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LICENSEE EVENT REPORT (LER)
FACILITY NAME (1)
DOCKET NUMSER (2)
PA(aE (Je Nine blile Point Unit I o l5 l0 lo l o l 2l2 0 tlOFj0l3 1
TITLE tel Design Calculations Were Found Not In Compliance With FSAR EVENT DATE (SI LER NUMSER ($)
REPORT DATE (7)
OTHER f ACILITIES INVOLVED tal MONTM DAY YEAR YEAR 58,0 8,
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NAME TELEPHONE NUMBER AREA CODE Robert G. Randall, Supervisor, Technical Support 3 ;1 f>
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ABSTRACT On January 18, 1986 with the plant operating at 82*. power, it was determined that the original calculations for jet impingement loading on the Emergency Condenser Steam Supply Isolation Valves, due to a break inside the guard pipe, were not in compliance with the Nine blile Point Unit I Final Safety Analysis Report. This was discovered while recalculating the jet impingement loads for the replacement of the Emergency Condenser Piping and Isolation Valves. The new calculations indicated that the actual loading conditions are greater than those incorporated into the original design. The isolation valves are being replaced as part of the upcoming Emergency Condenser Piping Replacement h!odification during the 1986 refueling outage.
Initial corrective action included a shutdown of the Nine blile Point Une I plant on January 18, 1986 in accordance with Technical Specifications. Also, an engineering investigation to determine if other systems were similarily affected was initiated.
This new analysis addressed the h!ain Steam, Feedwater, Core Spray, Shutdown Cooling, Reactor Water Cleanup and Control Rod Drive Ilydraulic Return Systems. These systems have penetrations which utilize a guard pipe configuration similar to that in the Emergency Condenser System. Of these systems only the Emergency Condenser Steam Supply, blain Steam, Feedwater and Reactor Water Cleanup are subject to significant thrust loads due to postulated pipe breaks within the guard pipes. The other systems have normally closed isolation valves and/or check valves which prevent pressurization of the piping within the guard pipes as a result of a postulated break during normal operation, gp 8602240721 860214 f
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EXPIRES 8/31/55 7AcaLeiv psAssE til DOCEET NURESER (2)
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. -== a= eas w anc e, assamm TEXT On January 18, 1986 with the plant operating at 829 power, it was determined that the original calculations for jet impingement loading, due to a pipe break inside the guard pipe on the Emergency Condenser steam supply line were not in compliance with the Nine Mile Point Unit I Final Safety Analysis Report. This condition was discovered during the preliminary engineering for replacement of the Emergency Cooling steam supply piping and isolation valves.
The loads on the valve anchors were recalculated and, when compared to those developed during the original plant design, were foucd to be greater. The major difference between the calculations was the original calculation assumed no pressure buildup within the guard pipe while the new analysis assumes limited venting due to restricted flow conditions while exiting the guard pipe. The resultant increase in load is approximately two times greater than the original jet impingement load.
(Reference NMPC - Nine Mile Point Unit I Guard Pipe Configuration Analysis, dated January 1986).
Similar guard pipe configurations exist on the Main Steam, Feedwater, Core Spray, Shutdown Cooling, Reactor Water Cleanup and Control Rod Drive Hydraulic Return Systems.
Of these systems only the Emergency Condenser Steam Supply, Main Steam, Feedwater, and Reactor Water Clearup are subject to significant thrust loads due to postulated pipe breaks within the guard pipes. The remaining systems have normally closed isolation and/or check valves which prevent pressurization of the piping within the guard pipes as a result of a postulated break during normal operation.
ASSESSMENT OF POTENTIAL SAFETY CONSEQUENCES The assessment of potential safety consequences was based on the Icak-before-break concept. A previous analysis performed for a leak-before-break scenario was submitted in conjunction with our response to IE Bulletin 80-11.
It included the Emergency Condenser, Main Steam, Feedwater and Reactor Water Cleanup Systems. Although the analysis only considered piping outside of primary containment it was re-evaluated for applicability to piping inside the drywell. The determination concluded that the stresses on the piping inside the drywell were no higher than those outside the drywell. Therefore, the analysis is applicable and demonstrates that for significant through-wall cracks, adequate margin against unstable pipe rupture exists.
