ML18065A281

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Insp Rept 50-255/95-11 on 950822-1011.Violations Noted.Major Areas Inspected:Operations,Engineering,Maint,Inservice Testing & Plant Support
ML18065A281
Person / Time
Site: Palisades 
Issue date: 11/02/1995
From: Kropp W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML18065A279 List:
References
50-255-95-11, NUDOCS 9511160353
Download: ML18065A281 (16)


See also: IR 05000255/1995011

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II I

REPORT NO.

50-255/95011

FACILITY

Palisades Nuclear Generating Plant.

LICENSEE

Palisades Nuclear Generating Plant

27780 Blue Star Memorial Highway

Covert, MI 49043-9530

DATES

August 22 through October 11, 1995.

INSPECTORS.

M. Parker, Senior Resident Inspector

P. Prescott, Resident Inspector

D. Passehl, Resident Inspector

J. Cameron,. DRSS Inspector

A. Dunlop, DRS Inspector

G. Hausman, .DRS Inspector

J. Guzman, DRS Inspector

D. Hartland, DRP Inspector

I. Yin, DRS Inspector

..

APPROVED BY

-

.. ~ ,~

//,,.*.


=---;:;Q -;4c/t~

  • tl W .. J. Kropp~* Chief

/

Re'actor p.rojects *Branch 3

AREAS INSPECTED

J- :;l - f;;;~

Date

A routine, unannounced inspection of operations, engineering, maintenance,

inservice testing, and plant support was performed.

Safety assessment and

quality verification activities were routinely evaluated .

9511160353 951102

PDR

ADOCK 05000255

G

PDR

SUMMARY OF INSPECTION RESULTS

The following material condition problems occurred during this inspection

period which resulted in plant transients that challenged the plant operators:

On August 30. a power reduction was performed in order to facilitate

repairing switchyard motor operated disconnects.

Thermography results

had indicated significant hot spots.

Operator actions were good;

however, some weaknesses were noted in three-way communications.

On September 3, operators experienced a loss of load on the main

generator when the number two governor valve failed closed.

The problem

was identified as a broken wire on the number two governor valve linear

variable differential transformer (LVDT).

On September 11, operations identified broken connections between the

main generator and isophase bus.

The discovery of the problem by

operations personnel was considered good.

On September 18, two cooling tower fans lost fan blades which caused the

tripping of two other cooling fans and damage to some deluge piping

Also the vibration trip for one cooling fan did not.work.

Othar material condition issues identified during this inspection were:

  • On Septembe~ 6, the variable speed charging pump was taken ~ut of

service to repack the plungers.

The problem of short packing life

expectancy continued, even though engineering had placed significant

resources to resolving the issue.

During the plant shutdown evolution on September 11, one of the

atmospheric steam dump .valves used to maintain primary coolant system

temperature, failed to open.

The inspectors noted the number of rags to catch oil throughout the

plant was considered excessive, and was another indicator of plant

material condition.

Managemeht response to these material conditions was considered conservative.

However, based on the number of material condition issues identified soon

after a refuel outage, material condition remains an area of concern.

Control of foreign materfal continued to be a weakness.

Several examples were

detailed in the previous inspection report S0-2SS/9S009.

The inspectors were

concerned with the uncontrolled use of rags with motors in the plant.

Examples of continued FME problems are:

On September 13, during decontamination of charging pump SSA, a rag was

sucked into the motor .

2

On October 3, a rag was found in the auxiliary feed pump, P-8C. The

licensee could not determine when this may have occurred.

The unexpected control rod drive mechanism (CROM) withdrawal which

occurred in the previous inspection period, was caused by an unattached

wire lug found lodged between two terminal strip connections.

The

mechanism was worked on during the outage.

ASSESSMENT BY FUNCTIONAL AREA

OPERATIONS (section I . 0) .

Operations performance in respon.se to several events that occurred

during the inspection period was good.

.Minor weaknesses in three-way communication were identified.

Operations management made conservative decisions in response to the

events.

During routing sampling of the safety injection tank, the operators

failure to open the fill valve and his subsequent unauthorized actions

to remedy the situation compounded the problem resulting in exceeding

the one hour sampling time .

MAINTENANCE (section 2.0).

When a cont~act valve technician was injured during maintenance on the

moisture separator drain tank level control valve, the inspectors noted

  • no formal administrative measures were instituted to avoid similar

occurrences in the future.

Poor worker practices from a safety and radiological stand point were

identified by the* inspectors.

Some of these *examples occurred *during

the refuel outage, and others were from this inspection period.

The material condition problems with the cracked gene~ator isophase bus

connectors and motor operated switthyard could have been detected prior.

to the refuel outage.

