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- 83' APPROVED OMG NO 319o-0104 LICENSEE EVENT REPORT (LER)
- ACiLITV NAa#E Hi DOCKET NUMSER (2)
PAGE 433 NINE MILE POINT UNIT 41 0l5l0l0l0l2l2lc 1 lOFl ol 7 TITLE (48 ATUOMATIC INITIATION OF REACTOR BUILDING EMERGENCY VENTILATION SYSTEM EVENT DATE 154 LER NUMBER (6)
REPORT DATE 17)
OTwtR F ACILITiES INVOLVED (8)
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,oe, ABSTRACT During normal operation on January 23, 1985, the first of three auto initiationc of the Reactor Building Emergency Ventilation System occurred (other initiations occurred on 1/24/85 and 2/7/85). The three initiations were a result of an off-normal spiking of No. 11 Reactor Building Ventilation Duct Radiation Monitor.
In each case a work request was issued to troubleshoot the problem and recalibrate the unit after corrections were made. After initially tightening, and then rewiring the sensor converter cable connectors, the sensor converter unit was replaced and source calibrated following the third emergency ventilation initiation.
Problems with No.
11 Reactor Building Ventilation Duct Radiation Monitor have been resolved and the unit is operating properly.
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- - TEXT During normal operation on three separate occasions No. 11 Reactor Building Ventilation Duct Radiation Monitor experienced a spurious spike which initiated the Emergency Ventilation System. The first two initiations occurred on January 23, and 24, 1985. Following the spike the indications returned to normal, the HI radiation signal was reset and system cleared. Work requests were issued following each initiation in order to troubleshoot and make the needed repairs. It was discovered that the automatic initiation of the Emergency Ventilation System occurred due to a malfunction of the sensor converter unit.
Following the first system initiation loose connectors were tightened on the sensor convertor cables. These connectors were later rewired after the second system initiation. The third automatic initiation occurred on February 7, 1985.- This time the Emergency Ventilation System was left in operation and a new sensor converter unit was installed. In each case No. 11 Reactor Building Ventilation Duct Monitor was source calibrated by Radiation Protection following repairs. Problems with the unit have been corrected and it is now operating properly.
ASSESSMENT OF' POTENTIAL SAFETY CONSEQUENCES Reactor Building Ventilation Duct Radiation Moni+qr No. 11 experienccd a spurious spike and initiated the Emergency Ventilation System on a reading greater than 5mR/hr. Since the system did initiate as designed and emergency vent operation is a conservative mode, the system initiation posed no threat to the safety of the plant.
A redundant reactor building ventilation monitor is provided. Therefore, had Radiation Monitor No. 11 been inoperable, redundant Reactor Building Ventilation Monitor No. 12 would have been available to initiate the Emergency Ventilation System on a reading above SmR/hr. The sensor converter for Reactor Buildina Ventilation Monitor No. 11 has been replaced and source calibrated. No furthei spiking problems with monitor No. 11 have been experienced.
Based on these results, there were no actual adverse consequences from this event and the potential consequences are within the design basis of the plant.
CORRECTIVE ACTION
The sensor converter cable connectors for Reactor Building Ventilation Duct Monitor No. 11 were initially tightened and then rewired in efforts to resolve the spiking problem. The sensor converter for ventilation Duct Monitor No. 11 was finally replaced and successfully source calibrated. Af ter Channel til was proved operational and returned to service, Channel #12 was inspected for loose connector connections and repaired accordingly.
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NMP-10624 NIAGARA MOHAWK POWER CORPORATION NIAGARA MOHAWK 300 ERIE BOULEVARD, WEST SYR ACUSE. N. Y.13 202 February 22, 1985 United States Nuclear Regulatory Commission Document Control Desk Washington,.DC 20555
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RE:
Docket No. 50-220 LER 85-01 Gentlemen:
In accordance with 10 CFR 50.73, we hereby submit the following Licensee Event Report:
LER 85-01 Which is being submitted in accordance with-10 CFR 50.73 (a)(2)(iv).
"Any event or condition that resulted in manual or automatic activation' of any Engineered Safety Feature."