In addition, an existing leakage detection system inside the primary containment can detect reactor coolant leakage of less than one gallon per minute. The leak-before-break analysis indicates that the leak rate for a postulated 90 degree circumferential break would exceed one gallon per minute.
Therefore, existing mechanisms p,rovide an adequate safety margin even though the new load analysis imposes loads due to pres-surization which are greater than those in the original design. As a compensatory measure, a standing order was issued to initiate a reactor shutdown if drywell leakage increases by 1 gallon per minute in a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period after attaining steady state operation.
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These assessments were discussed with the NRC during a meeting on January 23, 1986.
l As a result of this meeting, a waiver of compliance was issued on January 24, 1986 authorizing the restart of Nine Mile Point Unit I' An amendment to the operating license was also issued on January 28, 1986 allowing continued operation for the remainder of cycle 8.
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CORRECTIVE ACTION
l Initial corrective action included a shutdown of the Nine blile Point Unit I plant on January 18, 1986 in accordance with Technical Specifications. Also, an investi-gation to determine if other systems were similarily affected was initiated. This new analysis addressed the blain Steam, Feedwater, Core Spray, Shutdown Cooling, Reactor Water Cleanup and Control Rod Drive flydraulic Return Systems. These systems have penetrations which utilize a guard pipe configuration similar to that in the Emergency Condenser System. Of these systems only the Emergency Condenser Steam Supply, blain Steam, Feedwater and Reactor Water Cleanup are subject to significant thrust loads due to postulated pipe breaks within the guard pipes. The other systems have normally closed isolation valves and/or check valves which prevent pressurization of the piping within the guard pipes as a result of a postulated break during normal operation.
In addition, Nh!PC will evaluate the need to modify the affected systems and perform any required modifications during the 1986 refueling outage.
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'NMP-16193 NtAGARA MOH AWK POWER CORPORATION :
NIAGARA MOHAWK
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$YR ACU S E, N.Y.132 O 2
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February 14,1986-3 United States NacLeari Regulatory Comnission Document Contral Desk
- - Washingt.on, DC 20555 RE: Docket No. 50-220 LER 86-01 Gentlemen:
In accordance with 10 CFR 50.73(a)(2)(i) and (ii) we hereby submit the I
following Licensee Event Report:
4 LER 86-01 Which is being subnitted in accordance with 10 CFR 50.73(a)
(2)(i)(A): "The completion of any nuclear plant shutdown l
required by the plant's Technical Specifications," and 10 CFR 50.73(a)(2)(ii)(B): "Any event or condition that '
resulted in the condition of.the nuclear power plant, i
including its principal safety barriers, being seriously degraded, or that resulted in the nuclear power plant being in a conddion that uns outside the design basis of
.the plant."
A 10 CFR 50.72 notification report uns made at 1620 on 1/18/86.
This Licensee Event Report uns completed in.the format designated in NUREG-1022, dated September 1983.
Very truty yours,
- M.-
o Thomas E. Lempges Vice President Nuclear Generation TEL/tg cc:
Dr.~ Thomas E. Marley Regionai' Administrator V
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| 05000220/LER-1986-001, :on 860118,original Calculations for Jet Impingement Loading on ECCS Isolation Valves Found in Noncompliance W/Fsar.Caused by Break Inside Guard Pipe. Isolation Valves Will Be Replaced |
- on 860118,original Calculations for Jet Impingement Loading on ECCS Isolation Valves Found in Noncompliance W/Fsar.Caused by Break Inside Guard Pipe. Isolation Valves Will Be Replaced
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i) | | 05000410/LER-1986-001-01, :on 861105,two Reactor Scrams Occurred During Initial Fuel Loading.Caused by Spike on Intermediate Range Monitor D & High Level Scram Discharge Trip.Operator Training Mod Submitted |
