ML18012A426

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Insp Rept 50-400/96-09 on 960901-1012.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML18012A426
Person / Time
Site: Harris 
Issue date: 11/07/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18012A425 List:
References
50-400-96-09, 50-400-96-9, NUDOCS 9611180109
Download: ML18012A426 (30)


See also: IR 05000400/1996009

Text

U. S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket No:

License

No:

50-400

NPF-63

Report

No:

50-400/96-09

Licensee:

Carolina Power

8 Light (CPKL)

Facility:

Shearon Harris Nuclear Power Plant, Unit 1

Location:

5413 Shearon Harris Road

New Hill, NC 27562

Dates:

September

1

- October

12,

1996

Inspectors:

J.

Brady, Senior Resident

Inspector

D. Roberts,

Resident

Inspector

F. Jape,

Senior Project Hanager

(H6.1)

Approved by:

H. Shymlock, Chief, Projects

Branch 4

Division of Reactor

Projects

Enclosure

2

961ii80i09 9bii07

PDR

ADQCK 05000400

8

PDR

EXECUTIVE SUMMARY

Shearon Harris Nuclear

Power Plant, Unit 1

NRC Inspection Report 50-400/96-09

This integrated inspection included aspects of'icensee

operations,

engineering,

maintenance,

and plant support.

The report cover s

a six-week

period of resident inspection;

in addition, it includes the results of an

announced

inspection

by a regional project manager.

~0erations

Operator performance during

a plant trip and reactor startup

was good

(Sections

01.2 and 01.4).

-A violation with two examples of failure to

follow procedures

was identified.

One involved the inadvertent dilution

of the

RWST (Section 04.1),

and the other involved the use of a non-

approved procedure resulting in the inadvertent actuation of an

emergency ventilation fan in the fuel handling building (Section 04.2).

Self assessment

activities by the Nuclear Assessment

Section were good,

including one that resulted in the identification of a missed Technical

Specification surveillance

requirement

(Sections

07.1 and M8.7).

The licensee

reasonably

addressed

corrective actions for problems

identified during the period;

however those identified in Licensee

Event

Report 96-014 did not address

a 1989 inadequate reportability

determination

(Section 08.2).

Haintenance

~

One violation was identified for failure to properly implement the

maintenance

rule,

10 CFR 50.65 (Section H8.8).

The performance of on-

line maintenance

was found to be within the expectations

of NRC guidance

(Section M6.1) .

~

Several

Licensee

Event Reports were generated

involving Technical

Specification surveillance

implementation problems

(Section M8.1).

En ineerin

An unresolved

item was identified for the use of administrative

means

(Technical Specification Interpretation procedures)

in lieu of a license

amendment in relation to the ultimate heat sink (Section E1.2).

This

unresolved

item also involved discrepancies

between the Final Safety

Analysis Report

and parameters

used in defining the plant's design basis

as it relates to the ultimate heat sink.

A previous condition determined to be outside the plant's design basis

was identified in relation to non-seismic piping systems

being connected

to the Refueling Water

Storage

Tank (Section E8.1).

0

Licensee

personnel

appropriately

responded to Hurricane Fran and made

the proper

NRC notifications when emergency

response

capability was

hampered

and equipment

became unavailable

(Section

P2. 1).

One violation was identified f'r failure to close

a protected

area

boundary gate following vehicle access

(Section S1.2).

Re rt Details

Summar

of Plant Status

Unit 1 began this period operating in Hode

1 at 100 percent

power.

On

September

3,

1996, operators

manually tripped the reactor after receiving

indications of a loss of normal service water

(NSW).

The operating

"B" NSW

pump experienced

a sheared

shaft

and repeated

attempts to start the standby

"A" pump were unsuccessful.

The loss of this non-safety related

system

required that the plant be manually tripped per abnormal

operating procedures

in order to protect

numerous

secondary plant components that receive cooling

water from NSW.

Attempts to determine

why the "A" pump tripped on the initial

start attempt were unsuccessful;

however,

a temporary modification was

installed to monitor the pump's logic circuitry during future operation.

The

second

and third attempts apparently failed due to a timed protective

interlock of which operators

were unaware.

The plant remained

shutdown in Hode 3, Hot Standby,

through September

5 when

Hurricane Fran passed

near the site.

Electrical outages

caused

by the

hurricane resulted in the unavailability of approximately

90 percent of the

evacuation

sirens located in the Emergency Planning Zone.

As a result,

restart of the unit required the joint approval of the Federal

Emergency

Hanagement

Agency and the

NRC.

This approval

was granted

on September

9 and

the unit was restarted

at 10:32 p.m. that night.

The generator

was

synchronized to the grid at 3:42 a.m.

on September

10,

1996,

and the reactor

reached

100 percent

power on September

11,

1996.

On October 6,

1996, reactor

power was reduced to approximately 53 percent

following the loss of main feedwater

pump "B".

The pump was secured after

operators

noticed

a leaking outboard seal

and

a considerable

amount of oil and

water in the oil sump.

After repairs to the pump, reactor

power was returned

to 100 percent

on October 10, 1996.

01

Conduct of Operations

01.1

General

Comments

71707

I. 0

rations

Using Inspection Procedure 71707, the inspector s conducted

frequent

reviews of ongoing plant operations.

In general,

the conduct of

operations

was professional

and safety-conscious.

Specific events

and

noteworthy observations

are detailed in the sections

below.

01.2

Onsite

Res onse to Events

a.

Ins ection Sco

e

93702

The inspector

responded to the plant upon notification of a manual reactor trip on the night of September

3,

1996.

The plant was already

stabilized in Hode 3 when the inspector

arrived in the control

room.

The inspector

assessed

operator

performance

and plant response.

The

inspector

remained at the site to verify that the plant was stable

and

that the licensee

was addressing

the cause of the trip.

Observations

an

Findin s

On September

3,

1996 at approximately 11:42 p.m., operators initiated a

manual reactor trip after receiving indications of a total loss of

normal service water

(NSW).

The plant was tripped in accordance

with

abnormal

operating procedures

in order to protect secondary

system

components that receive cooling water from this non-safety related

service water system.

All control rods inserted into the core

and other

systems

responded

as expected,

including the standby train of the

emergency

service water

(ESW) system which started

on low ESW header

ressure.

The auxiliary feedwater

system automatically started

on low-

ow steam generator level,

due to the expected shrink in level following

the trip.

Operators

made the appropriate 4-hour notification to the

NRC

in accordance

with 10 CFR 50.72.

A 30-day Licensee

Event Report

(LER)

was submitted in accordance

with 10 CFR 50.73

and is briefly discussed

in section 08.3 of this report.

Licensee

personnel

determined the root cause of the trip to be

a

mechanical

failure of the "B" NSW pump combined with the failure of the

"A" NSW pump to remain running once manually started.

The "B" NSW

pump's impeller shaft sheared.

The discharge

valve for the "B" NSW pump

would not seal

and resulted in having to drain the service water header

to facilitate maintenance.

The valve was replaced,

the header filled,

and the "A" NSW pump started.

The "B" pump was disassembled

and the

shaft was sent to the corporate metallurgy lab for initial analysis.

A

preliminary report determined that the failure was not likely due to the

original manufacturing process.

At the end of the inspection period,

a

final metallurgical analysis

was in progress to determine the failure

mode.

The cause of the "A" pump's initial tr ip was not determined.

Two

subsequent

attempts to start the "A" pump in immediate succession

had

also failed.

The licensee's

root cause investigation determined that

a

timed protective interlock in the pump's starting logic prevented the

second

and third start attempts.

Control

room operators

were unaware of

this pt otective interlock at the time of the event.

This was determined

to be

a training issue.

The

NSW system operating procedures

were

revised to include this information for future reference.

The licensee

planned to incorporate this item along with the results of a pending

investigation into the initial pump trip into the operator training

progr am.

Troubleshooting

determined that

a common-mode failure did not exist for

the 'other

pump.

The "A" pump was returned to service

on September

7,

1996.

