ML18018B205

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Operating Statistics and Shutdown and Operating Experience for February 1988
ML18018B205
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 03/09/1988
From:
Niagara Mohawk Power Corp
To:
NRC/IE
References
Download: ML18018B205 (44)


Text

~ XVVAae HONTHLY REPORT NDE NILE POL%'UCLeea STATION PilIT . FOR FEBRUARY 1988 DOCUMENT TRANSMITTAL A%) VERIFICATION Title of Document ASS IGiiD T. Perkins TO P. Charles DATE 3/9/88 OUE DATE 3 15 88 ED DATE SUBJECT OPERATING STATISTICS 6 SHUTDOWN F. FBR ARY 1988 DOCUMENT DIRECTOR ADDRESSED T0 FFICE OF INSPECTION 6 ENFORCEMENT TEAR REG AT RY SSI N PREPARED BY P. Charles DATE 3/9/88 REVIEWED BY E. Tomlinson DATE o ATE <- -g DATE IP 31 88 DATE 3-!o-ss VERIFIED BY DATE DATE DATE CQbHF1TS RECEIVED FOR 0ATE TRANSMIT?'AL ~g/et SENT TO ADDRESSEE BY DATE COPY RETURNED TQ SITE BY LOGGED A I ATE FILED AT SITE DOC.CONTROL RE ORD DATE OFFICE STAMPS Dates entry is made into- report/response computer monitoring. systei frlI/ I AP!(- 16-6;; Det:6mb'er 1,980 '~ 1

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OPERATING DATA REPORT

~onTE ~>e 88 COSIPLETEO BY E. Tomlinson

... TELEFHOiVE ~~9-2761 OPERATING STATUS Nine Mile Point Unit 2 Notes

l. Unit Name:
2. Reporting period: 2/ 1/88 thr u 2 29 88
3. Licensed Thermal Po~er (MWt): 3323
4. Nameplate Rating (Gross MWe):
5. Design Electrical Rating (Net MWe):
6. Maximum Dependable Capacity (Gross MWe): NOT
7. Maximum Dependable Capacity (Net MWe):
8. IfChanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
9. Power Level To Which Restricted, IfAny (Net MWe):
10. Reasons For Restrictions, If Any:

This Month Yr. to.Date Cumulative 696 1,440 5,680

11. Hours In Reporting Period
12. Number Of Hours Reactor Was Critical 1,014 4,036.15
13. Reactor Reserve Shutdown Hours 0 0
14. Hours Generator On. Line 2 431.3 IS. Unit Reserve Shutdown Hours 0 0
16. Gross Thermal Energy Generated (MWH) 1,981,895.4 4,455,695.8
17. Gross Electrical Energy Generated (MWH) 1,265,700
18. Net Electrical Energy Generated (MWH)'9.

1,062,035 Unit Servic~ Factor

20. Unit Availability Factor N/A N A N/A N/A I
24. Shutdowns Scheduled Over Next 6 Months {Type, Date. and Duration of Each 1:

1 Planned Scram (Turbine Trip/Load Rejection) for Power Ascension,'/5/88.

P armed Outage thru 5 23 88

25. If Shut Down At End Of Report Period. Estimated Date of Startup:
26. Units ln Test Status (Prior to Commercial Operation): Forecast Achieved INITIALCRITICALITY 5/23/87 INITIALELECTRICITY ~sos/87 COMMERCIAL OPERATION ~311 88 Iu/77)

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50-4 10 UNIT SIIUTDOWNS AND POWER REDUCllONS DOCKET NO.

DATE 3 9 88 February )988 COMPLETED gy E. Toml in son REPORT MONT)l rE C Lice nscc V~

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88-01 02/01/88 131.4 88-0 ] LD FLT Operator isolated instrument air causing Condenser/Feedwater Minimum Flow Valves to open. Reactor scrammed on low (level 3) water level; Strengthened administrative controls for tag outs and valve position verification. Continuation from January report period.

123.8 N/A N/A N/A Planned scram for SUT-25-6 as part of 88-02 02/15/88 Initiated ower. Ascension Testing.

rith HSIV closure.

F: FEueed ItcasEnl: Method: Exhibit G - Instructions S: SchcdulcEI A.l:EIEElpnlCIII I ailuEC (LXPIJirr) I -Manual for Preparation of Data I) MainlerEanee Eri Test 2.Manua) Scram. Entry Sheets for L)eerrsec

( . 1(e fEEelint) 3-Autuntatrc Seran>. Event Report (LER) File (NUREG-I) ItcgEE)illE)ly ltcst r rcr EEnr 4-Otlrer (Explain) 0161)

I OI)clatElr 1 raining 4 I.iecllsc I'.xJlnlEIJllon I "AdIIIIEIIstI Jrrvc (a OllcrallEJIIJI LIEEEI (IEXIEIJIEI) Exhibit I Sarw'ource

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ER ACE DAILYL. iIT PO'4 ER LEVEL DOCKET IO.

NMP2 COMPLETED GY E. Tomlinson EPllONE <" ) '4 February 1988 MONTH DAY AVERAGE DAlLYPOtvER LEVEL DAY *VERACE DAlLYPOtvER LEVEL I Mtve.Net) IMtVe .'Vet) 0 0 IS 0

0 10 0 0 0 57 0 343 823 639 1038 496 15 1034',

10 735 1067 659 1054

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678 1058 881 1019 13 59 8tIO 30 559 IS l6 0 LNSTRUCTIONS Oa this furntat, list t/te uveagc daily unit p<nvur level iii lltVc Yet t'ur eueh day in ilia repiutniy. ni.uirli. ('.sunpute Iu the nearest v;hule ntemivat t.

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0 NIAGARA HOHAQK POWER CORPORATION NINE HILE POINT NUCLEAR STATION UNIT f2 NARRATIVE OF OPERATING EXPERIENCE Nine Mile Point Unit 2 entered the final Power Ascension Testing Condition (TC-6) during the month of February 1988.

Host of TC-6 testing was completed. Tests included Recirc System and Feedwater System testing, LPRM/APRM calibration and MSIV full isolation. During the MSIV isolation 2 SRVs were challenged automatically five (5) times. These 2 SRVs plus three (3) others were opened manually later in the event to control pressure. RCIC System was also initiated manually to aid in pressure control. The completion of TC-6 and warranty run and the declaration of Commercial Operation are expected in March.

