ML18018B205
| ML18018B205 | |
| Person / Time | |
|---|---|
| Site: | Nine Mile Point |
| Issue date: | 03/09/1988 |
| From: | Niagara Mohawk Power Corp |
| To: | NRC/IE |
| References | |
| Download: ML18018B205 (44) | |
Text
~ XVVAae NDE NILE POL%'UCLeea STATION PilIT DOCUMENT TRANSMITTAL A%) VERIFICATION HONTHLY REPORT
. FOR FEBRUARY 1988 Title of Document ASS IGiiD T. Perkins TO P. Charles DATE 3/9/88 OUE DATE 3
15 88 ED DATE SUBJECT OPERATING STATISTICS 6 SHUTDOWN F.
FBR ARY 1988 DOCUMENT ADDRESSED T0 DIRECTOR FFICE OF INSPECTION 6 ENFORCEMENT TEAR REG AT RY SSI N
PREPARED BY REVIEWED BY VERIFIED BY P. Charles E. Tomlinson 31 88 DATE 3/9/88 DATE o
ATE
<- -g DATE I P DATE 3-!o-ss DATE DATE DATE CQbHF1TS RECEIVED FOR TRANSMIT?'AL 0ATE
~g/et SENT TO ADDRESSEE BY DATE FILED AT SITE OFFICE STAMPS DOC.CONTROL RE ORD COPY RETURNED TQ SITE BY LOGGED A I
ATE DATE Dates entry is made into-report/response computer monitoring. systei frlI/ I AP!(-16-6;;
Det:6mb'er 1,980
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OPERATING DATAREPORT OPERATING STATUS Nine Mile Point Unit 2
- l. Unit Name:
- 2. Reporting period:
2/ 1/88 thr u 2
29 88
- 3. Licensed Thermal Po~er (MWt):
3323
- 4. Nameplate Rating (Gross MWe):
- 5. Design Electrical Rating (Net MWe):
- 6. Maximum Dependable Capacity (Gross MWe):
NOT
- 7. Maximum Dependable Capacity (Net MWe):
Notes
~onTE ~>e 88 COSIPLETEO BY E. Tomlinson
... TELEFHOiVE ~~9-2761
- 8. IfChanges Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report. Give Reasons:
- 9. Power Level To Which Restricted, IfAny (Net MWe):
- 10. Reasons For Restrictions, IfAny:
This Month Yr. to.Date Cumulative 1,440 696 5,680 4,036.15 2 431.3 1,981,895.4 4,455,695.8 1,265,700 1,062,035 N/A N A P armed Outage thru 5 23 88
- 11. Hours In Reporting Period
- 12. Number Of Hours Reactor Was Critical 1,014
- 13. Reactor Reserve Shutdown Hours 0
0
- 14. Hours Generator On.Line IS. Unit Reserve Shutdown Hours 0
0
- 16. Gross Thermal Energy Generated (MWH)
- 17. Gross Electrical Energy Generated (MWH)
- 18. Net Electrical Energy Generated (MWH)'9.
Unit Servic~ Factor
- 20. Unit AvailabilityFactor N/A N/A I
- 24. Shutdowns Scheduled Over Next 6 Months {Type, Date. and Duration of Each 1:
1 Planned Scram (Turbine Trip/Load Rejection) for Power Ascension,'/5/88.
- 25. IfShut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units ln Test Status (Prior to Commercial Operation):
INITIALCRITICALITY INITIALELECTRICITY COMMERCIALOPERATION Forecast
~311 88 Achieved 5/23/87
~sos/87 Iu/77)
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UNITSIIUTDOWNS ANDPOWER REDUCllONS REPORT MONT)l February
)988 50-4 10 DOCKETNO.
DATE 3
9 88 COMPLETED gy E. Tomlin son
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Licenscc Event lteport rr
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O CJ Cause 4 Cuncc live Actiun to Prcvcnt Rccurrcnec 88-01 02/01/88 131.4 88-0 ]
LD FLT Operator isolated instrument air causing Condenser/Feedwater Minimum Flow Valves to open.
Reactor scrammed on low (level 3) water level; Strengthened administrative controls for tag outs and valve position verification.
Continuation from January report period.
88-02 02/15/88 123.8 N/A N/A N/A Planned scram for SUT-25-6 as part of ower. Ascension Testing.
Initiated rith HSIV closure.
F: FEueed S: SchcdulcEI ItcasEnl:
A.l:EIEElpnlCIII I ailuEC (LXPIJirr)
I) MainlerEanee Eri Test
(. 1(e fEEelint)
I) ItcgEE)illE)ly ltcst r rcr EEnr I OI)clatElr 1 raining 4 I.iecllsc I'.xJlnlEIJllon I"AdIIIIEIIstIJrrvc (a OllcrallEJIIJI LIEEEI (IEXIEIJIEI)
II'Olllcl(I:xplJIEE)
Method:
I -Manual 2.Manua) Scram.
3-Autuntatrc Seran>.
4-Otlrer (Explain)
Exhibit G - Instructions for Preparation of Data Entry Sheets for L)eerrsec Event Report (LER) File (NUREG-0161)
Exhibit I
~ Sarw'ource
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ER ACE DAILYL.iITPO'4 ER LEVEL DOCKET IO.
NMP2 COMPLETED GY E. Tomlinson EPllONE <" )'4 February 1988 MONTH DAY AVERAGE DAlLYPOtvER LEVEL IMtve.Net) 0 DAY
- VERACE DAlLYPOtvER LEVEL IMtVe.'Vet) 0 0
0 0
57 343 639 IS 10 0
0 0
823 1038 10 13 IS l6 496 735 659 678 881 8tIO 559 0
15
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1067 1054 1058 1019 LNSTRUCTIONS Oa this furntat, list t/te uveagc daily unit p<nvur level iii lltVc Yet t'ur eueh day in ilia repiutniy. ni.uirli. ('.sunpute Iu the nearest v;hule ntemivat t.
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NIAGARA HOHAQK POWER CORPORATION NINE HILE POINT NUCLEAR STATION UNIT f2 NARRATIVE OF OPERATING EXPERIENCE Nine Mile Point Unit 2 entered the final Power Ascension Testing Condition (TC-6) during the month of February 1988.