- on 861105,two Reactor Scrams Occurred During Initial Fuel Loading.Caused by Spike on Intermediate Range Monitor D & High Level Scram Discharge Trip.Operator Training Mod Submitted
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-002-01, :on 861104,four Source Range Monitors (Srms) Downscale Channels Placed in Bypassed State When Jumpers Installed to Clear SRM Downscale Rod Blocks.Caused by Human Error & Procedure Deficiency.Procedure Revised |
- on 861104,four Source Range Monitors (Srms) Downscale Channels Placed in Bypassed State When Jumpers Installed to Clear SRM Downscale Rod Blocks.Caused by Human Error & Procedure Deficiency.Procedure Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000220/LER-1986-002, :on 860201,radioactive Gaseous Effluent Monitoring Sys Stack Gas Sample Pump 1 Tripped.Caused by Failed Board in Microprocessing Unit.Board Replaced |
- on 860201,radioactive Gaseous Effluent Monitoring Sys Stack Gas Sample Pump 1 Tripped.Caused by Failed Board in Microprocessing Unit.Board Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000220/LER-1986-003, :on 860308,attempt to Reset HPCI Following Manual Trip of Turbine Failed Because Contacts for Emergency Governor Limit Switch Did Not Change State.Caused by Stuck Plunger Assembly.Work Request Initiated |
- on 860308,attempt to Reset HPCI Following Manual Trip of Turbine Failed Because Contacts for Emergency Governor Limit Switch Did Not Change State.Caused by Stuck Plunger Assembly.Work Request Initiated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-003-01, :on 861108,partial Loss of Secondary Containment Isolation Actuation Instrumentation Occurred. Caused by Personnel Error.Training Mod Recommendation Initiated |
- on 861108,partial Loss of Secondary Containment Isolation Actuation Instrumentation Occurred. Caused by Personnel Error.Training Mod Recommendation Initiated
| | | 05000220/LER-1986-004, :on 860308,w/unit Shut Down for Refueling,High Reactor Water Level Signal Resulted in Turbine Trip Signal, Causing Feedwater Control Sys Transfer to HPCI Mode. Procedural/Hardware Changes Being Considered |
- on 860308,w/unit Shut Down for Refueling,High Reactor Water Level Signal Resulted in Turbine Trip Signal, Causing Feedwater Control Sys Transfer to HPCI Mode. Procedural/Hardware Changes Being Considered
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-004-01, :on 861109,unit Experienced Two Full Scrams W/Mode Switch in Refuel.Caused by Faulty Circuit Card.Root Cause Unknown But Random Infant Mortality Suspected.Circuit Card Replaced |
- on 861109,unit Experienced Two Full Scrams W/Mode Switch in Refuel.Caused by Faulty Circuit Card.Root Cause Unknown But Random Infant Mortality Suspected.Circuit Card Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1986-005, :on 860402,during Shutdown for Refueling,Full Scram Experienced.Caused by Loss of Power to Reactor Protection Sys Bus II Due to Deenergization of Brown Boveri ITE-27 Relay.Relay Repaired or Replaced |
- on 860402,during Shutdown for Refueling,Full Scram Experienced.Caused by Loss of Power to Reactor Protection Sys Bus II Due to Deenergization of Brown Boveri ITE-27 Relay.Relay Repaired or Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-005-01, :on 861105,source Range Monitor Channel C Erroneously Left in Bypass Position Following Surveillance Check.Caused by Failure of Operator to Adhere to Procedure. Procedure Revised & Staff Counseled |
- on 861105,source Range Monitor Channel C Erroneously Left in Bypass Position Following Surveillance Check.Caused by Failure of Operator to Adhere to Procedure. Procedure Revised & Staff Counseled
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000220/LER-1986-006, :on 860409,discovered That One of four-inch Sample Lines to Header Completely Plugged.Caused by Pebbles Washed Off Reactor Bldg Into Roof Drains.Roof Drain Screens Will Be Installed |
- on 860409,discovered That One of four-inch Sample Lines to Header Completely Plugged.Caused by Pebbles Washed Off Reactor Bldg Into Roof Drains.Roof Drain Screens Will Be Installed