10 CFR 50.72 reports were made at 0130 on 1/23/85, 1915 on 1/24/85 and 0833 on 2/7/85. This Licensee Event Report was completed in the format designated in NUREG-1022, dated September 1983.
Very truly yours, fgv>Hbj -
W Thomas E.
Lempges Vice President Nuclear Generation TEL/lo attachments-cc Dr. Thomas E. Murley Regional Administrator
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| 05000220/LER-1985-001, :on 850123,24 & 0207,automatic Initiations of Reactor Bldg Emergency Ventilation Sys Occurred.Caused by off-normal Spiking of Ventilation Duct Radiation Monitor 11.Sensor Converter Replaced |
- on 850123,24 & 0207,automatic Initiations of Reactor Bldg Emergency Ventilation Sys Occurred.Caused by off-normal Spiking of Ventilation Duct Radiation Monitor 11.Sensor Converter Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1985-002, :on 850214,auxiliary Control Room Fire Suppression Sys Inoperable.Caused by Inoperable Fire Dampers.Fire Dampers Repaired & Tested.Personnel Instructed in Tech Spec Requirements |
- on 850214,auxiliary Control Room Fire Suppression Sys Inoperable.Caused by Inoperable Fire Dampers.Fire Dampers Repaired & Tested.Personnel Instructed in Tech Spec Requirements
| | | 05000220/LER-1985-003, On 850304,reactor Scram Initiated.Caused by Technicians Trying to Rectify Error Condition in Transmitter During Monthly Surveillance.Procedure Revised to Caution Technicians on Effects of Errors | On 850304,reactor Scram Initiated.Caused by Technicians Trying to Rectify Error Condition in Transmitter During Monthly Surveillance.Procedure Revised to Caution Technicians on Effects of Errors | 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1985-004, :on 850304,during Shutdown,Turbine Trip Signal Led to HPCI Initiation.Caused by High Reactor Water Level.Level Control Adjusted.Water Level Returned to Normal |
- on 850304,during Shutdown,Turbine Trip Signal Led to HPCI Initiation.Caused by High Reactor Water Level.Level Control Adjusted.Water Level Returned to Normal
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1985-005, :on 850416,reactor Scram Occurred Due to APRM High Flux Level.Caused by Partial Closing of Turbine Control Valves Due to Disturbance in Turbine Control Sys.Work Requests Issued to Troubleshoot Sys |
- on 850416,reactor Scram Occurred Due to APRM High Flux Level.Caused by Partial Closing of Turbine Control Valves Due to Disturbance in Turbine Control Sys.Work Requests Issued to Troubleshoot Sys
| | | 05000220/LER-1985-006, :on 850419,automatic Initiation of Reactor Bldg Emergency Ventilation Sys Occurred.Caused by off-normal Spiking of Reactor Bldg Ventilation Duct Monitor 11.Sys Checked & Source Calibr.Sys Returned to Svc |
- on 850419,automatic Initiation of Reactor Bldg Emergency Ventilation Sys Occurred.Caused by off-normal Spiking of Reactor Bldg Ventilation Duct Monitor 11.Sys Checked & Source Calibr.Sys Returned to Svc
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1985-007, :on 850424,automatic Initiation of Reactor Bldg Emergency Ventilation Sys Occurred.Caused by Technician Shorting Wire in Cable Connector to Sensor for Emergency Condensor Ventilation Monitor 121 |
- on 850424,automatic Initiation of Reactor Bldg Emergency Ventilation Sys Occurred.Caused by Technician Shorting Wire in Cable Connector to Sensor for Emergency Condensor Ventilation Monitor 121
| | | 05000220/LER-1985-008-01, :on 850610,discovered That Temporary Jumper Block Log 2036 Not Reviewed by General Superintendent within 14-day Time Limit.Cause Unstated.Review Completed.New Procedure to Ensure Timely Reviews Implemented |
- on 850610,discovered That Temporary Jumper Block Log 2036 Not Reviewed by General Superintendent within 14-day Time Limit.Cause Unstated.Review Completed.New Procedure to Ensure Timely Reviews Implemented