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MODIFICATIONS ACCEPTED BY OPERATIONS FEBRUARY 1988 s

NOD NUMBER s NWR NUNBER SYSTEN DESCRIPTION l PN2Y87NX089 M20339 FPM lADD FIRE DETECTORS ZONE 248NZ s

s l PN2Y87NX224 M20410 l WS l DRNS LIQUID MONITOR 2LWS-CAB206 PURGE DISCH REROUTE l s s

PN2Y87NX238 M20347 FWS ~ ACTUATOR CHANGES FOR 2LWS LV10A~ B~ C l M20357 s N20359 M20366 s s

s s N20367 N20368 s l M20371 N20372 I N20386 N20390 l N20396 l N20397 s s

l N20442 s s

l M20443 Phl2Y87NX245 N20391 HVR s ADDITION OF INSTRUMENT TEST HOLES IN HVAC DUCTWORK N20413 l I l N20444 l

PI42Y87NX250 M20418 N20419 l FILTERING ROSENOUNT TRIP UNITS l M20420 s s

l l N20421 s s

N20422 l N20423 l N20424 s s

M20425 N20426 M20427 l

MODIFICATIONS ACCEPTED BY OPERATIONS FEBRUARY 1988 l l l MOD NUMBER l MWR NUMBER l SYSTEM DESCRIPTION I

l-M20428 M20429 I M20430 I M20431 M20432 I

I M20433 l M20434 l M20435 I M20445 M20446 l Phl2Y87MX257 l M20412 DFM l DRAINABE REVISIONS ELECTRICAL TUNNEL l lHVAC EQUIPMENT ROOM & CO2 TANK ROOM PN2Y88MX002 l M20450 A04. 720 l PROVIDE SEALINB BAPS FOR SMOKE AND HOT BASES l

PN2Y88MX003 M20456 RMS l REROUTE OF RETURN LINE FROM 2RMS-CAB180 I

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07: 37: 40 03-04-88 CLASS I WORK INSTRUMENT 5 CONTROL FEB 88 PACE: 1 MR Number EPN Number Feilure desc Corrective Action W110964 CSL-AOV101 INJECTION TESTABLE CHECK VALVE 2CSL-AOV101 NONEt PROBLEM WAS NOT AOV 101 BUT LEAK OF BOUNDARY VALVE 2CSL+HCV117t DESPITE REPEATED FLUSHE8 AND CYCLESt HCV WOULD NOT SEAT TIQHTLY SINCE VESSEL MATER LEVEL WAS ABOVE CSL LINEt NO REPAIR WAS DONEt BUT HIQH LEAKAQE WAS ACCEPTED PER N2-ISP-CNT-R-002 TYPE C TEST 2CSL-AOV101 LEAKAQE HAS INCREASED A FACTOR OF 10 PREVIOUS 1. 172 SEFH 860609 TO 10. 624 SCFH 870924 TROUBLESHOOT ONLY W110976 HVC-eACU2A 2HVCeACU2* IRD VIBRATION READINQS TAKEN AS PER BOB HAWHINNEY VIBRATION HIQH AFTER INSTALLATION OF NOTOR FOUNDATION STIFFNERS ON WR NO 113451 TAKE VIBRATION READINQS TO CONFIRH PROPER OPERATION CB EL 288 THIS MR REPLACES MR 113439 TO TRANSFER WORK FROH MCQ TO IhC W122025 BYS-A19 ANALOQ ISOLATORS APPARENTLY NOT MORKINQ REPLACED OPTICAL ISOLATOR CARDSt ISOLATOR CARDS ARE TO BE REMOVED PER PR 7498 AND HRF I20362.HAS BEEN ISSUED TO DO THIS WORK ERF CP BYSVA100 101 AND 102 ARE READINQ HIQHER THAN NORNAL (OFF SCALE). CHECK OUT CIRCUIT'ND ISOLATORS (ON ATTACHED SHEET) TAKE VOLTAQE READINQS THIS WILL CHECK IF BYSVA102 IS SCALED WRONQ.

W122467 NSS-TE48D 49 2MSS-TE48D (E31W029D) REMOVED LUQS FROM FIELD WIRES AT D TB1 NO 10 AND 16 AND LANDED WIRESt PERFORMED.N2 ISP LDS N009 ATT. 4t REMOVED LUQS AT TB1.'1 AND 17 AND LANDED WIRESt PERFORMED N2-ISP-LDS-8009 ATT 4 2NSS-TE49D (E31-N030D)

HSL TUNNEL DIFF TEMP E31-N61SD THE LUQS ON THE THERNOCOUPLE FIELD WIRES FOR TE48D AND TE49D NEED TO BE REMOVED AND THE WIRES LANDED IN PNL709A TH 107 TB1 10 AND 11 AND 16 AND 17 WHILE PERFORNINQ N2-ISPWDSW009 W122917 WCS-FT67XhY REACTOR WATER CLEANUP FLOW RENOVED SNUBBERS ON WCS%67Xt'CS67Y ALREADY REMOVED BY CR I DUR INQ HODt

07: 37: 40 03-04-88 CLASS I WORK INSTRUMENT h CONTROL FEB 88 PACE: 2 WR Number EPN Number Failure desc Corrective Action REPLACED WITH SOLID S/S LINES CONTINUE TO MONITOR TRANSMITTER OUTPUT ONCE PER SHIFT AND REMOVE TEMPORARY MODIFICATION AFTER FINAL ENQINEERINC DISPOSITION W124156 "