| | | 05000410/LER-1986-006-01, :on 861112,Tech Spec Hourly Fire Watch Patrol Surveillance Requirements Exceeded Twice.Caused by Cognitive Personnel Errors.Fire Dept Personnel Trained in Tech Spec Requirements & Patrol Methods Revised |
- on 861112,Tech Spec Hourly Fire Watch Patrol Surveillance Requirements Exceeded Twice.Caused by Cognitive Personnel Errors.Fire Dept Personnel Trained in Tech Spec Requirements & Patrol Methods Revised
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000410/LER-1986-007-01, :on 861120,two Electrical Protection Assemblies Spuriously Tripped,Resulting in Loss of Power to safety- Related Control Circuit.Root Cause Evaluation Will Be Performed |
- on 861120,two Electrical Protection Assemblies Spuriously Tripped,Resulting in Loss of Power to safety- Related Control Circuit.Root Cause Evaluation Will Be Performed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-007, :on 861120,ESF Actuation Occurred.Caused by Two Electrical Protection Assemblies (Epas) Tripping Twice in 2 H Causing Loss of Power to Circuit Bus Due to Personnel Error During MSIV Testing.Epas Reset |
- on 861120,ESF Actuation Occurred.Caused by Two Electrical Protection Assemblies (Epas) Tripping Twice in 2 H Causing Loss of Power to Circuit Bus Due to Personnel Error During MSIV Testing.Epas Reset
| | | 05000220/LER-1986-007, :on 860415,during Refueling Outage Acurex Fuel Zone Level Indication Instrumentation Found Inaccurate by 15 to 20 Inches in Nonconservative Direction.Ge to Correct Software & Acurex Instrumentation Recalibr |
- on 860415,during Refueling Outage Acurex Fuel Zone Level Indication Instrumentation Found Inaccurate by 15 to 20 Inches in Nonconservative Direction.Ge to Correct Software & Acurex Instrumentation Recalibr
| 10 CFR 50.73(a)(2)(1) | | 05000220/LER-1986-008, :on 860422,reactor Bldg Emergency Ventilation Sys Initiated Due to Undervoltage Condition on Instrument & Control Bus 30.Caused by Loss of Backfeed from Plant Switchyard.Investigation Continuing |
- on 860422,reactor Bldg Emergency Ventilation Sys Initiated Due to Undervoltage Condition on Instrument & Control Bus 30.Caused by Loss of Backfeed from Plant Switchyard.Investigation Continuing
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-008-01, :on 861117,discovered Potential Breaches in Fire Barriers During Control Rod Testing.Caused by Failure to Seal Penetrations.Fire Watches Established & Penetrations Sealed |
- on 861117,discovered Potential Breaches in Fire Barriers During Control Rod Testing.Caused by Failure to Seal Penetrations.Fire Watches Established & Penetrations Sealed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000410/LER-1986-008, :on 861117,discovered Potential Breaches in safety-related Fire Barriers.Caused by Contractor Failure to Follow Established Procedures for Identifying Incomplete Const Work.Breaches Sealed |
- on 861117,discovered Potential Breaches in safety-related Fire Barriers.Caused by Contractor Failure to Follow Established Procedures for Identifying Incomplete Const Work.Breaches Sealed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000410/LER-1986-009, :on 861124,reactor Bldg Ventilation Exhaust Damper 2HVR*AOD9B Closed Initiating Standby Gas Treatment Train A.Caused by Jumper Which Fell & Shorted to Ground. Alternate Installation Methods Under Review |
- on 861124,reactor Bldg Ventilation Exhaust Damper 2HVR*AOD9B Closed Initiating Standby Gas Treatment Train A.Caused by Jumper Which Fell & Shorted to Ground. Alternate Installation Methods Under Review
| | | 05000410/LER-1986-010-01, :on 861123,25% of Control Rods Received Full Scram Signal When All Group 2 Control Rod Solenoid Valves de-energized.Cause Undetermined.Investigation in Form of Supervisory Procedure S-SUP-1 Begun |
- on 861123,25% of Control Rods Received Full Scram Signal When All Group 2 Control Rod Solenoid Valves de-energized.Cause Undetermined.Investigation in Form of Supervisory Procedure S-SUP-1 Begun
| | | 05000410/LER-1986-010, :on 861123,25% of Control Rods Received Full Scram Signal When Group 2 Control Rod Scram Solenoid Valves Deenergized.Cause Not Positively Determined.Training Mod Request Will Be Issued.Procedures Revised |
- on 861123,25% of Control Rods Received Full Scram Signal When Group 2 Control Rod Scram Solenoid Valves Deenergized.Cause Not Positively Determined.Training Mod Request Will Be Issued.Procedures Revised
