LER-1978-003, Regarding Drywell High Pressure Switch RE04A Setpoint Drift and LER 78-003-00 |
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| 2201978003R00 - NRC Website |
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text
-0 REGULATORY INFORMATION DISTRIBUTION SYSTEN
<RIDS)
DISTRIBUTION FOR INCQNING NATERIAL 50-220 REC:
GRIER B
H NRC ORG:
SCHNEIDER R
R NIAGARA NOHAMK PMR DOCDATE: 01/31/78 DATE RCVD: 02f06/78 DOCTYPE:
LETTER NOTARIZED: 5O COPIES RECEIVED
SUBJECT:
LTR 1
ENCL 1
l.
LICENSEE EVENT REPORT 78-02 ON 1/6/78 CONCERNING SETPOINT DRIFT RE Nl-ISP RE04.
2.
LICENSEE EVENT REPORT 78-03 ON 1/6/78 CONCERNING SETPOINT DRIFT RE RE04A.
PLANT NAME: NINE NILE PT UNIT 1
REVIEWER INITIAL:
XEF DISTRIBUTOR INITIAL; DISTRIBUT1ON OF THIS NATERIAL IS AS FOLLOWS'44++<++<<<+<<<<+<+
INCIDENT REPORTS (DISTRIBUTION CQDE A002>
FOR ACTION:
INTERNAL:
EXTERNAL:
BRANCH CHIEF LEAR++M/4 ENCL EG FIL
+W/ENCL I 5 E4+W/2 FNCL SCHROEDER/IPPQLITO++W/ENCL NOVAK/CHECKS< W/ENCL KNIGHT++M/ENCL HANAUER++W/ENCL EISENHUT++W/ENCL SHAG~+M/ENCL KREGER/J.
COLLINS+>M/ENCL L.
CROCKER++M/ENCL LPDR'8 OSWEGO'Y++M/ENCL TIC~+WfENCI NSIC++W/ENCL ACRS CAT 844M/16 ENCL NRC PDR++W/ENCL MIPC++W/3 ENCI HOUSTON+>W/ENCL GRII"lE$4+WfENCL BUTLER++W/ENCL TEDESCO++W/ENCL BAER+~tM/ENCL VOLLMER/BUNCH+4M/ENCL ROSA~<~L J/ENCL gppZES ppT SUE",(ITTED PER REGULATORY GUIDE 10.1 DISTRIBUTIQN:
LTR 45 ENCL 45 S1ZE:
iP+2P CONTROL NBR:
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NIAGARAMOHAWKPOY/ER CORPORATION/300 LRIE BOULEVARDWEST. SYRACUSE. N.Y. 13202/TELEPHONE (315) 474-1511 Janua/Ly 31, 1978 JIk.
Boyce, H.
G/Li.e/L NAe&otc
'UI~ed S~e5 NucLea/L Reguj'+to/Ly Commission Region I 631 Parcfz Avenue, Km'( P~b~,
PA.
19406 RE:
Sock& No. 50-220 8ea/L N..
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" In accordance 1~ Nme h4Xe 'Poli< NucLea/L S~on UIM'??1 Technical'. Speci pc~one, I0e hetce6y au6~ Licensee Eve+4'epo~
LER 78-02 and LER 78-03, efu.ch arse in violin og 7echnicaZ Sperm.Pc~on
- 3. tl.2.
These /1.epo~
use/I.e complied in She (o/UIIaf: de5~gnMed in NL?REG-Olbl, dMed JuLy 1977.
Ve/Ly Wuly yOu/L5, ORIGINAL SIGNED BY R.R.
SCHNEI'DER R.R. Schneide/L Vi.ce Picm&eJ~-
tHePrcodu~oI1 8Kb(/mmmm Enc.
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UCLI:AIIIIL'GULAI L)H I LUBIhiI~yIs3,,1 LICENSEE EVENT REPORT NHC FORM 3GG (7.77)
C6NTROL BLOCK:
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~01 N
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1 Q2 0
0 8
9 LICENSEE CODE 14 15 LICENSE NUMBER CON'T 0
I soUBGE ~LQG 0
5 0
0 0
2 2
Q7 0
1 0
6 7
8 60 61 DOCKET NUMBER GB G9 EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO
~02 Durin stead tate era Q
(PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION) 6 0
0 0
0 0
0 0
Q34 1
1 1
1 Q4~Qs 25 26 LICENSE TYPE 30 57 CAT 58 8
QB0 1
3 QG 74 75 REPORT DATE 80
- RE04, found RE04A with a setpoint of 3. 30 psi, RE04B at 3. 30 si, and RE04C at 3.40 PSI.
