ML18038B486
| ML18038B486 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 10/11/1995 |
| From: | Lesser M, Wert L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18038B484 | List: |
| References | |
| 50-259-95-51, 50-260-95-51, 50-296-95-51, NUDOCS 9510240130 | |
| Download: ML18038B486 (80) | |
See also: IR 05000259/1995051
Text
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UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W., SUITE 2900
ATLANTA,GEORGIA 303234199
Report Nos.:
50-259/95-51,
50-260/95-51,
and 50-296/95-51
Licensee:
Valley Authority
6N 38A 'Lookout Pl ace
1101 Market Street
Chattanooga,
TN
37402-2801
Docket Nos.:
50-259,
50-260
License Nos.:
and 50-296
Facility Name:
Browns Ferry Units 1, 2,
and
3
Inspection at Browns Ferry Site near Decatur,
Inspection
Conducted:
August
13 - September
16,
1995
Inspector:
eonar
.
ert
J.
Hunday,
Resident
R. Husser,
Resident
H. Morgan, Resident
r.,
r.
ess
ent
nspector
Inspector
Inspector
Inspector
Approved by:
ar
.
esser,
ctlng
rane
1e
Reactor Projects,
Branch
4
Division of Reactor Projects
ate
1gne
SUMMARY
Scope:
This routine resident
inspection
involved inspection on-site in the areas of
operations
and plant support,
maintenance
and surveillance activities, Unit 3
recovery actions,
and review of open items, including
a Three Mile Island
item.
The Unit 3 inspection
included
numerous testing activities,
system
preoperational
checklist reviews,
drawing issues,
and review of foreign
material exclusion problems.
Testing of residual
heat removal, control air,
and
common accident signal logic was observed/reviewed
in detail.
Several
hours of backshift coverage
were routinely worked during most work
weeks.
Deep backshift inspections
were conducted
on August 13,
19,
20,
and
September
9,
10.
Enclosure
2
95i0240i30 95iOis
ADQCK 05000259
8
~ ~
4l
ll~
One violation was identified in the Haintenance
and Surveillance
area
and
one
noncited violation was identified in Operations:
Operations:
The noncited violation involved the licensee's
identification of a
mispositioned Unit 2 scram air header isolation valve.
The backup air
regulator
was isolated
and would not supply air pressure
when the in service
regulator
was isolated.
A personnel
error during valve position verification
contributed to the problem.
The associated
valve. has
been involved in
previous incidents including
a reactor
scram in 1994.
The inspectors
noted
that the licensee
conservati,vely
scheduled
the activity during
a reactor
shutdown.
(NCV 50-260/95-51-02,
CRD Scram Air Header Valve Out Of Position,
paragraph
2.3)
Inspectors
observed
good
use of procedures
and response
to annunciators
by
control
room, operators
following a Unit 2 scram.
Unnecessary
activities in
the control
room were appropriately minimized by the Unit 2 senior reactor
operator.
(paragraph
2.2)
During a Unit 3 core spray test,
inspectors
observed that control
room
personnel'ere
challenged
by the .number of ongoing activities.
Some
communications
problems
were also noted.
.Control
room SROs
and operations
management
did not correct the situation.
Observations
of subsequent
testing
activities were more positive.
Some operators
associated
with Unit 3
activities have not yet shifted to an "operational unit" approach
in their
duties.
(paragraph
2. 1)
Inspections of the Unit
1 reactor building identified no deficiencies with
direct operational
impact.
Several
minor conditions were noted that indicate
increased
attention to overall material conditions during tours is needed.
(paragraph
2. 1)
Maintenance
and Surveillance:
One violation was identified.
An NRC inspector
found equipment inside the
Unit 3 torus
(an established
foreign material
exclusion
zone)
which was not
recorded
on the foreign material
exclusion
zone accountability logs.
Other
deficiencies
were .noted in the logs.
This condition is similar to
deficiencies
previously .identified'y the
NRC during the last Unit 2 refueling
outage.
The violation is of particular concern
since several
recent foreign
material
problems
have occurred at Hrowns Ferry. (Violation 296/95-51-01:
Failure to Properly Control Foreign Naterial within an Exclusion Zone,
paragraph
4. 10)
During
a review of reactor building flood protection equipment,
the inspectors
identified that routine functional testing of the Unit
1 reactor building
water level sensors
had
been
suspended.
The sensors
would provide additional
means to alert operators
of a flooding condition.
After NRC identification,
the licensee
subsequently
returned the sensors
to the schedule,
(paragraph
2.5)
I
II
~
i
~i
Numerous observations
of Unit 2 routine testing
and .testing associated
with
the Unit 3'estart
were completed.
In most instances,
the inspectors
observed
good communications
and coordination
between
the different working groups.
(paragraphs
3. 1, 4.5, 4.6, 4.7.2, 4.7.3,
and 4.7.4)
Engineering
and Technical
Support:
Overall
assessment
of Unit 3 Configuration Control Drawings
was performed
after
NRC review of Potential
Drawing Discrepancy trend reports
and
a
1994
Independent
Review and Analysis report
had raised questions.
An inadvertent
ESF actuation
and
one scram occurred in the last two years that involved
drawing issues
to some degree.
The assessment
concluded that although the
Unit 3 configuration drawings
were not subjected
to the
same rigorous
. walkdowns
as the Unit 2 drawings, virtually all of the deficiencies identified
to, date
have not had
any operational
impacts.
Licensee
management
had
recognized
and users
have
been trained
on the limitations of the drawings.
The inspectors
concluded that the information reviewed indicates that while
drawing discrepancies
continue to be identified,
few have contributed to
safety significant operational
problems.
While it was difficult to obtain
useful data
from the current Potential
Drawing Discrepancy trending reports,
drawing deficiencies
were being adequately
tracked
and resolved.
(p'aragraph
4.8)
During observation of several
testing
and maintenance activities,
good support
by engineering
and technical
support
personnel
was noted.
(paragraphs
4.5,
and
4.7.2)
Unit 3 Recovery
Observations
of System Preoperational
Checklist
Phase
I walkdowns indicated
that the quality of the walkdowns continues to be high.
Deficiencies
were
identified and listed for correction.
The cognizant
engineers
made
appropriate
recommendations
to management
regarding delay of some portions of
the walkdowns
when it became clear that the effectiveness
would be limited due
to remaining work activities.
(paragraph
4.2)
During observation of a walk-through of Safe
Shutdown Instructions,
the
inspectors
considered
the number of labeling discrepancies
high for a
validated procedure.
(paragraph
4.3)
A NRC inspector identified that
a system valve position checklist
had not been
completed
on
a system which had
a completed
Phase
I System Preoperational
Checklist.
The, licensee
subsequently
identified several
other examples
and
initiated corrective actions.
Due to misunderstanding
of expectations,
operations
personnel
were signing off the checklist
because
the verifications
were in progress.
(paragraph
4.4)
A significant number of Unit 3 testing activities were observed.
Implementation of the Restart
Test
Program
was inspected.
The reviews
indicated that overall, the recovery of Unit 3 systems
is proceeding
in a well
managed
and properly controlled manner.
Emergent
equipment
issues
have
resulted
in numerous testing schedule
changes.
Restart
Test
Program
r
II
0'~
0
requirements
are being incorporated
into the System Test Specifications
and
procedures.
Deficiencies, were initiated when required
and resolved properly.
The licensee's
investigation into Core Spray
pump performance
data identified
that foreign material
had
become
lodged in the .pump.
Inspectors
noted poor
housekeeping
conditions inside
some control circuit enclosures
and paint
applied to
a few Core Spray piping snubber joints.
(Paragraphs
4.5,. 4.6, 4.7,
and 4.9).
II
0
O~
REPORT DETAILS
1.0
Persons
Contacted
Licensee
Employees:
G.
J.
- R
- C
J.
R.
G.
R.
- J
R.
- G
- E
S.
J.
- p
J.
- T
D.
- J
- S
- H.
- J
Ballew, Electrical
Engineer,
Transmission
8 Gusto
Br azell, Site Security Manager
Coleman,
Radiological
Controls Manager
Corey,
Chemistry
and Radiological Controls
Manage
Cornelius,
Emergency
Preparedness
Manager
Crane, Assistant Plant Manager
Johnson,
Site equality Manager
Jones,
Unit 3. Startup
Manager
Little, Operations
Superintendent
Hachon, Site Vice President,
Browns Ferry
Haddox,
Maintenance
and Modification Manager
Moll, Plant Operations
Manager
Pierce,
Technical
Support
Manager
Preston,
Plant Manager
Rudge, Site Support
Manager
Sabados,
Chemistry Manager
.Salas,
Licensing Manager
Shaw,
Manager,
Technical
Support
Shriver,
Nuclear Assurance
and Licensing Manager
Stinson,
Recovery Manager
Wallace,
Compliance
Engineer,
Site Licensing
Wetzel, Acting Compliance Licensing Manager
Williams, Engineering
and Materials Manager
White, Outage
Manager
mer Service
Other licensee
employees
or contractors
contacted
included licensed reactor
operators,
auxiliary operators,
craftsmen,
technicians,
and
public safety
officers;
and quality assurance,
design,
and engineering
personnel.
NRC Personnel:
J.
We'll)ams,
P
G. Wiseman,
DRS In
- Attended exit interview
- L. Wert, Senior Resident
Inspector
- H. Morgan,
Resident
Inspector
- J. Munday, Resident
Inspector
- R. Husser,
Resident
Inspector
R. Bernhard,
DRP Project Engineer
P. Byron, Resident
Inspector,
Brunswick
P. Fillion, DRS Inspector
D. Kern, Resident
Inspector,
Surry
G. MacDonald,
DRS Inspector
D. Starkey,
Resident
Inspector,
Sequoyah
roject Manager
spector
< ~
II
Qi
Acronyms, and initialisms used throughout this report are listed in the last
paragraph.
2.0
Plant Operations
and Support
(71707,
92901,
93702,
71750,
40500)
2. 1
Operations
Status
and Observations
Unit 2 operated
at power most of this inspection period.
On August 19, the
unit scrammed
when the turbine tripped due to low condenser.
vacuum.
The scram
is discussed
in detail in paragraph
2.2 of this report.
The unit was restored
to full power
on August 21.
Activities within the control
rooms were
monitored routinely.
Inspections
were conducted
on day and night shifts,
during weekdays
and
on weekends.
During a reduction in power due to an
indication of high generator
bus duct temperature,
the inspectors
noted that
the operators
performed the actions required in the alarm response
procedure
and
power reduction procedures.
Several
testing activities were observed
in the Unit 3 control
room.
On August
25, the inspector
observed
the performance of Loop I Core Spray flow testing
(3-SI-4.5.A. l.d ) in the control
room.
The operators
were simultaneously
performing the
CS flow rate surveillance
and exercising control rods.
Each of
the two
on duty were fully extended
during these. evolutions.
Both had
a
telephone
in one
hand
and
a radio in the other.
The control
room was
understaffed
and the
had difficulty in focusing their efforts
on the
primary tasks.
The,RO performing the
CS surveillance
was not very fami.liar
with the test requirements.
The
RO was requested
to notify the test director
when
a minimum flow valve went closed.
The inspector
observed that the RO's
attention
was focused
elsewhere
and
he notified the test director several
seconds after the valve closed.
The
SRO was not directly involved in the test
activities.
The inspector
noted that the operators
did not request
assistance
or slow the pace of the activities.
Operations
supervision
was present
during
some of testing
and did not intervene.
The inspector discussed
his
observations
with licensee
management.
The Division II CS flow rate
surveillance,
performed
on August
28 was,better
managed.
There were three
in the control
room and
no other test activities involving the
ROs.
The
running the test
appeared
to be knowledgeable
and
was clearly in charge.
It
was
a significant contrast to the performance of the previous surveillance.
The inspector
observed that the
SRO still'as not directly involved in the
testing.
These testing activities
and other previous observations
indicate that
some 'of
the Unit 3 operators
do not yet have
an operating plant attitude.
The
inspectors
communicated their observations
to plant management.
During
a routine tour on August 16,
one of the inspectors
noted that the
reactor
zone ventilation fans handswitch
(located
on
a back
CR panel)
had
a
caution tag installed that directed that
one of the fans should
be run only in
an emergency.
The inspector questioned
the onshift control
room operators
regarding the reason for the tag
and they were not sure of the condition.
The
clearance
(2-95-0385)
forms in the Shift Support Supervisor office,did not
contain sufficient amplifying guidance.
The inspectors
had previously noted
other simi.lar examples
involving caution tags
and the associated
clearance
41
ll
il~
forms.
The concern
was that the operators
should question the reason for such
tags during turnovers
and panel
walkdowns.
The underlying reason for the tag
should
be available through reference
to the clearance
sheets
or other work
documents
referenced
on the tags or sheets.
Subsequently,
the inspector
was
informed of the reason for the tag
and concluded that the caution tag was
a
reasonable
preventive action to minimize
a potential for unnecessary
plant
The observation
was communicated
to Operations
management.
On
August 17, -the acting Operations
Superintendent
issued
a note to Shift Support
Supervisors directing that caution order paperwork should contain amplifying
information.
The inspectors will continue to monitor the use
and control of
caution tags.
The inspectors
toured the protected
area
and noted that the perimeter
fence
was intact and not compromised
by erosion or disrepair.
The fence fabric was
verified to be intact and secured.
The inspectors
observed
personnel
and
packages
entering the protected
area
and verified they were searched
either by
special
purpose detectors
or physical
patdown.