| 10 CFR 50.73(a)(2)(i) | | 05000220/LER-1985-008, Corrected LER 85-008-00:on 850610,review by Operations Dept Discovered That Temporary Jumper/Block Log 2036 Not Reviewed by General Superintendent within 14-day Time Limit,Per Tech Spec 6.8.3.C | Corrected LER 85-008-00:on 850610,review by Operations Dept Discovered That Temporary Jumper/Block Log 2036 Not Reviewed by General Superintendent within 14-day Time Limit,Per Tech Spec 6.8.3.C | 10 CFR 50.73(a)(2)(i) | | 05000220/LER-1985-009, :on 850522 & 31,discovered Instrument Channel Tests Not Performed on Three of Four Emergency Condenser Sys Noble Gas Activity & Suppression Chamber Water Level Monitors.Cause Unknown.Tests Performed |
- on 850522 & 31,discovered Instrument Channel Tests Not Performed on Three of Four Emergency Condenser Sys Noble Gas Activity & Suppression Chamber Water Level Monitors.Cause Unknown.Tests Performed
| 10 CFR 50.73(a)(2)(1) | | 05000220/LER-1985-010, :on 850815,accidental Initiation of Reactor Bldg Emergency Ventilation Sys Occurred.Caused by Electrical Spike Experienced by Channel 12 Reactor Bldg Ventilation Duct Monitor.Ventilation Sys Reset |
- on 850815,accidental Initiation of Reactor Bldg Emergency Ventilation Sys Occurred.Caused by Electrical Spike Experienced by Channel 12 Reactor Bldg Ventilation Duct Monitor.Ventilation Sys Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1985-011, :on 850610,review Revealed That Radiological Habitability of Technical Support Ctr (TSC) Not Consistent w/NUREG-0737,Suppl 1.Cause Unstated.Tsc Being Relocated to Better Location Re Radiation Shielding |
- on 850610,review Revealed That Radiological Habitability of Technical Support Ctr (TSC) Not Consistent w/NUREG-0737,Suppl 1.Cause Unstated.Tsc Being Relocated to Better Location Re Radiation Shielding
| | | 05000220/LER-1985-012, :on 850916,reactor Cleanup Sys Isolated Due to High Area Temp.Caused by Steam Leaking from Gland Packing on 1-inch Vent Valve from Cleanup Nonregenerative Hx.Leak Repaired |
- on 850916,reactor Cleanup Sys Isolated Due to High Area Temp.Caused by Steam Leaking from Gland Packing on 1-inch Vent Valve from Cleanup Nonregenerative Hx.Leak Repaired
| | | 05000220/LER-1985-013, :on 850621 & 25,automatic Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Spurious Upscale Deflection of Control Room Vent Monitor Due to Line Noise.Involved Monitors Recalibr |
- on 850621 & 25,automatic Actuation of Control Room Emergency Ventilation Sys Occurred.Caused by Spurious Upscale Deflection of Control Room Vent Monitor Due to Line Noise.Involved Monitors Recalibr
| | | 05000220/LER-1985-014, :on 850819,during Surveillance Insp,Maint Electrician Inadvertently Grounded Main Generator Excitation Sys Amplidyne Motor Generator Set,Causing Main Generator & Turbine Trips & Reactor Scram |
- on 850819,during Surveillance Insp,Maint Electrician Inadvertently Grounded Main Generator Excitation Sys Amplidyne Motor Generator Set,Causing Main Generator & Turbine Trips & Reactor Scram
| | | 05000220/LER-1985-015, :on 850911,personnel Informed of Three Instances of Cable Routing Discrepancies.Operators Informed. Mods Designed & Will Be Installed in Timely Manner |
- on 850911,personnel Informed of Three Instances of Cable Routing Discrepancies.Operators Informed. Mods Designed & Will Be Installed in Timely Manner
| | | 05000220/LER-1985-016, :on 850927,three Normally Open Dampers Failed to Isolate on Halon Suppression Signal.Caused by Interruption to Initiation Circuit Due to Wiring Change on 850918.Wiring Corrected |
- on 850927,three Normally Open Dampers Failed to Isolate on Halon Suppression Signal.Caused by Interruption to Initiation Circuit Due to Wiring Change on 850918.Wiring Corrected
