significant deficiencies, made by the applicant pursuant to 10

-CFR 50.55(e) are revfewed upon receipt, or v.erbal notification, to determine

whether reporting requirements have been met, whether sufficient detail

has been provided to assess the significance of the event, whether the

cause appears adequately defined, whether corrective action appears

appropriate, and whether generic applicability can be ascertained.

These

reports are followed lip by site inspection to verify accuracy and to

ensure that corrective actions have been implemented.

Detailed below are several reports made by the applicant for which the

above reviews were made.

a.

By correspondence dated May 2, 1979, the applicant confirmed an

April 11, 1979 telephone report to NRC Region I relating to seismically

unqualified 4 KV Bus Differential Voltage relays. This item was

also reported for Unit 1 as LER 79-36.

Corrective action consisted

of replacement with qualified relays, and this action has been

completed (NRC Inspection Report 50-311/79-27 and 79-34 refer)..

The

inspector had no further questions on this item.

16

b.

By correspondence dated July 13, ,1979, the applicant confirmed a

June*l5, 1979 telephone report to NRC Region I relating to linear

indications. identified in installed component cooling pump impellers

manufactured by Gould Pumps.

Similar findings on Unit l were reported

as LER 79-45.

Based on evaluatiOn by the vendor and applicant, all

impellers will be replaced with stainless steel. This action has

been completed on Unit l. Replacements for Unit 2 have not been

. received..

Replacement of component cooling pump impellers is an

unresolved item (311/79~37-02).

c~

By correspondence dated October 5, 1979, the applicant confirmed an

August 30, 19.79 telephone report to NRC Region I relati-ng to potential

steam generator level errors which could result from reference leg

heatup in an accident environment.

This was reported as a generic

item by Westinghouse, is the subject of IE Bulletin 79-21, and was

reported for Unit l as LER 79-46.

Corrective action includes raising

the low-low level setpoint to 11%, for which ECN 35397 has been

issued.

This is an unresolved item, pending verification that the

ECN has been accomplished (311/79-37-03).

Additional corrective

actions include procedure modificatians and will be verified by

resolution of unresolved item 272/79-32-01.

d.

By correspondence dated October 5, 1979, the applicant confirmed an

August 30, 1979 telephone report to NRC Region I relating to potent.i al

inability of containment ventilation valves to close .under design

containment differential pressure conditions. This item was also

reported for Unit l as LER 79-55.

Corrective actions are identical

to those outlined in Detail 5 of this report.

Modifications of the

Unit 2 10

11 valves has not been completed.

This is an unresolved

item pending completion and testing of the modifications (311/79-37-04).

e.

By correspondence dated October 4, 1979, the applicant confirmed an

August 30, 1979 telephone report to NRC Region I relating to potential

RHR pump runout conditions under certain post-accident operating

configurations. This item was also reported for Unit l as LER

79-56.. Corrective action for both units is the same, and consists

of modifying a flow orifice downstream of the pump to increase

piping flow resistance. Modification to the flow orifice is an

unresolved item (311/79-37-05).

f.

By correspondence dated November 14, 1979, the applicant confirmed a

Westinghouse Part 21 report relating to an undetectable failure in

the engineering safety features actuation system.

Specifically, the

P-4 permissive signal is derived from auxiliary contacts on the

reactor trip breakers.

The permissive allows manual reset and block

of safety injection only when the reactor trip breakers are open.

Misoperation of the permissive, detected only by status lights,

could prevent post-accident reset for realignment to recirculation

17

or could prevent unblocking of SI when the trip breakers are closed.

Westinghouse letter dated November 8, 1979 provides a test procedure

-to verify operability of the P-4 interlock.

The i.nspector verified

that the procedure had been successfully performed on Unit 1 prior

to Mode 4 operation. Verification of operability on Unit 2 is an

unresolved item (311/79-37-01).

No periodic test procedure has been

issued to provide continued assurance that the interlock remains

functional.

Issuance of an appropriate surveillance test is also

unr~solved (272/ 79-32~04).

The inspector had no* further questions relative to reports received from.

the applicant.

9.

Operational Readiness

10 CFR 50.57 states that the issuance of an operating license is, in

part, contingent upon a finding that construction of the facility has

been substantially completed, in conformity with the construction permit

and the application, as amended, the provisions of the Act, and the rules

and.regulations of the Commission.

In order to provide a basis for this finding, the inspector is conducting

a continuing review of licensee readiness to operate the facility.

This

review includes, but is not limited to, the following areas:

  • --

-*--

Completion of the NRC inspection program to assess construction,

testing, and operational preparedness.

Status of facility operating procedures and personnel training.

Status of all enforcement items and unresolved matters.

Status of the- preoperational test program.

Status of construction activities_

Proposed facility Technical Specifications.

Review- of licensee outstanding items, particularly those identified

for completion or resolution after core load.

Implementation of corrective measures to Unit 2 as a result of items

identified in Unit l for Reportable Occurrences, inspection findings,

and IE Bulletin and Circulars.

Operational safety concerns arising from the above reviews will be promptly

identified to facility management for resolution prior to the inspector

reaching a finding of operational readiness.

No specific safety concerns

have been identified to date.

18

Site

10.

IE Bulletin*and Circular Followup

a..