Host of TC-6 testing was completed.
Tests included Recirc System and Feedwater System testing, LPRM/APRM calibration and MSIV full isolation.
During the MSIV isolation 2
SRVs were challenged automatically five (5) times.
These 2
SRVs plus three (3) others were opened manually later in the event to control pressure.
RCIC System was also initiated manually to aid in pressure control.
The completion of TC-6 and warranty run and the declaration of Commercial Operation are expected in March.
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MODIFICATIONS ACCEPTED BY OPERATIONS FEBRUARY 1988 NOD NUMBER s
s NWR NUNBER SYSTEN DESCRIPTION l
l l
l s
s l
I l
l l
l I
l l
l
- . l PN2Y87NX089 PN2Y87NX224 PN2Y87NX238 Phl2Y87NX245 PI42Y87NX250 l
l M20339 M20410 M20347 M20357 N20359 M20366 N20367 N20368 M20371 N20372 N20386 N20390 N20396 N20397 N20442 M20443 N20391 N20413 N20444 M20418 N20419 M20420 N20421 N20422 N20423 N20424 M20425 N20426 M20427 FPM l WS FWS HVR lADD FIRE DETECTORS ZONE 248NZ s
s l DRNS LIQUID MONITOR 2LWS-CAB206 PURGE DISCH REROUTE s
s
~ ACTUATOR CHANGES FOR 2LWS LV10A~ B~ C s
s s
s s
s s
s s ADDITION OF INSTRUMENT TEST HOLES IN HVAC DUCTWORK l
l FILTERING ROSENOUNT TRIP UNITS s
s s
s l
s s
l
MODIFICATIONS ACCEPTED BY OPERATIONS FEBRUARY 1988 l
l l
MOD NUMBER l
MWR NUMBER l
SYSTEM Il-DESCRIPTION II l
l Phl2Y87MX257 l
l PN2Y88MX002 l
PN2Y88MX003 M20428 M20429 M20430 M20431 M20432 M20433 M20434 M20435 M20445 M20446 M20412 M20450 M20456 I
I I
l DFM l DRAINABE REVISIONS ELECTRICAL TUNNEL lHVAC EQUIPMENT ROOM
& CO2 TANK ROOM A04. 720 l PROVIDE SEALINB BAPS FOR SMOKE AND HOT BASES l
RMS l REROUTE OF RETURN LINE FROM 2RMS-CAB180 II II g, P
P 1
1
07: 37: 40 03-04-88 MR Number EPN Number CLASS I WORK INSTRUMENT 5 CONTROL FEB 88 PACE:
1 Feilure desc Corrective Action W110964 CSL-AOV101 INJECTION TESTABLE CHECK VALVE 2CSL-AOV101 PER N2-ISP-CNT-R-002 TYPE C TEST 2CSL-AOV101 LEAKAQE HAS INCREASED A FACTOR OF 10 PREVIOUS
- 1. 172 SEFH 860609 TO 10. 624 SCFH 870924 TROUBLESHOOT ONLY NONEt PROBLEM WAS NOT AOV 101 BUT LEAK OF BOUNDARY VALVE 2CSL+HCV117t DESPITE REPEATED FLUSHE8 AND CYCLESt HCV WOULD NOT SEAT TIQHTLY SINCE VESSEL MATER LEVEL WAS ABOVE CSL LINEt NO REPAIR WAS DONEt BUT HIQH LEAKAQE WAS ACCEPTED W110976 HVC-eACU2A 2HVCeACU2*
VIBRATION HIQH AFTER INSTALLATION OF NOTOR FOUNDATION STIFFNERS ON WR NO 113451 TAKE VIBRATION READINQS TO CONFIRH PROPER OPERATION CB EL 288 THIS MR REPLACES MR 113439 TO TRANSFER WORK FROH MCQ TO IhC IRD VIBRATION READINQS TAKEN AS PER
" BOB HAWHINNEY W122025 BYS-A19 ANALOQ ISOLATORS APPARENTLY NOT MORKINQ ERF CP BYSVA100 101 AND 102 ARE READINQ HIQHER THAN NORNAL (OFF SCALE).
CHECK OUT CIRCUIT'ND ISOLATORS (ON ATTACHED SHEET)
TAKE VOLTAQE READINQS THIS WILL CHECK IF BYSVA102 IS SCALED WRONQ.
REPLACED OPTICAL ISOLATOR CARDSt ISOLATOR CARDS ARE TO BE REMOVED PER PR 7498 AND HRF I20362.HAS BEEN ISSUED TO DO THIS WORK W122467 NSS-TE48D 49 2MSS-TE48D (E31W029D)
D REMOVED LUQS FROM FIELD WIRES AT TB1 NO 10 AND 16 AND LANDED WIRESt PERFORMED.N2 ISP LDS N009 ATT. 4t REMOVED LUQS AT TB1.'1 AND 17 AND LANDED WIRESt PERFORMED N2-ISP-LDS-8009 ATT 4 W122917 WCS-FT67XhY 2NSS-TE49D (E31-N030D)
HSL TUNNEL DIFF TEMP E31-N61SD THE LUQS ON THE THERNOCOUPLE FIELD WIRES FOR TE48D AND TE49D NEED TO BE REMOVED AND THE WIRES LANDED IN PNL709A TH 107 TB1 10 AND 11 AND 16 AND 17 WHILE PERFORNINQ N2-ISPWDSW009 REACTOR WATER CLEANUP FLOW RENOVED SNUBBERS ON WCS%67Xt'CS67Y ALREADY REMOVED BY CR I DURINQ HODt
07: 37: 40 03-04-88 CLASS I WORK INSTRUMENT h CONTROL FEB 88 PACE:
2 WR Number EPN Number Failure desc Corrective Action W124156 W124157