Both of these problems led to plant shutdowns.

ENGINEERING (section 3.0).

During this inspection, the inspectors noted the following with engineering

evaluations:

Several submittals for a relief request to a Code alternative for the

core spray and low pressure safety injection pumps failed to have the

required technical justification and properly interpret lOCFR 50.55 a

guidance .

3

Progress appeared adequate on the P-55A charging pump packing problem

with management involvement being evident.

The tnspectors noted good

oversight of the job by engineering personnel.

Engineering resolution to a problem with bowed swithchgear cubicles was

weak.

This problem, identified a few years ago, led to station power

breaker 252-201, failing to close in.

The inspectors had the following observations pertaining to system

engineering:

During a plant tour, the inspectors noted the motor heater for the high

pressure system injection (HPSI) pump was not functioning.

This was

brought to the system engineer's attention.

The system engineer was

unaware of the existence of the motor heaters.

The system engineer

decided to check all safety-related pumps.

Duri~g the check of the status of motor heaters, the system engineer

found a rag in the air intake of the motor driven auxiliary feedwater

pump,

P~BC. The inspectors felt this was a good example of. thorough

followup of an issue.

PLANT SUPPORT (section 4.0).

The inspectors identified the following concerns:

The licensee experienced numerous challenges during the outage in

controlling station radiation dose and radiation worker practices, as

well as the pre-outage planning of ALARA packages.

Communication of management expectations app*eared weak in the area of

radiological protection.

During this inspection period, the residents also continued to identify

poor radiation work practices.

Summary Of Open Items

Violation:

One violation was identified.

The violation described in

paragraph 2.3.3 of the inspection report involved the failure to obtain* NRC

approval of reli~f request number 4, which established alternative vibration

acceptance criteria for the low pressure safety injection and containment

spray pumps (255/95011-01) .

4

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1.0

1.1

1.2

INSPECTION DETAILS

OPERATIONS

NRC Inspection Procedures 71707 were used in the performance of an

inspection of ongoing plant operations.

Switchyard Motor Operated Disconnect Repairs

On August 29, 1995, the licensee was notified of the results of

thermography testing performed in the switchyard. Thermography results

indicated significant hot spots {high resistance) on the "X" and "Z"

phases of the motor operated disconnect {26H5 MOD) in the switchyard

from the main transformer.

The thermography results noted the

temperature to be 120° C. above ambient on the "z" phase.

Normal

expected temperature is approximately 10° C. above ambient.

The

licensee's Lab Services Division recommends that the plant take action

to correct the problem when the temperature is greater than 40° C. above

ambient~ The main disconnects are unisolable from the switchyard

without taking the generator off line.* At midnight on August 30, 1995,

the licensee initiated a power reduction to 50 percent power.

At this

power level the temperature dropped to less than 53° C. above ambient

temperature.

The vendor recommendation for continuous operation is less

than 53° C.

Pl~nt operators commenced a further power reduction on

September 1, 1995, in preparation for taking the unit offline. The main

generator was taken of fl i ne on September 2, 1995.

The licensee

completed the necessary repairs to the motor operated disconnects in the

switchyard along with a short forced outage repairs and returned the

uriit back to service on September 2, 1995.

Damaged Isophase Bus Connectors

On September 11, 1995, the licensee reduced power to two percent and

took the main generator off-line.after discovering some damage to a

isophase bus flexible connector.

The connector was one of eight for

each phase which linked the main generator to the bus.

Each connector

was comprised of 44 individual copper sheets which were layered to form

a single bus bar.

The licensee discovered that six of the layers were

completely severed on the damaged connector and that a seventh layer was

cracked.* The licensee inspected the other connectors and discovered

cracks on one located on a different phase.

The licensee attributed the

damage to vibration-induced fatigue. Analysis of the connectors by the.

l.icensee's laboratory is still pending.

Due to 'the unavailability of replacement parts, the licensee performed a

temporary repair of the damaged connectors.

The licensee removed the

severed layers and installed stainless steel hardware on both ends of

each connector to aid in relieving stresses at those areas.

Following

the repairs, the licensee returned the unit* to service on September

13th.

The licensee intended to replace all of the connectors during a

future forced outage.

In the meantime, the licensee wa~ performing

5

.* ..

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1.3

2.0

periodic inspections of the connectors to ensure that further damage

does not develop. The inspectors expressed concern that not all

connections can be visually checked during operation.

Station Power Breaker Trip

On September 13, 1995, while transferring the 4160V non-safeguards bus

lB from startup to station power, breaker 252-201 failed to close during

the initial two attempts.