The licensee

completed

a safety analysis

using probabilistic risk

assessment

techniques to determine

compensatory

measur es for returning

the plant to service with only one

NSW pump available.

The reactor

was

restarted

on September

9,

1996 and the main generator

was synchronized

to the grid on September

10,

1996.

c.

Conclusions

The inspector

concluded that operator

performance

was satisfactory

during this event.

The licensee's initial efforts to determine

causes

for the

NSW pump problems were. commendable.

01.3

Post- Tri

Review

a.

Ins ection Sco

e

93702

The inspector

reviewed the licensee's

Post-Trip Review report for the

September

3 manual reactor trip to determine whether the licensee

thoroughly assessed

operator

and plant response

and made

sound

recommendations

for corrective actions where needed.

b.

Observations

and Findin s

In accordance

with procedure

OHH-004, Post-trip/Safeguards

Actuation

Review, Revision 7, plant personnel

completed the formal data collection

and investigation process for the September

3rd reactor trip.

The

inspector

reviewed instrument recorder graphs,

plant computer data,

historical

alarm printouts,

and personnel

statements

related to the

trip.

The reviewed data substantiated

the licensee's

assessment

of the

direct cause of the manual trip (loss of normal service water).

The

inspector independently

concluded that plant systems

responded

as

required.

Reactor coolant system temperature

cooled to 545 degrees

Fahrenheit

(F),

an improvement over the cooldown to approximately

535

degrees

F noted during the April 25,

1996 reactor trip discussed

in NRC

Inspection Report 50-400/96-05.

This improvement

was attributed to

better operator

performance in throttling AFW flow to the steam

generators.

Operators

noted indications of water

hammer in the turbine building

following the trip.

Plant personnel

performed walkdowns of the building

and found some minor damage to small pipe supports

and insulation.

The

inspector also conducted

an independent

walkdown and no additional

damage

was noted.

As noted in Section 01.2 above,

the licensee

conducted investigations

into the causes of the service water system problems.

The initial

engineering

assessment

of the "B" pump's shaft failure was documented in

the OHN-004 package.

An evaluation in accordance

with 10 CFR 50.59 was

performed for returning the plant to service with only the "A" NSW pump

available.

This evaluation concluded that while the

FSAR described the

plant as having two

NSW pumps, the

pumps were neither credited for

mitigating any Chapter

15 accidents

nor referenced

in any plant

Technical Specifications;

therefore,

having one unavailable for

maintenance

was acceptable.

The inspector

reviewed the

FSAR and

concluded that operating the plant with one

NSW pump available under

these

circumstances

was acceptable.

The OHH-004 package

was reviewed by the Plant Nuclear Safety Committee

(PNSC)

on September

7,

1996,

and permission to restart the plant was

granted

on September

9.

Investigations into the root causes for the "B"

NSW pump shaft break

and the "A" NSW pump initial trip were continuing

at the end of the inspection period.

c.

Conclusions

The post-trip review identified the direct cause,

evaluated

the

equipment actuations after the trip, and identified corrective actions

for equipment deficiencies.

01.4

Startu

Observations

a.

Ins ection Sco

e

71707

4

The inspector

observed the reactor

startup

on September

9,

1996 and

observed

generator

synchronization to the grid on September

10,

1996.

The inspector

observed

power ascension

to approximately

30 percent rated

. thermal

power .

b.

Observations

and Findin s

The inspector

observed that operators

were following procedures

and

ensuring that equipment

worked as expected.

Reactor criticality and

generator

synchronization

occur red with no problems.

Previous

problems

with a 6.9 kv unit auxiliary transformer breaker required that offsite

power

be fed through

a startup transformer breaker to the onsite 6.9 kv

distribution system.

Other secondary

equipment worked properly.

c.

Conclusions

The inspector

concluded that operator

performance during the startup

was

good.

04

Operator Knowledge and Performance

04. 1

Inadvertent Refuelin

Water

Stora

e Tank

RWST

Dilution Event

a.

Ins ection Sco

e

71707

90712

The inspectors

reviewed the circumstances

surrounding

an inadvertent

dilution of the

RWST.

In addition to gaining an understanding

of the

event, the inspectors verified that the licensee

per formed

a thorough

root cause determination

and that the proper

NRC reportability

determinations

were made.

b.

Observations

and Findin s

On September

6,

1996,

a licensed operator

was tasked with filling the

Condensate

Storage

Tank

(CST)

~

This direction was provided by the

shift's control

room supervisor.

The plant had been in Hot Standby

since September

3,

1996,

and the

CST was providing suction to the

AFW

system which was supplying the steam generator s.

The CST was already

filling using an alter nate source,

but was not filling at the desired

rate, thereby warranting the supplemental

action.

At approximately 7:30

p.m., the operator,

who had been

assigned. auxiliary operator duties that

shift, erroneously

proceeded to the

RWST pit and commenced fillingthat

tank by opening demineralized

water valve 1DW-5.

Approximately four

hours later, the

RWST HIGH LEVEL alarm was received in the main control

room.

Operators initially evaluated the alarm as being temperature

related.

Just'fter

midnight, following a routine check of RWST level

instruments

by the control

room operators,

they determined that the

RWST

was indeed filling.

The licensed auxiliary operator

was notified and,

realizing the error,

secured the

RWST fillingevolution.

The

RWST level increased

from 95 percent indicated level to 101 percent.

This equated to about 24,000 gallons of unborated

water

which, decreased

the boron concentration of the tank from 2476

ppm to approximately 2351

ppm.

Because this value was below the minimum limit of 2400

ppm

specified in Technical Specification Limiting Condition for Operation

(TS LCO) 3.5.4b, the

RWST was declared

inoperable.

The Boric Acid Tank

(BAT) had been declared

inoperable earlier because it was in a

recirculation lineup during an intentional fill process,

so the licensee

entered

TS

LCO 3.0.3 due to having the boration flow paths required by

TS

LCO 3.1.2.2 inoperable.

After securing the

RWST fill, plant

personnel

initiated actions to restore the boration systems to operable

status.

Normal standby

BAT alignment was restored

and its boration

flowpath declared operable within two hour s.

Operators

declared the

RWST oper able at approximately 2:00 p.m..on September

7, 1996, after

adding boric acid to the tank and mixing its contents with a containment

spray

pump operating in recirculation mode.

A 10 CFR 50.72 evaluation for immediate reportability concluded that the

reduced

RWST boron concentration

during this event would have been

adequate to achieve the required

shutdown margin at all times of core

life.

This evaluation also concluded that the lower concentration

should comply with the TS Bases stipulation of maintaining

a pH value

between 8.5 and 11.0 for the water solution recirculated within

containment after

a design basis accident.

Based

on this information,

the event

was determined not to require immediate

NRC notification'as

a

condition outside of the plant's design basis.

However,

because of the

required entry into TS

LCO 3.0.3..

the licensee

submitted

LER 96-20

(discussed

in report paragraph

08.4) in accordance

with 10 CFR 50.73.

The inspector discussed this event with plant personnel

and determined

that the communication to the operator

was clear in specifying the CST,

not the

RWST.

However, the operator

had developed

a mental picture of

the

RWST pit and was focused

on that tank when he was dispatched

by the

control

room.

The licensee's

investigation considered that

a

contributor could have been the failure to use specific valve numbers in

discussing

the upcoming task.

The inspector

found that filling the

CST

was covered in section 8.0, Infrequent Operations,

of operating

procedure

OP-134,

Condensate

System,

Revision 7.

The inspector noted

that the operator did not have

a copy of the procedure

present.

This error (and the one discussed

below in report section 04.2)

represented

a continuation of the negative

human performance trend

discussed

in Inspection Report*50-400/96-07.

The significance of this

example

was that it caused the plant to be without an operable boration

flow path for several

hour s until system restoration

was accomplished.

Technical Specification 6.8.1.a

and Regulatory Guide 1.33, Revision 2,

Appendix A, Section 3.1 collectively require that written procedures

be

established.

implemented,

and maintained for energizing, filling,

venting,

and draining the auxiliary feedwater

system (for which the CST

is a safety-related

water supply).