Required setpoint of these dr well hi h
ressure switches is 3.50 psi +/- 0.053 psi. This condition resulted in minimal safety implications. All switches drifted in a more conservative
~07 direction.
~08 7
8 9
80
~00 7
8 SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE
~IB Q>
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S T
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Q4
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10 11 12 13 18 19
- 20 SEQUENTIAL OCCURRENCE REPORT REVISION LER~BO EVENT YEAR REPORT NO.
CODE TYPE NO.
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~78 LJ
~00 2
~~
~03
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~0 21 22 23 24 2G 27 28 29 30 31 32 ACTION.FUTURE EFFECT SHUTDOWN ATTACHhIENT NPRD 4 PRIh'IE COhIP.
COAIPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBhIITTED FORhI SUB, SUPPLIER hIANUFACTURER Q18 ~ZQ19
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0 Qzs 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 27 0
These chan es in set oints ex erienced on the Barton Model 289 ressure indicatin switches were due to instrument drift. RE04A va r
3.50 psi, RE04B at 3.50 si, and RE04C at 3.50 si. Current 3
survei 1 1 ance testin schedules are ade uate to i ns ure earl detection of future instrument drifts.
7 8
9 FACILITY STATUS BI POWER OTHER STATUS Q E
Qss ~09 9
Qss NA 7
8 9
10 12 13 44 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITYQB Q>>
2 Qss NA 7
8 9
10 11 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q30
~I7 (000 00 JQsL Z
Qss NA 7
8 9
11 12 13 PERSONNEL INJURIES 7
8 9
11 12 I.OSS OF OB DAMAGETO FACILITYQ43 TYPE
DESCRIPTION
0 2
Q42 NA 8
9 10 PUBLICITY ISSUED DESCRIPTIONQ
~20
~NQ44 NA 7
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10 NAME QF PREPARER Denni s K.
Ma 80 80 80 80 80 PHONE:
80 NRC USE ONLY ssis s
80 g 0
0 METHOD OF DISCOVER Y DISCOVERY DESCRIPTION Q32
~B Q3I Surveillance Testin 45 46 LOCATIONOF RELEASE Q36 NA 45
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U~ NUCLSAR R8OULATOR MISSION NRC FQRM 196 I2 78)
NRC OISTRlBUllON FOR PART 50 DOCKET MATERlAt.
OQCXST NUMSSR
~- ZZN FII 8 NVMSSR
~cri4o TO:
Mr. Boyce H
Grier FROM:
Niagara Mohawk Pwr.
Corp
- Syracuse, New York Thomas ED Lem ges OATS QF OOCUMSNT 1/13/78
'AT8 RSCSIVSO 1/24/78 LKTTSR ABORIGINAL SCOPY QSSCRIPTION QNOTORIZSO JjVRCLASSIFi8O PRCF'NPUT FORM 8NCI,OSU RIL NUQSSR OF CQPISS RSCSIVSO
/ CC-Licensee Event Rept'RO 50-220/78-01) on Ol/04/78 concerning delta temperature of the discharge water exceeding spec 2' '
of the environ+ tech, specsi
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COPIES NOT SUBIIITTED PER REGULATORY GUIDE 10.1 (1-P)
PLANT'NA?IE: Nine Mile Point Unit No.
1 RJL 1/24/78 (1-P)+(2-P)
FOR ACTION/INFORMATION Ei VIRONi4ENTAL F:
PRO JECT !IIANAGER:
LIC. ASST:
ASSIGN AD'RANCH CHIEF:
8.
EARLESS INTERNALOISTRIBUTION YSTENS SiT SAFETY 6 EIiRON ANALYSiS DENTON Q 'NILLER GO CK C STAFF ON TECH
'IOSS OVAK "CH ijL 2
SZTOCZY CHECK L <Wo V
L.'KR vS TS EXTERNALOISTRIBUTIGN CONTROL NUMBER TTC at G 7
<J. P>ICKTT) 1 Cv SpiPi.