| 10 CFR 50.73(a)(2) | | 05000220/LER-1985-017, :on 850823,reactor Scram Initiated Due to Reactor Low Water Level.Caused by Detached Range Spring & Lock Screw in Valve Positioner Closing Valve on Feedwater Pump 11.Lock Screw & Addl Hardware Replaced |
- on 850823,reactor Scram Initiated Due to Reactor Low Water Level.Caused by Detached Range Spring & Lock Screw in Valve Positioner Closing Valve on Feedwater Pump 11.Lock Screw & Addl Hardware Replaced
| | | 05000220/LER-1985-018, :on 851010,low Air Pressure Start Test of Tech Spec Section 4.6.7.b.4 Failed.Caused by Need to Energize or Manually Bypass Solenoids on Governor Sys.Mods to Governor Sys & Sys Manual Start Performed |
- on 851010,low Air Pressure Start Test of Tech Spec Section 4.6.7.b.4 Failed.Caused by Need to Energize or Manually Bypass Solenoids on Governor Sys.Mods to Governor Sys & Sys Manual Start Performed
| | | 05000220/LER-1985-019, :on 851015,discovered Emergency Isolation Dc Motor Operated Valves 39-07 & 39-08 Might Not Close within 38 During Accident.Possibly Caused by Incorrectly Sized Electric Supply Cables.Cables Replaced |
- on 851015,discovered Emergency Isolation Dc Motor Operated Valves 39-07 & 39-08 Might Not Close within 38 During Accident.Possibly Caused by Incorrectly Sized Electric Supply Cables.Cables Replaced
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000220/LER-1985-020, :on 851030,momentary Loss of Output Power from Uninterruptible Power Supply Motor Generator Set 162 Experienced.Caused by Generator Undervoltage Relay Sensing Spurious Undervoltage |
- on 851030,momentary Loss of Output Power from Uninterruptible Power Supply Motor Generator Set 162 Experienced.Caused by Generator Undervoltage Relay Sensing Spurious Undervoltage
| | | 05000220/LER-1985-021, :on 851101,during Normal Operation,Feedwater Flow Control Valve 12 Malfunctioned Causing 95-inch Reactor Water Level Condition.Caused by Problem W/Instrument Air Sys |
- on 851101,during Normal Operation,Feedwater Flow Control Valve 12 Malfunctioned Causing 95-inch Reactor Water Level Condition.Caused by Problem W/Instrument Air Sys
| | | 05000220/LER-1985-022, :on 851107,turbine Bypass Valve 12-H Inadvertently Closed,Causing Decrease in Reactor Water Level & Subsequent Scram & Initiation of HPCI Mode of Feedwater. Valve to Be Inspected |
- on 851107,turbine Bypass Valve 12-H Inadvertently Closed,Causing Decrease in Reactor Water Level & Subsequent Scram & Initiation of HPCI Mode of Feedwater. Valve to Be Inspected
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1985-023, :on 851108,during Preparations for Main Turbine Startup,High Temp in Main Turbine Exhaust Hood Caused Turbine Trip & Actuation of HPCI Mode of Feedwater Flow |
- on 851108,during Preparations for Main Turbine Startup,High Temp in Main Turbine Exhaust Hood Caused Turbine Trip & Actuation of HPCI Mode of Feedwater Flow
| 10 CFR 50.73(a)(2) | | 05000220/LER-1985-024, :on 851212,turbine Trip & Subsequent HPCI Mode of Feedwater Initiation Occurred.Caused by Difference Between Level Indications Due to Different Indicator Mfg. Water Level Lowered & HPCI Reset |
- on 851212,turbine Trip & Subsequent HPCI Mode of Feedwater Initiation Occurred.Caused by Difference Between Level Indications Due to Different Indicator Mfg. Water Level Lowered & HPCI Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000220/LER-1985-025, :on 851215,reactor Power Reduction Initiated Due to Inability to Monitor Specified Core Thermal Parameters.Caused by Plant Process Computer Failure. Reactor Power Restored |
- on 851215,reactor Power Reduction Initiated Due to Inability to Monitor Specified Core Thermal Parameters.Caused by Plant Process Computer Failure. Reactor Power Restored
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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