Steps for fillingthe

CST [including

options to manipulate either

valve 1CE-23 (Step 2) or valves

1DW-490 and

1DW-486 (Step 3)3 are in subsection 8.3.2 of procedure

OP-134.

The

inadvertent

opening of valve lDW-5 and subsequent

dilution of the

RWST

resulted

from a failure to follow the steps in procedure

OP-134 and is

identified as

a violation of TS 6.8.1.a

(50-400/96-09-01).

Conclusions

The inadvertent

RWST dilution marked

a continuing adverse trend in human

performance

problems.

One violation was identified for failure to

properly implement operating procedures.

Inadvertent Actuation of Fuel Handlin

Buildin

Emer enc

Exhaust

Fan

Ins ection Sco

e

71707

The inspectors

reviewed the circumstances

surrounding

an inadvertent

actuation of a fuel handling building (FHB) emergency

exhaust

fan.

In

addition to gaining an understanding of the incident, the inspectors

verified that the licensee properly addressed

the root cause

and made

appropriate

recommendations

for corrective actions.

Observations

and Findin s

On September

29,

1996, auxiliary operators

were tasked with turning off

"spare" breakers

in various lighting and power panels throughout the

plant while conducting routine tours.

The operators

had been provided

an unapproved

and unverified list of breakers that was dated October

7,

1994 with the title "Spare Breakers

Found in ON Position".

While

performing the task,

one of the operators

turned off the breaker

for

circuit ¹17 in a power panel

labeled

PP 1-4833-SB.

This breaker

was on

the unverified list, but was part of the energized circuit powering

safety-related

radiation monitor RN-1FR-3564 B-SB.

With the operator's

action, the radiation monitor was de-ener gized which automatically

started

FHB emergency

exhaust

system fan, E-13B.

The fan started

as

designed

and caused

several

alarms in the main control

room, which was

the operators'irst

indication 'that

an error had occurred.

Upon

discovery,

the operators

stopped the evolution, generated

Condition

7

Report 96-03057,

and initiated actions to restore the radiation monitor

and secure the exhaust fan.

The inspector learned through reviewing the

CR and discussions

with licensee

personnel

that the operator

mistakenly

thought that all of the breakers identified on the list were spare

breakers

and that all were to be de-energized.

Because this error primarily involved performing changes to previously

completed

system lineups, the inspector

reviewed the licensee's

formal

process

as described in operations

management

manual

procedure

OHH-001,

Operations

- Conduct of Operations,

Revision 16.

Section 5.2.2 of this

procedure,

Electrical

and Valve Lineup Checklist, described the process

for documenting off-normal component positions, or positions not

specified

on component checklists in the various system operating

procedures.

Step 5.2.2.3.c directed personnel

to use Attachment

2 (of

OHH-001) to document the position of components for situations involving

small

changes to completed lineups;

The inspector

researched

the most

recently completed electrical lineup checklist for the radiation

monitoring system

(Attachment

1 to operating procedure

OP-118,

Radiation

Honitoring System,

Revision 4).

This review identified that the breaker

for circuit gl7 in panel

PP-1-4B33-SB

was last checked

and verified to

be

ON.

The inspector

concluded that had plant personnel

implemented the

instruction in OHH-001 step 5.2.2.3.c,

the completed proceduralized

lineup would have been

compared to the unreviewed list, which would have

identified the breaker's true function prior to the evolution taking

place.

The use of the unapproved list alone bypassed

the formal process

which the inspector concluded

was the root cause of the error .

Technical Specification 6.8.l.a

and Regulatory Guide 1.33, Revision 2,

Appendix A, Section 3.0 collectively require procedures f'r startup,

operation,

and shutdown of safety-related

PWR systems.

This requirement

is further implemented

by OHH-001, Section 5.2.1, Operating Unit

Procedure

Implementation,

which states in part that instructions for

energizing, filling, draining, starting up, shutting down,

and other

instructions appropriate for operations of systems

related to safety of

the plant shall

be delineated in system operating procedures.

The

licensee's

failure to implement procedure

OHH-001 step 5.2.2.3.c

contributed to the error resulting in the inadvertent actuation of FHB

emergency

exhaust

fan E-13B.

This failure to implement procedures

is

identified as the second

example of Violation 50-400/96-09-01

discussed

in section 04.1 above.

c.

Conclusions

Licensee

management

is continuing to address

the negative trend in human

performance in this area.

This trend was originally identified in NRC

Inspection Report 50-400/96-07.

A second

example to the violation

discussed

in section 04.1 of this report was identified f'r failure to

implement procedures.

07.1

a.

08.1

guality Assurance in Operations

Licensee

Self-Assessment

Activities

General

Comments

40500

During the inspection period, the inspectors

reviewed multiple licensee

sel f-assessment

activities, including:

~

Plant Nuclear Safety Committee

(PNSC) meetings

on September

5,

1996,

and September

25,

1996;

~

Nuclear Assessment

Section

(NAS) Audits on Steam Generator

Tube

Examination Records

(HNAS96-204),

and Operating

License

and

Technical Specification Compliance

(HNAS96-191).

These

assessments

were of good quality.

The assessment

documented in

HNAS96-191 lead to the identification of a missed

TS surveillance

requirement

(reference

report section

H8.7)

and demonstrated

good

questioning attitude on behalf of the

NAS auditor s.

Miscellaneous

Operations

Issues

(92700,

71707)

INPO Assessment

Ins ection Sco

e

71707

b.

The inspector

reviewed the

INPO report documenting

an assessment

that

was completed in Hay 1996.

This effort followed a preliminary review of

field notes discussed

in NRC Inspection Report 50-400/96-06.

Observations

and Findin s

The inspector

found that the issues identified were consistent with

those noted during the earlier review and with NRC perceptions of

licensee

performance.

No safety significant issues that required

immediate attention were identified.

C.

08.2

Conclusions

No regional

followup of the

INPO identified issues is planned.

0 en

LER 50-400/96-014:

Condition Outside of Design Basis in which

Two Charging/Safety Injection Pumps

(CSIPs)

were Inadver tently Connected

to the

Same

Emergency Electrical

Bus.

This

LER documented

the condition

described in NRC Inspection Report 50-400/96-06 in which the "B" CSIP.

and

"C" CSIP breakers

were both racked into the "B" 6.9kv electrical

bus

for approximately

10 minutes in 1989 during

a refueling outage.

The

licensee

rediscovered

the 1989 event while addressing

concerns

following

NRC identification of missing overload protective interlocks associated

with the emergency diesel

generators.

The 1989 event

happened with the

plant in Node 6 and no ongoing core alterations.

This event was

determined at that time not to be reportable

per

10 CFR 50.73 because

TS

action requirements for having no oper able diesels

(suspend

core

alterations

and vent the reactor)

wer e satisfied.

However, the

evaluation did not consider

the. situation

as

a condition outside of the

plant's design basis

(overloading the only operable diesel

generator).

Following the July 1996 NRC-identification of missing diesel

generator

overload protective interlocks (IR 50-400/96-06),

the inspectors

questioned

licensee

personnel

about the reportability of the 1989 event.

Per this review, the licensee

determined the condition to be reportable

on August 7,

1996 as

a condition outside of the plant design basis.

This

LER was issued

as

a result

and thoroughly described the

circumstances

concerning the 1989 event.

However,

completed corrective

actions

as stated in the

LER were limited to preventing recurrence of

the 1989 event (operating procedure revisions

and clearance tags).

Future corrective actions included plans to install mechanical

overload

protective interlocks for the charging

pump breakers

by the end of the

next refueling outage.

None of the corrective actions addressed

the

missed reportability call in 1989 for potentially placing the plant in

an unanalyzed condition.

The

LER will remain open pending further

NRC

review of the licensee's

actions to address

the reportability aspect of

this issue.

08.3

0 en

LER 50-400/96-018:

Hanual

Reactor Trip due to Loss of Normal

Service Water.

This LER described the manual reactor trip that occurred

on September

3,

1996 following indications of a loss of the non-safety

related

normal service water

system (section 01.2 and 01.3).