The feed from start-up power remained closed

during the attempts, which prevented de-energization of the bus~ The

licensee determined that the cause of the problem was vibration induced

during breaker closure due to bowed metal on the bottom of the cubicle. *

The vibration was transmitted to the breaker's foot pedal which impacted

the tfip latch; As corrective action, the licensee te~porarily *

installed some vice grips to secure the pedal in place during the

breaker closure. The licensee intends to* install a temporary

modification to bolt the pedal in place during a future activity

requiring operation of the breaker.

During follow-up discussions with the system ~ngineer, the inspectors

determined that the condition did not affect the auto-trip* function of

the breaker.

In addition, the system engineer was not concerned about a

spurious trip of the breaker, which would result in a reactor trip, due

to the magnitude of vibration required to trip the latch.

The inspectors als~ discovered that the licensee had identified the

problem with the bowed cubicle a few years ago after experiencing some .

problems with other breakers located adjacent to 252-201.

The licensee

determined at that time that the cause of the bowed cubicles was water

intrusion from outside a turbine building roll-up door*lo.cated near the

cubicles.

As corrective action to this condition, the licensee*bolted

down the bowed. cubicles during the last refueling outage.

However, this

action did not prevent the latest problem with breaker 252-201.

The

inspectors will review the licensee's investigation of C-PAL-95-1387,

which was initiated to document the condition, to ensure that actions

are taken to prevent recurrence.

MAINTENANCE

_NRC Inspection Procedures 62703, 61726 and 73756 were used to perform an

inspection of maintenance and testing activities.

2.1

Maintenance Activities

Portions of the.following maintenance activities were observed or

reviewed:

  • Repair of CV-0608, heater drain valve
  • Repair of motor operated disconnect (26H5 MOD)
  • Temporary repair of damaged isophase bus connector
  • Troubleshooting boric acid pump piping heat tracing
  • Governor valve no. 2, repair broken wire

6

  • Installation of 3/4" drain line on P-55A, charging pump
  • Installation of seal water filter and flow re.gulating valve on P-55A

2.1.1 Technicians Injured During Valve Troubleshooting

A contract valve technician was injured during maintenance to repair a

flow problem on moisture separator drain tank {MSDT) level control valve

CV-0608.

Maintenance technicians were troubleshooting CV-0608 to

investigate the reason why the valve would not automatically control

MSOT level. The upstream and downstream manual isolation valves were.

closed; however, the isolation valves were known to have seat leakage.

Further, there was no vent path to relieve internal system pressure

prior to starting work.

Workers were aware that the piping adjacent to

CV-0608 was pressurized prior to working the valve.

The work plan

instructed maintenance workers to adjust the valve's position to allow

the V-Ball inside CV-0608 to pass full flow when actuator was fn the

full open position.

The intent and nature of the work was not to breach

the pressure boundary.

However, during the initial disassembly to

-

adjust the position, the valve stem unexpectedly ejected from CV~0608,

allowing water at approximately 300 °F and 500 psig in the adjacent

piping to escape and flash to steam.

The worker closest to the valve

received serious burns; two others receiv~d less serious injuries. All

three workers were treated at area hd~pitals.

The licensee's initial *investfgation found that the split ring and

retaining rings on both ends of the valve stem were missing~ The split

and retaining rings would have held the stem in place during the

position adjustments.

The licensee concluded that the rings were

gradually worn away during plant op~ration, probably since 1988, when

maintenance ~as last performed on CV-0608.

The root cause of the

missing rings was indeterminate at the close of the inspection period.

The inspector found that the licensee's immediate response of taking

care of the injured workers and quarantining the area around the valve

was satisfactory.

The licensee's followup actions to replace CV-0608

with a new valve, and to modify the adjacent piping by installing a

vent, were acceptable.

The licensee decided not to initiate a work

request to repair the leaking isolation valves. This was based on the

installation of the vent, and the size of the leak, which was determined

to be fairly small.

The licensee is continuing to work with the vendor

to further investigate this event.

2.1.2 Poor Worker Practices

During troubleshooting of the boric acid pump system line heat tracing;

an inspector observed a worker in a designated contaminated area without

rubber booties, only cloth booties. Also the same worker was observed

stepping on heat traced piping., rather than using a ladder to work on a

junction box.

  • *

.7

--*

The inspector monitored installation of a modification to the P-55A

charging pump.

The modification involved installation of a filter to

the seal water line and rerouting of the seal drain line. A worker came

down to discuss problems being encountered during the modification

without a hard hat and ear plugs.