" CSH-.P1 CSL-P 1 CONTINUE TO MONITOR TRANSMITTER OUTPUT ONCE PER SHIFT AND REMOVE TEMPORARY MODIFICATION AFTER FINAL ENQINEERINC DISPOSITION HIGH PRESSURE CORE SPRAY PUMP PLACE IRD VIBRATION CHECKPOINTS IN VIBRATION DATA LOCATIONS AND SECURE WITH LOCTITE RC/620 OR APPROVED ADHESIVE CONTACT ISI PRIOR Td WORK FOR SPECIFIC VIBRATION LOCATIONS LOW PRESSUE CORE SPRAY PUMP PLACE IRD VIBRATION CHECKPOINTS IN VIBRATION DATA LOCATIONS AND SECURE WITH LOCTITE RC/620 OR APPROVED ADHESIVE CONTACT ISI PRIOR TO WORK FOR SPECIFIC VIBRATION LOCATIONS REPLACED WITH SOLID S/S LINES EPOXIED IRD STICKERS IN APPROPRIATE SPOTS PER CENE. 28 EPOXIED IRD STICKERS IN APPROPRIATE SPOTS PER CENE. 28 W124159 HVK-P1A CHILLED WATER PUMP 1A PLACE IRD VIBRATION CHECKPOINTS IN VIBRATION DATA LOCATIONS AND SECURE WITH LOCTITE RC/620 OR APPROVED ADHESIVE CONTACT ISI PRIOR TO WORK FOR SPECIFIC VIBRATION LOCATIONS EPOXIED IRD STICKERS IN APPROPRIATE SPOTS PER CENE. 28 W124284 W125252 W125253 W125254 HVK-P1B HVC-RR 18D CMS-RRYIOA HVC-RR18A CHILLED WATER PUMP 1B PLACE IRD VIBRATION CHECKPOINTS IN VIBRATION DATA LOCATIONS AND SECURE WITH LOCTITE RC/620 OR APPROVED ADHESIVE CONTACT ISI PRIOR TO WORK FOR SPECIFIC VIBRATION LOCATIONS CHART RECORDER NO RR18D OUT OF CAL CHART RECORDER FOR DRMS RIC ON 2CEC-PNL880A (CONTROL ROOM EL 306)
CHART RECORDER NO RRY10A OUT OF CALIBRATION CHART RECORDER FOR DRMS R1C ON 2CEC-PNL880A
<CONTROL ROOM EL 306)
CHART RECORDER NO RR18A OUT OF CAL EPOXIED IRD STICKERS IN APPROPRIATE SPOTS PER CENE. 28 CALIBRATED RECORDER CALIBRATED RECORDER RECALIBRATE CHART RECORDER
07: 37: 40 03-04-88 CLASS I WORK INSTRUMENT 5 CONTROL FEB 88 PACE:
3 WR Number EPN Number Failure desc Corrective Action W125255 SWP-RR146A CHART RECORDER FOR DRMS R1C ON 2CEC-PNLSSOA (CONTROL ROOM EL 306) 2HVC-RR18A CHART RECORDER NO RR 146A'UT OF, CALIBRATION CHART RECORDER FOR DRMS RIC ON 2CEC-PNLSSOB EL 306 CONTROL ROOM RECALIBRATED CHART RECORDER W125259 W125260 W125261 W125266 W125267 W128341 W128348 HVC-RR18B CMS-RRX10B SWP-RR146B HVR-RRX14A HVC-RR18C ICS-2ICS+PT1 B
ISC-2ISCeP15 1668A CHART RECORDER NO RR18B OUT OF CAL CHART RECORDER FOR DRMS Ric ON 2CEC-PNLSSOC (EL 306 CONTROL ROON) 2HVC-RR18B CHART RECORDER NO RRXIOB OUT OF CAL CHART RECORDER FOR DRMS'Ric ON 2CEC-PNL880C (EL 306 CONTROL ROON)
CHART RECORDER NO RR 146B OUT OF CALIBRATION CHART RECORDER FOR DBMS RIC ON 2CEC-PNL880D EL 306 CONTROL ROOM CHART RECORDER NO RRX14A OUT OF CAL CHART RECORDER FOR DRMS RIC ON 2CEC-PNL880A (CONTROL ROON)
CHART RECORDER NO RR18C OUT OF CAL CHART RECORDER FOR DRMS RIC ON 2CEC-PNL880A (CONTROL ROOM)
RCIC PRESSURE XMTR REGAL LOOP FOR 2ICS-PT1B RECAL REQD DUE TO TEST EQUIP BEINQ LOST SAFETY RELIEF VALVE ACTUATION TRIP UNIT INVESTIGATE CAUSE OF RAPID SAFETY RELIEF VALVE RECLOSURE ON PSV128 AND PSV133 DURINQ PERFORMANCE OF 1951V CLOSURE SCRAM CHECK RELIEF VALVE TRIP UNIT RESET VALVES TROUBLESHOOT ONLY CALIBRATED RECORDER CALIBRATED RECORDER CALIBRATED CHART RECORDER t
i RECALIBRATE CHART RECORDER PERFORMED CALIBRATION OF RECORDER CHECKED CAL LOOKS OK SEE CAL SHEETS RECALIBRATED TRIP UNITS RESET TRIP POINT TO CORRECT VALVESI 2ISC+PISihhSA AND 1668E
07:37: 40 03-04-88 CLASS I WORK INSTRUMENT 5 CONTROL FEB 88 PAGE:
4 WR Number EPN Number Failure desc Corrective Action W128410 W128420 W128431 W130154 W130155 ICS-PDIS167 168 RCS-C518-ARS 3
RCS-2RCSeFT8 3A HVC-2HVCeFS-23B CES-2CES%99-8CZIHAA01 RHR RCIC STEAM FLOW ISOLATION TRIP UNIT 2ICS%PDIS 167 168 N2-SUT-71-1 WAS PERFORMED TO OBTAIN DATA TO EVALUATE FINAL SETPOINTS FOR 2ICS%PDIS 167 168 FDDR KQ1-6022-REV 1
WAS ISSUED IN RESPONSE TO PR7403 TO CHANGE TECH SPEC NOMINAL TRIP SETPOINT TO 37. 4 INCHES H20.
CHANGE GUIDE VALUES IN N2-ISP-ICS-M001 AND RECALIBRATE RATED DRIVE FLOW AT 70-75 PERCENT POWER IN TC3 WAS DETERMINED TO BE 43600 QPM AT ALL 4 APRM FLOW UNITS ADJUST R4 FOR AN INDICATION OF 703V PLUS OR MINUS 10MV AS READ BETWEEN TP4 AND TP1 DURING SUMMER GAIN ADJUSTMENT (N2-ISP-RCS-Qioi)
RECIRCULATION SYSTEM DRIVE FLOW TRANSMITTERS 2RCSeFT83A/B ADJUST TRANSMITTER RESPONSE TIME AND PERFORM PROCEDURE TP 87-54 CONTROL ROOM ACUIB DISCHARGE AIR FLOW SWITCH WHILE PERFORMINQ 18 MONTH RECAL ON LCR NO.