CSH-.P1 HIGH PRESSURE CORE SPRAY PUMP EPOXIED IRD STICKERS IN APPROPRIATE SPOTS PER CENE. 28 PLACE IRD VIBRATION CHECKPOINTS IN VIBRATION DATA LOCATIONS AND SECURE WITH LOCTITE RC/620 OR APPROVED ADHESIVE CONTACT ISI PRIOR Td WORK FOR SPECIFIC VIBRATION LOCATIONS W124157 CSL-P 1 LOW PRESSUE CORE SPRAY PUMP EPOXIED IRD STICKERS IN APPROPRIATE SPOTS PER CENE. 28 PLACE IRD VIBRATION CHECKPOINTS IN VIBRATION DATA LOCATIONS AND SECURE WITH LOCTITE RC/620 OR APPROVED ADHESIVE CONTACT ISI PRIOR TO WORK FOR SPECIFIC VIBRATION LOCATIONS W124159 HVK-P1A CHILLED WATER PUMP 1A EPOXIED IRD STICKERS IN APPROPRIATE SPOTS PER CENE. 28 PLACE IRD VIBRATION CHECKPOINTS IN VIBRATION DATA LOCATIONS AND SECURE WITH LOCTITE RC/620 OR APPROVED ADHESIVE CONTACT ISI PRIOR TO WORK FOR SPECIFIC VIBRATION LOCATIONS W 124284 HVK-P1B CHILLED WATER PUMP 1B EPOXIED IRD STICKERS IN APPROPRIATE SPOTS PER CENE. 28 PLACE IRD VIBRATION CHECKPOINTS IN VIBRATION DATA LOCATIONS AND SECURE WITH LOCTITE RC/620 OR APPROVED ADHESIVE CONTACT ISI PRIOR TO WORK FOR SPECIFIC VIBRATION LOCATIONS W125252 HVC-RR 18D CHART RECORDER NO RR18D CALIBRATED RECORDER OUT OF CAL CHART RECORDER FOR DRMS RIC ON 2CEC-PNL880A (CONTROL ROOM EL 306)

W125253 CMS-RRYIOA CHART RECORDER NO RRY10A CALIBRATED RECORDER OUT OF CALIBRATION CHART RECORDER FOR DRMS R1C ON 2CEC-PNL880A

<CONTROL ROOM EL 306)

W 125254 HVC-RR18A CHART RECORDER NO RR18A RECALIBRATE CHART RECORDER OUT OF CAL

07: 37: 40 03-04-88 CLASS I WORK INSTRUMENT 5 CONTROL FEB 88 PACE: 3 WR Number EPN Number Failure desc Corrective Action CHART RECORDER FOR DRMS R1C ON 2CEC-PNLSSOA (CONTROL ROOM EL 306) 2HVC-RR18A W125255 SWP-RR146A CHART RECORDER NO RR 146A'UT RECALIBRATED CHART RECORDER OF, CALIBRATION CHART RECORDER FOR DRMS RIC ON 2CEC-PNLSSOB EL 306 CONTROL ROOM W125259 HVC-RR18B CHART RECORDER NO RR18B CALIBRATED RECORDER OUT OF CAL CHART RECORDER FOR DRMS Ric ON 2CEC-PNLSSOC (EL 306 CONTROL ROON) 2HVC-RR18B W125260 CMS-RRX10B CHART RECORDER NO RRXIOB CALIBRATED RECORDER OUT OF CAL CHART RECORDER FOR DRMS'Ric ON 2CEC-PNL880C (EL 306 CONTROL ROON)

W125261 SWP-RR146B CHART RECORDER NO RR 146B CALIBRATED CHART RECORDER OUT OF CALIBRATION t CHART RECORDER FOR DBMS RIC ON 2CEC-PNL880D EL 306 CONTROL ROOM i W125266 HVR-RRX14A CHART RECORDER NO RRX14A RECALIBRATE CHART RECORDER OUT OF CAL CHART RECORDER FOR DRMS RIC ON 2CEC-PNL880A (CONTROL ROON)

W125267 HVC-RR18C CHART RECORDER NO RR18C PERFORMED CALIBRATION OF RECORDER OUT OF CAL CHART RECORDER FOR DRMS RIC ON 2CEC-PNL880A (CONTROL ROOM) (2HVC-RR18C)

W 128341 ICS-2ICS+PT1 RCIC PRESSURE XMTR CHECKED CAL LOOKS OK SEE CAL SHEETS B

REGAL LOOP FOR 2ICS-PT1B RECAL REQD DUE TO TEST EQUIP BEINQ LOST W 128348 ISC-2ISCeP15 SAFETY RELIEF VALVE ACTUATION TRIP UNIT RECALIBRATED TRIP UNITS RESET TRIP 1668A POINT TO CORRECT VALVESI 2ISC+PISihhSA AND 1668E INVESTIGATE CAUSE OF RAPID SAFETY RELIEF VALVE RECLOSURE ON PSV128 AND PSV133 DURINQ PERFORMANCE OF 1951V CLOSURE SCRAM CHECK RELIEF VALVE TRIP UNIT RESET VALVES TROUBLESHOOT ONLY

07:37: 40 03-04-88 CLASS I WORK INSTRUMENT 5 CONTROL FEB 88 PAGE: 4 WR Number EPN Number Failure desc Corrective Action W128410 ICS-PDIS167 RHR RCIC STEAM FLOW ISOLATION TRIP UNIT 2ICS%PDIS CHANCE COMPLETED BY TCN TO 168 167 168 N2-ISP-ICS-M001 AND REPERFORMANCE OF SAID PROCEDURE N2-SUT-71-1 WAS PERFORMED TO OBTAIN DATA TO EVALUATE FINAL SETPOINTS FOR 2ICS%PDIS 167 168 FDDR KQ1-6022-REV 1 WAS ISSUED IN RESPONSE TO PR7403 TO CHANGE TECH SPEC NOMINAL TRIP SETPOINT TO 37. 4 INCHES H20. CHANGE GUIDE VALUES IN N2-ISP-ICS-M001 AND RECALIBRATE W128420 RCS-C518-ARS RATED DRIVE FLOW AT 70-75 PERCENT POWER IN TC3 WAS RAISED THE VOLTAGE BY USING 3 DETERMINED TO BE 43600 QPM N2-I SP-RCS-Q101 AT ALL 4 APRM FLOW UNITS ADJUST R4 FOR AN INDICATION OF 703V PLUS OR MINUS 10MV AS READ BETWEEN TP4 AND TP1 DURING SUMMER GAIN ADJUSTMENT (N2-ISP-RCS-Qioi)

W128431 RCS-2RCSeFT8 RECIRCULATION SYSTEM DRIVE FLOW TRANSMITTERS PERFORM TP 87-54 ON 2RCS%FT83A AND 3A 83Bi RESPONSE TIME FOR BOTH TRANSMITTERS HAVE BEEN SET TO 420 MSEC AT A 35 IN. H20/SEC AND 45 IN.