During decontamination activities on the "A" evaporator, a worker was

observed leaving the immediate area with his dosimetry and TLD on the

stepoff pad, to get poly bags for tools and trash, rather than keeping

his dosimetry with him.

2.2

Surveillance Activities

Portions of the following surveillance activities were observed or*

reviewed:

  • SOP-3, Safety Injection Tank Boron Sample
  • Ml-43, Reactor Vessel Level Monitoring System Channel Check

NMS~l-7, ExCore Monitoring Calibration

2.2.1 Safety Injection Tank (SIT) Sampling

On September 15, 1995, control operators initiated a routine sampling of

SIT-82A per Standard Operating Procedure (SOP-3).

During sampling, the

SIT pressure and_ level dropped below technical specification (TS) values

as expected, resulting in the licensee entering a one hour TS LCO .

After obtaining the SIT sample, control operators attempted to restore

the tank level and pressure by refilling the tank utilizing the high

pressure safety injection (HPSI) system.

Operators were unable to

achieve a normal f i 11 rate and noted a slow rise in both tank level and

pressure, but observed that -relief valve RV-3161 had lifted. Operators

throttled M0-3068 in an attempt to keep RV-3161 closed.

In an attempt

to facilitate the- fill, the control operator reduced T-82A pressure to

increase the fill rate. During the fill, it was observed that the SIT

fill and drain valve, CV-3039, was closed.

SOP-3 was reviewed and CV-

3039 was opened in accordance with procedure steps~ Level was restored

at the normal fill rate.

Level was restored to within the TS value

within the required time limit of one hour; however, due to the venting

of T-82A pressure by the operator, nitrogen addition was required to

restore nitrogen pressure to normal.

The subsequent nitrogen addition

exceeded the TS limit and resulted in the licensee entering a more

restrictive TS LCO.

TS 3.3.2 requires that if the SIT is not restored

to service within one hour, that the reactor be placed in hot shutdown

within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

The operators subsequently restored pressure within

the following 14 minutes (total LCO time 74 minutes). Although the

licensee determined that a violation of TS did not occur, the failure of

the operator to follow SOP-3 caused the licensee to exceed the one hour

TS LCO.

In addition, the shift's action to remedy the situation further

complicated and extended the out of service time, resulting in

exceeding the one hour LCO.

This licensee-identified and corrected

violation is being treated as a Non-Cited Violation, consistent with

Section VII of the *NRC Enforcement Policy.

8

2.3

Inservice Test Program (ISTl

The inspectors noted that the second IO-year IST i nterva 1 ended. in May

I995, and the licensee commenced the third IO-year program when they

exited the refueling outage in August 1995 .. The second IO-year program

was based on the 1983 edition of the ASHE Code, while the new program

was based on the 1989 edition (OM standards).

The new program was not

yet approved by the licensee or submitted to the NRC, although test

procedures were being revised to incorporate the new testing

requirements prior to their performance.

The inspectors reviewed the Safety Evaluation Report (SER) for the

second IO-year IST interval, dated April 20, I995, to determine the

status of relief requests that need approval prior to implementation.

Relief request number 4 was approved to use OM-6 for the second IO-year

IST interval; however, it denied the alternative to the Code vibration

limits for the containment spray (CS) and low pressure safety injection

(LPSI) pumps.

The licensee; however, previously i~plemented the revised

vibration limits for these pumps without prior NRC approval.

2.3.1 Background

The licensee initially requested relief to use velocity versus mils for

vibration measurements in a submittal dated June 28~ 1991.

The relief

stated prior NRC approval was not required as it met the guidance in

Generic Letter (GL) 89-04, "Guidance on Developing Acceptable Inservice

Test Programs."

However, this issue; was not addressed in the GL as

stated in a SER dated July 15, 1992.

The SER also denied this request

based on lack of information on the pumps, such as specific velocity

ranges for which this relief request applied.

Based on a

misunderstanding that prior approval was not required, the licensee had

previously implemented this relief request.

The relief request was resubmitted on December 29, 1992, which

identified the CS and LPSI pumps as'the components that required the

relief and provided specific velocity ranges.

The alert and required

action ranges for these pumps exceeded the OM-6 absolute limits, which

were approved for use by ASME Code Case 465 and 10 CFR 55.55a.

As

discussed above, this relief was also denied.

The SER stated that the

licensee must continue to meet the Code requirements for these pumps.

The SER further stated that if the licensee believed additional

information would support approval of an increased alert. range (required

action range maintained at OM-6 limits), a relief request should be

submitted with the third IO-year program; however, submittal with the

third ten-year interval program did not imply that the requirement to

meet the Code in the interim was not required.