CAT-GOR'-
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| 05000220/LER-1978-001, Submittal of Licensee Event Report LER 78-01 Concerning Delta Temperature of the Discharge Water Exceeded Environmental Tech. Spec | Submittal of Licensee Event Report LER 78-01 Concerning Delta Temperature of the Discharge Water Exceeded Environmental Tech. Spec | | | 05000220/LER-1978-003, Regarding Drywell High Pressure Switch RE04A Setpoint Drift and LER 78-003-00 | Regarding Drywell High Pressure Switch RE04A Setpoint Drift and LER 78-003-00 | | | 05000220/LER-1978-005, And LER 78-005-00 for Nine Mile Point, Unit 1 Re During Unit Shutdown, Reserve Power Breaker on Power Board II Failed to Close in After Loss of Normal Power and During Plant Outage While Marking Up Outside MSIV 01-03 Discovered | And LER 78-005-00 for Nine Mile Point, Unit 1 Re During Unit Shutdown, Reserve Power Breaker on Power Board II Failed to Close in After Loss of Normal Power and During Plant Outage While Marking Up Outside MSIV 01-03 Discovered That Valve | | | 05000220/LER-1978-006, Re During Steady State Operation, Performance of Surveillance Test IC-75 Found a Trip Setpoint of 22.5 Inches Water on One Vacuum Switch in the Vacuum Relief System from the Pressure Suppression Chamber to the | Re During Steady State Operation, Performance of Surveillance Test IC-75 Found a Trip Setpoint of 22.5 Inches Water on One Vacuum Switch in the Vacuum Relief System from the Pressure Suppression Chamber to the | | | 05000220/LER-1978-009-01, For Nine Mile Point Unit 1 Regarding Replacement of Explosive Charges in the TIP Shear Valves with New Charges and the Resulting Unsatisfactory Ohmmeter Continuity Test for Acceptable Electric Contact | For Nine Mile Point Unit 1 Regarding Replacement of Explosive Charges in the TIP Shear Valves with New Charges and the Resulting Unsatisfactory Ohmmeter Continuity Test for Acceptable Electric Contact | | | 05000220/LER-1978-009, And LER 78-010-00 for Nine Mile Point, Unit 1 Re Technical Specification Violations of Listed Sections | LER 78-009-00 and LER 78-010-00 for Nine Mile Point, Unit 1 Re Technical Specification Violations of Listed Sections | | | 05000220/LER-1978-013, And LER 78-013-00 for Nine Mile Point, Unit 1 Re Technical Specification Violations of Section 3.6.2 | And LER 78-013-00 for Nine Mile Point, Unit 1 Re Technical Specification Violations of Section 3.6.2 | | | 05000220/LER-1978-014, LERs 78-014,00, 78-016-00, and 78-016-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump on 102 D/G Would Not Fill the Day Tank, Discovery of RE18C with a Setpoint of 129 Inches Wc, and | LERs 78-014,00, 78-016-00, and 78-016-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump on 102 D/G Would Not Fill the Day Tank, Discovery of RE18C with a Setpoint of 129 Inches Wc, and RE04B | | | 05000220/LER-1978-015, And LER 78-015-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump in 102 D/G Would Not Fill the Day Tank and Discovery That 12 Control Room Air Treatment Fan Would Not Run | And LER 78-015-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump in 102 D/G Would Not Fill the Day Tank and Discovery That 12 Control Room Air Treatment Fan Would Not Run | | | 05000220/LER-1978-018, For Nine Mile Point Unit 1 Regarding Discovery of Main Steam High Flow Switch with a Setpoint of 106.2 PSI, Which Is Above the Technical Specification | For Nine Mile Point Unit 1 Regarding Discovery of Main Steam High Flow Switch with a Setpoint of 106.2 PSI, Which Is Above the Technical Specification | | | 05000220/LER-1978-019, For Nine Mile Point Unit 