H20/DRV RAMP RATEiMADE ADJUSTMENT TO DAMPINQ POTENTIOMETER 2RCSeFT83A/B ADJUST TRANSMITTER RESPONSE TIME AND PERFORM PROCEDURE TP 87-54 W130154 HVC-2HVCeFS- CONTROL ROOM ACUIB DISCHARGE AIR FLOW SWITCH REPLACED AND CALIBRATED NEW FLOW 23B SWITCH 2HVCeFS23B WHILE PERFORMINQ 18 MONTH RECAL ON LCR NO.

1L2HVC-066 UNDER N2-ICP-QEN-8001 FOUND CIRCUIT CARD FAULTY REPLACE AND CALIBRATE AS NECESSARY W130155 CES-2CES%99- OUTPUT OPTICAL ISOLATOR 99-8CZ1HAA01 REPLACED OUTPUT ISOLATOR CARD 8CZIHAA01 OPEN CIRCUIT OUTPUT ISOLATOR 99-CZIHAA01 IN PNL 837 ZT Z32 HAS CHAhWEL L IS OPEN REPLACE OUTPUT CARD PART NO. 93-05-698 REF WR 130075 W130517 ISCWDT14B FEEDWATER LEVEL TRANSMITTER B VENTED TRANSMITTER ISC+PT115u ISC+PT2Ce ISC+PT4Bt ISC%LT2Bn ISC+PI3Bn TERMINATED THIS WR DUE TO STARTUP NOISY SIGNAL THE B LEVEL TRANSMITTER IS MUCH NOISER THAN A OR C VENT TRANSMITTER AND ALL OTHER TRANSMITTERS WITH COMMON REF OR VARIABLE LEGS

07: 37: 40 03-04-88 CLASS I WORK INSTRUMENT 5 CONTROL FEB 88 PAGE: 5 WR Number EPN Number Failure desc Corrective Action VENT ILT CONNECTIONS TROUBLESHOOT FOR OTHER POSSIBLE CAUSES CONTACT DAN HOLLAND BEFORE BEGINNING WORK W130528 ISC-2ISC+PDT FEEDWATER CONTROL NARROW RANGE LEVEL XMITTERS 2ISC+PDT14A SEAL 03 AS FOUND 14A RESPONSE APPROX 80 MSECi AS LEFT RESPONSE APPROX 470 MSECe SEAL 02i 2ISC+PDT14B SEAL 02 AS FOUND RESPONSE APPROX 110 MSECi AS LEFT RESPONSE APPROX 470 MSECs SEAL 02 INCREASE THE DAMPENING OF 2ISC+PDT14A AND B (C33-N004A AND B) TO . 4 SEC USINQ THE SETTINGS (13 PERCENT OF SPAN) OR IF TIME ALLOWS SET THE TIME CONSTANT TO . 5 SEC USINQ TIME RESPONSE TESTING W130798 RMC-RODS4-39 ROD 54-39 CHECKED IN CRi ALL OK PROBABLY BAD REED SWITCH WHEN INSERTING ROD 54-39 FROM POSITION 06 TO 04 THE ROD LOST POSITIVE INDICATION AT POSITION 04 AS DETERMINED BY THE 4 ROD DISPLAY PLEASE TROUBLESHOOT W131103 WCS 2WCS FILTER 4C TEMPORARY MEASURES'EMPORARY INCREASED PRECOAT. FILL TIMER Ob015 TO 6 MIN TEMP MOD 88021 TEMP MOD CLEARED 2-4-88 TIMERS RETURNED TO 5 MIN C VESSEL DOES NOT DEPRESSURIZE PROPERLY IN STEP

4. 3 VENT VALVE 6ic ALSO THE START OF PRECOAT CYCLE INTERRUPTS 30 SECONDS INTO CYCLE QIVINQ THE SYSTEM A BACKWASH REQUIRED INTERLOCK LATCH WITH NO APPARENT REASON 328 RX SOUTH W131232 NMS-2NMSe IRM IRM F DRAWER REPLACED PRE-REGULATOR VR22 IN IRM F F WHILE PERFORMINQ N2-ISP-NMS-W-009 STEP 7. 3. 2 FOUND INDICATOR TO BE READING LOW-OUT OF SPEC TROUBLESHOOT W131239 MSS-2MSS+RE4 MAIN STEAM LINE RAD MONITOR C ADSUSTED TRIP SETPOINT ADJUSTMENTS hC R95i R94. R93 PER SURVEILLANCE N2-ISP-MSS-R 104 WHILE PERFORMINQ N2-ISP-MSS-M001 FOUND UPSCALE 1 AND 2 AND DOWNSCALE TO BE LOW TROUBLESHOOT ONLY W134338 MSS-2MSSeRE- MAIN STEAM LINE RADIATION MONITORS SETPOINT CHANCE RESET TRIP POINTS

07:37: 40 03-04-88 CLASS I WORK INSTRUMENT h CONTROL FEB 88 PAGE: 6 WR Number EPN Number Failure desc Corrective Action 46A RESET MAIN STEAM LINE RADIATION MONITOR TRIP SETPOINTS TO 1375 MR/HR BASED ON A NEW PROJECTED FULL POWER BACKGROUND LEVEL OF 500MR/HR SEE RADIOLOGICAL SUPPORT GROUP CALCULATION NO.