1L2HVC-066 UNDER N2-ICP-QEN-8001 FOUND CIRCUIT CARD FAULTY REPLACE AND CALIBRATE AS NECESSARY OUTPUT OPTICAL ISOLATOR 99-8CZ1HAA01 OPEN CIRCUIT OUTPUT ISOLATOR 99-CZIHAA01 IN PNL 837 ZT Z32 HAS CHAhWEL L IS OPEN REPLACE OUTPUT CARD PART NO.
93-05-698 REF WR 130075 CHANCE COMPLETED BY TCN TO N2-ISP-ICS-M001 AND REPERFORMANCE OF SAID PROCEDURE RAISED THE VOLTAGE BY USING N2-ISP-RCS-Q101 PERFORM TP 87-54 ON 2RCS%FT83A AND 83Bi RESPONSE TIME FOR BOTH TRANSMITTERS HAVE BEEN SET TO 420 MSEC AT A 35 IN.
H20/SEC AND 45 IN.
H20/DRV RAMP RATEiMADE ADJUSTMENT TO DAMPINQ POTENTIOMETER REPLACED AND CALIBRATED NEW FLOW SWITCH 2HVCeFS23B REPLACED OUTPUT ISOLATOR CARD W130517 ISCWDT14B FEEDWATER LEVEL TRANSMITTER B NOISY SIGNAL THE B LEVEL TRANSMITTER IS MUCH NOISER THAN A OR C
VENT TRANSMITTER AND ALL OTHER TRANSMITTERS WITH COMMON REF OR VARIABLE LEGS VENTED TRANSMITTER ISC+PT115u ISC+PT2Ce ISC+PT4Bt ISC%LT2Bn ISC+PI3Bn TERMINATED THIS WR DUE TO STARTUP
07: 37: 40 03-04-88 CLASS I WORK INSTRUMENT 5 CONTROL FEB 88 PAGE:
5 WR Number EPN Number Failure desc Corrective Action VENT ILT CONNECTIONS TROUBLESHOOT FOR OTHER POSSIBLE CAUSES CONTACT DAN HOLLAND BEFORE BEGINNING WORK W130528 ISC-2ISC+PDT FEEDWATER CONTROL NARROW RANGE LEVEL XMITTERS 14A 2ISC+PDT14A SEAL 03 AS FOUND
RESPONSE
APPROX 80 MSECi AS LEFT
RESPONSE
APPROX 470 MSECe SEAL 02i 2ISC+PDT14B SEAL 02 AS FOUND
RESPONSE
APPROX 110 MSECi AS LEFT
RESPONSE
APPROX 470 MSECs SEAL 02 W130798 RMC-RODS4-39 INCREASE THE DAMPENING OF 2ISC+PDT14A AND B (C33-N004A AND B)
TO
. 4 SEC USINQ THE SETTINGS (13 PERCENT OF SPAN)
OR IF TIME ALLOWS SET THE TIME CONSTANT TO
. 5 SEC USINQ TIME RESPONSE TESTING ROD 54-39 WHEN INSERTING ROD 54-39 FROM POSITION 06 TO 04 THE ROD LOST POSITIVE INDICATION AT POSITION 04 AS DETERMINED BY THE 4 ROD DISPLAY PLEASE TROUBLESHOOT CHECKED IN CRi ALL OK PROBABLY BAD REED SWITCH W131103 WCS 2WCS FILTER 4C C VESSEL DOES NOT DEPRESSURIZE PROPERLY IN STEP
- 4. 3 VENT VALVE 6ic ALSO THE START OF PRECOAT CYCLE INTERRUPTS 30 SECONDS INTO CYCLE QIVINQ THE SYSTEM A BACKWASH REQUIRED INTERLOCK LATCH WITH NO APPARENT REASON 328 RX SOUTH TEMPORARY MEASURES'EMPORARY INCREASED PRECOAT. FILL TIMER Ob015 TO 6 MIN TEMP MOD 88021 TEMP MOD CLEARED 2-4-88 TIMERS RETURNED TO 5 MIN W131232 W131239 NMS-2NMSe IRM F
MSS-2MSS+RE4 hC IRM F DRAWER WHILE PERFORMINQ N2-ISP-NMS-W-009 STEP 7. 3. 2 FOUND INDICATOR TO BE READING LOW-OUT OF SPEC TROUBLESHOOT MAIN STEAM LINE RAD MONITOR C WHILE PERFORMINQ N2-ISP-MSS-M001 FOUND UPSCALE 1
AND 2 AND DOWNSCALE TO BE LOW TROUBLESHOOT ONLY REPLACED PRE-REGULATOR VR22 IN IRM F
ADSUSTED TRIP SETPOINT ADJUSTMENTS R95i R94.
R93 PER SURVEILLANCE N2-ISP-MSS-R 104 W134338 MSS-2MSSeRE-MAIN STEAM LINE RADIATION MONITORS SETPOINT CHANCE RESET TRIP POINTS
07:37: 40 03-04-88 CLASS I WORK INSTRUMENT h CONTROL FEB 88 PAGE:
6 WR Number EPN Number Failure desc Corrective Action W137222 W137224 46A RRS-2RRS-BCO 7
GTS-2QTSeFRi OB RESET MAIN STEAM LINE RADIATION MONITOR TRIP SETPOINTS TO 1375 MR/HR BASED ON A NEW PROJECTED FULL POWER BACKGROUND LEVEL OF 500MR/HR SEE RADIOLOGICAL SUPPORT GROUP CALCULATION NO.
88-11 COMPUTER POINT RRS BC07 RRCS TROUBLE DIV I COMPUTER PT IS IN ALARM WITHOUT BRINQINQ IN ANN NO.