The tours in the Unit
1 areas
during this period focused
on general
conditions
and systems
required to be operable to ensure that appropriate
attention
was
provided to the shutdown unit.
During routine tours of Unit 1, the
inspectors
noted that water had overflowed the containers
placed
under the
drywell sand pit -drain lines
and ran across
the torus
area floor.
The
licensee
subsequently
confirmed that the water was not contaminated
and
installed sleeving to direct the drainage to floor drains.
The licensee
attributed the leakage
to ground water leaking into the reactor building but
because
the amount
was small
and the. water was radiologically clean it was not
believed to be cost effective to spend
a large
amount of time investigating.
One of the inspectors
found the vent hose
on the Unit
1 reactor building
equipment drain
had pulled free from its connection to the metal
ductwork.
The hose
was marked "contact
Radcon prior to disconnecting".
Unit
1 operators
were informed and corrected
the problem.
Paragraph
2.5 of
this report describes
inspection of the Unit
1 reactor building water level
switches.
While none of these
problems represent
a current safety issue,
they.
do indicate that more attention is needed
by the license'e
during routine tours
of Unit
1 spaces.
2.2
Unit 2 Reactor
On August
19, 1995, with Unit 2 at
100 percent
power,
an offgas holdup volume
high temperature
was received in the main control
room followed by
isolation of the steam jet air ejectors.
This resulted
in a main condenser
vacuum decrease.
Operations
personnel
began reducing reactor
power in
anticipation of a 'turbine trip:
Vacuum continued to decrease
until the low
condenser
vacuum turbine trip occurred which subsequently
caused
a reactor
The initial cause of the vacuum loss
was thought to be
as
a result of
the tripping of the offgas dehumidification chiller.
Following repairs,
the
chiller was placed
back into service
and the plant was restarted,
however;
the
offgas temperatures
were still. high.
Further investigation identified that
the level in the offgas condenser
was high.
The level
was manually lowered
and the offgas temperature
immediately started
decreasing.
Troubleshooting
by
maintenance
personnel
determined that the power supply for the offgas
(~
Cl
~
'
>
condenser
level control valves
had failed.
This resulted
in the valves .going
closed.
When this occurred,
the level in the offgas condenser
increased
which
resulted
in an increase
in the offgas temperature
and
caused
the steam jet air
ejectors to isolate.
Initially, the identification of the root cause of the scram
was masked
by
several
factors.
The high level in the offgas condenser
was not identified
because
the power supply which failed also supplied
power to the annunciator
circuitry.
The mode of failure was not catastrophic,
which would have
been
readily identifiable, but was rather
a slow degradation
of a capacitor.
This
resulted
in a slow decrease
.in operating voltage to the level control valves
and alarm circuit which caused. the annunciator to fail to alarm
on high
condenser
level.
The licensee
is reviewing the design
aspects
of this
circuit.
Additionally, an annunciator for offgas high temperature
immediately
downstream
from the offgas condenser
had previously
been disabled
because
operation during hot weather resul.ted
in the normal offgas temperature
exceeding
the upper range
of, the instrument.
Lastly, the annunciator
response
procedure for the temperature
alarm that was received,
High Offgas Holdup
Volume Temperature,
directed Operations
to verify proper operation of the
offgas dehumidification chiller, which,
as previously discussed,
was found
tripped
and therefore
.assumed
to be the cause of the high offgas temperature.
Following identification .of the faulty power supply it was determined that the
chiller had actually tripped due to being overloaded
by attempting to cool the
abnormally high offgas temperature.
Immediately following the scram,
the inspector
responded
to. the site
and
observed that the o'perators
were following the appropriate .procedures
and
responding
well to annunciators
while restoring
systems
to service.
The
inspectors
subsequently
reviewed the scram data in more detail
and verified
that safety equipment
such
as the safety relief valves
(pressure
peaked just
below the value at which the valves should
open)
and other
ESF equipment
had
operated
as expected.
The inspectors
reviewed the licensee's
Incident
Investigation concerning the scram
and concluded that the issues
involved in
this event
had
been appropriately
addressed.
2.3
Nispositioned
On August 19, with Unit 2 in hot shutdown,
a half scram occurred
due to low
pressure
while aligning the scram air system for filter
replacement.
To replace
the filters, the associated
pressure
control valve
had to be isolated.
The
AUO verified the backup pressure
control valve was
aligned for operation
by checking the cross
connect
valves85-244
and 85-262,
open.
He then isolated the lead pressure
control .valve.
System pressure
began to fal.l and at approximately
65 psig, the backup pressure
control valve
did not take over control
as expected.
The
AUO attempted
to determine
the
cause of the problem,
but when system pressure
dropped to approximately
60
psig,
a half scram signal
was generated.
Upon recognizing what had occurred,
the
AUO reopened
the isolation valves for the lead pressure
control valve and
system pressure
was restored.
Troubleshooting
determined that the cross
connect valve 85-244,
was closed rather than opened.
When questioned,
the
stated that
he checked
the valve open
by attempting to open it further rather
than
by moving the valve in the closed direction.
The valve was subsequently
0
0
ili
placed in the appropriate position
and the filter change
out completed.
BFPER951118
was initiated to document the event,
to determine
how the valve
was first mispositioned,
and to develop corrective actions
as
needed.
At the conclusion of this report period the licensee
had not determined
why or
when the valve was mispositioned
and stated that it was doubtful that they
would ever
know definitively.
Failing to maintain valve 85-244 in the open
position is
a Violation of TS 6.8.1. l.a which states
that procedures
shall
be
established,
implemented,
and maintained for applicable
procedures
recommended
in Appendix A of Regulatory
Guide 1.33,
Rev.
2,
1978-.
The safety significance
of this incident was small since the work was intentional,ly performed while
the unit was
shutdown with 'all control rods inserted.
The licensee
placed the
'alve in the correct position
upon discovery.
In addition, licensee
management
discussed
this event with each operating shift during shift
turnover
and reviewed the importance of properly checking valve positions
and
their expectations
in this regard.
Reviews indicated that there
have not been
other safety significant examples of improperly positioned valves in the last
two years.
The second
issue
in this event involved the
AUO incorrectly
checking the position of valve 85-244.
SSP-12.1,
Conduct of Operations
states
that when checking
a manual valve's position, it must always
be operated
in a
closed position.
Had the valve position
been verified according to this
procedure
the
AUO would have determined that the 85-244
was not in its correct
position prior to isolating the lead pressure
control valve
and the half scram
would not have occurred.
This violation will not be subject to enforcement
action
because
of the licensee's
efforts in identifying and correcting the
violation meet the criteria specified in Section VII.B of the Enforcement
Policy.
This matter is identified as
NCV 50-260/95-51-02,
Header Valve Out Of Position.
The inspectors
also noted that this particular valve and air supply path
had
been
involved in operational
events
in the past
two years.
It would be
expected that management
and operator.'s
attention
would be heightened
during
any activities involving these
components.
2.4
Technical Operabi,lity Evaluation for Inoperable Position Indication for
RHR Valve
On August 23,
1995,
the
open
(green) position indicating light for RHR Loop II
LPCI injection valve,
2-74-69 extinguished for unknown reasons.
This is
a
manually operated
valve located
in the drywell.
The licensee
determined that
the problem with the position indication was associated
with that portion of
the circuitry located inside the drywell.
Technical Specification 4.5.B.l.f
requires that
a monthly verification be
made of all valve positions located in
the
RHR LPCI injection flowpath which are not locked,
sealed,
or otherwise
secured
in its correct position.
With the position indication inoperable for
this valve, the visual verification cannot
be verified without entry into the
drywell.
The drywell is maintained
locked closed with an inert atmosphere
and
is therefore
inaccessible
without shutting the plant down.
Technical
Operability Evaluation 2-95-074-9007
stated that it was not credible for the
valve to be mispositioned with the drywell entrance
secured
and access
prohibited.
It further stated that there is no plant operating history which
would indicate that the valve could
be repositioned
due to vibration, flow, or
0
~
i
other dynamic effects.
Based
on this information and the valve having been
known to be open prior to losing the position indication the licensee
made the
determination that the valve was
open
and capable of performing its intended
function.
Further,
the licensee
stated that maintaining the drywell locked
met the intent of the
TS requirement
which states
"locked, sealed,
or
otherwise secured."
The inspector
reviewed the
TOE and the
TS and concluded
that the licensee's
resolution of this matter
was reasonable.
The issue
was
discussed
by phone with NRR personnel
and it was concluded that the
TS
requirements
were being met.
2.5
Review of Reactor Building and Turbine Building Flood Protection
As discussed
in paragraph
5.7 of this report,
the inspectors
reviewed aspects
of reactor building flood protection pertaining to
a
1986 devia'tion.
The
deviation
was closed,
however; additional
review of overall reactor building
and turbine flood protection
was completed
since
such flooding is considered
significant in the multiple unit plant safety
assessment.
The inspector
toured all three reactor buildings
and located the flood level switches.
The
eighteen
switches
were located
as
shown
on drawing 0-47E600-8.
The switches
in Units
2 and
3 were clearly labeled.
There
was
no apparent
damage to any of
the switches.
The inspector verified that the power supply breakers
to the.
switches
were closed.
Procedure
2-EOI-3 reflected the correct designations
for the switches.
The watertight doors
between
the reactor buildings
(519
levels)
were shut.
The inspector verified that the Alarm Response
Procedures
in the Unit I control
room for seismic events
referenced
the operators
to
Procedure
0-AOI-100-5.
The procedures
require that
an inspection of the
519
levels of all three reactor buildings
be performed if seismic activity is
detected.
The inspector also noted 'that 0-AOI-100-5 requires that functional
testing of the switches
be performed after
a seismic event.
With the assistance
of a licensee
engineer,
the inspector confirmed that
Procedure
EPI-0-077-SWZ002,
Inspection
and Operability Check of the Reactor
Building Flood Level Switches,
was listed
as
a repetitive task in the
preventive
maintenance
program.
The inspector" reviewed the procedure
and
concluded that it would adequately
demonstrate
operability of the switches.
The inspector
also reviewed records indicating that the procedures
were being
completed
on Units
2 and 3.
The inspector noted that the procedure
was listed
as in "layup" on Unit I and the testing
has
been deferred.
After this item
was discussed
with maintenance
management,
the inspector
was informed that
functional testing of two of the switches
(torus area
and
RHR loop II) would
be returned to the "active" preventive maintenance
schedule.
The inspector
noted that the drawing which depicted
the power supply breaker to the Unit I
switches
was marked
as "Unit I and
3 equipment required for Unit 2
operations".
Two of the Unit I switches
had Temporary Alterations active
on
them because
the switches
had
been
upgraded with a newer model.
The
inspectors verified that the temporary alterations files and
CR tags contained
these alterations.
The inspector
noted that the required Temporary Alteration
checks
were being completed
on the switches.
Browns Ferry does not have
a distinct turbine building flood alarm or
procedure.
On routine tours,
the inspectors
observed that the Unit 2 and Unit
3 turbine building sumps
were clean
and being maintained.
Preparations
for
0
Il
O~
painting were in progress
on Unit 3 and the
sump cover joints and motors were
covered/sealed
to prevent concrete
dust entry.
The radwaste facility
operators
were appropriately sensitive to sump alarms.
A small packing leak
on Condenser Circulating Inlet valve (2-FCV-27-55)
had
an active work request
and drain sleeving
had
been installed to port the leakage to the drain system.
This review indicated that the licensee
adequately
was maintaining equipment
associated
with flood detection
and protection.
One noncited violation was identified.
3.0
Maintenance Activities and Surveillance Testing
(62703,
92902,
61726,
92901,
37551,
92903)
3.,1
Maintenance
Observations
Maintenance activities were observed
and/or reviewed during the reporting
period to verify that work was performed
by qualified personnel
and that
approved
procedures
in use adequately
described
work that was not within the
skill of the trade.
Activities, procedures,
and'work requests
were examined
to verify proper authorization to begin work, provisions for fire hazards,
cleanliness,
exposure control, proper return of equipment to service,
and that
limiting conditions for operation
were met.
The following maintenance
activities were reviewed
and witne'ssed
in whole or
in part:
Work Order
(WO) 95-15175-00
Stator Cooling Temperature
Switch
On August 28, the inspector witnessed
maintenance
troubleshooting
activities
on stator cool,ing. annunciator relay 74-C61.
The annunciator
alarms
on high stator cooling water temperature
and
was in constant
alarm in the Unit 2 control
room.
It had previously been determined
that
a true high temperature. condition did not exist.
This activity was
identified as
a high risk activity due to the fact that the required
work was to be conducted
in a cabinet containing other sensitive
equipment
associated
with main turbine trip logic.
The inspector
witnessed
the pre-job briefing and portions of the troubleshooting
activities.
The details of the activity were discussed
in adequate
detail with the control
room staff.
Performance
of those activities
were conducted
as discussed
and determined that the relay was faulty and
needed
replacement.
The inspector verified the drawings being
used
were
correct for the job, the personnel
performing the work were qualified,
and the appropriate
approvals
were obtained prior to beginning th'
activity.
WO 95-06101-00
Compensatory
Action Fire
Pump Six-Honth Test
As stated
in the licensee's
Fire Protection
Report,
in the event that
all of the normally aligned,
high-pressure fire pumps
become
an alternative
(compensatory
action), trailer-mounted,
diesel-driven
if
1l
gg~
fire pump is made available.
This
pump can
be placed in service at most
any on-site location that
has
a water supply,
and the discharge
can
be
aligned to BFNP's fire main loop via an available hydrant.