The licensee revised the

test procedures to incorporate the OM-6 required action range; however,

in most cases the alert ranges were deleted or exceeded the OM-6

absolute limits. A relief request, however, was not submitted

requesting approval to use this alternative, yet the alternative was

implemented by the licensee .

9

-~*

2.3.2 Discussion

The licensee believed that changing Code acceptance criteria was allowed

by 10 CFR 50.55a(f)(5)(iv) since it was impractical to meet the Code

limits during low flow testing. The use of impracticality in this

context was incorrect, as impractical conditions apply to physical

design constraints or high dose rate due to design configurations, and

not to elements of the required testing, with possible exceptions where

physical constraints actually limit the licensee's ability to perform

elements of the test. This was riot the case in the specific testing, as

the options open to the licensee included placing the pumps on an

increased testing frequency during an interim period while awaiting NRC

approval of the requested alternative. The establishment of less

conservative vibration limits than required by the Code would constitute

an alternative to the Code and required prior NRC approval before

implementation.

The NRC issued guidance on implementing alternatives to

Code requirements in Section 6 of NUREG-1482.

2.3.3 Conclusion

2.4

Since implementation of the Code alternative was not authorized prior to

implementation, this is considered ~ violation {255/95011-01) of 10 CFR

50.55a(3).

The licensee did not identify any additional relief requests

for the third 10-year interval that required prior NRC approval .

. The licensee submitted a revised relief request, dated September 18,

1995, that proposed an alert limit established based on past pump

hi story for each bearing direction. * The required action range for the

pumps would not exceed the OM-6 absolute limits. Until this relief is

approved by the NRC, the licensee stated alert limits would be in

accordance with OM-6 and increased testing would be performed as

necessary to meet the Code requirements.

Action on Previous Inspection Findings

2.4.1 (Closed) Unresolved Item 50-255/92028-01:

This item concerned the

adequacy of low flow inservice test (IST) of the P-8B auxiliary

feedwater pump (AFW) to ensure the pump's operational readiness .. Based

on discussions with NRR, it was concluded that the flow rates used fo~

IST could be determined by the licensee as the ASME Code only specifies

a repeatable value for the t~st. The licensee; however, must ensure

that the testing used to verify the pump's operational readiness was

acceptable to meet design requirements.

The licensee performed the full

flow special test T-187, "AFW Turbine K-8 and Pump P-8B Performance," on

a 10 year frequency or following major maintenance.

Although the pump*

performance was less than the original pump curve during the tests

performed in 1990 and 1991, the pump still met the design requirements.

Based on the 1991 test results, the pump has a 50 gpm margin.

The

licensee also performed a correlation of the design requirements and the

acceptance criteria established in the IST.

The IST acceptance criteria

appeared to provide sufficient assurance that the licensee would be able

to verify AFW pump degradation.

This item is closed.

10

2.4.2 (Closed) Violation 50-255/92028-02: This item concerned the inadequate

acceptance criteria for testing the low pressure safety injection (LPSI)

and primary coolant system (PCS) loop check valves to the full open

position. Q0-88, "ESS theck Valve Operability Test," was revised to

incorporate the design required flow rate of 1601 gpm for the LPSI *check

valves as determined by engineering analysis EA-E-PAL-93-004E-Ol.

The

valves successfully met the acceptance criteria during subsequent tests.

The PCS loop check valves were full stroked per R0-105, "Full Flow Test

for SIT Check Valves and PCS Loop Check Valves," with the use of non-

intrusive testing techniques during the 1995 refuel outage.

The PCS

loop check valves were also partially stroked per Q0-88 on a cold

shutdown frequency.

The licensee also reviewed other check valves in the IST program to

. ensure test procedures contained adequate acceptance criteria to verify

the full open stroke test. Several discrepancies were identified and in

most cases adequately resolved.

However, the resolution identified in

E-PAL-93-004-0 for check valves CVC-2099 and CVC-2105 did not appear

appropriate.

The maximum accident flow the valves were required to pass

was 40 gpm; however, the test procedure, Q0-17, "lnservice Test

Procedure: Charging Pumps," a~ceptance criteria was based on the

acceptance criteria for the positive displacement pump, which could be

as low as 35.1 gpm.

This did not meet the guidance in Generic Letter 89-04, Position 1.

The licensee previously performed non-intrusive testing {NIT) on these

valves~ which indicated the valves would open at the lower flow rate.

The NIT was going to be performed on a refueling outage frequency {one

valve every other outage).

NUREG-1482, "Guidelines for Inservice

Testing at Nuclear Power Plants," section 4.1.2; stated that a sampling

program for NIT could be used; however, the sampling must be performed

based on the testing frequency.