603445 OR SHOWING A PROBLEM AT P001 OR P002 PNL TROUBLESHOOT ONLY 2QTS%FRiOB FLOW RECORDER ON 2CEC-PNL871 2QTS-FR10B(RED PEN)
ON 2CEC-PNL871 IS FAILED UPSCALE DOES NOT VARY WITH FLOW TROUBLESHOOT ONLY REPLACED BOARD AZA3N15 IN ANNUNCIATOR SYSTEM RESET ELECTRONIC RELAYS 2GTS+PVSB NOW WORKS FINE> RECORDER CONTINUES TO WORK FINE W137225 QTS-2QTS%PNL LOW AIRFLOW CREEN LIGHT AT 2GTSePNL30B 30B TROUBLESHOOT 2QTS+CHIB HEATER LOW AIR FLOW LIGHT AT 2QTS+PNL30B DIV II STBY QAS BLDG 261 DOES NOT EXTINGUISH WHEN TRAIN B IS RUNNINQ W137227 MSS-2MSSwE31 MAIN STM LINE TUNNEL DELTA T TMP UNIT
-N615D MSL DELTA T TMP UNIT ON 2CEC+P611 INDICATES DOWNSCALE INVESTIGATE AND CORRECT INPUT TO NSSS ISOLATION LOGIC D4 W137270 WCS-2WCS+F16 WCS SYSTEM FLOW INDICATION (TRANSMITTER) 7X FT67X INDICATES 900 GPM WHEN ACTUAL FLOW IS 700 QPM W137276 QTS-2QTSePV5 SBGT FLOW CONTROL VALVE B
VALVE WILL NOT OPERATE RECALIBRATED FLOW SWITCH 2QTS+FS25i LOOP SEEMS TO FUNCTION CORRECTLY NOW REPLACED TRANSMITTER/SWITCH 2MSS+TS-1615D AND PERFORMED PROCEDURE N2-ISP-LDS-M009 900 GPM IS EXACTLY WHAT IT SHOULD READ.
CALIBRATION IS CORRECT PER, ALBERT HWU.
QE INSTALLED NEW MOTORS RUSTY GIBSON CRIMPED LEADS TORGUED MOTOR STUDS AND COVER
WR Number EPN Number 07: 37: 40 03-04-88 CLASS I WORK - INSTRUMENT h CONTROL FEB 88 PAGE:
7 Failure desc
~
Corrective Action W137353 W137358 W137380 W137389 W137431 W138121 W138123 EGA-PS9B NMS-2NMS+APR ME NMS-2NMSeIRM
-G NMS-2NMS>IRM
-Q HVR-2HVR+FS3 6B NMP-2NMP+APR MB NMS-2NMS+C51
-K605B 2EGA-PS9B DIV II AIR COMPRESSOR START SWITCH 2EQA-PS9B NOT ALLOWINQ AIR COMPRESSOR TO START PRIOR TO RECEIVINQ LOW AIR PRESSURE AT 233 PSIQ DQ BLDG EL 261 DIV II APRM E K18 RELAY WHILE PERFORMINQ N2-ISP-NMS-WR007 K18 RELAY WAS FOUND TO BE DEFECTIVE REPLACE K18 RELAY IRM-G IRM-G WHEN UNBYPASSED BRINGS IN THE FOLLOWINQ ALARMS-ANN 603201 UPSCALE-INOP RED LIGHT ON P603 AND DOWNSCALE REMAINS IN NO ONE HALF SCRAM OR RPS TRIP~OCCURS AND NO DRAWER INOP OR UPSCALE TRIP LIGHT OCCURS TROUBLESHOOT INTERMEDIATE RANGE MONITOR -G-IRM-G READS 20 WHILE ALL OTHERS READ 0 IRM-G READS 20 WITH MODE SWITCH IN ZERO 2 POSITION PLEASE TROUBLESHOOT FLOW SWITCH AIR EXHAUST ABOVE REFUEL FLOOR CALIBRATION APPEARS TO HAVE DRIFTED CHECK CAL APRM -B-LOCAL INDICATION READS 61 PERCENT WHILE PNL603 CHART INDICATES 70 PERCENT RX PWR 56 PERCENT APRM HI/TING UPSCALE ALARM EARLY TROUBLESHOOT AVG PWR RANGE MONITOR B WHILE PERFORMING N2-ISP-NMS-9107 FOUND METER ZERO OUT-OF-SPEC UNABLE TO ADJUST 'USINQ DC AMP TROUBLESHOOT ONLY FOUND PS 19B TO BE HIGH ALARM COMING IN BEFORE PS9B ACTIVATING REPLACED RELAY K18 PER SSS REPLACED DUAL TRIP UNIT Z17 194X382G3 REPLACED PREREQULATOR CARD VR27 8/N TGAL7-30,
FS 36B FOUND TO BE OUT OF SPECe NOMINAL MV IS 487MV THEREFORE TRIP CANNOT BE SET AT 460MV MIGHT NEED NEW FLOW PROFILEi PERFORMED GEN-003 NEW SETPOINT 590MV.
SATISFACTORY CAL PERFORMED N2-ISP-NMS-Q107 ADJ ZERO PER N2-ISP-NMS-Q107
07: 37: 40 03-04-88
'CLASS I WORK INSTRUMENT h CONTROL FEB 88 PACE:
8 WR Number EPN Nueber Failure desc Corrective Action W138127 WCS-2WCSeFT6 9X REACTOR WATER CLEANUP BLOWDOWN FLOW TRANSMITTER P
DIVISION 1A FOR RWCU DELTA FLOW READS LOWER THAN IT SHOULD AND BARELY WITHIN SPECIFICATION PER SHIFT CHECKS RECALIBRATE WCS+FT 69X SEE ATTACHED FOR ADDITIONAL DATA VENTED WCS-FT69X AND WCSMT68X AT THE TRANSMITTER AND DRAINS.
POTH TRANSMITTERS HAD A 1. 00 VDC OUTPUT WHEN EQUALIZED. SEE NO NEED FOR CAL.
