05000255/LER-1980-020-01, /01T-0:on 800711,control Rod Drive Mechanism Failed to Operate Properly,Resulting in Rod Being Misaligned for Approx Five Minutes.Caused by Dirty Control Relay Armatures & Contractor Interlock Which Resulted in Sticking

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/01T-0:on 800711,control Rod Drive Mechanism Failed to Operate Properly,Resulting in Rod Being Misaligned for Approx Five Minutes.Caused by Dirty Control Relay Armatures & Contractor Interlock Which Resulted in Sticking
ML18045A421
Person / Time
Site: Palisades Entergy icon.png
Issue date: 07/29/1980
From:
CONSUMERS ENERGY CO. (FORMERLY CONSUMERS POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML18045A420 List:
References
LER-80-020-01T, LER-80-20-1T, NUDOCS 8008050080
Download: ML18045A421 (1)


LER-1980-020, /01T-0:on 800711,control Rod Drive Mechanism Failed to Operate Properly,Resulting in Rod Being Misaligned for Approx Five Minutes.Caused by Dirty Control Relay Armatures & Contractor Interlock Which Resulted in Sticking
Event date:
Report date:
2551980020R01 - NRC Website

text

"4 PALISADES PLANT NRC FORM366 17-771 U.S. NUCLEAR REGULATORV COMMISSION LICENSEE EVENT REPORT CONTROL BLOCK: I 10 IP'LEASE PRINT OR TYPE ALL REQUIRED INFORMAT10NI 1

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REP'ORT DATE ID EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES {iO)

[))IJ I Following control rod ma.nipula't1.ons during normal pover. operation, III!J CRDM No 39 drove in *apPro.x 39 inches.

As a result I the rad vas

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misaligned :from the remaining rods in its group for about 5 minutes *

!l!Imedia:te action consisted o:f halting rod invard I110tion, manual exercising [TI]) I

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Reportable per TS S-5.1 and 3.10. 4c.

Similar event occurred on July 24,

[)))) 1 1980, b'at did not result in misaligned rod.

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OJ:[] I CRDM control relay armatures and UP/do'W?l contractor interlock were dirty.

causing them to stick.

Contactors and interlock for CRDM 39 have been cleaned and lubricated.

Cleaning and lubrication of remaining contactors IIIIJ 1 is in progress.

A PM to perform this function on a re:fueling G:ycle is [Ir!J I being developed.

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