Since the valves were tested on a

quarterly basis, the NIT must also be on one of the valves each quarter.

The licensee indicated the procedure would be revised to include NIT on

a quarterly sampling basis. This item is closed.

3.4.3 (Closed) Violation 50-255/94014-29:

This item concerned the failure to

test check valves CVC-2138 and CVC-2139 to the full open position.

Surveillance procedure Q0-18, "Inservice Test Procedure: Conceritrated

Boric Acid Pumps," was revised and the valves tested in May 1994.

This

item is closed.

3.0

ENGINEERING

3.1

NRC Inspection Procedure 37551 was used to perform an inspection of

engineering activities. The findings showed performance was good.

Unexpected Control Rod Withdrawal:

On August 17, 1995, during low power physics testing, the licensee

experienced a control rod drive mechanism (CROM) withdrawal demand when

a CROM insertion demand was initiated. The control room operators were

11

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3.2

3.2.1

inserting the Group 4 control rods {38, 39, 40 and 41}, when a rod

deviation alarm was received. Subsequent checks determined that control

rod 40 was greater than 4 inches higher than the other Group 4 control

rods and had traveled in the opposite direction.

CROM-40 was declared

inoperable and the reactor was borated to a shutdown condition for

troubleshooting (see LER 255/95011}.

The licensee replaced CROM-40 and determined that a foreign material

exclusion (FME} problem caused the CRDM-40 failure.

Visual inspection

of CROM-40's motor junction box, revealed that the "up" and "down" limit

switches (LS-40/1 and LS-40/2, respectively) were shorted by an

unattached wire lug.

The unattached wire lug was found lodged between

the LS-40/1 and LS-40/2 terminal strip connections.* Several CROMs were

worked on during the recent outage; however, the exact time when the

wire lug was introduced into the motor junction box could not be

determined.

The licensee speculated that the FME problem was probably

introduced during earlier maintenance work.

CROM ground detection troubleshooting isolated a 45-50 Vac (400 Hertz)

ground in CROM-15.

The CRDMs power source was ungrounded and the

circuitry did not contain a ground detection system." As a result,

ground detection troubleshooting was performed to determine if CROM-40

was masking an additional problem.

Troubleshooting isolated the ground

-to CROM-15, which was removed and subsequently replaced with the

original retested CROM-40 .

The inspe.ctors concluded that the licensee's investigation, evaluation

and resolution of the CROM withdrawal problem was good.

A team approach

was taken for coordination of the conducted activities. Engineering

directed troubleshooting efforts to isolate and evaluate the problem.

Operations was actively involved in the engineering directed effort.

Steps were taken to ensure that all personnel were aware of their

assigned tasks.

The licensee issued an informational licensee event

report (LER) 255/95011, which identif~ed the proposed long term

corrective actions.

Action on Previous Inspection Findings

CClrised) LER 255/92026-01: The licensee failed to ensure changes to

station operating procedures did not conflict system configuration

requirements identified in the licensee design basis documents.

The

affected operation was revised.

The licensee follow up actions were

considered adequate.

This LER is closed.

3.2.2 (Closed) LER 255/94006: February 1994 through-wall leak of containment

sump check valve CK-ES3166.

The plant was taken to cold shutdown and

actions were initiated to identify the failure mechanism, the extent of

degradation,

repair method, and actions required to prevent recurrence.

Metallurgical analyses and nondestructive examination techniques were

used to identify the failure mechanism as intergranular attack (IGA) due

to sensitization in a weld-repaired region of the valve casting. These

welds were made during the time of original plant construction.

12

  • ,,

The repair consisted of a weld overlay on the check valve (and also~

conservatively, on the opposite train valve, CK-ES-3181) per ASME Code

Case N504-1.

The repair efforts were reviewed by both NRC Region III

and NRR cognizant engineers and were found to be satisfactory. The

repair process and actions taken are described in further detail in

inspection report 50-255/94004.

To prevent recurrence, Palisades reassessed stainless steel weld

practices to ensure controls exist to minimize corrosion stemming from

IGA, performed a historical review of modifications to identify high

risk susceptible components, and completed further destructive

metallurgical exams to evaluate the prevalence of IGA on susceptible

components.

The destructive testing was conducted on similar check

valves that were used in a similar service and enviroriment that were

replaced in 1995.

No IGA or cracking was observed. These actions were

reviewed by the NRC and found acceptable. This LER is closed .

. 3.2.3 {Closed) Unresolved Item 50-255/92028-03:

This item concerned the

capability of the fire water system to provide a backup water supply to

the AFW system.