88-11 W137222 RRS-2RRS-BCO COMPUTER POINT RRS BC07 RRCS TROUBLE DIV I REPLACED BOARD AZA3N15 IN 7 ANNUNCIATOR SYSTEM COMPUTER PT IS IN ALARM WITHOUT BRINQINQ IN ANN NO. 603445 OR SHOWING A PROBLEM AT P001 OR P002 PNL TROUBLESHOOT ONLY W137224 GTS-2QTSeFRi 2QTS%FRiOB FLOW RECORDER ON 2CEC-PNL871 RESET ELECTRONIC RELAYS 2GTS+PVSB OB NOW WORKS FINE> RECORDER CONTINUES TO WORK FINE 2QTS-FR10B(RED PEN) ON 2CEC-PNL871 IS FAILED UPSCALE DOES NOT VARY WITH FLOW TROUBLESHOOT ONLY W137225 QTS-2QTS%PNL LOW AIRFLOW CREEN LIGHT AT 2GTSePNL30B RECALIBRATED FLOW SWITCH 2QTS+FS25i 30B LOOP SEEMS TO FUNCTION CORRECTLY NOW TROUBLESHOOT 2QTS+CHIB HEATER LOW AIR FLOW LIGHT AT 2QTS+PNL30B DIV II STBY QAS BLDG 261 DOES NOT EXTINGUISH WHEN TRAIN B IS RUNNINQ W137227 MSS-2MSSwE31 MAIN STM LINE TUNNEL DELTA T TMP UNIT REPLACED TRANSMITTER/SWITCH

-N615D 2MSS+TS-1615D AND PERFORMED PROCEDURE N2-ISP-LDS-M009 MSL DELTA T TMP UNIT ON 2CEC+P611 INDICATES DOWNSCALE INVESTIGATE AND CORRECT INPUT TO NSSS ISOLATION LOGIC D4 W137270 WCS-2WCS+F16 WCS SYSTEM FLOW INDICATION (TRANSMITTER) 900 GPM IS EXACTLY WHAT IT SHOULD 7X READ. CALIBRATION IS CORRECT PER, ALBERT HWU. QE FT67X INDICATES 900 GPM WHEN ACTUAL FLOW IS 700 QPM W137276 QTS-2QTSePV5 SBGT FLOW CONTROL VALVE INSTALLED NEW MOTORS RUSTY GIBSON B CRIMPED LEADS TORGUED MOTOR STUDS AND COVER VALVE WILL NOT OPERATE

07: 37: 40 03-04-88 CLASS I WORK - INSTRUMENT h CONTROL FEB 88 PAGE: 7 WR Number EPN Number Failure desc ~ Corrective Action W 137353 EGA-PS9B 2EGA-PS9B DIV II AIR COMPRESSOR START SWITCH FOUND PS 19B TO BE HIGH ALARM COMING IN BEFORE PS9B ACTIVATING 2EQA-PS9B NOT ALLOWINQ AIR COMPRESSOR TO START PRIOR TO RECEIVINQ LOW AIR PRESSURE AT 233 PSIQ DQ BLDG EL 261 DIV II W137358 NMS-2NMS+APR APRM E K18 RELAY REPLACED RELAY K18 PER SSS ME WHILE PERFORMINQ N2-ISP-NMS-WR007 K18 RELAY WAS FOUND TO BE DEFECTIVE REPLACE K18 RELAY W137380 NMS-2NMSeIRM IRM-G REPLACED DUAL TRIP UNIT Z17

-G 194X382G3 IRM-G WHEN UNBYPASSED BRINGS IN THE FOLLOWINQ ALARMS-ANN 603201 UPSCALE-INOP RED LIGHT ON P603 AND DOWNSCALE REMAINS IN NO ONE HALF SCRAM OR RPS TRIP~OCCURS AND NO DRAWER INOP OR UPSCALE TRIP LIGHT OCCURS TROUBLESHOOT W 137389 NMS-2NMS> IRM INTERMEDIATE RANGE MONITOR -G- REPLACED PREREQULATOR CARD VR27 8/N

-Q TGAL7-30 ,

IRM-G READS 20 WHILE ALL OTHERS READ 0 IRM-G READS 20 WITH MODE SWITCH IN ZERO 2 POSITION PLEASE TROUBLESHOOT W137431 HVR-2HVR+FS3 FLOW SWITCH AIR EXHAUST ABOVE REFUEL FLOOR FS 36B FOUND TO BE OUT OF SPECe 6B NOMINAL MV IS 487MV THEREFORE TRIP CANNOT BE SET AT 460MV MIGHT NEED NEW FLOW PROFILEi PERFORMED GEN-003 NEW SETPOINT 590MV. SATISFACTORY CAL CALIBRATION APPEARS TO HAVE DRIFTED CHECK CAL W138121 NMP-2NMP+APR APRM -B- PERFORMED N2-ISP-NMS-Q107 MB LOCAL INDICATION READS 61 PERCENT WHILE PNL603 CHART INDICATES 70 PERCENT RX PWR 56 PERCENT APRM HI/TING UPSCALE ALARM EARLY TROUBLESHOOT W138123 NMS-2NMS+C51 AVG PWR RANGE MONITOR B ADJ ZERO PER N2-ISP-NMS-Q107

-K605B WHILE PERFORMING N2-ISP-NMS-9107 FOUND METER ZERO OUT-OF-SPEC UNABLE TO ADJUST 'USINQ DC AMP TROUBLESHOOT ONLY

07: 37: 40 03-04-88 'CLASS I WORK INSTRUMENT h CONTROL FEB 88 PACE: 8 WR Number EPN Nueber Failure desc Corrective Action W138127 WCS-2WCSeFT6 REACTOR WATER CLEANUP BLOWDOWN FLOW TRANSMITTER VENTED WCS-FT69X AND WCSMT68X AT 9X THE TRANSMITTER AND DRAINS. POTH TRANSMITTERS HAD A 1. 00 VDC OUTPUT WHEN EQUALIZED. SEE NO NEED FOR CAL. DELTA FLOW READINQ APPROX 75 P QPM FOR BOTH X AND Y DIVISION 1A FOR RWCU DELTA FLOW READS LOWER THAN IT SHOULD AND BARELY WITHIN SPECIFICATION PER SHIFT CHECKS RECALIBRATE WCS+FT 69X SEE ATTACHED FOR ADDITIONAL DATA W138135 IAS-2IAS%V16 MSIV 7C INST AIR SUPPLY REMOVED TEMP MOD 88-067 15 FABRICATE AND INSTALL PRESSURE INDICATINQ AND VENT RIQ DOWNSTREAM OF 2IAS%V1615(C-)