| | | 05000220/LER-1986-010, :on 860505,reactor Bldg Emergency Ventilation Sys Initiation & Isolation of Normal Reactor Bldg Ventilation Occurred.Caused by Blown Fuse in Control Circuit in Reactor Protection Sys Bus 11 |
- on 860505,reactor Bldg Emergency Ventilation Sys Initiation & Isolation of Normal Reactor Bldg Ventilation Occurred.Caused by Blown Fuse in Control Circuit in Reactor Protection Sys Bus 11
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-011, :on 861127 & 1208,automatic Initiation of Standby Gas Treatment Sys Divs I & II Occurred.Caused by Spurious Reactor Bldg Exhaust Ventilation Duct High Radiation Signals.Accumulator Added to Lines |
- on 861127 & 1208,automatic Initiation of Standby Gas Treatment Sys Divs I & II Occurred.Caused by Spurious Reactor Bldg Exhaust Ventilation Duct High Radiation Signals.Accumulator Added to Lines
| | | 05000220/LER-1986-011, :on 860508,contractor Received Contaminated Injury to Hand from Cut Section of Piping.Caused by Personnel Error.Medical Attention Administered & Radiation Exposure Survey Conducted |
- on 860508,contractor Received Contaminated Injury to Hand from Cut Section of Piping.Caused by Personnel Error.Medical Attention Administered & Radiation Exposure Survey Conducted
| | | 05000410/LER-1986-011-01, :on 861127 & 1208,automatic Initiation of Standby Gas Treatment Sys Div I & II Occurred.Caused by Reactor Bldg Refuel Area Exhaust Ventilation Duct Radiation High Signal |
- on 861127 & 1208,automatic Initiation of Standby Gas Treatment Sys Div I & II Occurred.Caused by Reactor Bldg Refuel Area Exhaust Ventilation Duct Radiation High Signal
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1986-012, :on 860516,both Fire Pumps Taken Out of Svc to Allow Diver to Work in Station Svc Water Intake Tunnel. Telephone Notification to Region I Not Made Until 860517. Personnel Counseled |
- on 860516,both Fire Pumps Taken Out of Svc to Allow Diver to Work in Station Svc Water Intake Tunnel. Telephone Notification to Region I Not Made Until 860517. Personnel Counseled
| | | 05000410/LER-1986-012, :on 861128 & 29,series of Related Automatic Initiations of Standby Gas Treatment Sys Occurred.Caused by Clogged Filters & Personnel Error.Approx 50% of First Stage Filters Replaced & Training Mod Initiated |
- on 861128 & 29,series of Related Automatic Initiations of Standby Gas Treatment Sys Occurred.Caused by Clogged Filters & Personnel Error.Approx 50% of First Stage Filters Replaced & Training Mod Initiated
| 10 CFR 50.73(a)(2) | | 05000410/LER-1986-012-01, :on 861128 & 29,automatic Initiation of Standby Gas Treatment Sys Divs I & II & Emergency Recirculation Subsystem of Secondary Containment Ventilation Sys Occurred. Caused by Supply Fan Trip |
- on 861128 & 29,automatic Initiation of Standby Gas Treatment Sys Divs I & II & Emergency Recirculation Subsystem of Secondary Containment Ventilation Sys Occurred. Caused by Supply Fan Trip
| 10 CFR 50.73(a)(2) | | 05000220/LER-1986-013, :on 860518,reactor Bldg Emergency Ventilation Sys Initiated Due to Blown Fuse.Caused by Damaged Timer Relay.Timer Repaired,Fuse Replaced & Sys Returned to Svc.W/ |
- on 860518,reactor Bldg Emergency Ventilation Sys Initiated Due to Blown Fuse.Caused by Damaged Timer Relay.Timer Repaired,Fuse Replaced & Sys Returned to Svc.W/
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-014-01, :on 861203,scram Experienced to one-quarter of Control Rods During Recovery from Earlier Scram & Containment Isolation.Caused by Personnel Error.Addl Licensed Operator Training Requested |
- on 861203,scram Experienced to one-quarter of Control Rods During Recovery from Earlier Scram & Containment Isolation.Caused by Personnel Error.Addl Licensed Operator Training Requested
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1986-014, :on 860603,reactor Scram Occurred During Surveillance Test.Caused by Instantaneous Inlet of Water in Transmitter RE-16B.Surveillance Test Will Be Revised & Technicians Cautioned |
- on 860603,reactor Scram Occurred During Surveillance Test.Caused by Instantaneous Inlet of Water in Transmitter RE-16B.Surveillance Test Will Be Revised & Technicians Cautioned