1 Regarding Discovery That Hydraulic Snubber 31-HS-1 Had Failed and Was Empty of Hydraulic Fluid and Disconnected from Its Anchor at the Feedwater Pipe | For Nine Mile Point Unit 1 Regarding Discovery That Hydraulic Snubber 31-HS-1 Had Failed and Was Empty of Hydraulic Fluid and Disconnected from Its Anchor at the Feedwater Pipe | | | 05000220/LER-1978-020, LERs 78-020-00, 78-021-00, 78-022-00, and 78-023-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery of RE18A with a Setpoint of 135 Inches Wc, Discovery of RE04A and RE04B with a Setpoint of 3.65 PSIG, Discovery o | LERs 78-020-00, 78-021-00, 78-022-00, and 78-023-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery of RE18A with a Setpoint of 135 Inches Wc, Discovery of RE04A and RE04B with a Setpoint of 3.65 PSIG, Discovery of Turbine . | | | 05000220/LER-1978-024, For Nine Mile Point Unit 1 Regarding Discovery That Test N1-St-Q2,4,5,7,8,9, and 10 Had Not Been Performed During a Review of Quarterly Surveillance Test Results | For Nine Mile Point Unit 1 Regarding Discovery That Test N1-St-Q2,4,5,7,8,9, and 10 Had Not Been Performed During a Review of Quarterly Surveillance Test Results | | | 05000220/LER-1978-025, LERs 78-025-00, 78-026-00, and 78-027-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery of RE04D with a Setpoint of 3.70 PSIG, Discovery of Numerous Small Leaks in Small Sample and Instrument Pipes, and Discovery | LERs 78-025-00, 78-026-00, and 78-027-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery of RE04D with a Setpoint of 3.70 PSIG, Discovery of Numerous Small Leaks in Small Sample and Instrument Pipes, and Discovery of RE22D Wit | | | 05000220/LER-1978-028, For Nine Mile Point Unit 1 Regarding Discovery of the Allowable Test Interval of TS 4.1.4c for the Core Spray Power-Operated Valves Had Been Exceeded | For Nine Mile Point Unit 1 Regarding Discovery of the Allowable Test Interval of TS 4.1.4c for the Core Spray Power-Operated Valves Had Been Exceeded | | | 05000220/LER-1978-029, Regarding Discovery of High Drywell Pressure Switches RE04A, RE04B, and RE04C with Setpoints Less Conservative than the Technical Specifications | Regarding Discovery of High Drywell Pressure Switches RE04A, RE04B, and RE04C with Setpoints Less Conservative than the Technical Specifications | | | 05000220/LER-1978-030, 78-031-00, and 78-032-00 for Nine Mile Point Unit 1 Regarding, Respectively, Unavailability of Feedwater Pump 29-03 While Its Pump Seals Were Replaced, Unavailability of Liquid Poison Pump NP02A While a Frozen Valve | 78-031-00, and 78-032-00 for Nine Mile Point Unit 1 Regarding, Respectively, Unavailability of Feedwater Pump 29-03 While Its Pump Seals Were Replaced, Unavailability of Liquid Poison Pump NP02A While a Frozen Valve | | | 05000220/LER-1978-033-03, /03L-0 on 780916:Surveillance Tests on Barton Model 289 Pressure Indicating Switches Showed Changes in Setpoints Due to Instru Drift.Rev Surveillance Test Scheds Now Adequate to Ensure Early Detection of Drifts | /03L-0 on 780916:Surveillance Tests on Barton Model 289 Pressure Indicating Switches Showed Changes in Setpoints Due to Instru Drift.Rev Surveillance Test Scheds Now Adequate to Ensure Early Detection of Drifts | | | 05000220/LER-1978-034, Regarding an Environmental Contractor Obtaining 22 Hourly Fish Impingement Samples, and One Two-Hour Sample, Which Is Contrary to the Technical Specification Requiring 24 Hourly Samples | Regarding an Environmental Contractor Obtaining 22 Hourly Fish Impingement Samples, and One Two-Hour Sample, Which Is Contrary to the Technical Specification