PRESSURE QAUQE SHOULD BE AT LEAST 0-150 PSIQ REMOVE TEST RIQ WHEN TROUBJ ESHOOTINQ IS COMPLETE W138142 RCS-2RCSeB35 FLOW UNIT A B35-K607A REPLACE SUMMER CARD 136B3088AAQ003

-K607A WHILE PERFORMINQ N2-ISP-RCS-M8001 FUSE F8 ON SUMMER CARD ZQ WAS FOUND TO BE BLOWN REPLACE FUSE OR SUMMER CARD a TROUBLESHOOT W138196 ICS-2ICS%PDI RHR/RCIC FLOW HIQH SLAVE TRIP UNIT MTUi STU AND TDPU RELAY ALL TESTED 8168 SAT TRIP UNIT E31-691B PICKS UP RELAY ESi-K85 AND WILL NOT RESET RELAY WHEN CONDITIONS ARE NORMAL K85 RESETS WHEN E31-691B IS PULLED TROUBLESHOOT 49 records listed.

07: 36: 57 03W4-88 CLASS I WORK - HECHANICAL HAINTENANCE FEB 88 PACE: 1 MR Number EPN Number Failure desc Corrective Action W122279 RCS-HOV18A RECIRC ISOL VALVE 18A TOOK UP ON PACKINO EVENLY'TROKED VALVE.WORKED SHOOTHLY THE VALVE HAD A SHALL STEAN LEAK DURINO OPERATION TAKE UP ON PACKINO AND OR IF REGD ADD 1 OR 2 RINGS OF PACKINO W122359 CSLWCV117 2CSL-HCV117 RETORQUE TO 600 FT LBS ALL BONNET BOLTINO. NO NUTS ROVED RETORQUE PRESSURE SEAL BONNET PER ANSMER TO PR 7242 TORQUE IN HANUAL 430004354 SEE ATTACHED SHEET W 122360 CSH-HCV120 2CSH-HCV120 RETORQUE TO 600 FT LBS ALL BONNET BOLTINOs NO NUTS HOVED RETORQUE PRESSURE SEAL BONNET PER ANSWER TO PR 7242 TORQUE IN HANUAL 430004354 SEE ATTACHED FOR TORQUE M122369 RHS-HCV53A 2RHS-HCV53A B C RETORQUED ALL BONNET BOLTINO TO 600 FT LBSi NO NUTS HOVED RETORQUE PRESSURE SEAL BONNET PER ANSWER TO PR 7242 TORQUE IN HANUAL 430004354 SEE ATTACHED FOR TORQUE W 122370 RHS-HCV54A 2RHS-HCV54A B C RETORQUED BONNET BOLTINO TO 600 FT LBSt NO HOVEHENT WAS DETECTEDs VALVE HCV54C DOES NOT EXIST RETORQUE PRESSURE SEAL BONNET PER ANSWER TO PR 7242 TORQUE'N MANUAL-430004354 SEE ATTACHED FOR TORQUE W122371 RHS-HCV131 2RHS-HCV131 RETORQUED BONNET BOLTINQ TO 600 FT LBS>BOLT8 DID NOT HOVE RETORQUE PRESSURE SEAL BONNET PER ANSWER TO PR 7242 TORQUE IN MANUAL-430004354 TORQUE PER ATTACHED SHEET W 122372 RHS-V 143 2RHS-V143 CHECK PREBSURE SEAL BONNET BOLTS PER TORQUE SPEC8 RETORQUE PRESSURE SEAL BONNET PER ANSWER TO PR 7242 TORQUE IN HANUAL-430004354 TORQUE TO ATTACHED SHEET W 125365 CSH-AOV108 HPCS INJECTION LINE TESTABLE CHECK VALVE REPLACED PACKINO AND ONE SEAL 0ASKET REPACK VALVE (2CSH-AOVI08)

. ~

07:36: 57 03W4-88 CLASS I WORK MECHANICAL MAINTENANCE FEB 88 PACE: 2 WR Number EPN Number Failure desc Corrective Action VLVE IS ON EL 306 IN THE DRYWELL OR ADD PACKINQ M127706 HVC-ACU2A 2HVC-ACU2A INSTALLED JACKINQ ASSEMBLIES ON FAN ROTOR HOUNTS INPROPER PARTS E AND DCR NO C47625A REQUIRES JACKINQ ASSEMBLIES INSTALLED ON ROTOR. AMOUNTS THIS MR REPLACES MR NO 110646 W127707 HVC-ACU1B 2HVC-ACU1B INSTALLED JACKINQ ASSEMBLIES AND .

NEW SX3Xi/2 ANQLE HOTOR MOUNTS SEE WR127706 FOR HcDCR'8 IHPROPER PARTS E AND DCR NO C47625A REQUIRES ANQLE IRON STIFFENERS AND JACKINQ ASSEHBL'IES ON ROTOR MOUNTS THIS MR REPLACES WR NO 110646 M127718 WCS-V47 WCS-V47 TORQUE ON FACE PLATE(COVER) ~ 8TILL LEAKS PER Q PROSSER 871102.

VALVE LEAKINQ 50 DROPS PER HINUTE-RETORGUE BONNET UNDER PRESSURE TORGUE TO THE ATTACHED TABLE 871102 STILL LEAKS AFTER TORGUINQ DISASSEHBLE INSPECT AND REPLACE PRESSURE SEAL M128151 HVC-UC105 ELECT TUNNEL UNIT COOLER CHANQED FILTERS UNIT COOLER SHOWS HIQH FILTER DP-CHANQE W128702 RCS-2RCSeNOV 2RCSeMOVIOB TAKE UP ON THE PACKINQ 10B QLAND, PACKINQ QLAND IS NOW BOTTOHED OUT. ABOUT TWO NORE RINQS WOULD BE JUST RIQHT TAKE UP ON PACKINQ AT 900 LBS IF REGD M128/69 RCS-2RCS+HOV RCS NOViSA REPLACED PACKINQ 18A PULL PACKINQ TO INSPECT LOWER PACKINQ AREA W128800 RCS-2RCSeHOV RCS+NOV10A TAKE UP ON THE PACKINQ 10A CLANDi PACKINQ QLAND IS NOM BOTOHED OUTe ABOUT TWO NORE RINQS WOULD BE JUST RIQHT TAKE UP ON PACKINQ AT 900 LBS IF REGD W129457 RHS-2RHS+PSS SNUBBERS (BZ-71ADC) ALIQNED SNUBBERS P807A2 OUT OF TOL SNUBBER 2RHS-PSSP 807AZ (A)