On September
6,
an inspector witnessed testing of the pump. Periodically, during the
run, the inspector
scanned
the diesel/pump
area
and ensured all
parameters
were within specification.
After approximately
one (I) hour
of operation,
the inspector
noted satisfactory operation of the diesel
and
pump.
Specifics of the work package,
diesel
technical
manual
and
enclosed
Surveillance Instruction,
O-FP-026-INS034,
were reviewed
and
found to be satisfactory.
3.2
Surveillance Testing Observations
Surveillance tests
were reviewed
by the inspectors
to verify procedural
and
performance
adequacy.
Testing
was witnessed
to ensure that approved
procedures
were used, test
equipment
was calibrated,
prerequisites
were met,
test results
were acceptable,
and system restoration
was completed.
The following surveillance instruction (SI) activities were reviewed
and
witnessed
in whole or in part:
O-SI-4.7.B.4
SBGT System In-Place
Leak Test of HEPA Filter Banks.
On September
7,
an inspector witnessed
various portions of this
surveillance
being -performed
on the
C train of the
SBGT System.
During
preparations
for the test,
the challenging
medium, the Dioctyphtalate
(DOP) solution,
became
unusable
because
the craft performing the
surveillance
used air which contained
too much moisture.
The craft
immediately stopped
the test,
prepared
a new
DOP solution
(used
a dryer
air source)
and continued with the SI.
The surveillance
was again
stopped
during testing of the second
bank of HEPA filters because
the
test meter probe
was unable to pick-up
some of the challenging
medium.
After changing
and repositioning
the probe the test
was again continued
without further probl,em'he
SI package,
performance
and results
were
satisfactory
and
no test discrepancies
were noted
by .the inspector.
O-SI-4.7.B.8
SBGT "C" Train Housing Door Gasket
Seal
Test
On September
7,
an inspector witnessed this surveillance
being performed
on the
"C" train of the
SBGT System.
Using
a plant-'approved
ventilation
smoke tube kit, craft personnel
applied
"smoke" around the
perimeter of the
SBGT housing doors, verified that gaskets
provided
a
full seal
and noted that
no smoke
was entering the
SBGT System via the
sealed
area.
The SI package,
performance
and results of the test
were
satisfactory
and
no test discrepancies
were noted
by the inspector.
During
a fol.low-up walkdown of the test area,
the inspector
noted that
a
plant work request,
(requesting tightening of one of the unit
door latches)
remained outstanding.
The inspector
was informed by the
SBGT system engineer that this
WR should
be completed after proposed
door latching surface repairs
are approved
and performed.
This
outstanding,
WR did not effect the test
and
no "smoke" entered
the system
via this latched
area.
v ~
A
II
il
il~
Other surveillance testing
and maintenance
activities were observed
as part of
the inspection of Unit 3 recovery activities
and are described
in paragraphs
4.5, 4.6,
and 4.7 of this report.
In general,
the observed activities
indicated that maintenance
and testing personnel
were following procedures,
were competent
in the associated
activities,
and properly completed the
required documentation for the work.
No violations or deviations
were identified.
4.0
Unit 3 Restart Activities
(37828,
61726,
61700,
62703,
37550,
37551,
92903,
40500)
4. 1
Unit 3 Status
and General
Observations
The inspectors
reviewed
and observed
the licensee's
activities involved with
the Unit 3 restart.
This included reviews of procedures,
post-job activities,
and completed field work; observation of pre-job field work, in-progress field
work,
and gA/gC activities;
attendance
at restart
progress
meetings,
and
management
meetings;
and periodic discussions
with both
TVA and contractor
personnel.,
skilled craftsmen,
supervisors,
and managers.
One of the inspectors
observed
some of the ongoing receipt inspection of the
new Unit 3 fuel.
The inspector
noted that the
SRO on the refueling floor was
actively supervising
the workers
and that procedures
were being, utilized
during the work.
The inspector'verified that several
important actions
were
being completed
as required
by the procedures.
The inspector also noted that
the concerns
involving the use of service air noted during the last outage
had
been. addressed
appropriately.
During closure of VIO 296/88-04-03,
Failure to Correctly Translate
Design
Requirements
Into..Drawings (IR 95-31),
a minor deficiency involving
locknuts/loctite not being
used
on Dresser
was identified by the
inspectors.
DCA notes indicated that locknuts/loctite,
in. accordance
with
specification
G-53,
was to be used,
however; further examination
revealed that
peening of threads
was also
adequate
as
a "locking device"
and conformed to
the intent of G-53.
On July 7, the licensee,
in fol'low-up to this item,
issued
a memorandum to TVA's Civil Engineering
personnel.
This
memo included
specific guidance that if any of the locking devices specified in G-53 can
be
used,
as is generally the case,
this should
be clearly stated
on the drawing.
Likewise, if restrictions
must
be
imposed,
the drawing must specify the
acceptable
locking devices
and also state that they are the only methods
allowed.
The inspectors
concluded that the licensee's
actions
adequately
addressed
the issue.
The inspectors
reviewed the results of the Institute of Nuclear
Power
Operations
Unit 3 restart assist visit.
The results
were also discussed
with
Unit 3 quality assurance
management
in some detail.
The issues identified
.
were consistent
with overall
NRC perception of the licensee's
readiness
to
startup
and operate
Unit 3.
NRC inspection of Unit 3 recovery will continue
as planned.
The inspectors
have also
been routinely meeting with the leader
of the licensee's
Operational
Readiness
Review Team to discuss
the progress
of
~2
0
il~
il~
10
that effort.
To date,
the inspectors
have noted that the
ORRT has
been 'very
thorough in their reviews.
4.2
Walkdown Observations
On August 22,
1995,
an inspector
accompanied
licensee
personnel
during the
performance of the SSP-12.55
Unit 3 Phase
I SPOC walkdown of the
HPCI system.
The inspector attended
the walkdown pre-brief and observed
the. HPCI walkdown
in the drywell, torus area,
main steam valve room and the
pump room.
The
system
walkdown was led by .the system engineer.
Numerous minor maintenance
deficiencies
were noted
by the walkdown team.
These deficiencies
included
missing bolts from Limitorque valve actuator
covers
(valve testing
was still
incomplete),
bent instrumentation
tubing, loose conduit'ittings at junction
boxes,
and general
housekeeping.
The main steam valve room was particularly
noted
as needing
housekeeping
attention.
Maintenance activities,
including
painting,
were in progress
in the
HPCI pump room during the walkdown which
made it difficult to assess
the extent of housekeeping
attention
needed
in
that area.
No major deficiencies,
however,
were noted during the walkdown by
either the walkdown team or the inspector.
The inspector
concluded that the
walkdown was adequate
and met the requirements
of SSP-12.55.
During the walkdown of the
pump room, the inspector
observed
a small
puddle of water which had developed
from a leaking
hose connection
on
a drain
hose attached
to
a catch basket
which was positioned
beneath
a steam line trap
bypass
valve.
The catch basket'had
a radcon tag attached
which indicated that
leakage
from the valve had
been
surveyed
on June
5,
1995
and
on that date
.indicated less
than
1000
cpm smearable.
However, during the
pump room
walkdown, the inspector
observed
several
individuals walk through the puddle
without questioning its source or whether it was potentially contaminated.
A
radcon technician
was subsequently
requested
to survey the area
and again it
measured
less
than
1000
cpm smearable.
The inspector
concluded that, in this
instance,
licensee
personnel
were not sensitive to
a potential radiological
condition which could have resulted in'the spread of contamination.
On August 24,
1995,
the inspector
accompanied
licensee
personnel
on
a Unit 3
Phase
I SPOC walkdown of the
RCIC system.
At the walkdown pre-brief, the
system engineer
provided
each
walkdown team
member with an itinerary which
l.isted the various locations
and system
components
to .be walked down.
Also
given to each
team member
was
a copy of SSP-12.55,
Appendix D,
Malkdown
Instruction.
The inspector
observed that the itinerary was
a useful aid for
team
members
.and helped to,keep the team focused
on what needed to be
accomplished.
The walkdown team documented
numerous
minor deficiencies
during
the walkdown and
was thorough in inspecting electrical
boards,
breakers
and
instrument panels,
as well
as various mechanical
components of the
system.
The walkdown team noted,
and the inspector
agreed,
that the
RCIC pump
room, including the turbine,
pump,
and associated
equipment,
was still
undergoing
maintenance
to the extent that it was inappropriate
at that time to
conduct
a
Phase
1 walkdown of those
components.
Because of the
disassembled
condition of the
RCIC pump/turbine,
the
Phase
1 walkdown for the
RCIC pump
room was rescheduled
to
a later date.
The inspector concluded, that
the
SPOC walkdown of the
RCIC system
was well planned,
was timely (with the
~,
k~
'
il~
exception of the
RCIC pump room),
and
was well executed
and met the
requirements
of SSP-12.55.
On September
8,
an inspector
accompanied
licensee
personnel
on
a
phase I
Hain Steam
(HS) system walkdown.
A pre-walkdown meeting
was held
and the
walkdown leader,*the
assigned
system engineer,
highlighted SSP-12.55,
"Unit 3
SPOC",
Appendix 0,
"SPOC Walkdown Guidelines"
and conducted
a brief of
previously identified
HS system discrepancies.
The test
and system engineers
provided'etails of what had
been previously discovered
on
a "pre-SPOC"
walkdown performed in August.
About two hours into the walkdown, the licensee test engineer
found that many
of the previously discovered
system discrepancies
which had
been
observed
in
the
"pre-SPOC"
walkdown were still present.
The walkdown was stopped
and,
after conferring with the plant system engineer,
the test engineer
presented
his concerns
to licensee
management.
The walkdown itself was performed
by the
team in
a direct/methodical
and straight-forward
manner
and in accordance
with
SSP-12.55,
Appendix D, guidelines.
Although this walkdown was postponed;
pending completion of previously-identified deficiencies,
a post-walkdown
meeting
was held.
This meeting
was thorough
and met SSP-12.55
guidelines.
This walkdown is to be rescheduled
and is to be conducted
during the riext
.
reporting period.
Another
NRC inspector
reviewed the two Phase
I SPOC packages
to ensure
they
complied with SSP 12.55, Unit 3 System Pre-Operability Checklist,
Revision
13.
The inspector
noted that the walkdown teams
had identified
a substantial
number
(60 to over 90 items per system) of deficiencies,
during the system
walkdowns.
The list of the items identified during the walkdown reflected the
thoroughness
of the inspection effort.
Items ranged
from missing equipment
identification labels,
damaged
valve hand wheels,
improperly mounted Hotor
Operated
Valve
(HOV) limit switch brackets, lifted wire leads,
and
indications'f
system leaks.
The inspector
noted that the walkdown teams
paid particular
attention to the condition of HOVs, labeling, piping supports,
hangers
and re-
straints,
and general
housekeeping
and material conditions of the systems.
The inspector returned to portions of the
HPCI system previously reviewed,
conducted
an independent
partial walk-down of the system with the associated
CCD Flow and Control
Diagrams
3-47E812-1,
Revision
28 and 3-47E610-73-1,
revision
15 to verify the as-constructed
configuration with the drawings.
The inspector
concluded that the
HPCI system configuration
was in agreement
with the flow and control diagrams,
and could not'ind any other system defi-
ciencies
not already identified by the
SPOC walk down team.
The inspector
concluded that the system
walkdown process
was effective in id'entifying
problems
and issues
which need to be corrected 'prior to system operability.
The 'inspections
indicated that the quality of (POC
1 walkdowns continued to be
high.
Deficiencies
were identified and listed for correction.
The cognizant
engineers
made appropriate
recommendations
to management
regarding delay of
some portions of the walkdowns
when it became clear that the effectiveness
would be limited due to remaining work activities.
I
1
t
4l
O~
'l~
12
4.3
Unit 2/3 Safe
Shutdown Instructions
On September
7,
1995,
two of the inspectors
accompanied
operations
personnel
on
a walk through of a simulated
Appendix
R fire in fire area
16 (control bay,
including control room).
This effort was intended to be training on the
combined
U2/U3 SSIs
as well as
a enhancement
of the procedures.
This area is
regarded
as the most chall'enging
safe
shutdown scenario
due the extensive
number of in-plant activities required.
Operators
simulated
performance of
plant activities
on Units
2 and 3'hile the simulator was shutdown
as the
"non
fire" unit.
The inspectors
(and operators)
noted
numerous differences
between
the labels
on the installed equipment
and the procedures.
The procedures
had
been through validation.
The inspectors
discussed
with management their
conclusions that the exercise
involved more procedural
validation effort
rather than operator training and verification of time requirements.
These
observations
were
made in response
to an Inspector
Followup Item (296/95-37-
02),
Performance of Simulated
Shutdown for an Appendix
R Event,
opened during
review of the U2/U3 Appendix
R program.
The licensee
stated
they will perform
additional walk through demonstrations
of the SSIs during the next several
weeks.
The inspectors will monitor the licensee's
efforts in this'area.
4.4
Phase
I Process
Deficiency
During review of an open
(USI A-48),
an inspector
noted that the drywell
control air system valve position checklist
was not complete.
The
SPOC I
checklist for the system
(the point in the Unit 3 recovery process
where plant
technical
support
recommends
that the system is ready for return to service
testing)
'had
been previously
signed off.which requires operations
to: have
system status control.
Nore specifically,
SSP-12.55,
Unit 3
SPOC,
requires
that Operations
establish
status
control of systems
at
Phase
I by
completion of the valve position checklists.