The licensee developed engineering analysis EA-A-PAL-

94-095 that verified the fire water system would be able to provide

sufficient net positive suction head (NPSH) to the AF.W pumps as required

by Technical Specifications. This item is closed.

3.2.4 {Closed) Inspection Follow-up Item 50-255/94014-26:

This item concerned

the component cooling water (CCW) heat exchanger differential pressure

and CCW flow correlation to determined flow rate from special test T-213

used in the CCW pump tests~ The DET also identified that during a

licensee review in late 1993, two questions were identified with the

curve developed by T-213.

These were documented on D~PAL-93-272 in

January 1994.

First, the curve did not take the expected hyperbolic

sh.ape, but was more of a straight line. .The second question concerned

the lack of verification of valve positions *in the test flow path.

The licensee conducted T-213 during the recent refueling outage.

The

test ensured valves in the test flow path were in.the open position

prior to performance.

The curve produced by test, when extrapolated,

produced the expected hyperbolic shape.

The licensee was still

reviewing the test results to determine if any changes needed to be made

to the IST pump test. Based on these results and intended actions, this

item is closed.

3.2.5 (Closed) Inspection Follow-up Item 50-255/94014-27:

This item concerned

the root cause of a stroke time increase for motor-operated valves M0-

3064 and M0-3066.

The valves' gear ratios were modified in the 1993

refuel outage.

The next two ISTs showed no change in the valve stroke

times and as such, the valves' reference values were not changed.

The

stroke time in December 1993, and subsequent test data increased from

  • the previous measurements.

The licensee contributed the stroke time

increase to the gear change modification, although initial testing did

not indicate an increase in the stroke time .. The licensee was unable to

determine why the stroke times did not increase initially with the gear

13

, ...

3.2.6

change modification. Test results since December 1993 remained

consistent. Based on the consistent test results, there did not appear

to be a problem with the valves.

This item is closed.

(Closed) Inspection Follow-up Item 50-255/94014-30:

This item concerned

the testing of manual valve FW-150, which was relied on in emergency

operating procedures to be used as a backup steam supply regulator for

the AFW turbine driven pump.

Based on the plant's design basis, the

licensee concluded that the valve did not meet the criteria for

inclusion in the IST program; however, a periodic predetermined activity

control (PPAC) was developed to lubricate and stroke the valve on a

yearly basis.

The inspectors considered this acceptable.

The PPAC,

however, was not performed as scheduled during the recent refuel outage.

A corrective action document was initiated to address the missed PPAC.

The valve was successfully exercised on September 18, 1995.

This item

is closed.'

3.2. 7 COPEN> LER 50-255/95006: Inadequate auxiliary feedwater pump low suction

pressure trip setpoints. Originally identified on condition report C-

PAL-95-0877, the design of the AFW pump suction did not adequately

consider pump protection form air entrapment at low condensate storage

tank levels.

Inspectors reviewed the corrective*actions specified for

the AFW system and concluded that they were acceptable.

The lER also

raised a concern with the suction from the safety injection and

refueling water tank (SIRW) and concluded that it was acceptable based

on engineering judgement.

Further evaluation was *planned for the SIRW

and other large pumps; therefore this LER is open pending completion of

the licensee's evaluation. *

4.0

PLANT SUPPORT

4 .1

NRC Inspection Procedure 83750 was used to perform an inspection of

Plant Support Activities, with an emphasis on outage activities. The

level of performance in radiological protection was considered adequate.

No single finding was considered significant; however, the licensee *

experienced numerous challenges during the outage in controlling station

radiation dose and radiation worker practices, as well as the pre-outage

planning of ALARA packages.

The underlying weakness appeared to be

ineffective communication of management expectations in the area of

radiological protection.

External Exposure Control

The licensee completed the outage on August 17, 1995 with an outage dose

of 348 person-rem (3.48 person-sievert), versus an outage ALARA goal of

286 person-rem (2.86 person-sievert).

The outage dose was based upon

electronic dosimeter (ED) readings.

Actual reported doses will be based

upon thermoluminescent dosimeter (TLD) readings and will be 10 to 14

percent higher.

The reason for the higher TLD readings is discussed

below in Section 4.4. Notwithstanding the higher TLD readings, the

licensee experienced several challenges in meeting its outage ALARA

goal.

Two primary reasons for this were poo*r radiation work.er practices

14

  • 4.2

4.3

and mixed performance du,ring the prejob ALARA reviews..

Both of those

challenges were discussed in Inspection Report 50-255/95008{DRP) and

additional information is provided below.

Pre-Job ALARA Planning

The licensee's performance during the completion of pre-job ALARA

reviews was mixed.