Corrective

actions specified in the

LER were still ongoing at the end of the

inspection period and will be addressed

later.

This LER will remain

open pending further

NRC review of the licensee's

corrective actions.

08.4

0 en

LER 50-400/96-020:

Inadvertent

RWST Boron Dilution Event Caused

By Personnel

Error.

This

LER documented the event described in section

04.1 of this report.

The

LER properly described the circumstances

surrounding the inadvertent dilution and subsequent

TS

LCO 3.0.3 entry.

The safety significance of this event

was still under investigation

and

will be provided in a supplement to the

LER.

The

LER will remain open

pending receipt of the supplement

and

NRC review of the licensee's

corrective actions.

The

LER and its supplement will be tracked jointly

with the first example of Violation 50-400/96-09-01.

10

II. Maintenance

Hl

Conduct of Haintenance

H1.1

General

Comments

a.

Ins ection Sco

e

62707

The inspectors

observed all or portions of the following work

activities:

~

WR/JO 96-AEGY1, Replace

8 Normal Service Water Discharge Valve

~

WR/JO 96-AGBW1, Troubleshoot

8 Normal Service

Water

Pump

~

WR/JO 96-AJNN1,

8 Main Feed

Pump Repair

~

PH AMXF 001, Rebuild 8 Normal Service Water

Pump

b.

Observations

and Findin s

The inspectors

found the work performed under these activities to be

professional

and thorough.

All work observed

was performed with the

work package

present

and in active use.

Technicians

were experienced

and knowledgeable of their assigned

tasks.

The inspectors

frequently

observed

supervisors

and system engineers

monitoring job progress,

and

quality control personnel

were present

whenever required by procedure.

c.

Conclusions

Haintenance

personnel

were following procedures.

H2

Maintenance

and Material Condition of Facilities and Equipment

H2.1

Surveillance Observation

a.

Ins ection Sco

e

61726

The inspectors

observed all or portions of the following surveillance

tests:

HST-I0320, Train

8 Solid State Protection

System Actuation 5

Logic, Revision 12.

~

HST- I0070, Calibration of NIS Power Range

Overpower Trip High

Range Bistables,

Revision 3.

b.

Observations

and Findin s

The inspector

found that the testing

was adequately

performed.

c.

Conclusions

11

The surveillance

performances

were adequately

conducted.

H6

Haintenance

Organization

and Administration

H6. 1

On-line Maintenance

Plannin

62707

a.

Ins ection Sco

e

The inspector performed

a limited review of the licensee's

program for

scheduling

and performing on-line maintenance.

This program is

described in plant procedure

PLP-710,

Work Coordination Process,

Rev. 7,

WCW-001, Work Coordination

Manual Procedure,

Rev.

1,

and ADH-NGGC-0101,

Maintenance

Rule Program,

Rev. 3.

b.

Observations

and Findin s

These procedures

prescribe the responsibilities of management,

supervisory

and working level personnel

involved in the planning and

scheduling process.

Various desk top guides are provided to planners,

schedulers

and operators

in the work control center for .implementing the

program.

The work coordination process

makes

use of a 12-week rolling

window to schedule

work which has

been systematically planned.

Each

plant system is assigned

a specific week in the 12-week rolling window.

The weeks are either A train or

B train.'uring an A train week,

work

is not planned for 8 train equipment

and vice-versa.

The final schedule

for preventative or corrective on-line maintenance is approved at least

one week in advance.

The final schedule is approved

by both maintenance

and operations

supervision.

This schedule

al'lows plant personnel

to

prepare for work on specific safety systems in advance.

The preplanned rolling 12-week schedule

has

been reviewed

and approved

by the Probabilistic Safety Assessment

(PSA) Engineer to ensure that the

removal of systems

from service is acceptable

from a risk perspective.

If any combination not allowed by the preplanned matrix requires on-line

maintenance.

consultation with the

PSA engineer

is required before the

work can

be scheduled.

The

PSA engineer

is located conveniently at the

site.

Special

contingency plans or compensatory

measures

may be

appropriate

for risk-significant systems that are to be removed from

service.

c.

Conclusions

The inspector

concluded that the control of on-line maintenance

was

within the expectations

of NRC guidance.

Personnel

were aware of and

are trained

on the proper

and safe methodology to perform on-line

maintenance.

12

M8

M8.1

M8.2

M8.3

Miscellaneous

Maintenance

Issues

(92902,

90712)

General

Comments

90712

As evidenced

by the multiple LERs gener ated in recent months,

a trend

was noted in the number of recently identified procedural

deficiencies

that have,

in the past,

resulted in either missed Technical

Specification surveillance

requirements

or other problems associated

with equipment operability.

Several of the problems

have been

identified by the licensee's

ongoing review per Generic Letter 96-01,

Testing of Safety Related Logic Circuits.

Other

LERs involved unrelated

longstanding

procedural

deficiencies that affected various systems.

Many of the problems were historical in nature

and were identified as

the result of increased

licensee sensitivity to procedural

content

and

adherence

to Technical Specification requirements.

While many of the

specific deficiencies

have

been corrected,

several

corrective actions

were outstanding

and the

LERs remained

open.

These

LERs will be

reviewed individually and collectively with other

LERs for overall

surveillance

program adequacy.

A management

meeting in the

NRC Region

II office was planned for October 21,

1996 for licensee

management to

discuss

surveillance procedure

problems.

Discussions for each of the

LERs follows.

0 en

LER 50-400/96-002:

Failure to Properly Perform Technical

Specification Surveillance Testing.

Thi's

LER was discussed

in

Inspection Reports 50-400/96-02,

96-04, 96-05,

and 96-06,

and is the

result of the licensee's

ongoing Technical Specification Surveillance

Review related to Generic Letter 96-01.

Since Inspection Report

50-400/96-06

was issued,

three supplements to this

LER have been

generated.

Supplement

10 reported two additional deficiencies.

One

involved load sequence

timing circuits for the Emergency Safeguards

Sequencer.

The other dealt with parallel circuits which operate

an

inlet damper

associated

with computer/communication

room emergency

ventilation.

Supplement

11 reported three additional testing

deficiencies

associated

with ventilation systems for the

ESW intake

structure,

the

125

VDC emergency battery rooms,

and the control

room.

Supplement

12 discussed

inadequate testing of the respective

pressure

control valves for each motor-driven

AFW pump.

This

LER and its

supplements will remain open until further

NRC review of the licensee's

corrective actions,

including retest

requirements,

is completed.

0 en

LER 50-400/96-010:

Residual

Heat Removal

(RHR) System

Surveillance Testing Deficiency that Caused

Past Entries Into TS 3.0.3.

This

LER described

procedural

revisions (to test procedures

OST-1008,

1A-SA RHR Pump Operability Quarter ly Interval

Modes 1-2-3;

and OST-1092,

18-SB

RHR Pump Operability Quarter ly Interval

Modes 1-2-3) in October

1992 that resulted in several

subsequent

entries into TS

LCO 3.0.3

during

RHR system testing.

The situations

arose

from valve alignments

which cross-tied the two redundant trains of RHR while one was

inoperable for the test.

The proceduralized

valve line-ups resulted in

the operable train being unable to provide the minimum required low head

13

safety injection flow to the

RCS during

a postulated large break loss of

coolant accident.

Supplement

1 to this

LER was issued in July 1996 to describe

a similar

situation that had been discovered while investigating the

RHR scenario.

A deficiency in original procedure

HST-I0417, Containment Ventilation

Isolation Area Radiation Honitors Relay Actuation Logic Test, resulted

in both redundant

containment

vacuum relief system valves isolating.

This caused

both trains of the containment

vacuum relief system to be

inoperable for approximately 45 minutes during each performance of the

test since

1987.

This item had been originally identified as

a concern

due to required entries into TS 3.0.3 back in December

1995, but the

repor tability aspect of such entries

was missed.

This LER supplement

addressed

corrective actions for both the procedural

deficiencies

and

the missed reportability determination in December.

Supplement

2 was issued during this inspection period and discussed

the

safety significance of both of the above items.