The Phase
I SPOC
was signed
without completion of the list.
This matter
was brought to the attention of
operations
management.
An audit by operations
management
revealed
two
additional
phase
I SPOCed
systems
which did not have completed valve position
checklists.
Operations
management
stated that the personnel
completing the
checklist were under the impression that the valve position checklists
could
be in progress
rather than being complete
when making the signoff.
Operations
personnel
involved in future
Phase
I signoffs have
been briefed
on
management
expectation that system status files be completed prior to
completion of the
Phase
I process.
The inspectors will continue to
monitor the results of the licensee's
corrective actions in this area.
4.5
RHRSW System Restoration Activities and Testing Observations
Several
inspectors
reviewed
and witnessed
RHRSW system recovery activities,
including restart testing
and followup of deficiencies identified durin'g the
testing.
The inspectors
reviewed the status of the
RHRSW restart test
program
and related
maintenance
activities to determine
whether the
RHRSW system
was
ready to support fuel load
and
power ascension
testing.
Inspection activities
included interviews with engineers
and operations
personnel,
field walkdowns
of system
components,
direct observation of system
performance testing,
and
various document reviews.
II
4I~
13
The
RHRSW system
serves
as the plant's ultimate heat sink to support certain
ECCS functions.
Several
major design
changes
were implemented during the
extended
outage to improve
RHRSW system performance.
DCN W17620A replaced all
RHRSW piping within the Unit 3 reactor building because
of excessive
corrosion
and pipe wall thinning.
DCN T35994, modified all four
outlet valves to reduce flow resistance
and increase
the
SW flow rate which
could
be achieved
through the
HX.
Additional modifications replaced
the
pump Bl impeller,
upgraded
MOV actuators
to meet
NRC GL 89-10 requirements,
and
added
RHRSW temperature
monitoring.
Site engineers
evaluated
the status
of all system
DCNs as part of the
RHRSW SPAE.
The inspectors
reviewed
DCN
status with the system restart test engineer.
All DCN action items required
for SPOC
Phase II closeout
were complete.
Pending
DCN action items which
affected fuel load
and plant restart
were clearly identified in the
SPAE.
The
inspectors
concluded that
DCN status tracking was thorough.
Post modification test 3-PMT-BF-023.038,
RHRSW Flow Test,
was written and
performed, to:
Demonstrate
that the
RHRSW pumps
can deliver 4500
gpm of raw water
at the discharge of each associated
Unit 2 and Unit 3 heat
exchanger.
Verify the pressure
boundary integrity for the. Process
Radiation
Monitoring System.
Verify that the interlock for the emergency transfer switch
and the
RHRSW pumps functions.
Verify that temperature
elements
3-TE-23-4100
and
4101 are connected
to
~
the correct points.
The inspector
reviewed the
PMT and considered it adequate.
The procedure
contained
enhancements
intended to reduce errors involving procedural
compliance.
The required actions
such
as; verify, check,
open, etc.
were
highlighted by larger
and bold type.
The inspector
concluded that these
highlights improved the procedure effectiveness.
The Baseline Test
Requirement
Document,
2/3-BFN-BTRD-023, for the
RHRSW System
was reviewed.
This document identifies the test which is required prior to restart to
demonstrate
the
RHRSW system's
capability to support safe
shutdown
and satisfy
design baseline
requirements
for combined Unit 2/3 operation.
The testing
specified in the
PMT satisfied the testing requirements
of Attachments
A, B,
E,
F,
and
H of the baseline test requirement.
On August 29,
1995,
the inspector
observed
the performance of portions of 3-
PMT-BF,-023.038.
The licensee
deferred testing of the
"C" loop because
of
discrepancies
with its flow transmitter which will performed
upon the
completion of maintenance.
The prejob brief was thorough
and the test
provided
an ample opportunity for questions
from the test participants.
The
test director also
asked
questions
to verify that the craft and operators
were
familiar with the test.
The inspector
observed that
a flow of 4500
gpm was
obtained
as required.
The transfer switch logic functioned
as designed.
The
test director
had
a copy of the procedure with him and gave specific
direction.
The operators
repeated
back instructions for both face to face
and
telephonic
communications.
The inspector considered
that this testing
was
well planned
and executed.
4I
ik~
14
During the
RHRSW pipe replacement
(DCN W17620A) engineers
observed
a
significant amount of loose
MIC corrosion pipe scale
in portions of RHRSW
supply piping.
This piping, located outside of the reactor building, had
been
isolated
in dry layup
and
was not replaced during the extended
Unit 3 outage.
MIC buildup typically adheres tightly to wet piping.
Engineers
postulated
that the prolonged period of dry layup caused
the
MIC scale layer to exfoliate
and collect at the bottom portion of the
The
licensee
performed extensive
piping flushes at rated flow, 4500
gpm, to clear
the loose debris prior to reconnecting
RHRSW system piping for operation.
On August 22,
1995,
procedure 3-SI-4.5.C. 1(3),
Pump
and Header
Operability and
Flow Test, revision
4 was successfully
completed to verify
that service water flow to each
HX satisfied
TS requirements.
On
August 26, preventive
maintenance
procedure
O-TI-63,
RHRSW Flow Blockage
Monitoring, revision II was performed to establish
a baseline for RHR
performance
trending.
Abnormally high differential pressure
(dp)
and slightly
reduced
flow were observed
on the
C
Engineers initially attributed
the low HX flow and high tube sheet
dp to
a faulty flow instrument.
The
instrument
was recalibrated and'-TI-63
was repeated
twice more with similar
results.
Mechanics
removed the
HX .head for inspection
and found
a large
amount of corroded
pipe scale buildup fouling the tube sheet.
Engineel s
determined that the scale
was residue left over in'he pipe from the earlier
flushes discussed
above.
'The inspectors
noted that the scale
removed
from the
HX tubesheet
was identical to that photographed
during the
RHRSW piping
replacement
project.
All four
HX were. promptly cleaned
to remove scale
debris.
The
C
RHR HX continued to indicate fouling on the subsequent
retest.
The,inspectors
questioned
whether the
RHRSW supply piping integrity had
been
degraded
and whether.
pipe wall thickness
was adequate.
The inspector
reviewed
design calculation MD-f2023-870104 for the
ASME Class
3
RHRSW piping and noted
that
RHRSW supply header piping was required to be at least 0. 178 inches
thick.
Engineers
informed the inspectors
that pipe wall thickness
had
been
evaluated, prior to system restqration
and was determined to be acceptable.
The minimum measured
pipe wal.l thickness
was 0.26 inches.
The inspectors
questioned
why, after identifying the corrosive scaling,
the pipe wall
thickness
measurements
and evaluation
had not been
documented.
Engineers
responded
that the evaluation
was not required
by
DCN W17620A and that pipe
integrity was subsequently
verified by code required ISI testing.
The
inspectors
reviewed 3-SI-3.3. 13,
ASME Section
XI Hydrostatic System
Pressure
Test of the
RHRSW System,
revision 0/TN-03 and confirmed that system integrity
was properly verified.
Minor test documentation
'errors
were identified and
promptly corrected.
The inspectors
concluded that the licensee
adequately
confirmed
RHRSW piping wall thickness
and integrity to meet
code requirements.
The licensee
performed 0-TI-63 approximately ten additional
times to flush
pipe scale
from the system
and evaluate
HX flow performance.
The inspectors
observed
performance of O-TI-63 and resultant
on several
occasions.
Test equipment
was in calibration
and foreign material
exclusion
controls were appropriate.
Procedure
0-TI-63 was modified to maximize
SW flow
through the
C
HX to enhance
the system flush.
The restart
engineer
briefed operators
on the modified test
and operators
established
the intended
lineup.
However, during
a post test review, the inspector
noted that
0
il~
4Q~
15
procedure
O-TI-63, revision ll/UIC-14 was not properly modified to reflect how
the test
was run.
The inspectors
determined that the procedure
issue
had
minimal safety significance.
The inspector discussed
this observation with
engineering
management
for correction prior to the next 0-TI-63 performance.
The last three 0-TI-63 flow tests
were performed at
a 5400
gpm flowrate which
is twenty percent
above the flow required
by TS.
The inspectors
confirmed
that flow remained within the maximum flow recommended
by the
HX manufacturer
in service information letter No. 337, Flushing of Heat Exchangers.
The
duration of the last test
was extended to simulate the use the system would
experience
during
a six month interval.
Observed
HX fouling was minor.
Procedure 3-SI-4.5.C.l(3)
was subsequently
performed to confirm TS required
flowrate.
Engineers
concluded that the
RHRSW flowrate
met
TS requirements,
and periodically scheduled
0-TI-63 (six month intervals)
would provide sufficient information to identify fouling prior to significant
HX performance
degradation.
Additionally, design modifications to monitor and
inhibit corrosion
are nearing completion.
The inspectors
concluded that the
RHRSW piping/HX fouling evaluation
and actions to address
future corrosion
concerns. were technically sound.
The inspectors
closely observed
licensee activities
and the process
used to
resolve the
The system restart testing engineer
was the
lead person responsible for issue resolution.
The inspector
noted that the
restart
engineer
worked closely with maintenance,
operations,
and, other
engineers
and tracked the issue to closure.
However,
the inspector questioned
how the information learned
would be captured for future reference
and similar
issue resolution.
According to SSP-3.4,
Corrective Action, revision
14, the
issue
met the criteria for a level
C
PER,
although
a
PER for this issue
was
not established.
The Balance of Plant engineering
supervisor
subsequently
informed the inspector that
a Level
C
PER was appropriate
and would be
established
to document the issue.
The inspectors
determined that this action
was consistent
with the licensee
corrective action program.
The inspectors
reviewed the following records,
performed
system walkdowns,
and
discussed
SW system restart
assessment
with various licensee
engineers.
The review included:
RTP test requirements
and results,
Phase
I SPOC
walkdown report,
SPAE,
SNPL,
and the
Phase II checklist.
The inspectors
confirmed that
Phase
I was complete.
All open work was
properly prioritized and tracked
on the
SHPL.
The
RTP properly addressed
all
RHRSW related
TS and
UFSAR requirements.
All RHRSW
Phase II activities
(includes entire
RTP)
have
been sat'isfactorily completed or scheduled for
completion coincident with testing of other systems.
Specifically the
following two tests
have
been
scheduled
with other systems to eliminate
duplicate testing:
Verify any Unit 3 Core Spray
pump start will start the
(EECW and swing)
RHRSW pumps A3, Bl, C3, Dl, and Verify both Unit 3
common
accident signals
A and
B will start
RHRSW pumps Al, A3, Bl, B3, Cl,
C3, Dl and
D3.
This testing is tracked in 3-STS-057-5.
The inspectors
walked down portions of the
RHRSW system within the Unit 3
reactor building during system operation.
System integrity was good.
No
indication of leakage,
excessive
vibration, or material degradation
were
HL
E
<g~
16
identified with the exception of limited RHR HX blockage described
above.
This condition was properly resolved.
Through the extensive
review and observations
discussed
above
and in previous
IRs, the inspectors
concluded that the
RHRSW system restoration
was being
completed in a controlled
and thorough manner.
Management tools for tracking
system material
and test condition were comprehensive.
Actions to resolve
emergent
issues
were appropriate.
The licensee
was completing the last
portion of the
Phase II SPOC at the close of the report period.
The
inspectors
concluded that appropriate
programs
were established
and were being
properly implemented to support
RHRSW system restoration
in accordance
with TS
requirements.
4.6 Control Air System
and Restart
Test Program
Review
The inspectors
reviewed the
DCN listing for System 32, Control Air System,
and
System
33,. Service Air System,
to determine i.f all the system
DCNs were
included in the site master
punch list (SMPL).
The Browns Ferry Design
Schedule,
from August 6,
1990 through October
1,
1999,
dated August 23,
1995
was reviewed against
the historical
SMPL for Systems
32 and
33 dated
August
24,
1995.
The inspectors
noted that all
DCNs in the
Browns Ferry Design
Schedule for Systems
32 and
33 were include'd in the .SMPL.
The inspectors
performed
a review of the Control Air and Drywell Control Air
System
Design Criteria,
BFN-50-7032,
Revision 3,
and
FSAR Section
10. 14 to
determine
the system safety functions.
The Control Air System Baseline Test
Requirements
Document
(BTRD), 3-BFN-BTRD-032, Revision 0,
Change Notice No.
1,
was reviewed.
The
BTRD adequately
included the system safety .functions.
The
inspectors
reviewed the Control Air System Test Specification
(STS),
3-STS-
032,
Revision 00,
and verified
that the testing specified
met the safety
related functions outlined in the Control Air BTRD.
The Control Air STS also identified testing, required to verify adequacy of
system plant modifications.
The following DCNs were reviewed:
DCN
DESCRIPTION
W17185 Sl
and
S3
Conceptual
Design For Primary Containment
Isolation System Modifications
W17044
S2
W18703
Control
Room Design
Review Modifications
Valve Operability 3-FCV-32-62
and 3'-FCV-32-63
W21917
S7
Replace Electrical
Breakage
Components
The post modification testing
(PMT) specified for these
4 modifications
was 3-
PMT-BF-032.043,
Drywell Air SyStem Valves Functional Testing,
Revision 0.
The
inspectors
reviewed the
PMT and concluded that it adequately verified the
functions specified in the
above listed modifications.
The completed testing
package for modification W33292 S2, Unit 2-3 Crosstie
2-PCV-032-3901
was
reviewed.