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1986-015, :on 860530,reactor Scram Occurred,Initiating Reactor Bldg Emergency Ventilation.Caused by Lifted Neutral Leg of Output Protective Relaying Circuit.Lifted Lead Replaced & Reactor Scram Reset |
- on 860530,reactor Scram Occurred,Initiating Reactor Bldg Emergency Ventilation.Caused by Lifted Neutral Leg of Output Protective Relaying Circuit.Lifted Lead Replaced & Reactor Scram Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-015-01, :on 861203,reactor Scram Occurred While in Shutdown Mode.Caused by Reactor Protection Sys Power Supplies Inadvertently Cross Connected,Resulting in Loss of Power.Design Change Built Into MSIV |
- on 861203,reactor Scram Occurred While in Shutdown Mode.Caused by Reactor Protection Sys Power Supplies Inadvertently Cross Connected,Resulting in Loss of Power.Design Change Built Into MSIV
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-016, Informs That Condition Reported in LER 86-016 Re Incorrect Location of Flow Switches in Standby Gas Treatment Sys Could Create Substantial Safety Hazard & Also Reportable Per 10CFR21 | Informs That Condition Reported in LER 86-016 Re Incorrect Location of Flow Switches in Standby Gas Treatment Sys Could Create Substantial Safety Hazard & Also Reportable Per 10CFR21 | | | 05000410/LER-1986-016-01, :on 861207 & 08,during Surveillance Procedure, Filter Train Heaters Intermittently Deenergized on Low Flow Signal.Caused by Flow Switch Design Deficiency.Sensing Line Relocated |
- on 861207 & 08,during Surveillance Procedure, Filter Train Heaters Intermittently Deenergized on Low Flow Signal.Caused by Flow Switch Design Deficiency.Sensing Line Relocated
| 10 CFR 50.73(a)(2) | | 05000220/LER-1986-016, :on 860523,Channel 11 High Reactor Water Level Feedwater Pump Trip Found Inoperable Until Feedwater Flow Control Valve 11 Opened Approx 50%.Jumpers Installed to Bypass Flow Control Valve Position Contacts |
- on 860523,Channel 11 High Reactor Water Level Feedwater Pump Trip Found Inoperable Until Feedwater Flow Control Valve 11 Opened Approx 50%.Jumpers Installed to Bypass Flow Control Valve Position Contacts
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000220/LER-1986-017, :on 860615,reactor Scram Occurred.Caused by Reactor Low Water Level Setpoint Being Reached During Operator Surveillance Test for Automatic Startup of HPCI Mode of Feedwater Sys |
- on 860615,reactor Scram Occurred.Caused by Reactor Low Water Level Setpoint Being Reached During Operator Surveillance Test for Automatic Startup of HPCI Mode of Feedwater Sys
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-018-01, :on 861216,while Testing Off Normal Status Sys Isolators,Electrician Placed Jumpers from 120-volt Dc Source to 120-volt Ac Line Source,Resulting in Blown Fuse.Caused by Test Engineer Error.Engineer Disciplined |
- on 861216,while Testing Off Normal Status Sys Isolators,Electrician Placed Jumpers from 120-volt Dc Source to 120-volt Ac Line Source,Resulting in Blown Fuse.Caused by Test Engineer Error.Engineer Disciplined
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1986-018, :on 860618,reactor Scram Occurred Due to Inventory Requirements Exceeding Capability of Condensate & Feedwater Booster Pumps.Caused by Operator Error.Event Reviewed W/Operating Personnel |
- on 860618,reactor Scram Occurred Due to Inventory Requirements Exceeding Capability of Condensate & Feedwater Booster Pumps.Caused by Operator Error.Event Reviewed W/Operating Personnel
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-019-01, :on 861215,reactor Scram Signal on Scram Discharge Vol Received Following Preplanned Scram.Caused by Operator Failure to Adhere to Scram Recovery Procedure. Procedure Revised.Training Mod Recommended |
- on 861215,reactor Scram Signal on Scram Discharge Vol Received Following Preplanned Scram.Caused by Operator Failure to Adhere to Scram Recovery Procedure. Procedure Revised.Training Mod Recommended
| | | 05000220/LER-1986-019, :on 860618,control Rods Moved While Rod Worth Minimizer Inoperable.Caused by Software Problem in Minimizer Program.Plant Shut Down.Indexing Problem in Computer Software Corrected |