The IE Bulletins and Circulars discussed below were reviewed to verify

that:

Licensee management forwarded copies of the response to the

bulletin to appropriate onsite management representatives.

Information discussed in the licensee's reply was supported by

  • * facility records or by visual examination of the facility.

Corrective action taken was effected as described in the reply.

The licensee's reply was prompt and within th~ time period

described in the bulletin.

  • The reviews included discussions with licensee personnel and obser-

vation and review of items discussed in the details below *

. b.

By correspondence dated May 3, 1979, September 14, 1979, October 11,

1979, and October 18, 1979, the licensee responded to IE Bulletin

79-07,. Seismic Stress Analysis. of Safety Related Piping.

On November 13, 1979, the licensee's Phase I program, as defined in

the October 11 correspondence had been completed, and the unit

entered operating Mode 4.

After an intervening cooldown to repair

leaks around thermocouple seals and a pressurizer manway, criticality

was achieved on December 1, 1979.

On December 3, the reactor tripped

automatically from zero power when an.instrument technician conducting

tests on one.fntermediate range nuclear instrument channel operated

a test switch on the operating channel.

The plant was again brought

critical and startup testing resumed~

.

.

During the course of plant operation and testing, seismic reanalysis

continued.

As supports in the remaining systems to be analyzed were

identified which were deficient in design using newly calculated

loads, the associated subsystems were declared inoperable and the

appropriate Technical Specification action statement imposed.

On

December 4, 1979, a number of pipe supports in diesel generator

systems were found which failed to meet design requirements.

En-

gineering review of the calculations concluded that similar conclusions

followed relating to the same hangers on all three diesel generators.

All three diesel generators were declared inoperable and the require-

ments of Technical Specification 3.0.3 invoked.

The plant was

brought to cold shutdown.

Due to the potential for similar cases of

identical redundant system problems, a decision was made to remain

.

.

in cold shutdown .until it could be determined that all such cases

had *been re-evaluated under the conditions of IE Bulletin 79-07.

Salem Unit.l remained in Mode 5 (cold shutdown) at the end of this

reporting period.

The inspector reviewed the procedures used in the seismic: recalcu-

lations. Initially, information from field-verified piping isometrics

is. used as input to the stress program, which takes into account

. SRSS load. combinations as required by the Bulletjn.

The output data

provides piping stress values and support point loadings under

. earthquake conditions. The supports are evaluated for all three

orthogonal loads and their combinations as well as torsion loads.

Pipe stresses*.have been found to be within limits for calculations

completed to date.

Support evaluations are done separately, and

have identified approximately 800 supports requiring modifications.

A significant number of these have been pipe anchors which failed to

meet design criteria for torsion capability. The inspector identified

a sample of 50 supports which had been evaluated as unacceptable.

Quality evidence available at the site confirmed that 43 of these

had been modified.

After some research at the corporate office,

evaluations were found which concluded that the remaining 7 were

acceptable as built..

The inspector expressed his concern over the

lack of a single tracking mechanism by whkh it could be concluded

that all supports in safety related systems had been found acceptable

or had been modified.

No actual failure to account for a support

was i dent i fi ed.

The 1 i censee acknowledged the inspector 1 s concerns-.

The inspector had no further questions on this Bulletin at this

time.

c.

By correspondence dated April 4, 1979, the licensee responded to IE

Bulletin 79-03, Longitudinal Weld Defects in SA-312 Type 304 Stainless

Steel Pipe Spools Manufactured by Youngstown Welding andEngineering

Company.

The response addresses both Units 1 and 2.

The licensee

concludes that none of the suspect. material. is installed in safety.

related systems at Salem. l or 2 .. This conclusion is based* on a

review. of heat numbers for material supplied by Youngstown to eight

piping fabricators and vendors who, in turn, provided material to

the Salem project.

The inspector had no further questions on this Bulletin.

d.

By correspondence dated October 24, 1979, the licensee responded to

IE Bulletin 79-24, Frozen lines, for both Units 1 and 2.

The licensee

concludes that no unprotected safety related lines were identified

in his review.

The inspector verified that unprotected lines which

had caused problems for Salem Unit l during past winters (e.g.,

turbine impulse pressure sensor) had .also been modified through an

  • appropriate ECN on Unit 2.

20

The i.nspector had no further questions on this. Bulletin.

e.

IE Circular discussed below was reviewed to verify that. it had been

reviewed for applicability by cognizant management, and approriate

action i~itiated .

. The review included discussions with licensee personnel and observation

  • and review of items discussed in the details below. -

.

.

. .

.

. .

.

.

.

.

IE. Circular 78-19 addressed the potential for manual override

or bypass of safety system actuation signals, particularly by

reset on non-associated systems such as radiation monitoring.

The inspector reviewed a Controls Division Safety Evaluation

(CD-SE-9) dated January 10, 1979, which documents the review

conducted by the licensee.

The analysis concludes that sufficient

annunication of SI overrides at the system level are available

and that the design provides for adequate administrative control

over manual reset actions.

The inspector had no further questions relative to this Circ.ular.

ll. Unresolved Items

Areas for which more information is required to determine acceptability

are considered unresolved.

An unresolved item is contained in Paragraph

11.c of this report.

12.

Exit 1nterview

At periodic intervals during the course of this inspection, meetings were

held with senior facility management to discuss inspection scope and

findings.