The test
package,
3-PMT-BF-032.037,
Revision 0, Control Air Cross
0
il~
il>>
17
Tie Valve Functional Test,
documented satisfactory
performance of the auto
isolation functions identified in
DCN W33292 S7.
The inspectors
selected
the
ADSRV accumulator safety function for testing
review.
The
PHT specified
was MSI-0-001-TST-001, Testing of Air Supply
Systems
For Hain Steam Isolation Valves (HSIVs), Revision 0.
The specified
PHT measured
the leak rate from the accumulators
to be
< 10 psi/hour.
The
inspectors
reviewed calculation,
MD-(0032-870288,
Control Air Volume and Wall
Thickness of Accumulators,
Revision
3 and verified that the
ADSRV accumulator
sizing calculation 'incorporated
a'eakage
of 10 psi/hour
and required five
ADSRV actuations.
The inspectors
concluded that this
PHT was adequate
to
verify the
ADSRV accumulator safety function.
The Control
Rod Drive (CRD) Scram Pilot Air Header
Low Pressure
Scram function
was not listed in System
32 STS.
The licensee
indicated that this fun'ction
will be tested
as part of System
85
CRD Technical Specification
(TS) required
testing.
The inspectors
reviewed several
non-safety related
Control Air System
functions to determine if the licensee
had verified that non-safety related
functions were operational.
The Control Air and Drywell Control Air
compressor
function and the Service Air backup function were reviewed.
The inspectors
determined that the Service Air automatic
backup to Control Air
was not tested
as part of the Unit 3 Control Air Restart Testing.
Review of
the Unit 2
STS indicated that the Service Air backup function was not tested
as part of the Unit 2 restart testing.
The Service Air system provides, an
alarm
and automatically connects
Service Air to the Control Air System at
a
low control air pressure
of 85 psig.
Coincidently,
on September
7,
1995,
during the implementation of modification W33292 Stage
8 on Control Air
Compressor
C, low control air, header .pressure
occurred with only one Control
Air Compressor
loaded to the system.
The service air backup function operated
and the alarm was received indicating that this function was operational.
The status of the Control Air and Drywell Control Air compressors
was
reviewed.
The Control Air System
was maintained
operational
through 'the
extended
outage,
however the Drywell Control Air system
was secured.
The
Drywell Control Air System
was exposed
to atmosphere
during the extended
outage.
The resident. inspectors
had previously questioned
the potential for
drywell air piping corrosion
and contamination with the licensee.
The
licensee
prepared
work orders to perform flushing of the drywell air piping
and accumulators.
The outboard
HSIV accumulators
and control air piping was
also flushed.
The work orders
were performed to. procedure
3-TI-337 and the acceptance
.
criteria was from HSI-0-000-PR-0001,
Cleanliness
of Fluid Systems.
The
flushing was performed using air from a portable breathing air compressor
.
The acceptance
criteria required
2 successiv'e
flushes of 2 minutes duration
with no hydrocarbons
and
no visible particulates.
The inspectors
witnessed
the flushing of Drywell Air Compressor
(DAC) 3B,
flush path no.
5,
OAC 3B through the
DAC 3B air dryer,
and flush path no.
6,
li
I.Il
~
il~
18
DAC 3B through the
DAC 3B air dryer and air receiver.
Visible particles
were
noted during the initial flushes.
The final flushes
met the acceptance
criteria of no visible particulate.
The flushing evolution was performed
according to procedure
and
was considered
acceptable.
Upon completion of all
flushing the licensee
planned to place the drywell air system in service
and
perform an air quality sample of the drywell control air system.
The Control Air System
was maintained operational
through the extended outage.
The control
and service air compressors
receive quarterly flow capacity tests,
and control air dryer dewpoint checks
were performed monthly.
Control Air
System air quality tests
were performed
once every
6 months.
The inspectors
reviewed the database
printout of closed, work orders
and verified that the
control air dryer dewpoint checks
had
been performed.
The recent control air
quality test results
were reviewed
and the inspectors
noted that the results
met the acceptance
criteria of <
1
ppm hydrocarbon
and
<
1 particle
~ 5
microns.
The latest Control Air System air quality sample results
had not
been received
from the sample laboratory.
The last air. quality sample data
showed
one sample point at 4.3 particles
~ 5 microns,
however,
the average
was
g
1 particulate for a background
value of 0.3 particulate.
The inspectors
performed
an independent
walkdown of the control air and
drywell control air, to determine if the licensee's
threshold for identifying
system
problems
was adequate.
A small air leak was noted at the packing gland
for service air backup valve 0-PCV-33-1
bypass
valve.
A work request
was
written for this minor air leak:
DAC 3B local control station handswitch,
3-
HS-032-0067,
was found in the auto position while the tagout
(Tag 3-91-0325-8)
required it to be in the Off position.
The switch was discovered
at
1530 on
August 24,
1995.
Licensee shift management
was informed and action
was
initiated to reposition the switch.
The inspectors verified that the circuit
breaker for compressor
3B was tagged
open.
This was similar to
a previous
finding by the resi'dent
inspectors.
The switch is located at shoulder height
on
a route frequently used
by personnel.
The inspectors
noted that the switch
for DAC 3A had
been
equipped with a guard to prevent inadvertent
repositioning.
PER BFPER950600
had
been initiated on the
DAC 3B local control
handswitch
and requested
a guard
be built over the switch.
The inspectors
concluded that the switch had
been inadvertently
bumped out of position.
The
breaker
being tagged
open resulted
in the safety significance of the issue
being'mall.
The Control Air Compressor
Control Panel,
O-LPNL-925-0118,
was inspected.
The
panel
was very dirty and foreign material
was noted in the panel.
Pieces of
wire trays,
terminal lugs
and screws
were noted loose
on or near terminal
blocks.
Wire markers
were noted
on top of several
open type relays
near the
relay contacts.
The licensee
was informed and licensee
management
initiated
corrective. action
and the panel
was cleaned.
The inspectors
noted
an oily
residue'hich
appeared
to be exuding from some of the cables
in this panel.
The licensee
was informed of a similar occurrence
at Sequoyah
Nuclear Plant
where Polyvinylchloride
(PVC) cable jackets
had experienced
a release
of
plasticizer
compound
from the
PVC which had exuded
from the cables.
No
significant amount of the material
had collected near
any relay contacts
or
other equipment.
The Control Air Compressor
Control
Panel
had
been
included
in the Unit 2
SPOC walkdowns but not in the Unit 3
SPOC walkdowns.
The
0,
ii
]5~,
l9
inspectors
concluded that the licensee
was adequately
identifying and
resolving system deficiencies..
As stated earlier,
on September
7,
1995, the licensee
experienced
a
Low
'Control Air Pressure
Event.
The control air header
pressure
dropped to
approximately
82 psig
and the service air backup alarm was received.
PER
BFPER950990
was initiated for resolution.
The low control air header
pressure
occurred during implementation of DCN W33292 Stage
8 on the control air
compressor
control circuit.
This
DCN was considered
non-outage
work.
The
inspectors
witnessed
the troubleshooting activities which were conducted
according to work order
WO 95-14644-05.
The troubleshooting activity involved personnel
from Technical
Support,
Nuclear Engineering,
Modifications, Instrument Maintenance,
and Operations.
The troubleshooting
was coordinated
as
a high risk activity.
At the time of
the .low control air header
pressure
only control air compressor
A was loaded.
Compressors
B and
D were running unloaded
and compressor
C was off.
The
control air compressors
had not tripped.
The service air backup function and
alarm worked during the event.
Operations
personnel
manually loaded control
air compressors
to restore
system pressure.
Manual control air compressor
loading
was not included in Control Air System Operating Instruction, 0-0I-32,
Revision
28.
The licensee
was initiating a procedure
change to incorporate
this hand control
mode into the Control Air System Operating Instruction.
The
resident
inspectors verified that the procedure
change
was approved
and
reflected the manual operation'utilized to recover the air system.
The control air compressor
programmable controllers were tested
and
no
problems
were noted.
The control air compressor
control circuit voltage
and
comp'onents
were tested
and
no problems
were noted.
The control air
compressors
were operated
through all switch positions
and
no failure to load
was noted.
No definitive root cause
was noted
and the problem could not be
repeated.
The inspectors
reviewed the
PMT, used following the installation of the Control
Air System
programmable controllers
(DCN W33292).
The testing
included
comparing the contents of the controller registers
(loaded software)
against
the required software
as
shown
on Mechanical
Real
Time Data Acquisition and
Control Software Drawings.
The inspectors
concluded that the
PMT demonstrated
proper compressor
loading control
and controller operation.
The inspectors
concluded that the restoration activities
and testing of the
control air systems
were proceeding
in a controlled manner.
Testing
adequately
addressed
demonstration
of the required functions.
Emergent or
postulated
issues
were being addressed
appropriately.
4.7
Unit 3 Testing Observations
During this reporting period
a selection of routine surveillance tests
and
other testing
conducted
in preparation for the re-start of Unit 3 were
observed
and evaluated
by the inspectors.
Details are discussed
in the
following paragraphs.
0
Oi
i
20
4.7. I
Core Spray Testing
The inspector
observed
the performance of Core Spray Flow Rate
and Valve
Differential Pressure
Testing for both loops.
These
were performed using
'Procedures
3-SI-4.5.A. l.d(dp)(I) and (II).
On August 25,
1995, the licensee
performed the surveillance for Loop I.
The inspector
noted that the operators
alternately
used
a telephone
and radio to communicate with the personnel
in
the field.
Background noise
was very high which made it difficult for either
party to understand
what the other was saying.
There were numerous
requests
for repeatbacks
and clarification.
The inspector considered
the
operators'erformance
to be weak. Additional details
are discussed
in Paragraph
2.1.
When the operator started
Pump 3C, the inspector
observed that the ammeter
for CS
Pump
3A dropped
approximately
20 amps.
He noted that
Pump
3A had
previously been drawing approximately
80
amps
and leveled out at
76
amps while
Pump
3C leveled out at 84
amps.
A review of the data revealed that the
differential pressure
across
Pump
3A was less
than the acceptance
criteria
of 220-251 psi.
On August
29 the inspector
attended
a meeting which was 'held
to discuss
the cause of the low d/p for CS
Pump 3A.
An engineer,
after
reviewing the data,
concluded that low pump speed
was the cause of the
deficiency.
The inspector questioned
his conclusion
as the
pump is powered
by
a two pole induction motor and
speed is controlled
by system frequency.
Pump
binding could have
been the only other contributor and it would have
been
audible.
Several
other po'tential contributors relating to the physical
condi.tion of the
pump were discussed.
The inspector considered
that foreign
material
in the
pump was the most likely cause
since other
NRC inspectors
had
observed material
in the Unit 3 torus during the test.
The licensee
developed
an action plan which required
a new set of pump curves to be developed.
Trouble shooting/testing
revealed that the motor speed
was 3600
rpm and the
problem was in the
pump.
The licensee
believed it was
a worn wear ring.
Discussions
with the vendor revealed that the
pump
had two inspection ports
which would enable
the licensee
to inspect the
pump internals without
disassembling
the
pump.
The inspection of the
pump internals
revealed that
debris
was lodged in the
pump.
The blockage could explain the disparity in
the operating current in the two pumps.
Two of the resident
inspectors
also observed
portions of the testing in the
room and the torus area.
The inspectors
id'entified that paint
had
been
improperly applied to several
on the test return 'line and
a room
temperature
sensor.
These observations
were discussed
with Unit 3 recovery
management
and were corrected
promptly.
The inspectors
have not identified any
other problems with painting
on Unit 3 and concluded that this was
an isolated
instance.
Additionally, the inspectors
observed
some material in,the water
inside the torus during the test.
The inspectors
could not identify the
material
since they were observing:from
above the Foreign Haterial
Exclusion
caging
and the torus interior was not lighted.
Because
FHE control
had
already
been established
in the torus,
the inspectors
promptly informed Unit 3
management
of the observations.
This issue is described
in more detail in
paragraph
4.9.
ik
i
<gi
4.7.2
Common Accident Signal
Logic
21
As described
in
FSAR Section 8.5.4. 1, Automatic Starting
and Loading, certain
~ combinations of abnormal
plant parameters
at either Unit 2 or Unit 3 shall
cause starting of all eight diesel
generators.
The circuitry which implements
this design
requirement
was referred to as
"Common Accident Signal
(CAS)
Logic."
Pursuant
to Technical Specification 4.9.A.3.a the
CAS logic is tested
each l8 months.
The inspectors
performed
a detailed review of the testing of
the
Common Accident Signal logic.
Applicable portions of surveillance
procedures
for testing the .CAS logic,
CS system logic,
480 volt load shedding
logic,
and the
DG load acceptance
tests
were reviewed to verify adequate
overlap in the testing of the
CAS logic.
The:inspectors
found that
Common
Accident Signal
Logic Surveillance Instructions I/2-SI-4.9.A.3.a,
Revision 20,
and 3-SI-4.9.A.3.a,
Revision
13, tested
the
TS required logic functions.
Some
non-TS functions,
including some alarm logic,
and
some
CAS contacts
associated
with the
DG stop logic, were not tested
in this procedure.
These
items will
not impact the ability of the Biesels to autostart
from a
CAS signal.
The
initiation signal
was simulated in the testing
by energizing the
CS relay
.
which provides the signal.
The inspector
concluded that this was
a good
practice to insure
adequate
overlap in testing.
The inspectors
evaluated
the first .performance of Surveillance Instruction
3-
SI-4.9.A.3.a since the Unit 3 plant parameter
signals to the
CAS logic were
re-instated
(wires re-landed).