Although some reviews exhibited e*xce 11 ent

performance and vigilance on the part of ALARA planners, such as the 1-

24, or reactor vessel internals inspection project, the planners showed

poor performance in others, namely, the Alloy 600 ~roject. The initial

dose projections indicated 32 person-rem for the I-24 project. A

majority of the work was to be performed by workers standing on the edge

of the reactor vessel over a dry cavity.

The ALARA group rejected that

dose projection and sent the package back to the project engineers for

dose savings techniques. Through various changes to the work package,

including the use of a mock-up and partially filling the cavity, the

revised dose projection was 4.8 person-rem.

The actual total dose for

the project was 4.2 person-rem.

The licensee's challenges with regard

to the Alloy 600 project are fully described in Inspection Report 50-

255/95008(DRP).

In summary, due to equipment clearance constraints and

the erroneous use of the vendor's time estimate to complete the project,

the licensee's total dose for the Alloy 600 inspection project was 23

person-rem, versus an ALARA projection of 11 person-rem.

Radiation Worker (Radworker) Practices

Inspection Report 50-255/95008(DRP) described inspector observations of

poor radworker practices during the performance of two projects with

high radiological significance; the removal of the Core Support Barrel

and the Transfer of the Incore Detector Cask.

During both projects, the

inspectors observed radworkers loitering in areas with elevated dose

rates.

In neither case were the workers' behavior challenged,

suggesting a lack of aggressiveness by the licensee in reducing

individual dose.

Although these two projects are the only ones observed

by the inspectors that i-nvo 1 ved poor radworker practices, other

.

information was available to suggest that these were not isolated cases.

During the review of personnel contamination incidents (PCis), the

inspector observed an adverse trend in the number of PCis early in the

outage.

At the end of the outage, the licensee had recorded

approximately 1000 PCis.

Although none of the PCis were radiologically

significant to the contaminated individuals, they do suggest unchecked

poor radworker practices in contaminated areas.

The licensee.

..

acknowledged this possibility and was in the process of developing plans

to limit PCis and correct the poor radworker practices. Details of

those plans were not immediately available, but will be reviewed during

future inspections prior to the next outage .

15

4.4

Electronic Dosimeter/TLD Discrepancies

5.0

Personnel radiation dose received during the second quarter of 1995, as

determined by TLD, exceeded the dose recorded by electronic dosimetry

(ED).

Prior to the outage, the licensee changed vendors for the supply

and processing of TLDs, the primary source of recording exposure.

Due

to differences in the processing technique of each vendor, the average

TLD dose deviation between the two vendors was 12 percent.

The previous

vendor, actually the Consumers Power Co. laboratory, consistently

reported doses that were approximately 4 percent lower than the expected

dose on spiked TLDs.

The new vendor, a laboratory independent of

Consumers Power Co., reported doses that were approximately 8 percent

higher that the expected dose on spiked TLDs.

Differences of 10 percent

are acceptable for NVLAP.accreditation.

Since the EOs were calibrated

against expected TLD results from the former processor, this resulted in

them reading less than the TLD results from the new processor. Thus,

the outage dose, as reported to date via ED results, will be adjusted

higher approximately 12 percent, based on actual TLD readings, which are

reported quarterly, when they become available.

The adjusted exposure

results will not result in anyone receiving a reported dose in excess of

NRC regulatory, or licensee administrative, dose limits.

PERSONS CONTACTED AND MANAGEMENT MEETINGS

The inspectors contacted various licensee operations, maintenance,

engineering, and plant support personnel throughout the inspection

period.

Senior personnel* are listed below .

At the conclusion of the inspection on October 11, 1995, the inspectors

met with licensee representatives (denoted by*) and *summarized the

scope and findings of the inspection activities. The licensee did not

identify any of the documents or processes reviewed by the inspectors

are proprietary.

R. A.

  • T. J.
  • K. P.

G. B.

R. M.

  • O. W.
  • D. J.

s. y.

  • R. B.
  • C. R.

J. P.

H. L.

D. P.

  • D. W.
  • R. A .

Fenech, Vice President, Nuclear Operations

Palmisano, Plant General Manager

Powers, Nuclear Services General Manager

Szczotka, Nuclear Performance Assessment Manager

Swanson, Design Engineering Manager

Rogers, Operations Manager

Malone, Chemical & Radiological Services Manager

Wawro, Planning & Scheduling Manager

Kasper, Maintenance & Construction Manager

Ritt, Admini*stration Manager

Pomaranski, Deputy Maintenance & Construction Manager

Linsinbigler, Projects & Contracts Manager

Fadel, System Engineering Manager

Smedley, Licensing Manger

Vincent, Licensing Supervisor

16