- on 860618,control Rods Moved While Rod Worth Minimizer Inoperable.Caused by Software Problem in Minimizer Program.Plant Shut Down.Indexing Problem in Computer Software Corrected
| | | 05000410/LER-1986-020-01, :on 861218,Div 1 ECCS Initiation Experienced Due to Spurious High Drywell Pressure Signal.Caused by Electricians Replacing Relay.Electrical Maint Training Initiated |
- on 861218,Div 1 ECCS Initiation Experienced Due to Spurious High Drywell Pressure Signal.Caused by Electricians Replacing Relay.Electrical Maint Training Initiated
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1986-020, :on 860618,during Startup from Refueling Outage,Pinhole Leak Discovered in newly-installed 3/4-inch Sample Line Outside Primary Containment.Caused by Flaw in Pipe.Line Disconnected,Capped & Tested |
- on 860618,during Startup from Refueling Outage,Pinhole Leak Discovered in newly-installed 3/4-inch Sample Line Outside Primary Containment.Caused by Flaw in Pipe.Line Disconnected,Capped & Tested
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000220/LER-1986-021, :on 860619,reactor Scram & HPCI Initiation Occurred.Caused by Fuse Pulled During Replacement of Relay for intermediate-range Monitor.Scram & HPCI Initiation Signals Reset |
- on 860619,reactor Scram & HPCI Initiation Occurred.Caused by Fuse Pulled During Replacement of Relay for intermediate-range Monitor.Scram & HPCI Initiation Signals Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-021-01, :on 861210 & 11,HPCS Sys Initiation Experienced Due to lo-lo Water Level Signal.Caused by Inadvertent Movement of 4 Ft Section of Flexible Steel Piping Creating Hydraulic Surges.Steel Plate Removed from Rack |
- on 861210 & 11,HPCS Sys Initiation Experienced Due to lo-lo Water Level Signal.Caused by Inadvertent Movement of 4 Ft Section of Flexible Steel Piping Creating Hydraulic Surges.Steel Plate Removed from Rack
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-022-01, :on 861222,Div I-III Diesel Generators Declared Inoperable During Simultaneous Draining of Day Tank During Chemistry Surveillance Test.Caused by Procedure Deficiency. Procedure Revised.Personnel Counseled |
- on 861222,Div I-III Diesel Generators Declared Inoperable During Simultaneous Draining of Day Tank During Chemistry Surveillance Test.Caused by Procedure Deficiency. Procedure Revised.Personnel Counseled
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000410/LER-1986-023-01, :on 861223,inoperable Fire Detector Discovered During Routine Insp.Caused by Personnel Removing Detector from Base Prior to Replacement,Per 861222 Work Request. Surveillance Procedure Will Be Developed |
- on 861223,inoperable Fire Detector Discovered During Routine Insp.Caused by Personnel Removing Detector from Base Prior to Replacement,Per 861222 Work Request. Surveillance Procedure Will Be Developed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000220/LER-1986-023, :on 860801,discovered Failure to Perform Radiation Protection & Fire Dept Surveillance Tests During 850319-1216.Caused by Personnel Error.Personnel Advised of Tech Spec Requirements & Staff Increased |
- on 860801,discovered Failure to Perform Radiation Protection & Fire Dept Surveillance Tests During 850319-1216.Caused by Personnel Error.Personnel Advised of Tech Spec Requirements & Staff Increased
| 10 CFR 50.73(a)(2) | | 05000220/LER-1986-024, :on 860803,turbine Trip & Subsequent Scram Occurred.Caused by Increase in Reactor Water Level.Hpci Mode of Feedwater Reset,Reactor Water Level Restored & Instrument & Control Personnel Notified to Remove Signal |
- on 860803,turbine Trip & Subsequent Scram Occurred.Caused by Increase in Reactor Water Level.Hpci Mode of Feedwater Reset,Reactor Water Level Restored & Instrument & Control Personnel Notified to Remove Signal
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000410/LER-1986-024-01, :on 861231,visible Corrosion Observed on Div I & II Battery Bus Bars & Terminals.Caused by Naturally Occurring Leakage from Battery Seals.Corrosion Removed |
- on 861231,visible Corrosion Observed on Div I & II Battery Bus Bars & Terminals.Caused by Naturally Occurring Leakage from Battery Seals.Corrosion Removed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability |
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