Substantial
portions of the surveillance
were
observed
in progress.
The inspectors
also reviewed the completed surveillance
record.
All the steps
were successfully carried out.
However,
a problem was
identified during performance of,the surveillance.
The problem was that
a
local annunciator
window went to the alarm conditio~ when
a hand reset lockout
relay was reset.
The annunciator
was
"4160
V Shutdown
Board
3EA [EB,
EC,
ED]
Transferred."
The alarm was spurious in the sense that
no actual transfer
had
taken place.
Review of the schematic
diagrams
led to the conclusion that the
"as-designed"
logic for the annunciator
was correct.
Resetting the, lockout
relay merely restored its contacts
to the pretest position.
A normally closed
contact
from the lockout relay was wired into the alarm circuit to block the
alarm for certain conditions.
There. were four lockout relays,
one for each
Unit 3 diesel
generator.
Since they were tri'ggered
by both divisions, there
were eight of these
lockout relay operations
during the surveillance.
In
seven
out of eight times,
the spurious
alarm was initiated.
The problem was
identified as
a Test Deficiency to be resolved
by Work Request
No.
C308048.
The work request
was scheduled
to be worked September
19,
1995,
and its
completion tied to the System 57-5, 4. 16
kV Distribution,
SPOC.
The inspectors
also reviewed schematic
diagrams
in light of the
CAS design
requirements
and surveillance instruction.
They concluded that pe'rformance of
3-SI-4.9.AD 3.a demonstrated
that the
CAS logic meets
the design
requirements
in
FSAR Section 8.5.4. I, and that the Unit 3 initiating signals
had
been re-
instated correctly.
The test deficiency
was
an emergent
problem that must
be
resolved,
but which did not affect the
CAS logic itself.
Other observations
made
by the inspectors
while witnessing the surveillance
were that plant
operators
conducting the test at several
locations maintained
good
communications
and positive control of plant systems.
In addition, there
was
good support
from engineering
personnel.
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4.7.3
Degraded
Voltage Relays Calibration
The inspectors
witnessed
the performance of the calibration of the Division I
degraded grid voltage protection relays .(two sets of three relays).
The
calibration was carried out under Surveillance Instruction 3-SI-4.9.A.4.c(I),
4160
V Shutdown
Board
3EA and
3EB Under/Degraded
Voltage [and] Time Delay
Relay Calibration.
The calibration was performed
by the Transmission
8
Customer Service group,
who maintain
many protective relays at the Browns
Ferry facility.
The pick-up and drop-out voltage
was found within the "leave-
as-is"
band for five relays.
One relay was found slightly out of the band,
and
was easily adjusted to the desired
value.
The inspectors verified the
test set
up at the start of the test.
The inspector verified that calibration
stickers.
on the test instruments
indicated the instruments
were calibrated.
The inspectors
noted that persons
conducting the calibration obtained
permission
from the appropriate
operations
personnel
before removing any relay
from its case.
The inspectors
also noted that the inoperable. time was
recorded.
Inoperable time was about
one hour for each set of relays.
Restoration of the relays
was verified by a person
not associated
with the
test itself.
The inspectors
also verified that the, acceptance
criteria fo}
relay operation
on decreasing
and increasing
voltage in the surveillance
instruction matched
values
in the Technical Specification.
The inspectors
concluded that the degraded
voltage relays
were correctly set
and functioning
properly.
In addition,
performance of the calibration
was in accord with NRC
requirements
in the areas
of operating
and administrative procedures.
Personnel
performing the calibration demonstrated
competency.
The relays
were removed
from the shutdown
boards
(switchgear)
and brought to a
room in the control building .to be calibrated.
This room was called the
communications
room as it contained
relays
and communications
equipment
associated
with the Transmission
System.
The inspector
observed that this
room contained
several
temporary fans of various sizes
which were running.
The inspector learned that there
was
a problem with the
HVAC System,
and the
fans were
needed to maintain proper ambient temperature
for the equipment
in
this room.
The inspector discussed
this matter with the Hanager of Technical
Support.
Nodifications
had
been
implemented during the extended
shutdown
on
the
HVAC System,
causing
the system to become
unbalanced:
The licensee's
engineers
expect that once the system is balanced
through performance of
Surveillance Instruction SI 35, Control
Bay Flow Balancing,
the temperature
in
all rooms in the control
bay should
have proper temperature.
The flow
balancing is scheduled for completion prior to Unit 3 restart.
4.7.4 Installation
and Testing of Potential
Transformers
One of the three potential
transformers
which sense
voltage
on the
500
kV bus
for use in metering
and relaying circuits had failed.
As
a result,
the
Transmission
and Customer Service
group replaced that potential transformer
and conducted testing
on the other two.
The potential transformers
were
located at 500
kV bus
1-1
and the failed unit was sensing
voltage
on phase
A.
The inspectors
witnessed
the testing of the phase
B potential
transformer
and
portions of the phase
A potential
transformer
changeout.
0
~i
ii)
23
First, oi1 samples
were taken
and sent offsite for analysis.
The following
tests
were conducted:
Power factor (Ooble), Insulation resistance,
Ratio,
Resistance
readings with bridge ins'trument to check secondary
wires, and
connections,
and Pressure
switch operability.
All of the tests
had good
results.
The inspector
noted that the test set
had
been calibrated
on June 8,
1995,
as indicated by,the sticker
on the instruments.
The inspector
observed that safe work practices
were maintained.
The
potential
transformers
were returned to service.
The work evolution
represented
an example of coordination
between
the nuclear plant operators.
and
outside
groups
in performing work on
an important to safety
system interface
or boundary.
The inspector concluded that the coordinati'on
was
we11
planned
and managed.
At the junction box in which the potential transformer
secondary
were
collected
the inspector
noted the following conditions.
The wire insulation
was embrittled, spl'it and cracked.
On one wire, the insulation deterioration
had
advanced
to the point where
a portion of the conductor
was exposed.
Three
or four terminal points
on the terminal blocks
had significant corrosion.
Several
ring tongue terminal lugs appeared
to be improperly crimped
(undercrimped)
as the barrel
crimp dimple was not visible.
The inspector
identified these conditions,
and pointed
them out to persons
in charge of the
potential transformer work.
A PER (95-1243)
was initiated to document
these
conditions.
Later, the inspector
learned that
a terminal block was replaced
and corrosion cleaned off.
The'wires
passed
an insulation resistance
test.
Sealant
was applied to where water could have entered
the box.
Also, the
inspector
was told by a plant system engineer
and
a Transmission
and Customer
Service engineer that the problem of cracked insulation
on wires running
between
equipment in the switchyard
had
been identified
a few years previous.
The approach
has
been to inspect wiring when maintenance
is performed
on
equipment
and to .schedule
replacement of wires that are found deteriorated.
4.7.5 Motor Operated
Valve Diagnostic Testing
The inspector witnessed
ongoing work to perform diagnostic testing
on two
valves.
The first valve was .3-FCV-73-44,
The High Pressure
Coolant Injection
discharge
valve.
The objective of this diagnostic test
was to measure
the
thrust delivered
by the operator to the valve
and
compare
the measured
value
to predetermined limits.
The work was being performed
under Work Plan
No.
18966-010.
The inspector
observed
attempts
to set
up the gauge
which would
measure thrust
and torque.
- Problems
were encountered
locating
a gauge
which
would fit the dimensions of the valve.
Also,
one gauge that
may have worked
was found broken
and unusable.
As
a result of these
problems the craftsmen
worked about
seven
hours
and actually accomplished
nothing toward completing,
the task.
The work was rescheduled
to
a time beyond the inspection period.
The inspector
concluded that this particular 'evolution represented
a case of
poor planning.
The second
valve was 3-FCV-74-57,
Residual
Heat
Removal
Pressure
Suppression
Chamber isolation valve.
This valve had failed its leak test,
and, therefore,
the torque switch was being adjusted
to al'low the actuator to deliver maximum
allowable thrust to .the valve.
The inspector witnessed all adjustments
to the
ll'~
24
torque switch and associated
diagnostic testing.
The torque switch was
increased
in increments,
and torque
and thrust were checked after each
increment until the maximum allowable
and practical setting
was achieved.
The
final setting resulted
in a total thrust of 62,048 lbs.
and total torque of
1348 ft-lbs.
These
values
were within the maximum allowable total thrust of
64,298 lbs and the maximum allowable total torque of 1670 ft-lbs.
The
inspector
noted that technicians
kept track of the number of starts
given to
the motor,
and their procedure
provided guidance
on the number of starts to
avoid overheating
the motor.
The work proceeded
in a controlled
and orderly
manner.
The inspectors
concluded that the above discussed
testing indicated that,
in
general,
Unit 3 surveillance testing is being performed professionally.
Some
problems
were noted with one test involving core spray.
The reviews indicated
that the testing fully demonstrated
the required functions of the systems.
The inspectors
observed
several
examples of good coordination
between
different working groups.
Engineering
personnel
supported
the testing well.
4.8
Assessment
of Recent
Drawing Issues
The inspectors
performed
a review of recently identified design
drawing
deficiencies
in order to assess
the significance
and look for common causes.
The inspectors initially focused
on
NRC identified issues
and then reviewed
some of the licensee's
programs for drawing control issues.
A matrix of all drawing issues
described
in NRC IRs within the last two years
was developed
by the inspectors.
A total of 14 issues
which 'involved drawing
deficiencies
were discussed.
The majority of the identified problems
(9) were
of small safety significance
and were addressed
in 'IRs primarily since they
were
NRC identified.
One of the drawing problems contributed to
a scram in
1994
and two others contributed to missed local leak rate testing of
containment isolation valves.
One drawing error could have resulted
in
incorrect installation of Thermol ag. material.
Errors during incorporation of
DCAs into base
drawings played
a role in some of the issues.
The drawing
problems which contributed to the scram
and
a missed test
on
an exces's
flow
check valve involved programmatic
(drawing control
program)
issues.
For
example,
the decision to omit excess
flow check valves
on .some drawings
contributed to missing required leak rate testing
on
a valve.
In these
cases,
drawing errors
were not made.
Four of the
14 issues
involved drawing problems
which would be classified
as configuration control weaknesses.
The inspectors
reviewed
Procedure
SSP-2. 11, Drawing Deviation Program,
which
established
the requirements
for evaluating,
dispositioning,
and documenting
apparent
discrepancies
between
actual plant configuration
and as-constructed
configuration control drawings.
Procedure
SSP-2. 11 requires
the Technical
Support group 'to resolve
a potential
drawing discrepancy
following initiation
of a drawing deviation.
The inspectors
reviewed in detail the licensee's
Potential
Drawing Discrepancies
(PDDs) trend reports for the period of
January
I to June
30,
1995.
The quarters
ending
December,
1994
and March
1995
each
had over 270
PDDs initiated.
Many of these
PDDs were attributed to the
security modifications.
The most recent data available,
the qua} ter ending
June
1995,
had only 165
PDDs initiated.
1
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25
The trend reports
indicated that about
30 to 40 percent of the
PDDs involved
drawings associated
with Critical Systems,
Structures,
or Components
as set
forth in procedure
SSP 2.8,
Drawing Control.
Use of the
CSSC list should
be
minimal once the 9-List is completed.
The
PDD trend reports stated that in
the quarter ending in March 1995,
84 percent of the,PDDs
were attributed to
drawings being incorrect.
In the quarter ending June
1995,
67 percent of the
PDDs were attributed to incorrect drawings.
The majori.ty of drawing
discrepancies
were associated
with Unit 3 in both quarters.
The inspectors
estimated that in the period of April to June
1995, approximately
32
CSSC
drawings required corrections.
Sixty percent of these
involved Unit 3
drawings.
Th'ese
numbers
appeared
to be larger than expected.
'No one type of
drawing was implicated in a majority of the drawing discrepancies.
The
inspectors
noted that the licensee
tracks timeliness of PDD dispositions.
About 16 percent of the
PDDs were dispositioned later than the licensee's
goals.
The inspector's
observations'egarding
the
PDD trends
were communicated
to management.
The licensee's
response
to questions
about the
PDD trends
was
an attempt to
bound the scope
and significance of the issues.
The
139
PDDs generated
in the
period April
1 to June
30,
1995 were examined.
Ninety-two of these
PPDs
involved Unit 3 drawings.
Of these,
27 were determined to be
PDDs associated*
with the list of drawings specified in 'Browns Ferrp'ngineering
Project
Instruction 89-06:
Design 'Change Control.
Licensee
personnel
indicated that
this set of drawings is the "baseline" list of drawings
as stated
in the
Browns Ferry Nuclear Performance
Plan.
The inspectors
were informed that
59 (of 92 total) of these
PDDs involved Unit
3 primary (Category
1)
and secondary
(Category 2-4) drawings associated
with
Critical Systems,
Structures,
or Components
issued
as Configuration Control
Drawi.ngs
(CCDs).
Licensee
personnel
indicated that the total
number of Unit 3
CCDs included in the
DVBP,
SPAE/SPOC,
and
DCN programs to be issued prior to
U3 Restart
are:
0
Category
1 drawings - 848 (UO),
492 (Ul), 815 (U2), 863
(U3)
= 3,018
CCD
'rawings
Secondary
drawings - 5467
(UO),
1744 (Ul), 5123
(U2), 6302
(U3)
= 18,636
CCD
-drawings
Based
on this additional information, the inspectors
concluded
that the
number of identified
PDDs involving incorrect Unit 3 drawings
was less
than
1%
of the total Unit 3 CCDs.,
None of the
27
PDDs impacted nuclear safety or
operability.