Requiring 24 Hourly Samples | | | 05000220/LER-1978-035, Forwards LER 78-035/01T-0 | Forwards LER 78-035/01T-0 | | | 05000220/LER-1978-035-01, /01T-0 on 781020:all Main Steam High Flow Pressure Indicating Instr Were Found W/Setpoints Less than Tech Specs.Heise 0-200 PSIG Test Gauge Calibrated & Used in Test Had Loose Screw & Was Recalibrated | /01T-0 on 781020:all Main Steam High Flow Pressure Indicating Instr Were Found W/Setpoints Less than Tech Specs.Heise 0-200 PSIG Test Gauge Calibrated & Used in Test Had Loose Screw & Was Recalibrated | | | 05000220/LER-1978-036-04, /04T-0 on 781025:improper Appl of Brook Model 9456 Oval Gear Flowmeter Combined W/Failed Seal on Caustic Addition Pump Caused High Concentration of Sodium & Sulfate & Degraded Capability to Control Rate of Discharge | /04T-0 on 781025:improper Appl of Brook Model 9456 Oval Gear Flowmeter Combined W/Failed Seal on Caustic Addition Pump Caused High Concentration of Sodium & Sulfate & Degraded Capability to Control Rate of Discharge | | | 05000220/LER-1978-036, Forwards LER 78-036/04T-0 | Forwards LER 78-036/04T-0 | | | 05000220/LER-1978-037, Forwards LER 78-037/03L-0, 78-038/03L-0 & 78-039/03L-0 | Forwards LER 78-037/03L-0, 78-038/03L-0 & 78-039/03L-0 | | | 05000220/LER-1978-037-03, /03L-0 on 781027:test Revealed Trip Setpoint of 26.5 Inches Water on One Vacuum Switch in Vacuum Relief Sys from Pressure Supression Chamber to Rx Bldg.Caused by Instru Drift in a Mercoid Model CP4122 Vacuum Switch | /03L-0 on 781027:test Revealed Trip Setpoint of 26.5 Inches Water on One Vacuum Switch in Vacuum Relief Sys from Pressure Supression Chamber to Rx Bldg.Caused by Instru Drift in a Mercoid Model CP4122 Vacuum Switch | | | 05000220/LER-1978-038-03, /03L-0 on 781025:review of N1-ISP-RE22 Test Results Found 12 Instances Where Procedure Was Violated. Caused by Carelessness in Procedure Implementation. Re-instruction & Closer Supervision Instituted | /03L-0 on 781025:review of N1-ISP-RE22 Test Results Found 12 Instances Where Procedure Was Violated. Caused by Carelessness in Procedure Implementation. Re-instruction & Closer Supervision Instituted | | | 05000220/LER-1978-039-03, /03L-0 on 781103:surveillance Test N1-ISP-RE02 Revealed Rx Lo-Lo Water Level Switch W/Trip Setpoint of +2 Inches Water.Caused by Instru Drift.Setpoint Reset | /03L-0 on 781103:surveillance Test N1-ISP-RE02 Revealed Rx Lo-Lo Water Level Switch W/Trip Setpoint of +2 Inches Water.Caused by Instru Drift.Setpoint Reset | | | 05000220/LER-1978-040-03, /03L-0 on 781113: 112 Core Spray Topping Pump Motor Breaker Closed Starting Pump But Breaker Closing Spring Motor Was Running Continuously & Not Charging Closing Spring.Caused by Misaligned Motor Assembly at Latching Pawl | /03L-0 on 781113: 112 Core Spray Topping Pump Motor Breaker Closed Starting Pump But Breaker Closing Spring Motor Was Running Continuously & Not Charging Closing Spring.Caused by Misaligned Motor Assembly at Latching Pawl | | | 05000220/LER-1978-040, Forwards LER 78-040/03L-0 | Forwards LER 78-040/03L-0 | | | 05000220/LER-1978-041, Forwards LER 78-041/04T-0 | Forwards LER 78-041/04T-0 | | | 05000220/LER-1978-041-04, /04T-0 on 781220:during Impingement Sampling Only 23 Samples (22 Hourly Samples & One 2-hr Sample) Were Collected Instead of 24 Required Samples,Caused by one-time Personnel Scheduling Change | /04T-0 on 781220:during Impingement Sampling Only 23 Samples (22 Hourly Samples & One 2-hr Sample) Were Collected Instead of 24 Required Samples,Caused by one-time Personnel Scheduling Change | |
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