The licensee's

analysis

of the

RHR situation demonstrated

that while the

pump not being tested

would have inadequately split flow between

a recirculation path cr eated

by the test lineup and the intended

RCS path, the availability of the

pump under test would have also provided split flow through

a

recirculation path

and the

RCS.

The combined flows from each of the

pumps to the

RCS injection path were determined

by the licensee to meet

minimum system flow requirements for accident conditions.

A

probabilistic safety assessment

was also 'cited in the

LER as having

analyzed the degraded testing condition and determining the increase in

annual

core

damage

frequency to be 0.0065 percent.

An analysis of the

containment

vacuum relief system situation found that reliance

on

operator

action would be needed to mitigate the effects of an

inadvertent actuation of the containment

spray system (for which the

system

was designed)

coincident with the test lineup.

This

LER will remain open pending

an independent

NRC review of the above

items, their safety consequences,

and the licensee's

corrective actions.

Any enforcement

decisions will be made following the additional review.

H8.4

0 en

LER 50-400/96-011:

Inadequate

Surveillance

Procedures

Failed to

Provide

a Heans for Identifying Deactivated Automatic Containment

Isolation Valves Which Are to be Subjected to Verification Every 31 Days

in Accordance with Technical Specifications.

Two automatic containment

isolation valves,

1FW-221 and 1FW-223,

had been deactivated

and shut in

December

1995 after

1FW-221 failed stroke time testing required by

TS 3.6.3.

During a walkdown in June

1996,

an operator questioned

whether

or not the deactivated

shut status of the valves

had been

verified every 31 days

as required by TS Surveillance Requirement 4.6.1.1.a.

The licensee

determined later that compliance with

TS 4.6. 1. l.a had not been met for these valves.

The cause of the

failure to perform the required verification was

an incorrect

interpretation of the TS 4.6.1.1.a

requirement during initial procedure

development.

The earlier interpr'etation did not consider those

penetr ations which were normally capable of automatic isolation, but

14

H8.5

H8.6

whose isolation valves were deactivated

for compliance with other

Technical Specifications.

The safety consequences

of the failure to perform the monthly

verification were mitigated by the fact that the deactivated

valves were

placed under clearance

in accordance

with plant procedures.

Equipment

under

clearance

is usually reviewed by the Superintendent

of Shift

Operations at each shift turnover.

The two valves in question

were

verified to be deactivated

and shut on June 30,

1996.

Corrective

actions to revise procedures

and perform an additional

review for

possible similar situations with other containment isolation valves were

still ongoing at the end of the inspection.

The

LER will remain open

pending licensee

completion of the corrective actions

and further

NRC

review.

0 en

LER 50-400/96-015:

Unplanned Partial

Engineered Safety Feature

Actuation (Hain Steam Isolation Signal) During Surveillance Testing

Due

to Operator Error .

This

LER described

the event discussed

in detail in

NRC Inspection Report 50-400/96-07 which was example

2 of Violation 96-

07-01.

The corrective actions stated in the

LER, along with additional

corrective actions to address

the recent negative trend in personnel

error s, will be tracked in conjunction with the violation.

This LER and

the violation will remain open pending licensee

completion

and

NRC

review of corrective actions.

0 en

LER 50-400/96-016:

Failure to Perform Reactor Trip Bypass

Breaker

Surveillance

Testing Required by Technical Specifications.

This

LER reported

a Technical Specification violation in which the licensee

failed to test reactor trip bypass

breakers prior to placing them in

service.

This was

a historical

problem that dated

back to original

development of the surveillance

procedures

(HST-I0001, Train A Solid

State Protection

System Actuation Logic & Haster

Relay Test;

and

HST-I0320, Train

B Solid State Protection

System Actuation Logic &

Haster Relay Test) in 1986.

The licensee attributed the procedural

oversight to a possible misinterpretation of the term "in-service" and

how it applied to the reactor trip bypass breakers.

A licensee

review

of the

FSAR later found that it contained conflicting information with

the TS related to testing the breakers.

The

FSAR incorrectly stated

that the licensee

"does not propose to verify the operability of each

bypass

breaker prior to placing it in service

each time the main reactor

trip breakers

are to be tested."

The safety consequences

of not testing the bypass

breakers prior to

placing them in service

was mitigated by the fact that the

breakers'emote

manual

shunt trips were tested

by the

same surveillance

procedures

after placing them in service but prior to removing the main

reactor trip breakers

from service.

Corrective actions will include

revising the

HSTs and conflicting section of the

FSAR,

and training

procedure writers to emphasize

the importance of fully under standing

TS

testing requirements.

The

LER will remain open pending licensee

completion

and

NRC review of the corrective actions.

15

H8.7

0 en

LER 50-400/96-017:

Failure to Perform Surveillance Testing

Required by Technical Specifications.

This

LER described

a missed

18-

month surveillance test for the Reactor Auxiliary Building Emergency

Exhaust

System.

The test

was scheduled to be performed during Refueling

Outage

Number Six in October

1995.

A recent Nuclear Assessment

Section

audit of the plant's

document control program could not find a copy of

the completed procedure in the records storage vault.

The procedure

(OST-1052,

Reactor Auxiliary Building Emergency Exhaust

System,

18-month

Operations Surveillance Test) did not turn up during subsequent

searches

of other offices.

A review of control

room logs indicated that the test

had not been performed

even though the licensee's

tracking system for

Technical Specification surveillance tests indicated successful

test

performance

on October 5, 1995.

The 18-month frequency established

by

the TS for. this test would have

been exceeded

on Harch 11,

1996 based

on

the last previous completion in April of 1994'he

emergency

exhaust

system

was successfully tested

on June 6,

1996 (prior to the

identification of this issue

and done to resolve another

issue

referenced

in LER 96-009).

Failure to perform the test between

Harch

and June of 1996 constituted

a violation of TS 4.7.7.d.

The licensee

had not completed its investigation into the cause of this

event

and its safety consequences.

The results of that investigation,

along with recommended

corrective actions, will be presented

in a

supplement to the LER.

The

LER will remain open pending issuance of the

supplement

and further

NRC review.

Possible

enforcement

actions will be

considered

at that time.

The inspectors

considered

the identification

of this issue

by the licensee's

NAS organization to be an example of

good performance.

H8.8

Closed

Unresolved

Item 50-400/96-07-02:

Corrective Actions for

Haintenance

Rule Implementation

Problems

This item was unresolved

pending licensee

completion

and

NRC review of

an impact assessment f'r maintenance

rule scoping problems.

Inspection

report 50-400/96-07

documented that

NRC inspectors

found

a problem with

the maintenance

rule scoping for Boric Acid Filter Inlet Valve 1CS-559

in the Equipment Data Base

System

(EDBS).

Valve 1CS-559

was designated

in EDBS as not within the scope of the maintenance

rule,

even though it

is in the emergency boration flow path which is used to mitigate

accidents.

The licensee informally decided to use this existing data

base to implement the expert panel

maintenance

rule scoping

determinations.

The expert panel

scoping determination

was accurate in

identifying the boration flow path (which includes

1CS-559)

as

a

maintenance

rule function.

However, the valve had been identified in

the wrong system (filter backwash)

when the

EDBS was originally created.

The filter backwash

system

had been determined

by the expert panel

not

to have

a maintenance

rule function and all of its components

were

classified in the

EDBS as Haintenance

Rule

- No.

The erroneous

classification of 1CS-559 in the

EDBS,

and other errors discovered later

by the licensee,

indicated that the licensee

had not done

an adequate

quality check of the

EDBS prior to implementation of the maintenance

rule.

16

The inspector

reviewed the licensee's

root cause investigation for

condition report. 96-2175, written to address

the

NRC finding.

The

licensee

reviewed approximately

1200 components that could have

been

subject to the

same misclassification

as

1CS-559

and found multiple

components

in each of 9 different systems, that were not scoped correctly

in EOBS because

they wer e listed in incorrect systems.

In addition, the

licensee

found boundary valve scoping problems, similar to that of 1CS-

559, with multiple components

in 3 systems that interface with the

chemical

and volume control

system requiring maintenance

rule scoping

changes.