(Examples
included vent valves not shown, labeling,
and contact
positions
on electrical drawings.)'he
licensee
indicated that only two of
these
PDDs addressed
issues within the Safe
Shutdown Analysis Program.
The inspectors
reviewed
an Nuclear Assur ance
and Licensing assessment
of the
Unit 3
DBVP which was performed in August 1994.
The report indicated that
Unit 3
CCDs were not as reliable
as Unit 2 CCDs.
The assessment
team
was not
able to find documentation of the process
used to develop the Unit 3 CCDs.
Numerous
drawing deficiencies
were identified during the assessment
involving
I
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26
recently issued
CCDs.
The report stated that the
CCDs have limitations and
that these limitations are not always understood
by drawing users.
The inspectors
reviewed the actions
taken in response
to the assessment
and
held additional discussions
with licensee
personnel.
As
a result of these additional
reviews,
the inspectors
concluded'hat
although the Unit 3 configuration drawings
were not subjected
to the
same
rigorous walkdowns
as the Unit 2 drawings, virtually all of the deficiencies
identified to date
have not had
any nuclear safety or major operational
.
impacts.
A deliberate decision
was
made
by l.icensee
management
that the
potential
increase
in overall drawing quality was not worth the large effort
necessary.
Licensee
management
had recognized
and users
have
been trained
on
the limitations of the drawings.
The inspectors
reviewed previous
IRs and
correspondence
associated
with the Unit 3 drawing programs
and concluded that
specific
were being met.
While it was difficult to
obtain specific data
from the current Potential
Drawing Discrepancy trending
reports,
drawing deficiencies
are being adequately
tracked
and resolved.
The
licensee
indicated that the methodology
used for PDD trending will be changed.
The inspectors
concluded that the information reviewed indicates that while
drawing discrepancies
continue to be identified, few have contributed to
safety significant operational
problems.
A large
number of the drawing errors
were identified during the
SPAE/SPOC "roll up" process
after
DCN completion
when
DCAs are incorporated into the "as constructed"
drawings.
These
identified errors
appear to be at least partially attributed to complexities
in the drawing
and modification control processes.
Some of the less
significant drawing .issues
continue to adversely
impact the licensee.
For
example,
PER 951081 described
extensive efforts required to determine
the
material
used
on pressure
transmitter piping (from a main steam)
due to
drawing errors.
The inspectors
continue to review drawings during inspection of Unit 3
recovery activities.
Paragraph
4.2 of this report describes
some
NRC review
of installed equipment
versus
the drawings.
4.9
Foreign Material Within 3A Core Spray
Pump
On August 25,
1995, during testing of the Core Spray System,
the
3A Core Spray
pump was unable to achieve rated flow.
Initial troubleshooting
and inspection
(boroscopic
inspection of the
pump bowl) of the
pump revealed that foreign
material
was lodged within the
pumps impeller.
The licensee initially
postulated that the material
most likely came from the condensate
transfer
system during torus fill.
A PER
(BFPER951168)
was generated
to document the
condition
and
an Incident Investigation
team
was formed to determine
and
correct the cause of the incident.
Attempts to retrieve the material
through
the
pumps casing
were unsuccessful
making it necessary
to remove the
motor/pump assembly.
The inspectors
observed this evolution
as well the
retrieval of the foreign material. Initially, the material
removed
was thought
.
to be
a welders sleeve,
however; after further examination,
the material
was
determined
to be
an underwater
vacuum bag. This type of vacuum
bag
was
I~
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~
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27
utilized during the clean out of the
CSTs in 1985.
The vacuum
bag
was mostly
intact with a small portion missing.
The II team
recommended
that the underwater portions of the torus
as well as
the five condensate
storage
tanks
be inspected.
TVA contr acted divers to
perform these
inspections.
The first area
inspected
was the torus
and its
associated
While inspecting this area,
the divers located
portions of the vacuum bag,
a few pieces of duct tape with plastic attached,
and
a small
snap ring (5/8" diameter)
on the torus bottom in the vicinity of
the
3A Core Spray
pump discharge.
The duct tape
and plastic were apparently
what the inspectors
observed floating in the torus
as discussed
in paragraph
4.7. 1.
and 4. 10.
Other than
some minor silt on the torus bottom,
no other
substantial
foreign material
was observed.
Inspection of the
CSTs did not
reveal
any additional material similar to that which was found in the
pump.
The licensee
determined that it was not practical to inspect
2 due to
safety concerns for the divers
as the possibility existed that
HPCI could
initiate during the underwater inspection.
This
CST will be inspected
during
the next Unit 2 outage.
The II teams preliminary conclusions
are that the vacuum
bag
was left in the
CST 3 during its clean out in 1985.
The II team evaluated
the alig'nment
used
to fill the Unit 3 torus
and determined that there
was
no potential for
foreign material
from Unit 3 to have
been flushed into the Unit 2
ECCS systems
through the condensate
cross ties.
The inspectors
concurred with this
conclusion.
Additionally, the licensee II team is recommending that
a flush
of condensate
and condensate
suction lines to the
RHR pumps
be
performed using the
RHR drain
pumps.
The inspectors will continue to monitor
the licensee's
efforts in this area.
The deficiencies
in FHE practices
which caused this incident apparently
occurred years
ago.
The licensee's
testing
program
and review of data
resulted
in the identification of the problem.
The inspectors
concluded that
the licensee's
actions after the material
was identified were adequate
to
ensure that Unit 2
ECCS systems
were not affected
by the material.
4. 10
Foreign Material Exclusion Accountability Control
Problem
On August 28, while observing
a portion of a Unit 3 Core Spray flow test,
the
inspectors
observed
a number of what appeared
to be pieces of foreign material
floating on the surface of the torus water.
This observation
was
made
from
the outside of the torus through .the torus hatch.
At the time of the
observation,
the torus proper
was being controlled
as
a foreign material
exclusion
area in accordance
with SSP-12.8.
The torus
has
been maintained
as
a foreign material
exclusion
area
since being refilled in
April 1995.
As
a
result of these
observations,
the inspectors
entered
the torus
(on August 30)
to determine
the extent of condition of foreign material within the torus
water.
During the internal
inspection of the torus,
no foreign material
was
identified in the torus water due to low water clarity.
However, during
a
review of the
FNE accountability log for the torus,
the inspectors
noted that
the temporary light stringer located within the torus
was not documented
in
~ the log.
The inspectors
informed the licensee of this matter
and
a
PER
(BFPER951184)
was generated.
As discussed
in paragraph
4.9 above,
duct tape
0
O~
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28
and plastic material
were subsequently
recovered
from the torus
by divers
and
this material
was apparently
what the inspectors
had seen.
This failure to follow plant procedure
SSP-12.8,
Control, represents
a violation of 10 CFR 50, Appendix B, Criterion V.
This
matter is similar in nature to violation 50-260/94-27-01,
(example,2),
in
which equipment
being utilized within the Unit 2 torus
was not recorded
in the
FME accountability log.
The current matter represents
a continuing problem
with the control of foreign material
and will be tracked
as violation 50-
296/95-51'-01,
Failure to Properly Control Material within an
FHE Zone.
5.0
Review of Open
Items
(92700)
(92901)
(92902)
(92903)
(92904)
The open
items listed below were reviewed to determine if the information
provided met
NRC requirements.
The determinations
included the verification
of compliance with TS and regulatory requirements,
and addressed
the adequacy
of the event description,
the corrective actions taken,
the existence of
potential generic
problems,
compliance with reporting requirements,
and the
relative safety significance of each. event.
Additi'onal in-plant reviews
and
discussions
with plant personnel,
as appropriate,
were conducted.
5. 1.
(CLOSED)
VIO 259,
260, 296/92-09-03,
Failure
To Control Access
To
Protected
Area.
This violation occurred
when two individuals whose
employment
had
been
terminated
entered
the protected
area.
The proper procedures
for employee
check out had not been followed by the employees
nor their supervisors.
As
a
result, their access
badges
which allowed access
to the protected
area
and
vital areas
were not revoked
and were subsequently
used
by the terminated
employees
to gain access
to the protected
area.
Upon discovery of this event,
'he
licensee
removed the employees
badges
to prevent further entrance
into the
protected
area.
TVA Nuclear Business
Practice
BP-108,
Processing
Employees
In
And Out Of TVA Nuclear,
a corporate level procedure,
was revised to provide
a
clear methodology for out-processing
of employees.
In addition,
BP-308,
Browns Ferry Check-In/Check-out
Procedure,
was written to provide
a check-out
form and
a step-by-step
procedure for processing
out.
This procedure
describes
the responsibilities
and provides guidance to both the person
whose
employment is being terminated
and that employees
supervision.
Included
on
the check-out
form is
a signature
by site security indicating that protected
area
access
has
been
revoked.
This procedure
and check-out
form is required
to be completed
by all site personnel
whose
employment is terminated.
This
violation is being closed
based
on these corrective actions.
5.2
(CLOSED)
Unit 2 Scram
From 54 Percent
Power Caused
By
Balance
Of Plant
Equipment Failure.
This event occurred
on December
2,
1994,
when
a faulty stator water cooling
temperature
switch generated
a false high temperature
signal
and tripped the
main turbine which resulted
in a reactor
The licensee
determined that
the switch
had
been calibrated
two months earlier
and
had exhibited
an
unusually high reset
dead
band.
However, there
was
no procedural
guidance
'e
4i
4I~
~ ~
29
which described
what constituted
an unsatisfactory
setting
and the. switch was
left installed.
Following the event the licensee
developed
a procedure for
calibrating this switch and it was subsequently
replaced.
In addition, the
licensee
developed
a list of fifty-three balance of plant devices
which were
capable of individually initiating a turbine/generator trip or other major
equipment operation.
A cost benefit analysis
was performed for the items
on
the list and determined that thirty-three of the items would be modified to
alleviate the single failure vulnerability.
In the interim period, the
preventive
maintenance
and calibration procedures
for the components
on the
lis't were reviewed to determine if additional action
needed to be taken to
provide added
assurance
that the components
would not fail.
This review did
not identify any needed
changes
to the existing maintenance
schedule.
In
addition, training was provided to maintenance
and engineering
personnel
on
this event
as well as the proper
use of electronic temperature
calibrators
and
the identification of degrading
equipment.
This item is closed.
5.3
(CLOSED)
IE Bulletin 79-12 (Unit 3), Short Period
at
Facilities.
An inspector
reviewed Bulletin 79-12;
as it pertained to Unit 3; in order to
determine
the current status of licensee efforts in addressing
the issue.
In
this review, the inspector
noted the following:
In TVA's initial response
to Bulletin 79-12;
as presented
in letters
dated
June
30,
1979
and August 19,
1981;
TVA tendered
a commitment to
perform both unit and cycle-specific analyses
of rod withdrawal
sequences
to ensure
notch worths of individual control rods were
minimized.
The bulletin was subsequently
closed
as part of USNRC
Inspection
Report '50-296/81-18.
In a .letter .dated January
4,
1990,
the licensee
requested
to use
vendor/NRC-approved,
banked withdrawal
sequences
and reduced
notch worth
procedures
for future startups.
In the
same letter, the licensee
requested
a revision to
a commitment regarding fast period
and to
no longer require either cycle or unit specific analysis of rod notch
worths.
In an
NRC to licensee letter,
dated
January
25,
1990,
the
NRC
found the licensee's
revised
commitment to the bulletin to be
'cceptable.
Unit 3 Technical Specification
LCOs 3.3.B.3.b
8 3.3.B.3.c
and
Surveillance
Requirements
4.3.B.3.b.
1
8 4.3.B.3.b.2 appropriately
reflect TVA's current position
on withdrawal
sequences
and reduced
notch
worths.
An SI, 3-SI-4.3.B. I.a,
"Coupling Integrity Check" procedure,
(effective
September
1,
1995),
has
been
approved for use in the. Unit 3 restart.
This SI implements
an
RWH sequence
which incorporates
procedures
for
Reduced
Rod Notch Worth and
Banked Position Withdrawal
Sequences.
A
similar Unit 2 SI has
been successfully
used for previous Unit 2 start-
ups.
et
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30
Based
on this review, the inspector concluded that the,licensee's
corrective
actions properly addressed
bulletin concerns
and were acceptable
for the
upcoming Unit 3 restart.
This item is closed.
'5.4
(CLOSED) Multi-Plant Action Item (HPA) COll (Unit 3),
(TAC H08931);
Power Supply.
In an
NRC August 7,
1978 letter, the licensee
(TVA) was told of defects
identified in
TVA was further asked to evaluate
BFNP's design
and to commence
a heightened
surveillance of the,RPS
power supplies.
In an
NRC September
24,
1980 letter,
TVA was informed, that based
upon
NRC
evaluations,
BFNP
RPS power supply modifications should
be implemented to meet
Class
lE requirements,
single failure criteria and seismic requirements.
The
NRC also stated that appropriate
RPS power supply Technical Specification
changes
should
be implemented.
In a TVA to
NRC December
4,
1980 letter,
made
a commitment to install
such modifications,
submit
TS changes.
These
activities were completed
by March,
1985.
In the
NRC Safety Evaluation
(June,
1985),
the
NRC stated that based
upon their review of TVA's modifications
and
the specific actions taken,
TVA had satisfactorily resolved
the issue.
A
related
issue;
(comparable
RPS power supply modifications to
HG set output breakers)-
was closed
as part of IR 50-296/95-22.