LINE NO 2RHS-018-24-2 NORTH SIDE OF PIPE AND PIPE

lg 07: 36: 57 03-04-88 CLASS I WORK MECHANICAL MAINTENANCE FEB 88 PACE: 3 Failure'e WR Number EPN Number desc Corrective Action CLAMP IS 7 DECREES OUT OF ALIQNMENT AND PADDLES ARE NOT AT 90 DEQREES TO PERMIT ROTATION ALSO 2RHS-PSSP807A2(B) SOUTH SIDE AND PIPE CLAMP'S 8 DECREES OUT OF ALIQNMENT CORRECT ALIQNMENT AND PADDLE POSITION RHS B PUMP RM S AUX BAY EL 175 W130786 RCS-MOV10A RECIRC -A- SUCTION VALVE INSTALLED 3 SETS OF PACKINQ REPAIR PACKINQ LEAK W130787 RCS-MOV10B RECIRC -B- SUCTION VALVE REPLACED PACK INQ REPAIR PACKINQ LEAK W130788 RCS-MOV18A RECIRC -A- DISCHARGE VALVE INSTALLED 3 RINQS OF PACKINQ REPAIR PACKINQ LEAK W13P789 RCSWOV18B RECIRC -B- DISCHARGE VALVE REPACKED V~VE PACKINQ LEAK REPAIR PACKINQ LEAK W131167 ZZZ-PCB-DRA5 NORTH DRYWELL EQUIPMENT PERSONNEL HATCH DISABLED DRYWELL PERSONNEL HATCH INTERLOCKS INTERLOCKS.

DISABLE INTERLOCKS DISABLE DRYWELL EQUIPMENT HATCH INTERLOCKS (NORTHSIDE)

TO ALLOW BOTH DOORS TO BE OPENED SIMULTANEOUSLY WHEN DIRECTED BY SSS RESTORE INTERLOCKS TO NORMAL W131185 ZZZ SUPPRESSION CHAMBER'NORTH HATCH CLOSED 5 TORGUED TO SPECS OPEN HATCH TO FACILITATE PERFORMANCE OF CONTAINMENT BYPASS.LEAKAQE TEST W134302 QTS-2QTSeFLT STANDBY QAS TREATMENT SYS-2QTS-FLT1A SYSTEM SURVEILLANCE TESTINQ 1A PROVIDE LABOR SUPPORT TO ASSIST VENDOR IN TESTINQ ABOVE SYS WORK TO INCLUDE REMOVAL AND REPLACEMENT WITH DOORS AND PANELS ETC FOR COMPLETION OF SYSTEM'SURVEILLANCE TESTINQ THE WORK OF FEB 22-26 1988 W137321 EQA-2EQA+V14 BOLTS ON FLANCES BETWEEN 2EQAeV14B AND 2EQAePCV25B REPLACED NUTS 4 TIQHTENED B

2 BOLTS AND ASSOCIATED NUTS ON FLANQE CONNECTIONS BETWEEN 2EQAeV14B AND 2EQAePCV25B HAVE VIBRATED LOOSE AND MUST BE REPAIRED AND RETORGUED REPAIR AS NECESSARY

07: 35: 25 03W4-88 CLASS I WORK - CONSTRUCTION FEB 88 PACF: 1 WR Number EPN Number Feilure desc Corrective Action C127950 HVC-ACU3B REHOTE SHUTDOWN RKN AIR COND ITIONINO UNIT CROUND OFF REHAINS OF OLD STUD-REPLACED STUD USINO PROC WPS-STUDS-AWS.RETURNED UNIT TO ORI4 CONDITION PHYSICAL FAULT ACCESS DOOR TO FAN HAS BROKEN STUD NEAR LOWER RIOHT CORNER OF OPENINO THIS WR REPLACES WR 118575 - ATTACHED COPY-LOC4TED EL 275 IN DIV II SWITCHOEAR ROON C131189 BLDQ-S4175-1 WATER TIOHT DOOR LOOSE PARTS. 4EARS ADJUSTED'H 2-I-88>LOOSE SET SCREWS ON OEARS TIOHTENED AND BOLT RETRACTS BUT DOOR STILL HAS HISSINO AND SHE4RED OFF BOLTS IN LOCKINQ HECH HECHANICAL FAILURE LOWER LEFT SLIDE Bm T FAILS TO RETRACT SAFETY HAZARD C131250 BLDO WATER TICHT DOOR BETWEEN CSL AND RHR A PUHP ROOHS OEARS ADJUSTED SH 2-I-BBi SET SCREWS ON OEARS TIOHTENED AND LATCH OPERATES BUT DOOR STILL HAS HISSINC AND SHEARED OFF BOLTS IN J OCKINO HECHANISH BOTTOH LATCH (OPP HINCE SIDE)

DOES NOT OPERATE-FAILS TO LATCH OR FAILS TO UNLATCH (DEPENDINC ON LATCH POSITION)

REPAIR AS NECESSARY 3 records listed.

r 07: 36: 05 03W4-88 CLASS I WORK ELECTRICAL NAINTENANCE FEB 88 PAOE: 1 WR Number EPN Number Failut ~ desc Corrective Action W115941 RRS-P001-2 RRS DISPLAY PANEL WORK DONE BY SUPPORT CROUP.

BROKEN MIRE SUPPORT CABLE A130-P3 HAS A BROKEN WIRE SUPPORT AT THE DOOR PLUOS INSTALL NEW CABLE SUPPORT W122458 MC8-EFV222 '2WCSeEFV222 RRPLhCED PER FDDR KOI-5S27WEV 0 ON HotIAN FACTORS NOD., NOD OPN2YS6NX084 LF100. NO WORK REQUIRED ON THIS WR.