The licensee

performed

an impact assessment,

covering the last

3 years, to determine if any failures of maintenance

rule components

had

been missed

and concluded that one

had been missed,

but it was

determined

not

a maintenance

preventable

functional failure.

The root

cause investigation also determined that

an action item previously

assigned to review this exact area (in early 1996)

had been left off the

site wide tracking system

and was

a significant contributor to this

problem.

Inspection report 50-400/96-07

had noted previous

opportunities to fully identify and fix this problem prior to the

July 10,

1996 implementation of the maintenance

rule.

10 CFR 50.65 (b) establishes

that the scope of the maintenance

rule

monitoring program shall include safety-related

structures.

systems,

or

components that are relied upon to remain functional during and

following design basis events to ensure the integrity of the reactor

coolant pressure

boundary,

the capability to shut

down the reactor

and

maintain it in a safe shutdown condition,. and the capability to prevent

or mitigate the consequences

of accidents that could result in potential

offsite exposure

comparable to the

10

CFR part 100 guidelines;

and non-

safety related structures,

systems or components that are relied upon to

mitigate accidents or transients

or are used in the plant emergency

operating procedures,

or whose failure could prevent safety-related

structures,

systems,

and components

from fulfillingtheir safety-related

function, or whose failure could cause

a reactor

scr am or actuation of a

safety-related

system.

Procedure

ADA-NGGC-0101, Haintenance

Rule Program,

Revision 3,

implements

10 CFR 50.65 and provides maintenance

rule implementation

instructions.

Section 9.3.1,

under scoping, directed personnel

to

obtain systems lists from the Equipment Data Base System

(EDBS) and

supply to the Expert Panel

for evaluation.

Attachment 1, List of CP&L

Haintenance

Rule Systems, lists the

EDBS system

name,

system

number,

and

the exper t panel determination.

The expert panel

system determinations

were loaded into EDBS with all components in each

system receiving the

determination

for the system.

The inspectors

concluded that the improper

scoping of 1CS-559

and the

other

components

found by the licensee

was

a violation of 10 CFR 50.65(b)

under the maintenance

rule (50-400/96-09-02).

17

III. En ineerin

E1

Conduct of Engineering

El.l

General

Comments

37551

Engineering support for various activities including the

NSW pump

troubleshooting effort and routine support during the September

9

reactor startup

was good.

E1.2

Technical

S ecification Inter retation 95-003

Ultimate Heat Sink

a.

Ins ection Sco

e

37551

The inspector

reviewed Technical Specification Interpretation

(TSI) 95-

003, Ultimate Heat Sink (UHS), Revision 3,

and referenced

documentation

to determine

why the interpretation

was needed,

what affect it had on

the associated

Technical Specifications

(TS) and Final Safety Analysis

Report

(FSAR),

and whether regulatory requirements

were met.

b.

Observations

and Findin s

The TSI stated that TS 3.7.5 Limiting Condition for Operation

(LCO)

action statement

should be applied for the main reservoir

at the 215

foot elevation (instead of the TS 205.7 foot elevation value);

and apply

the action at 94 degrees

F for either reservoir with at least

one

emergency

service water

pump running, or use 86 degrees

F if neither

emergency service water

pump is running (instead of the TS reservoir

temper ature value of 95 degrees

F).

TSI 95-003, Revision

0 was issued

on June 28,

1995 and included only the

215 foot elevation for applying the TS 3.7.5

LCO action.

The TSI stated

that the limit is expected to be temporary,

and will remain in effect

until engineering analysis

supports rescission.

Revision

1 was issued

September

1,

1995, which included the 215 foot elevation

and established

a new reservoir

temperature limit of 89 degrees

F to apply the

LCO

action.

Revision

2 was issued October 5, 1995, which included the 215

foot elevation,

but changed temperature to apply the

LCO action at 95

degrees

F for either

reservoir with at least

one emergency service water

pump running, or use 86 degrees

F if neither

emergency service water

pump is running.

Revision 3 was issued

Harch 29,

1996, which included

the 215 foot elevation,

but lowered the 95 degrees

F to 94 degrees

F,

leaving the 86 degrees

F as previously stated.

The TSI and revisions

were reviewed

and approved

by plant management

and the Plant Nuclear

Safety Committee.

TSI Basis

The inspector

researched

the basis for this TSI through review of

Engineering Service Requests

(ESRs)

9500548,

9500707,

9500726.

Adverse

Condition and Feedback

Reports

(ACFRs) 95-00129

and 95-01464,

TSs 3.7.5

18

and 3.7.4,

and the associated

TS bases.

The ACFRs and

ESRs were

generated

as

a result of question

number

8 from the Service Water System

Operational

Performance

Inspection

(SWSOPI)

conducted

by the licensee.

The SWSOPI questioned

how the TS 3.7.5 value of 95 degrees

F would

prevent the ultimate heat sink from exceeding the 30 day post accident

value of 95 degrees

F.

A calculation effort to determine the

appropriate starting value was what resulted in the 94/86 degree

F

reservoir

temperature

value.

The licensee

discovered during the temper ature resolution effort that

although the TS 3.7.5

LCO main

r eservoir

level of 205.7 feet was

adequate

volume to dissipate

the design heat load over

a 30 day period

(stated in TS Bases),

the level

was not adequate for the emergency

service water

system to provide sufficient flow for all components to

remove the design heat generated.

Since

an

ESW pump upgrade could not

be immediately conducted to incr ease flow, an alternative that could be

immediately put in place

was to raise the limit on reservoir level.

A

calculated reservoir level of 215 feet was determined to provide

adequate

flow to all components

serviced

by ESW to maintain them

operable.

This administrative limit was put in place through the TSI.

The inspector's

review of PNSC meeting minutes for the TSI found that

the licensee felt the TSI required

them to apply the

LCO "early" as

compared to the TS value and therefore the interpretation

was more

conservative

than TS.

No discussion of a license

amendment/TS

change

was documented.

The inspector

found that the conclusions of ESR 9500548,

issued August

25.

1995,

were that the 215 foot elevation main reservoir administrative

limit (TSI) needed to be maintained to ensure operability of some

ESW

components.

The inspector

found that later

ESRs used the 215 foot

elevation

as

an assumption

and did not support retr acting that limit.

The

FSAR change

markup did not include the 215 foot elevation

administrative limit and stated that

a license

amendment

was not

necessary.

The

ESR stated that main reservoir level

has never

been

below approximately 217 feet elevation during the history of the plant.

The inspector

reviewed

FSAR section 2.4.11.7,

Heat Sink Dependability

Requirements,

FSAR section 9.2.1, Service Water System,

and

FSAR section

9.2.5, Ultimate Heat Sink.

None of the

FSAR sections

mention the main

reservoir level needing to be 215 feet to provide adequate

ESW flow for

heat removal.

These sections

were changed

by Amendment 46, submitted

April 12,

1996, to include many of the results

from the

SWSOPI question

on this issue.

ESR 9500707,

issued January

17,

1996, provided the basis

for the

FSAR changes to those sections

and included those

from ESR

9500548,

but made

no mention of the 215 foot level.

The 10 CFR 50 '9

safety evaluation for ESR 9500707 concluded that

a license

amendment

was

needed for UHS temperature.

No change

was mentioned for level.

Licensee Administrative Procedure

(AP) 107, Technical Specification

Interpretations,

Revision 7. governs the TSI process

and indicated that

TSIs are intended to provide

a consistent

and reasonable

position on the

meaning

and applicability of the TSs.

An annual

TSI audit required by

19

AP-107 was conducted

and issued

on December

29,

1995.

It concluded that

TSI 95-003 should remain in place

and did not need to be incorporated

into a TS change.

The reason

given in the audit report for

a TS change

not being needed

was that it was "too costly."

The inspector noted that

TSIs are not required by AP-107 to receive

a review under

10 CFR 50.59.

Licensee

management

had authorized the regulatory affair s organization

to develop

a TS change

on May 21,

1996 that encompassed

TSI 95-003.