Based
upon the
above
and the inspector's
review of the Unit 3 modifications
and related
documentation,
this issue is closed for Unit 3.
Similar work on the Unit 2
RPS power supply was noted
as complete in 1990
and
an analogous
Unit 2 issue
was closed in Inspection
Report',
50-260/90-40.
5.5
(CLOSED) THI Action Item II.K.3.57 (Unit 3), Identify Water Sources
Prior to Hanual Activation of ADS.
An inspector
reviewed
item II.K.3.57 and noted that
a TVA to
NRC letter
(December
23,
1980) stated that
TVA would ensure that related
procedures
contained verifications of low pressure
water source availability prior to
manual
actuations of the
ADS.
The inspector further reviewed the present
status of TVA's Unit 3 response
and noted the following:
In almost all cases,
any Unit 3
EOI action step which requires
manual
actuation of the
ADS is prefaced
by
a "note" or "substep".
This
"note" or "substep" highlights the need for operator verification of a
low pressure
water source
(or sources)
prior to manual
ADS actuation.
In some cases;
where
emergency
Unit 3 reactor depressurization
is
required,
but
an undesired
reactor repressurization
is
a distinct
possibility; the
EOI directs the operator in the elimination of low
pressure
water sources
which could repressurize
the reactor.
This
action step
change
has
been
made
subsequent
to the original concerns
presented
by the THI action .item.
The inspector
observed that the
above
changes
were complete
and that similar,
Unit 2 EOIs have
been
approved for use during the operation of BFP Unit 2.
NRC review of the
EOIs has
been
completed.
Based
upon the above
and the
inspector's
specific review of the Unit 3 EOIs
and related documentation,
this
THI Action Item is closed for Unit 3.
8V
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5.6
31
(Closed)
Unresolved Safety Issue A-48, Hydrogen Control Measures
and
Effects of Hydrogen Burns
on Safety Equipment.
This item in conjunction with Generic Letter 84-09
(Recombiner Capability
Requirements
of 10 CFR 50.44 (c)(3)(ii)), discusses
the potential for the
evolution
and burning of hydrogen within containment.
The burning of high
hydrogen concentrations
could lead to
a challenge of containment integrity and
the mal.function of safety equipment within the containment.
The containment
at Browns Ferry Unit 3 is
a standard
BWR Mark I containment.
To mitigate the possibility of a high hydrogen concentration
occurring
and its
associated
burn, the following actions
are in place;
TS require that within
24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of placing the reactor in the run mode,
the containment
atmosphere
oxygen content shall
be reduced to less than
4 percent (inerted)
and
maintained
in this condition.
In addition to maintaining
an inerted
containment,
the licensee
is required to maintain two independent
trains of
the Containment Atmospheric Dilution (CAD) system in an operable status.
The
CAD system is utilized in a post
LOCA condition to prevent the containment
from reaching
a combustible mixture by diluting the containment
atmosphere
with nitrogen
and venting
as necessary.
Additionally, the pneumatic control
system for the drywell (drywel) control air) utilizes nitrogen
as its source
of air by taking
a suction
from the containment
(inerted with nitrogen).
The
air is compressed
and stored in the drywell control air system
and utilized as
necessary
for drywell pneumatic
loads.
Through
a recent modification,
a
backup supply for the drywell control air system is the
CAD system.
By a
series of manual
actions in the control
room and in the plant, operations
personnel
can align the
CAD system to supply compressed
air (nitrogen) to the
drywell.
By utilizing the
CAD system
as
a backup to the drywell control air
system
no oxygen will be introduced into containment.
Although this
modification alleviates
the need to use plant control air as
backup to the
drywell control air system, this capability still exists.
However, if the
plant control air system is utilized in this manner,
plant
TS require the unit
to placed in cold shutdown within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />
due to the potential of introducing
oxygen into the containment
atmosphere.
The inspector
reviewed all correspondence
related to
(Status:of Safety Issues
at Licensed
Power Plants),
and portions of DCN W17937
(Modification which provided the
CAD system
as the backup pneumatic
source for
drywell control air) to ensure all aspects
related to USI A-48 have
been
completed.
Additionally, the inspector
went to the local public document
room
to review
(SECY Paper which informed the Commission of the 'basis
for resolution of USI A-48) to verify the licensee
had completed all required
actions related to this matter.
Based
on this review of the above stated
licensee
actions
and controls,'this'matter
is closed.
5.7
(CLOSED)
DEV 259,
296/85-36-04:
Torus Flood Level Switches.
This issue
addressed
the seismic qualifications of the reactor building flood
detection
switches.
The licensee
responded
to the deviation in correspondence
dated
September
22,
1985.
The item was closed for Unit 2 in IR 89-19.
The
underlying issues
have
been
addressed
in subsequent
LERs and corrective
actions
completed.
t
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ggi
Oi
32
The original deviation
addressed
the failure to meet
a
FSAR statement
(Section
10. 11.5) which stated that the reactor building flood switches
were
seismically qualified.
IR 89-36 also noted that the switches
were not tested.
The switches
were to be seismically mounted
and tested periodically.
Subsequent
to this,
was issued
when the switches
and electrical
circuitry was found. to be not seismically qualified.
The
FSAR was revised to
reflect that the switches
were not seismic.
Credit was taken, for operator
actions.
This
LER was closed
in IR 90-29.
The licensee recently completed
a
Commitment Evaluation
(SSP
Form-17) which justified deleting the commitment
for seismically qualified switches
on Units
1 and 3.
The inspector
reviewed Section 4.5 of the current Fire Protection
Plan
describing the operator
actions
and level switch functions in case of a
failure of the fire protection piping in the reactor building.
Additionally,
the safety evaluation, (July 25,
1988) which justified the switches
not being
seismic
was reviewed.
The inspector verified that the assumptions
and actions
stated
in the
documents
remained valid.
The inspector. concluded that the
concerns
in the deviation
had
been
adequately
addressed.
However,
since
flooding, is
a significant risk factor in the recently completed multiple unit
operation
Plant Safety Assessment,
the inspectors
performed additional
review
of
overall flood protection issues
as described
in paragraph
2.5 of this
report.
Based
on this review, the deviation is closed for Units
1 and 3.
5 '
(CLOSED)
URI 296/95-10-01:
Inadequate
Second
Party Verification by Craft
Worker.
Extensive
NRC review of this item is documented
in IRs 94-35,
95-14,
and 95-
20.
NRC inspectors
have verified numerous re-inspections
of cables
and
splices.
It was concluded that the licensee's
investigative
and corrective
actions
were adequate
to address
potential
concerns
regarding quality control
practices.
Based
on those reviews, this item is closed.
5.9
(CLOSED)
IF.I 259,
260,
296/94-07-04:
Identification of System Test
Boundaries
This IFI was
opened to track questions
raised
regarding the identification of
system test boundaries.
In discussions
with licensee
personnel, it was noted
that procedures
did not require that
SPAE boundaries
be developed with the
concurrence
of operations
and technical. support personnel.
The inspector
was
also concerned
about the use of color-coded
drawings
used to indicate
operational
boundaries
between
the units.
The licensee
provided the inspector with a copy of BFEP PI 88-07,
"System
Plant Acceptance
Evaluation."
Subsection
4.2. 1 of this procedure,
"SPAE
Boundary,"
has
been revised to require that the cognizant
system design
engineer
determines
the
SPAE boundary with appropriate
coordination with
groups responsible
for definition of SPOC boundary
scope.
This requirement
addresses
the concerns with test boundaries.
The licensee
provided the inspector with a copy of revision
17 to SSP-12.50,
"Unit Separation
for Recovery Activities," dated
February 8,
1995.
In part,
this procedure
provides the process
for revision of color-coded
drawings
as
F
C)
~
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il~
33
modifications
and tests
are completed
and systems
are returned to operation.
The licensee
has indicated that it does not plan to continue color-coding
drawings for systems that are fully restored
and operational.
Separation
drawings
and clearances will remain in place
as required to isolate
unqualified
BFN Unit
1 components.
This plan was discussed
in
a public
meeting
on July 20,, 1995 with NRC personnel
monitoring
BFN Unit 3 restart
activities.
The revisions to SSP-12.50
are responsive
to the concerns
expressed
in IFI 94-07-04.
The issues
raised
by IFI 94-07-04
have
been
addressed
by the licensee
as noted
above.
Therefore,
IFI 94-07-04 is closed.
The effectiveness
of the
licensee's
implementatiori of the
SPAE program
and return of systems
to service
continues
to be monitored
by igspectors.
6.0
Exit Interview (30703).
The inspection
scope
and findings were summarized
on September
19,
1995, with
those
persons
indicated in paragraph
1 above.
The inspectors
described
the
areas
inspected
and discussed
in detail the inspection findings listed below.
Although proprietary material
was reviewed during the inspection,
proprietary
information is not contained
in this report.
Dissenting
comments
were not
received
from the licensee.
Item Number
Status
Descri tion and Reference
296/95-51-01
Opened
VIO-Failure to Properly Control
Naterial within an
FHE
Zone, (paragraph
4. 10)
260/95-51-02
Opened
8 Closed
NCV-CRD Scram Air Header Valve Out
Of Position,
(paragraph
2.3)
259,260,296/92-09-03
Closed
VIO-Failure To Control Access
To
Protected
Area,
(paragraph
5.1)
260/94-013
HPA COll
TNI II.K.3.57
Closed
Closed
Closed
Closed
LER-Unit 2 Scram
From 54 Percent
Power
Caused
By Balance
Of Plant
Equipment Failure,
(paragraph
5.2)
Short Period
at
Facilities (Unit 3)
(paragraph
5.3)
Power Supply (Unit 3) (paragraph
5.4)
Identify Water Sources
Prior to
Nanual Activation of ADS (Unit 3)
(paragraph
5.5)
+i0
~
/Q>
USI A-48
Closed
34
Hydrogen Control Measures
and
Effects of Hydrogen Burns
on Safety
Equipment
(paragraph
5.6)
DEV 259,296/85-36-04
Closed
Torus Flood Level Switches
(Units
153)
(paragraph
5.7)
URI 296/95-10-01
IFI 259,260,296/
94-07-04
Closed
Closed
Inadequate
Second
Party Verification
by Craft Worker (paragraph
5.8)
Identification of System Test
Boundaries
(paragraph
5.9)
7.0
and Initialisms
ADSRV
AOI
ASHE
BFEP
BTRD
CCD
CFR
CPH
CR
CSSC
DBVP
DCN
DEV
DP
EHS
F
FHE
Automatic Depressurization
System
Automatic Depressurization
System Relief Valve
Abnormal Operating Instruction
American Society of Mechanical
Engineers
Assistant Unit Operator
Browns Ferry Engineering
Procedure
'Browns Ferry Nuclear Plant
Baseline Test Requirements
Document
Boiling Water Reactor
Containment Air Dilution
Common Accident Signal
Configuration Control Drawing
Code of Federal
Re'gulations
Counts
Per Minute
Control
Room
Control
Rod Drive
Condensate
Storage
Tank
Critical Structures,
Systems,
And Components
Design Baseline
and Verification Program
Drawing Change Authorization
Design
Change Notice
Deviation
Dioctyphtalate
Differential Pressure
Demonstration
Power Reactor
Division of Reactor Safety
Emergency
Core Cooling, Systems
Emergency 'Equipment Cooling Water
Emergency Diesel
Generator
Equipment
Management
System
Emergency Operating Instruction
Engineered
Safety Feature
Fahrenheit
Flow Control Valve
Final Safety Analysis Report
4
0
~
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GL
gpm
IFI
II
IR
LER
HOV
HPA
HS
HSIV
NRC
,NRR
ORRT
.
PDD
PER
PHT
PPH
SMPL
SPAE
TI
35
Generic Letter
Gallons
Per Minute
High Efficiency Particulate Activity
High Pressure
Coolant Injection
Heating, Ventilation,
and Air Conditioning
Keat Exchanger
Inspector
Followup Item
Incident Investigation
Inspection
Report
Inservice Inspection
Inservice Testing
Licensee
Event, Report
Loss of Coolant Accident
Low Pressure
Coolant Injection
Microbiological Induced Corrosion
Motor Operated
Valve
Hulti-Plant Action Item
Hain Steam
Hain Steam Isolation Valve
Non-Cited Violation
Nuclear Regulatory
Commission
Nuclear Reactor Regulation
Nuclear Steam Supply System
Operational
Readiness
Review Team
Potential
Drawing Discrepancy
Public Document
Room
Problem Evaluation Report
Post. Modification Testing
Parts
Per Million
Pounds
Per Square
Inch Gauge
Polyvinylchloride,
Quality Assurance
Quality Control
Reactor
Core Isolation Cooling
Residual
Heat
Removal
Residual
Heat
Removal
Service
Water System
Reactor Operator
Reactor Protection
System
Restart
Test
Program
Standby
Gas Treatment
Safety Evaluation Report
Surveillance Instruction
Site .Master
Punch List
System Plant Acceptance
Evaluation
System Preoperational'hecklist
Senior Reactor Operator
Safe
Shutdown Instructions
Site Standard
Practices
System Test Specification
Service
Water
Temporary Instruction
0
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0
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0>>
THI
TOE
TS
T.VA
'.UFSAR
WO'R
36
Three Hile Island
Technical Operability Evaluation
Technical Specifications
Valley Authority
Updated Final, Safety Analysis Report
Unresolved Safety Issue
Violation
Work Order
Work Request
4 I
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