THE LIQHT ON PANEL 602 LABELED 2RCSeEFV222 SHOULD BE LABELED 2MCSeEFV222 M127863 BYSWHRO 2A1 2BYS-CHQR 2Ai HETER ACCURACY MAS CHECKED WITH h CALIBRATED FLUKE AND THE READINQS WERE WITHIN TlK ACCEPTABLE VALVE OF

+-, 3V AS STATED ON ~PN~~5.

NO ACTION REQUIRED AT THIS Tits.

VOLTtKTER NEED8 TO BE CALIBRATED READINO IS 9 VOLTS LOW W128747 EHS-2EHSeNCC 2EHSeNCC201MUB2A REPLACE TERNIHAL BLOCKS'EPLACED 201-2A TERMINAL BLOCKS FRON SPARE BREAKER 4

~ Ot1 '~eNCC201 CUB 2Bi WR 128748 WRITTEN TO REPLACE TERtIINAL BLOCKS ~

2EOTeCHI REPLACE TERN BLOCKS NO. 6 AND 7 ON ttCC IARICT h/ ~$

AH5 CUBICLE BOTH 8TATIONARY AND SEPARABLE PART8 NEED!a REPLACEHENT OBTAIN PARTS PRON SPARE CUB. NO. 2B REF WR 128748 W128785 EHSMCC101 2EHS-HCC101 CUB 7B 8PARE BRSQQiR FRtg EHSttCC1011 CUB 2C WAS PE~tD AND PASSED CONTACT RRSfSff4hE TEST N2-EPEE~582 AND fQCfA4Llm IN BREAKER 7B AND RS ukOCa, REPLACE NOLDED CASE BREAKER WITH IRN QK (OLD ONE USED FOR 2SMP-NOVIC)

EHS NCC101 CUB 2C REF WR NO 128783 W128791 SMP-SSR 3A-6 DIV I SERVICE WTR RACK BAR HEATER8 CQR@A'EADINOS FOR 2SWPXSSR3Ah6A A Attf'.1'I; 7 EACH CURRENTS FOR 2SMP-SSR3A AND 6A READINQ 5. SA AND

4. 2A RESPECTIVELY PREVIOUS WK READINOS WERE 12. OA AND 11. SA INVESTIOATE AS NECESSARY CECWNL628 DIV I ADS RELAY PANEL P'NSTALLED LUO ON TBHH POINT 49 AND W 129335

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07: 36: 05 03-04-88 CLASS I MORK ELECTRICAL HAINTENANCE FEB 88 PACE: 2 MR Number EPN Number Failure desc Corrective Action ON POINT 014 IN 2CECePNL628.

INSTALL PERHANANT STAK-ONS ON RICHT SIDE OF TERN STRIP HH NO 9 AND RIGHT SIDE OF TERN STRIP HH NO 14 TO ALLOW EASIER AND SAFER CONPLETION OF N2-OSP-ADS-H002 TO ALLOW HANDS-FREE ATTACHMENT OF A DVH (REF E AND DCR NO C95078) (REF INT CORR NO NHP2-2420 AND NNP2-320 ATTACHED)

M129336 CEC-PNL631 DIV II ADS RELAY PANEL INSTALLED LUO ON TBAA POINT ()9 AND ON POINT ()14 IN 2CEDePNL 631 INSTAL'L PERHANENT STAKE-ONS ON LEFT SIDE OF TERN STRIP AA NO 9 AND LEFT SIDE OF TERN STRIP AA NO 14 TO ALLOW EASIER AND SAFER COHPLETION OF N2-OSP-ADS-H002 TO ALLOW HANDS-FREE ATTACHMENT OF A DVH (REF E AND DCR NO 95078) (REF INT CORR FILE CODES-NNP22420 AND NHP2-320 ATTACHED)

M1 30748 RPS-C72-P510 RECIRC PUMP TRIP SYSTEH A FOR TSV2 REPLACED SOCKET NEON LAMP SOCKET DETER IORATINO PLEASE REPLACE M132300 ISC JET PUNP 10 PASS ISOLATOR VALVE ADJUSTED LINIT SWITCHES.

CREEN INDICATOR LICHT DOES NOT LIGHT WHEN VALVE SWITCHED TO CLOSED THERE IS

  • OREEN FLICKER WHEN VALVE TURNED TO OPEN HOWEVER RED INDICATOR DOES NOT.LIOHT SWITCH LOCATION ON 237 CB W1 37201 ISC 2ISC-RV33B RV34B RV35B RV36B TAPED SPARE CONDUCTOR ON 21SCeRV3SBi INTERMITTENT OROUND DUE TO LIHIT SMITCH SEGUENCINO DRYWELL VACUUN BREAKERS TESTINO CIRCUIT BLOWS FUSE CKT NO 2ISCN04 (ESK 2ISC04) FUSE Fi INVESTICATE CAUSE AND CORRECT RESULTS IN INABILITYTO TEST VACULN BREAKERS AND LOSS OF POSITION INDICATION W137373 ICS-2ICS%AOV RCIC INJECTION TESTABLE CHECK VALVE INBOARD NONE. LIHIT SWITCHES FUNCTIONINO 157 PROPERLY.

2ICSeAOV157 INDICATED CLOSED DURINO RCIC INJECTION TO RPV 12 records listed.

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07: 36: 57 03W4-88 CLASS I WORK HECHANICAL HAINTENANCE FEB 88 PAOE: 4 WR Number EPN Number Failure desc Corrective Action W138125 ICS-2ICS+ROi 2ICS-R0155 REHOVED ORIFICE FRON LINE AND 55 CLEANED'EPLACED WITH NEW CASKET CHECK RO FOR BLOCKACE. MILL NOT ALLOW HIOH ALARM TO CLEAR WHEN RCIC IS IN STANDBY DUE TO INSUFFICIENT PRESSURE ON DRAIN POTMAS TO DRAIN THRU LS DRAIN V277 W138130 SVV-2SVVeRVV SAFETY RELIEF VLV TAILPIECE VACUUM BKR SPRINQ WAS DIRTY ALL WE DID WAS 104 CLEAN IT 2SVVeRVV104 STUCK OPEN TROUBLESHOOT LOCATED IN PRI. CONTAINMENT ELEV 246 8. SIDE OUTBOARD OF THE -A- RECIRC PHP 26 records listed.

t,