The

licensee

had not made

any meaningful

progress

on the change prior to the

inspector

discussing

the issue.

Licensee Corrective Actions

The inspector

found that the licensee

was adequately

pursuing corrective

action of the technical

issue

from a hardware standpoint including

modifications during the upcoming outage

(RF07) to replace the "B" ESW

pump with a larger capacity

pump and to enlarge the containment

fan

cooler orifices to allow greater flow.

The replacement of the "A" pump

is scheduled for the following outage

(RF08).

As a result of the

inspector's

concern regarding whether the TS met the requirements of 10 CFR 50.36, the licensee

intends to submit

a TS change

by November 1,

1996,

and revise the

FSAR to include all the information in the TSI.

However, at the time of the inspection the TSI remained the only safety

barrier.

c.

Conclusions

Licensee corrective action for dealing with the hardware

and design

problem was prompt.

However, this issue is unresolved

based

on the

inspector reviewing the previous main reservoir level history to

determine whether the plant operated outside the design basis,

and an

overall regulatory impact assessment

including whether

the TS and

FSAR

met regulatory requirements

(Unresolved Item 50-400/96-09-03.

UHS/ESW

Technical Specification Interpretation).

E7

Quality Assurance in Engineering Activities

E7.1

S ecial

FSAR Review

37551

A recent discovery of a licensee operating their facility in a manner

contrary to the Updated Final Safety Analysis Report

(UFSAR) description

highlighted the need f'r a special

focused review that compares plant

practices,

procedures

and/or parameters

to the

FSAR descriptions.

While

performing the inspections

discussed

in this report, the inspectors

reviewed the applicable portions of the

FSAR that related to the areas

inspected.

The licensee

made

a presentation

to the

NRC on May 31,

1996 concerning

their corporate-wide

plan for reviewing the

FSAR at the

CPSL sites.

The

program has generated

a large

number of condition reports at the Harris

Plant

(252 by the end of the inspection period).

Three

have resulted in

LERs.

The results

from this program will be reviewed in the closure of

20

Unresolved

Item 50-400/96-04-04,

Tracking

FSAR Discrepancy Resolution.

A discrepancy

was identified by the inspectors

between the

FSAR wording

and plant engineering

documents

related to the emergency service water

system

and ultimate heat sink as described in section El.2.

E8

E8. 1

Hiscellaneous

Engineering Issues

(92700)

0 en

LER 50-400/96-013:

Condition Outside of Design Basis where the

RWST Had Been Connected to

a Non-seismically Qualified System.

This

LER

reported

a long-standing

design

and operational

issue related to non-

seismic portions of piping systems

being connected to the Refueling

Water Storage

Tank

(RWST) during routine operations.

Specifically, the

non-seismic portion of the spent fuel pool purification system

had

routinely been aligned to the

RWST for pool cleanup,

and non-seismic

piping to the hydrostatic test

pump had been aligned to the

RWST for

fi'lling the safety injection accumulator

tanks inside containment.

These problems dated back to original procedural

development

and the

failure to adequately reconcile operating procedures

with the plant's

design basis.

The licensee

evaluated the safety significance of not having the

RWST

available during

a seismic event using probabilistic risk assessment

and

determined that the increase to conditional core

damage

was small.

Currently, valves isolating the non-seismic portion of the systems

trom

the

RWST are locked shut

and under clearance.

The inspectors

have

verified these valve configurations during routine plant walkdowns.

The

licensee

was still developing contingency plans for purifying the spent

fuel pools

and fillingthe safety injection accumulators

at the end of

the inspection period.

This LER will remain open pending completion of

the licensee's

ongoing actions

and further review by the inspectors.

R1

R1.1

P2

P2.1

IV. Plant

Su

rt

Radiological Protection

and Chemistry (RPK) Controls

General

Comments

71750

The inspector

observed radiological controls during the conduct of tours

and observation of maintenance activities and found them to be

acceptable.

The general

approach to the control of contamination

and

dose for the site was good.

Teamwork between the various departments

continued to be

a major contributor to the good control of dose,

A

resin spill in the waste processing building that occurred during this

period was handled well.

Status of Emergency Preparedness

(EP) Facilities, Equipment,

and

Resources

Hurricane

Fran

71750

71707

21

a.

Ins ection Sco

e

The licensee

made preparations for Hurricane Fran prior to and on the

September

5,

1996, arrival of the hurricane.

Licensee

Procedure

AP-301,

Adverse Weather Operations,

Revision 15,

was used for the preparations.

The inspectors

observed

the licensee's

preparations

and response

to

determine whether they met regulatory requirements.

b.

Observations

and Findin s

The Harris plant was shutdown in Hot Standby

due to the loss of normal

service water on September

3,

1996,

as discussed

in section 01.2 of this

report.

The Hurricane caused

no damage to safety or balance of plant

equipment

on site.

The only damage

observed

on site were several

panels

from the administration building that blew off and were found after the

hurricane against the security fence.

Offsite equipment

such

as evacuation

sirens lost power during the

hurricane.

Two reports were made under

10 CFR 50.72 by the licensee

related to offsite situations.

The first was on September

6,

1996 when

the licensee

began losing power to the offsite emergency evacuation

sirens.

The report was

made when 20 percent of the sirens

were lost.

When the hurricane

was over the licensee

had lost power to approximately

90 percent of the 81 offsite sirens.

The local area

had received

significant rain for the week prior to the arrival of the hurricane

which had softened the ground.

As a result,

a significant number of

trees

were uprooted by the Hurricane winds which gusted to 80 miles per

hour.

These trees fell on the power lines which caused the loss of

power

.

The licensee

had returned

90 percent of the sirens to service by

September

9,

1996 when the

NRC (and FEN) gave permission for the plant

to restart.

The second report related to restricted plant access

due to downed trees

and power lines on the plant access

road and local area roads.

Sufficient additional operators

were available to maintain minimum

required shift coverage.

The 10 CFR 50.72 report was

made at 5:41 a.m.

on September

6, 1996.

Access to the plant was restored

by approximately

9:00 a.m. that

same day.

LER 96-019 addresses

this issue.

c.

Conclusions

The licensee appropriately

responded to the hurricane

and made the

proper notifications as required by the regulations

when emergency

response

capability was hampered

and emergency

equipment

was

unavailable.

P8

Hiscellaneous

EP Issues

(71750)

P8.1

Closed

LER 50-400/96-019:

Hurricane Fran Hampered Site Personnel

From

Accessing

The Plant.

This LER reported

degraded

road conditions which

were caused

by the hurricane

on September

5,

1996,

and were determined

by the licensee to have significantly hampered site personnel

in the

performance of their duties.

Approximately 3.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after the initial

22

S1

S1.1

S1.2

a.

b.

1-hour non-emergency notification was made to the

NRC, plant access

roads were cleared which allowed site personnel

to get into and out of

the plant.

No further corrective actions

were required for this

condition and this

LER is closed.

Further discussion of the hurricane

appears

in section

P2.1 of this report.

Conduct of Security and Safeguards Activities

General

Comments

71750

The inspector observed security

and safeguards activities during routine

plant tours

and during the response to Hurricane Fran on September

5 and

6, 1996.

Compensatory

measures

during the hurricane,

including security

staff support to plant personnel,

were good.

General

Inte

r it of Protected

Area

PA

Barriers

Ins ection Sco

e

71750

The inspectors

toured the facility to ensure that protected

area

and

vital area barriers

were separated

and that the barriers

had no openings

and. were not damaged or in an otherwise degraded

condition.

Observations

and Findin s

During a plant tour

on September

13,

1996, the inspector

observed

protected

area gate

1B open approximately three to four feet.

This gate

is located at the vehicle "tr ap" adjacent to the security building and

is the protected

area gate where vehicle access is granted.

The outer

vehicle trap gate

was secured.

The inspector

was concerned

because

there

was

an opening into the protected

area

and security personnel

were

neither

aware of the opening nor in a position to 'fully observe

and

control access

into the protected

area.