DELTA FLOW READINQ APPROX 75 QPM FOR BOTH X AND Y W138135 W138142 W138196 IAS-2IAS%V16 15 RCS-2RCSeB35
-K607A ICS-2ICS%PDI 8168 MSIV 7C INST AIR SUPPLY FABRICATE AND INSTALL PRESSURE INDICATINQ AND VENT RIQ DOWNSTREAM OF 2IAS%V1615(C-)
PRESSURE QAUQE SHOULD BE AT LEAST 0-150 PSIQ REMOVE TEST RIQ WHEN TROUBJ ESHOOTINQ IS COMPLETE FLOW UNIT A B35-K607A WHILE PERFORMINQ N2-ISP-RCS-M8001 FUSE F8 ON SUMMER CARD ZQ WAS FOUND TO BE BLOWN REPLACE FUSE OR SUMMER CARD a
TROUBLESHOOT RHR/RCIC FLOW HIQH SLAVE TRIP UNIT TRIP UNIT E31-691B PICKS UP RELAY ESi-K85 AND WILL NOT RESET RELAY WHEN CONDITIONS ARE NORMAL K85 RESETS WHEN E31-691B IS PULLED TROUBLESHOOT REMOVED TEMP MOD 88-067 REPLACE SUMMER CARD 136B3088AAQ003 MTUi STU AND TDPU RELAY ALL TESTED SAT 49 records listed.
07: 36: 57 03W4-88 CLASS I WORK - HECHANICAL HAINTENANCE FEB 88 PACE:
1 MR Number EPN Number Failure desc Corrective Action W122279 W122359 W122360 M122369 RCS-HOV18A RECIRC ISOL VALVE 18A THE VALVE HAD A SHALL STEAN LEAK DURINO OPERATION TAKE UP ON PACKINO AND OR IF REGD ADD 1
OR 2 RINGS OF PACKINO CSLWCV117 2CSL-HCV117 RETORQUE PRESSURE SEAL BONNET PER ANSMER TO PR 7242 TORQUE IN HANUAL 430004354 SEE ATTACHED SHEET CSH-HCV120 2CSH-HCV120 RETORQUE PRESSURE SEAL BONNET PER ANSWER TO PR 7242 TORQUE IN HANUAL 430004354 SEE ATTACHED FOR TORQUE RHS-HCV53A 2RHS-HCV53A B C
RETORQUE PRESSURE SEAL BONNET PER ANSWER TO PR 7242 TORQUE IN HANUAL 430004354 SEE ATTACHED FOR TORQUE TOOK UP ON PACKINO EVENLY'TROKED VALVE.WORKED SHOOTHLY RETORQUE TO 600 FT LBS ALL BONNET BOLTINO. NO NUTS ROVED RETORQUE TO 600 FT LBS ALL BONNET BOLTINOs NO NUTS HOVED RETORQUED ALL BONNET BOLTINO TO 600 FT LBSi NO NUTS HOVED W122370 W122371 RHS-HCV54A RHS-HCV131 2RHS-HCV54A B C
RETORQUE PRESSURE SEAL BONNET PER ANSWER TO PR 7242 TORQUE'N MANUAL-430004354 SEE ATTACHED FOR TORQUE 2RHS-HCV131 RETORQUE PRESSURE SEAL BONNET PER ANSWER TO PR 7242 TORQUE IN MANUAL-430004354 TORQUE PER ATTACHED SHEET RETORQUED BONNET BOLTINO TO 600 FT LBSt NO HOVEHENT WAS DETECTEDs VALVE HCV54C DOES NOT EXIST RETORQUED BONNET BOLTINQ TO 600 FT LBS>BOLT8 DID NOT HOVE W122372 W125365 RHS-V143 2RHS-V143 RETORQUE PRESSURE SEAL BONNET PER ANSWER TO PR 7242 TORQUE IN HANUAL-430004354 TORQUE TO ATTACHED SHEET CSH-AOV108 HPCS INJECTION LINE TESTABLE CHECK VALVE REPACK VALVE (2CSH-AOVI08)
. ~
CHECK PREBSURE SEAL BONNET BOLTS PER TORQUE SPEC8 REPLACED PACKINO AND ONE SEAL 0ASKET
07:36: 57 03W4-88 WR Number EPN Number Failure desc CLASS I WORK MECHANICAL MAINTENANCE FEB 88 Corrective Action PACE:
2 M127706 HVC-ACU2A VLVE IS ON EL 306 IN THE DRYWELL OR ADD PACKINQ 2HVC-ACU2A INPROPER PARTS E AND DCR NO C47625A REQUIRES JACKINQ ASSEMBLIES INSTALLED ON ROTOR. AMOUNTS THIS MR REPLACES MR NO 110646 INSTALLED JACKINQ ASSEMBLIES ON FAN ROTOR HOUNTS W127707 M127718 M128151 HVC-ACU1B 2HVC-ACU1B IHPROPER PARTS E AND DCR NO C47625A REQUIRES ANQLE IRON STIFFENERS AND JACKINQ ASSEHBL'IES ON ROTOR MOUNTS THIS MR REPLACES WR NO 110646 WCS-V47 WCS-V47 VALVE LEAKINQ 50 DROPS PER HINUTE-RETORGUE BONNET UNDER PRESSURE TORGUE TO THE ATTACHED TABLE 871102 STILL LEAKS AFTER TORGUINQ DISASSEHBLE INSPECT AND REPLACE PRESSURE SEAL HVC-UC105 ELECT TUNNEL UNIT COOLER UNIT COOLER SHOWS HIQH FILTER DP-CHANQE INSTALLED JACKINQ ASSEMBLIES AND.
NEW SX3Xi/2 ANQLE HOTOR MOUNTS SEE WR127706 FOR HcDCR'8 TORQUE ON FACE PLATE(COVER) ~ 8TILL LEAKS PER Q PROSSER 871102.