The inspector

noted that the

security personnel

were located in a gate

house inside the vehicle trap

(approximately

20 feet away)

and appeared to be engaged in duties

related to a vehicle that was exiting the plant.

The inspector gained

the attention of the officer in the gate

house

who approached

the gate.

The inspector informed the officer that the gate

was open

and the

officer, via radio communications with the Facility Access Control

(FAC)

operator,

directed complete closure of the gate.

The inspector reported this finding to security management

personnel

who

initiated Condition Report 96-02886

and an investigation.

The

licensee's

investigation determined that the gate

had only been

opened

for approximately two minutes

and that the officer failed to ensure

complete closure of the gate once the vehicle was inside the trap.

The

officer had directed the

FAC to close the gate

once the vehicle was

inside and then turned his back on the gate in route to the gate house.

The

FAC operator

apparently did not complete the gate closure

sequence.

Once the officer was informed by the inspector that the gate

was opened,

prompt actions to secure the gate were taken.

23

The inspector determined through discussions

with licensee

personnel

and

reviews of security procedures

that the officer failed to perform

specified duties

as outlined in procedures

SP-005,

Security Search

and

Contraband Denial, Revision 5;

and SP-004,

Security Post Duties,

Responsibilities,

and Patrol

Procedures,

Revision 2.

Procedure

SP-004,

Section

12 delineates

the duties of guards/armed

responders

which

includes ensuring integrity of protected

area barriers.

Procedure

SP-005,

Section 7.0, Vehicle Searches,

Step

7 specified that, following

access

by the vehicle, the gate

and the vehicle barrier

system active

barrier shall

be closed

and returned to the blocking position.

These

procedures

implement the licensee's

security plan

(CP8L Physical

Security and Safeguards

Contingency Plan,

Revision 0).

Section 4.0 of

this plan prohibits protected

area barrier

openings of greater

than 96

square

inches.

The failure to secure the protected

area barrier created

a short-term vulnerability in that the integrity of the protected

area

bar rier was not maintained

and

an opening in excess of the requirements

in the security plan existed for approximately two minutes.

The

inspector investigated the vehicle trap area

by observing gate

operations

from the

FAC and locally surveying accessibility to the

vulnerable area.

The inspector

concluded that although the officer in

the gate

house

and personnel

at three other watch stations with video

monitoring capability were unaware that the gate

was left open, the

vulnerability was neither easily or likely to be exploitable.

Technical Specification 6.8.1.c requires that written procedures

shall

be established,

implemented,

and maintained covering Security Plan

implementation.

The failure to properly secure

gate

1B constituted

a

failure to follow procedure

SP-005

and is a Violation of TS 6.8.1.c

(50-

400/96-09-04).

Immediate corrective actions for this error included counseling the

officer and training other security personnel

on this event

and the

contributing factors.

The inspector verified that the incident was

recorded in the Quarterly Safeguards

Event Log in accordance

with the

requirements of 10 CFR 73.71, Reporting of Safeguards

Events.

Security

management's

response to this finding was prompt and appropriate.

c.

Conclusions

The protected

area

boundary was generally intact;

however, the inspector

identified a short-term vulnerability caused

by personnel

error.

One

violation was identified for failure to follow security procedures.

F1

Control of Fire Protection Activities

F1.1

General

Comments

71750

The inspector

observed fire protection equipment

and activities during

the conduct of tours

and observation of maintenance activities and found

them to be acceptable.

24

X1

Exit Meeting Summary

V. Mana ement Meetin s

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on October

18,

1996.

The

licensee

acknowledged the findings presented.

The inspectors

asked the licensee

whether

any of the material

examined

during the inspection should

be considered proprietary.

No proprietary

information was identified.

25

Licensee

PARTIAL LIST OF PERSONS

CONTACTED

D. Alexander,

Super visor, Licensing and Regulatory Programs

D. Batton, Superintendent,

On-Line Scheduling

D.

Br aund,

Superintendent,

Security

B. Clark, General

Hanager,

Harris Plant

A. Cockerill, Superintendent,

I8C Electrical

Systems

J. Collins, Hanager,

Training

J.

Dobbs,

Hanager,

Outage

and Scheduling

J.

Donahue,

Director Site Operations,

Harris Plant

R. Duncan,

Superintendent.

Hechanical

Systems

W. Gautier,

Hanager,

Haintenance

W. Gurganious,

Superintendent,

Environmental

and Chemistry

H. Hamby,

Super visor, Regulatory Compliance

H. Hill, Hanager,

Nuclear Assessment

D. HcCarthy, Superintendent.

Outage

Hanagement

K. Neuschaefer.

Superintendent,

Radiation Protection

W. Peavyhouse,

Superintendent,

Design Control

W. Robinson,

Vice President,

Harris Plant

G. Rolfson.

Hanager,

Harris Engineering Support Services

S. Sewell,

Hanager,

Operations

T. Walt, Hanager,

Performance

Evaluation

and Regulatory Affairs

NRC

T. Le, Harris Project Hanager,

NRR

H. Shymlock, Chief, Reactor Projects

Branch 4

26

IP 37551:

IP 40500:

IP 61726:

IP 62707:

IP 71707'P

71750'P

90712:

IP 92902:

IP 93702:

INSPECTION PROCEDURES

USED

Onsite Engineering

Effectiveness of Licensee Controls in Identifying, Resolving,

and

Preventing

Problems

Surveillance Observations

Maintenance Observation

Plant Operations

Plant Support Activities

In-office Review of LERs

Followup

- Maintenance

Onsite Response to Events

~0ened

50-400/96-09-01

VIO

50-400/96-09-02

VIO

50-400/96-09-03

URI

50-400/96-09-04

VIO

Closed

ITEMS OPENED,

CLOSED.

AND DISCUSSED

Failure To Follow Operating Procedures,

Paragraph

04.1.

Inadequate

Maintenance

Rule Scoping,

Paragraph

M8.8.

Technical Specification Interpretation for Ultimate

Heat Sink 5 FSAR Discrepancy,

Paragraph

E1.2

Failur e To Properly Secure Protective Area Gate,

Violating Security Procedures,

Paragraph

S1.2.

50-400/96-07-02

URI

Corrective Actions for Maintenance

Rule Implementation

Problems,

Paragraph

M8.8

50-400/96-019

LER

Hurricane Fran Hampered Site Personnel

from Accessing

the Plant,

Paragraph

P8.1.

Discussed

50-400/96-014

LER

50-400/96-018

LER

50-400/96-020

LER

50-400/96-002

LER

50-400/96-010

LER

50-400/96-011

LER

Condition Outside of Design Basis in which Two

Charging/Safety Injection Pumps

(CSIPs)

were

Inadvertently Connected to the

Same

Emergency

Electrical

Bus,

Paragraph

08.2.

Manual Reactor Trip due to Loss of Normal Service

Water,

Paragraph

08.3.

Inadvertent

RWST Boron Dilution Event Caused

by

Personnel

Error, Paragraph

08.4.

Failure to Proper ly Perform Technical Specification

Surveillance Testing,

Paragraph

M8.2.

Residual

Heat Removal

(RHR) System Surveillance

Testing Deficiency that Caused

Past Entries into TS

3'.3,

Paragraph

M8.3.

Inadequate

Surveillance

Procedures

Failed to Provide

a

Means for Identifying Deactivated Automatic

Containment Isolation Valves which are to be Subjected

50-400/96-015

LER

50-400/96-017

LER

50-400/96-013

LER

50-400/96-016

LER

27

to Verification every 31 Days in Accordance with

Technical Specifications,

Paragraph

H8.4.

Unplanned Partial

Engineered Safety Feature Actuation

(Hain Steam Isolation Signal) During Surveillance

Testing

Due to Operator. Error, Paragraph

H8.5.

Failure to Perform Reactor Trip Bypass Breaker

Surveillance Testing Required by Technical

Specifications,

Paragraph

H8.6.

Failure to Perform Surveillance Testing Required by

Technical Specifications,

Paragraph

H8.7.

Condition Outside of Design Basis where the

RWST had

been Connected to a Non-seismically Qualified System,

Paragraph

E8.1