CHANQED FILTERS W128702 RCS-2RCSeNOV 2RCSeMOVIOB 10B TAKE UP ON PACKINQ AT 900 LBS IF REGD M128/69 RCS-2RCS+HOV RCS NOViSA 18A PULL PACKINQ TO INSPECT LOWER PACKINQ AREA W128800 RCS-2RCSeHOV RCS+NOV10A 10A TAKE UP ON THE PACKINQ QLAND,PACKINQ QLAND IS NOW BOTTOHED OUT. ABOUT TWO NORE RINQS WOULD BE JUST RIQHT REPLACED PACKINQ TAKE UP ON THE PACKINQ CLANDiPACKINQ QLAND IS NOM BOTOHED OUTe ABOUT TWO NORE RINQS WOULD BE JUST RIQHT W129457 RHS-2RHS+PSS P807A2 TAKE UP ON PACKINQ AT 900 LBS IF REGD SNUBBERS (BZ-71ADC)
OUT OF TOL SNUBBER 2RHS-PSSP 807AZ (A)
LINE NO 2RHS-018-24-2 NORTH SIDE OF PIPE AND PIPE ALIQNED SNUBBERS
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07: 36: 57 03-04-88 CLASS I WORK MECHANICAL MAINTENANCE FEB 88 PACE:
3 WR Number EPN Number Failure'e desc Corrective Action W130786 W130787 W130788 W13P789 W131167 W131185 W134302 RCS-MOV10A RCS-MOV10B RCS-MOV18A RCSWOV18B ZZZ-PCB-DRA5 ZZZ QTS-2QTSeFLT 1A CLAMP IS 7 DECREES OUT OF ALIQNMENT AND PADDLES ARE NOT AT 90 DEQREES TO PERMIT ROTATION ALSO 2RHS-PSSP807A2(B)
SOUTH SIDE AND PIPE CLAMP'S 8 DECREES OUT OF ALIQNMENT CORRECT ALIQNMENT AND PADDLE POSITION RHS B PUMP RM S AUX BAY EL 175 RECIRC -A-SUCTION VALVE REPAIR PACKINQ LEAK RECIRC -B-SUCTION VALVE REPAIR PACKINQ LEAK RECIRC -A-DISCHARGE VALVE REPAIR PACKINQ LEAK RECIRC -B-DISCHARGE VALVE PACKINQ LEAK REPAIR PACKINQ LEAK NORTH DRYWELL EQUIPMENT PERSONNEL HATCH INTERLOCKS DISABLE INTERLOCKS DISABLE DRYWELL EQUIPMENT HATCH INTERLOCKS (NORTHSIDE)
TO ALLOW BOTH DOORS TO BE OPENED SIMULTANEOUSLY WHEN DIRECTED BY SSS RESTORE INTERLOCKS TO NORMAL SUPPRESSION CHAMBER'NORTH HATCH OPEN HATCH TO FACILITATE PERFORMANCE OF CONTAINMENT BYPASS.LEAKAQE TEST STANDBY QAS TREATMENT SYS-2QTS-FLT1A PROVIDE LABOR SUPPORT TO ASSIST VENDOR IN TESTINQ ABOVE SYS WORK TO INCLUDE REMOVAL AND REPLACEMENT WITH DOORS AND PANELS ETC FOR COMPLETION OF SYSTEM'SURVEILLANCE TESTINQ THE WORK OF FEB 22-26 1988 INSTALLED 3 SETS OF PACKINQ REPLACED PACKINQ INSTALLED 3 RINQS OF PACKINQ REPACKED V~VE DISABLED DRYWELL PERSONNEL HATCH INTERLOCKS.
CLOSED 5 TORGUED TO SPECS SYSTEM SURVEILLANCE TESTINQ W137321 EQA-2EQA+V14 B
BOLTS ON FLANCES BETWEEN 2EQAeV14B AND 2EQAePCV25B REPLACED NUTS 4 TIQHTENED 2 BOLTS AND ASSOCIATED NUTS ON FLANQE CONNECTIONS BETWEEN 2EQAeV14B AND 2EQAePCV25B HAVE VIBRATED LOOSE AND MUST BE REPAIRED AND RETORGUED REPAIR AS NECESSARY
07: 35: 25 03W4-88 WR Number EPN Number Feilure desc CLASS I WORK - CONSTRUCTION FEB 88 PACF:
1 Corrective Action C127950 HVC-ACU3B REHOTE SHUTDOWN RKN AIR CONDITIONINO UNIT PHYSICAL FAULT ACCESS DOOR TO FAN HAS BROKEN STUD NEAR LOWER RIOHT CORNER OF OPENINO THIS WR REPLACES WR 118575 - ATTACHED COPY-LOC4TED EL 275 IN DIV II SWITCHOEAR ROON C131189 BLDQ-S4175-1 WATER TIOHT DOOR HECHANICAL FAILURE LOWER LEFT SLIDE Bm T FAILS TO RETRACT SAFETY HAZARD CROUND OFF REHAINS OF OLD STUD-REPLACED STUD USINO PROC WPS-STUDS-AWS.RETURNED UNIT TO ORI4 CONDITION LOOSE PARTS. 4EARS ADJUSTED'H 2-I-88>LOOSE SET SCREWS ON OEARS TIOHTENED AND BOLT RETRACTS BUT DOOR STILL HAS HISSINO AND SHE4RED OFF BOLTS IN LOCKINQ HECH C131250 BLDO WATER TICHT DOOR BETWEEN CSL AND RHR A PUHP ROOHS BOTTOH LATCH (OPP HINCE SIDE)
DOES NOT OPERATE-FAILS TO LATCH OR FAILS TO UNLATCH (DEPENDINC ON LATCH POSITION)
REPAIR AS NECESSARY OEARS ADJUSTED SH 2-I-BBiSET SCREWS ON OEARS TIOHTENED AND LATCH OPERATES BUT DOOR STILL HAS HISSINC AND SHEARED OFF BOLTS IN J OCKINO HECHANISH 3 records listed.
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07: 36: 05 03W4-88 CLASS I WORK ELECTRICAL NAINTENANCE FEB 88 PAOE:
1 WR Number EPN Number Failut ~ desc Corrective Action W115941 W122458 RRS-P001-2 MC8-EFV222 RRS DISPLAY PANEL BROKEN MIRE SUPPORT CABLE A130-P3 HAS A BROKEN WIRE SUPPORT AT THE DOOR PLUOS INSTALL NEW CABLE SUPPORT
'2WCSeEFV222 THE LIQHT ON PANEL 602 LABELED 2RCSeEFV222 SHOULD BE LABELED 2MCSeEFV222 WORK DONE BY SUPPORT CROUP.
RRPLhCED PER FDDR KOI-5S27WEV 0 ON HotIAN FACTORS NOD., NOD OPN2YS6NX084 LF100.
NO WORK REQUIRED ON THIS WR.
M127863 BYSWHRO 2A1 2BYS-CHQR 2Ai VOLTtKTER NEED8 TO BE CALIBRATED READINO IS 9 VOLTS LOW W128747 EHS-2EHSeNCC 2EHSeNCC201MUB2A 201-2A 4
2EOTeCHI REPLACE TERN BLOCKS NO.
6 AND 7 ON ttCC IARICT AH5 CUBICLE h/ ~$
BOTH 8TATIONARY AND SEPARABLE PART8 NEED!a REPLACEHENT OBTAIN PARTS PRON SPARE CUB.
NO.
2B REF WR 128748 HETER ACCURACY MAS CHECKED WITH h CALIBRATED FLUKE AND THE READINQS
. WERE WITHIN TlK ACCEPTABLE VALVE OF
+-,
3V AS STATED ON ~PN~~5.
NO ACTION REQUIRED AT THIS Tits.
REPLACE TERNIHAL BLOCKS'EPLACED TERMINAL BLOCKS FRON SPARE BREAKER
~
Ot1 '~eNCC201 CUB 2Bi WR 128748 WRITTEN TO REPLACE TERtIINAL BLOCKS
~
W128785 EHSMCC101 2EHS-HCC101 CUB 7B 8PARE REPLACE NOLDED CASE BREAKER WITH IRN QK (OLD ONE USED FOR 2SMP-NOVIC)
EHS NCC101 CUB 2C REF WR NO 128783 BRSQQiR FRtg EHSttCC1011 CUB 2C WAS PE~tD AND PASSED CONTACT RRSfSff4hE TEST N2-EPEE~582 AND fQCfA4Llm IN BREAKER 7B AND RS ukOCa, W128791 SMP-SSR 3A-6 A
DIV I SERVICE WTR RACK BAR HEATER8 CURRENTS FOR 2SMP-SSR3A AND 6A READINQ 5. SA AND
- 4. 2A RESPECTIVELY PREVIOUS WK READINOS WERE 12. OA AND 11. SA INVESTIOATE AS NECESSARY CQR@A'EADINOS FOR 2SWPXSSR3Ah6A Attf'.1'I; 7 EACH W129335 CECWNL628 DIV I ADS RELAY PANEL
\\P'NSTALLED LUO ON TBHH POINT 49 AND
07: 36: 05 03-04-88 MR Number EPN Number Failure desc CLASS I MORK ELECTRICAL HAINTENANCE FEB 88 Corrective Action PACE:
2 M129336 M130748 M132300 W137201 CEC-PNL631 RPS-C72-P510 ISC ISC INSTALL PERHANANT STAK-ONS ON RICHT SIDE OF TERN STRIP HH NO 9 AND RIGHT SIDE OF TERN STRIP HH NO 14 TO ALLOW EASIER AND SAFER CONPLETION OF N2-OSP-ADS-H002 TO ALLOW HANDS-FREE ATTACHMENT OF A DVH (REF E AND DCR NO C95078)
(REF INT CORR NO NHP2-2420 AND NNP2-320 ATTACHED)
DIV II ADS RELAY PANEL INSTAL'L PERHANENT STAKE-ONS ON LEFT SIDE OF TERN STRIP AA NO 9 AND LEFT SIDE OF TERN STRIP AA NO 14 TO ALLOW EASIER AND SAFER COHPLETION OF N2-OSP-ADS-H002 TO ALLOW HANDS-FREE ATTACHMENT OF A DVH (REF E AND DCR NO 95078)
(REF INT CORR FILE CODES-NNP22420 AND NHP2-320 ATTACHED)
RECIRC PUMP TRIP SYSTEH A FOR TSV2 NEON LAMP SOCKET DETER IORATINO PLEASE REPLACE JET PUNP 10 PASS ISOLATOR VALVE CREEN INDICATOR LICHT DOES NOT LIGHT WHEN VALVE SWITCHED TO CLOSED THERE IS
- OREEN FLICKER WHEN VALVE TURNED TO OPEN HOWEVER RED INDICATOR DOES NOT.LIOHT SWITCH LOCATION ON 237 CB 2ISC-RV33B RV34B RV35B RV36B DRYWELL VACUUN BREAKERS TESTINO CIRCUIT BLOWS FUSE CKT NO 2ISCN04 (ESK 2ISC04)
FUSE Fi INVESTICATE CAUSE AND CORRECT RESULTS IN INABILITYTO TEST VACULN BREAKERS AND LOSS OF POSITION INDICATION ON POINT 014 IN 2CECePNL628.
INSTALLED LUO ON TBAA POINT ()9 AND ON POINT ()14 IN 2CEDePNL 631 REPLACED SOCKET ADJUSTED LINIT SWITCHES.
TAPED SPARE CONDUCTOR ON 21SCeRV3SBi INTERMITTENT OROUND DUE TO LIHIT SMITCH SEGUENCINO W137373 ICS-2ICS%AOV 157 RCIC INJECTION TESTABLE CHECK VALVE INBOARD 2ICSeAOV157 INDICATED CLOSED DURINO RCIC INJECTION TO RPV NONE. LIHIT SWITCHES FUNCTIONINO PROPERLY.
12 records listed.
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07: 36: 57 03W4-88 CLASS I WORK HECHANICAL HAINTENANCE FEB 88 PAOE:
4 WR Number EPN Number Failure desc Corrective Action W138125 W138130 ICS-2ICS+ROi 55 SVV-2SVVeRVV 104 2ICS-R0155 CHECK RO FOR BLOCKACE. MILL NOT ALLOW HIOH ALARM TO CLEAR WHEN RCIC IS IN STANDBY DUE TO INSUFFICIENT PRESSURE ON DRAIN POTMAS TO DRAIN THRU LS DRAIN V277 SAFETY RELIEF VLV TAILPIECE VACUUM BKR 2SVVeRVV104 STUCK OPEN TROUBLESHOOT LOCATED IN PRI.
CONTAINMENT ELEV 246 8.
SIDE OUTBOARD OF THE -A-RECIRC PHP REHOVED ORIFICE FRON LINE AND CLEANED'EPLACED WITH NEW CASKET SPRINQ WAS DIRTY ALL WE DID WAS CLEAN IT 26 records listed.
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